ENS 40362: Difference between revisions

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| event date = 11/28/2003 22:02 CST
| event date = 11/28/2003 22:02 CST
| last update date = 11/29/2003
| last update date = 11/29/2003
| title = Automatic Scram Due To Low Reactor Water Level
| title = Automatic Scram Due to Low Reactor Water Level
| event text = At 2202 CST, a low Reactor Water Level Scram (Level 3) occurred due to lowering feedwater flow.  All control rods inserted on the Scram.  The Scram resulted in actuation of HPCI and RCIC on low Reactor Water level (Level 2), and the low level ATWS Recirculation Pump Trip (RPT).  HPCI and RCIC initiated and both Reactor Recirculation pumps tripped.  It is estimated that RCIC injected approximately 500 to 600 gallons, and HPCI injected less than 100 gallons.  HPCI was secured early in the transient, and RCIC operated for approximately 2 minutes.  Reactor Water level was recovered and maintained with the operating feedwater pump.   
| event text = At 2202 CST, a low Reactor Water Level Scram (Level 3) occurred due to lowering feedwater flow.  All control rods inserted on the Scram.  The Scram resulted in actuation of HPCI and RCIC on low Reactor Water level (Level 2), and the low level ATWS Recirculation Pump Trip (RPT).  HPCI and RCIC initiated and both Reactor Recirculation pumps tripped.  It is estimated that RCIC injected approximately 500 to 600 gallons, and HPCI injected less than 100 gallons.  HPCI was secured early in the transient, and RCIC operated for approximately 2 minutes.  Reactor Water level was recovered and maintained with the operating feedwater pump.   
The Reactor Water low level (Level 3) also resulted in Group 2 (Primary Containment), Group 3 (Reactor Water Cleanup), and Group 6 isolations (Secondary Containment Isolation and Control Room Ventilation system start).  All isolations functioned as designed.
The Reactor Water low level (Level 3) also resulted in Group 2 (Primary Containment), Group 3 (Reactor Water Cleanup), and Group 6 isolations (Secondary Containment Isolation and Control Room Ventilation system start).  All isolations functioned as designed.

Latest revision as of 22:24, 1 March 2018

ENS 40362 +/-
Where
Cooper Entergy icon.png
Nebraska (NRC Region 4)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge

10 CFR 50.72(b)(3)(iv)(A), System Actuation
Time - Person (Reporting Time:+-1.25 h-0.0521 days <br />-0.00744 weeks <br />-0.00171 months <br />)
Opened: John Myers
02:47 Nov 29, 2003
NRC Officer: Mike Ripley
Last Updated: Nov 29, 2003
40362 - NRC Website
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