ML18009A704: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by StriderTol
Created page by program invented by StriderTol
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM 1 I REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)ACCESSION NBR:9010250009 DOC.DATE: 90/10/11 NOTARIZED:
{{#Wiki_filter:ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM 1
NO FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina AUTH.NAME AUTHOR AFFILIATION RICHEY,R.B.
I REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
Carolina Power 6 Light Co.RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
ACCESSION NBR:9010250009                   DOC.DATE:   90/10/11     NOTARIZED: NO           DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina                         05000400 AUTH. NAME             AUTHOR AFFILIATION RICHEY,R.B.           Carolina Power 6 Light Co.
RECIP.NAME             RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)


==SUBJECT:==
==SUBJECT:==
Special rept:on 900922,main steam line radiation monitor declared inoperable due to communication failure.DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR
Special rept:on 900922,main steam line radiation monitor declared inoperable due to communication failure.
/ENCL i SIZE: TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.NOTES:Application for permit renewal filed.DOCKET 05000400 05000400 RECIPIENT ID CODE/NAME PD2-1 LA BECKER, D COPIES LTTR ENCL 1 1 1 1 RECIPIENT COPIES ID CODE/NAME l LTTR ENCL PD2-1 PD 1 1 INTERNAL: ACNW AEOD/DOA AEOD/ROAB/DSP NRR/DET/EMEB 7E NRR/DLPQ/LPEB10 NRR/DST/SELB SD~X%48 EXTERNAL: EGGG BRYCE,J.H NRC PDR NSIC MURPHY,G.A 2 2 1 1 2 2 1 1 1 1 1 1 1 1 1 1 1 1 3 3 1 1 1 1 ACRS AEOD/DSP/TPAB NRR/DET/ECMB 9H NRR/DLPQ/LHFBll NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB L ST LOBBY WARD NSIC MAYS,G NUDOCS FULL TXT 2 2 1 1 1 1 1 1 2 2..1 1 1 1 1 1 1 1 1 1 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
DISTRIBUTION CODE: IE22D             COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER),
PLEASE HELP US TO REDUCE KVASTE!CONTACT THE DOCUMENT CONTROL DESK, ROO.'il P 1-37 (EXT.20079)TO ELliillNATE YOUR NAiblE FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32 Carolina Power 8 Light Company P.O.Box 165~New Hill, N.C.27562 R.B.RICHEY Vice President Harris Nuclear Project ggQ LB',ii 8 Letter Number', H0-900149 (0)U;S.Nuclear Regulatory Commission ATTN: NRC Document~Control Desk Washington, DC 20555 HARRIS NUCLEAR POWER PROJECT UNIT 1 DOCKET.'O.
                                                                          /ENCL Incident i    SIZE:
50-400 LICENSE NO.NPF-63 NRC 14-DAY SPECIAL EVENT REPORT Gentlemen:
Rpt, etc.
In accordance with Technical Specifications 3'.3.6 and 6.9.2 for the Shearon Harris Nuclear Power Plant, Unit No.1, Carolina Power and Light Company hereby submits this Special Report.This Special Report concerns the operability of a radiation monitor.Very truly yours, R.B.Richey Vice President Harris Nuclear Project RBR:slc Enclosure cc.'r.R.A.Becker (NRR)Mr.S.D.Ebneter (NRC" RII)Mr.'.E.Tedrow (NRC-SHNPP)MEM/HO-9001490/1/OS1 Z CRk l(g
NOTES:Application for permit renewal filed.                                               05000400 RECIPIENT                   COPIES            RECIPIENT            COPIES ID CODE/NAME               LTTR ENCL       ID CODE/NAME     l   LTTR ENCL PD2-1 LA                        1      1    PD2-1 PD                 1     1 BECKER, D                      1      1 INTERNAL:   ACNW                           2      2    ACRS                      2    2 AEOD/DOA                       1      1    AEOD/DSP/TPAB            1    1 AEOD/ROAB/DSP                   2      2    NRR/DET/ECMB 9H          1    1 NRR/DET/EMEB 7E                 1      1    NRR/DLPQ/LHFBll          1    1 NRR/DLPQ/LPEB10                 1      1    NRR/DREP/PRPB11          2    2..
              ~X NRR/DST/SELB SD
                            %48 1
1 1
1 1
1 1
1 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB 1
1 1
1 1
1 EXTERNAL: EGGG BRYCE,J.H                    3      3    L ST LOBBY    WARD      1     1 NRC PDR                        1       1     NSIC MAYS,G              1     1 NSIC MURPHY,G.A                1       1     NUDOCS FULL TXT          1     1 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE KVASTE! CONTACT THE DOCUMENT CONTROL DESK, ROO.'il P 1-37 (EXT. 20079) TO ELliillNATEYOUR NAiblE FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
TOTAL NUMBER OF COPIES REQUIRED: LTTR                   32   ENCL     32


ACCIDENT RADIATION MONITOR SPECIAL REPORT Descri tion of Event On September 22, 1990 at 0130, the Main Steam Line Radiation Monitor RM-01MS-3593SB was declared inoperable due to a communication failure and keyboard lockout.This monitor is identified in the Harris Technical Specifications Table 3.3.10 as Item 19..The preplanned alternate method of monitoring the appropriate channels is to take hourly readings off the main steam/feedwater tunnel floor area monitor.This action was performed while the monitor was inoperable.
Carolina Power 8 Light Company P. O. Box 165 ~ New Hill, N. C. 27562 R. B. RICHEY Vice President Harris Nuclear Project LB',ii 8 ggQ Letter        Number', H0-900149  (0)
The monitor was out of service for greater than 7 days;thus, a Special Report is required to be submitted per the Technical Specification 3[3.3.6.c.
U;S. Nuclear Regulatory Commission ATTN:        NRC Document ~Control Desk Washington, DC 20555 HARRIS NUCLEAR POWER PROJECT UNIT                1 DOCKET.'O. 50-400 LICENSE NO. NPF-63 NRC 14-DAY SPECIAL EVENT REPORT Gentlemen:
Cause Corrective Action On September 22, 1990, Monitor ARM-01MS-3593SB was taken out of service due to a communication failure and keyboard lockout.The logic power supply for the main steam line monitor was replaced.on September 25, 1990.The vendor representative suggested that the power supply be allowed to burn-in for several days.On October 3, 1990, MST-I0409"Main Steam Line Monitor RM-01MS-3593-SB Calibration" was satisfactorily performed and the monitor was returned to service.}}
In accordance with Technical Specifications 3 '.3.6 and 6.9.2 for the Shearon Harris Nuclear Power Plant, Unit No. 1, Carolina Power and Light Company hereby submits this Special Report.                This Special Report concerns the operability of a radiation monitor.
Very    truly yours, R. B. Richey Vice President Harris Nuclear Project RBR:slc Enclosure cc.'r.        R. A. Becker (NRR)
                                                " RII)
Mr. S. D. Ebneter (NRC Mr.'. E. Tedrow (NRC  SHNPP)
MEM/HO-9001490/1/OS1 Z CRk l(g
 
ACCIDENT RADIATION MONITOR SPECIAL REPORT Descri tion of Event On September   22, 1990 at 0130, the Main Steam Line Radiation Monitor   RM-01MS-3593SB   was declared inoperable due to a communication failure and keyboard lockout.       This monitor is identified in the Harris Technical Specifications Table 3.3.10 as Item 19.. The preplanned alternate method of monitoring the appropriate channels is to take hourly readings off the main steam/feedwater tunnel floor area monitor.         This action was performed while the monitor was inoperable. The monitor was out of service for greater than 7 days; thus, a Special Report is required to be submitted per the Technical Specification 3[3.3.6.c.
Cause Corrective Action On September 22, 1990, Monitor ARM-01MS-3593SB was taken out of service due to a communication failure and keyboard lockout. The
 
logic power supply for the main steam line monitor was replaced .on September 25, 1990. The vendor representative suggested that the power supply be allowed to burn-in for several days. On October 3, 1990,   MST-I0409 "Main Steam     Line Monitor RM-01MS-3593-SB Calibration" was satisfactorily performed and the monitor was returned to service.}}

Revision as of 05:36, 22 October 2019

Special Rept:On 900922,main Steam Line Radiation Monitor Declared Inoperable Due to Communication Failure
ML18009A704
Person / Time
Site: Harris 
Issue date: 10/11/1990
From: Richey R
CAROLINA POWER & LIGHT CO.
To:
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
HO-900149, NUDOCS 9010250009
Download: ML18009A704 (5)


Text

ACCELERATED DISTMBUTION DEMONSTRATION SYSTEM 1

I REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:9010250009 DOC.DATE: 90/10/11 NOTARIZED: NO DOCKET FACIL:50-400 Shearon Harris Nuclear Power Plant, Unit 1, Carolina 05000400 AUTH. NAME AUTHOR AFFILIATION RICHEY,R.B. Carolina Power 6 Light Co.

RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)

SUBJECT:

Special rept:on 900922,main steam line radiation monitor declared inoperable due to communication failure.

DISTRIBUTION CODE: IE22D COPIES RECEIVED:LTR TITLE: 50.73/50.9 Licensee Event Report (LER),

/ENCL Incident i SIZE:

Rpt, etc.

NOTES:Application for permit renewal filed. 05000400 RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME l LTTR ENCL PD2-1 LA 1 1 PD2-1 PD 1 1 BECKER, D 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB 7E 1 1 NRR/DLPQ/LHFBll 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DREP/PRPB11 2 2..

~X NRR/DST/SELB SD

%48 1

1 1

1 1

1 1

1 NRR/DST/SICB 7E NRR/DST/SRXB 8E RES/DSIR/EIB 1

1 1

1 1

1 EXTERNAL: EGGG BRYCE,J.H 3 3 L ST LOBBY WARD 1 1 NRC PDR 1 1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL "RIDS" RECIPIENTS:

PLEASE HELP US TO REDUCE KVASTE! CONTACT THE DOCUMENT CONTROL DESK, ROO.'il P 1-37 (EXT. 20079) TO ELliillNATEYOUR NAiblE FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!

TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32

Carolina Power 8 Light Company P. O. Box 165 ~ New Hill, N. C. 27562 R. B. RICHEY Vice President Harris Nuclear Project LB',ii 8 ggQ Letter Number', H0-900149 (0)

U;S. Nuclear Regulatory Commission ATTN: NRC Document ~Control Desk Washington, DC 20555 HARRIS NUCLEAR POWER PROJECT UNIT 1 DOCKET.'O. 50-400 LICENSE NO. NPF-63 NRC 14-DAY SPECIAL EVENT REPORT Gentlemen:

In accordance with Technical Specifications 3 '.3.6 and 6.9.2 for the Shearon Harris Nuclear Power Plant, Unit No. 1, Carolina Power and Light Company hereby submits this Special Report. This Special Report concerns the operability of a radiation monitor.

Very truly yours, R. B. Richey Vice President Harris Nuclear Project RBR:slc Enclosure cc.'r. R. A. Becker (NRR)

" RII)

Mr. S. D. Ebneter (NRC Mr.'. E. Tedrow (NRC SHNPP)

MEM/HO-9001490/1/OS1 Z CRk l(g

ACCIDENT RADIATION MONITOR SPECIAL REPORT Descri tion of Event On September 22, 1990 at 0130, the Main Steam Line Radiation Monitor RM-01MS-3593SB was declared inoperable due to a communication failure and keyboard lockout. This monitor is identified in the Harris Technical Specifications Table 3.3.10 as Item 19.. The preplanned alternate method of monitoring the appropriate channels is to take hourly readings off the main steam/feedwater tunnel floor area monitor. This action was performed while the monitor was inoperable. The monitor was out of service for greater than 7 days; thus, a Special Report is required to be submitted per the Technical Specification 3[3.3.6.c.

Cause Corrective Action On September 22, 1990, Monitor ARM-01MS-3593SB was taken out of service due to a communication failure and keyboard lockout. The

logic power supply for the main steam line monitor was replaced .on September 25, 1990. The vendor representative suggested that the power supply be allowed to burn-in for several days. On October 3, 1990, MST-I0409 "Main Steam Line Monitor RM-01MS-3593-SB Calibration" was satisfactorily performed and the monitor was returned to service.