ENS 43976: Difference between revisions
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StriderTol (talk | contribs) (Created page by program invented by Mark Hawes) |
StriderTol (talk | contribs) (Created page by program invented by StriderTol) |
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| event date = 02/10/2008 22:07 CST | | event date = 02/10/2008 22:07 CST | ||
| last update date = 02/13/2008 | | last update date = 02/13/2008 | ||
| title = Manual Reactor Scram Due | | title = Manual Reactor Scram Due to Increasing Reactor Vessel Level | ||
| event text = On February 10, 2008, at approximately 2207 hours CST, the 'B' Reactor Recirculation pump tripped from fast speed to off. The resultant reactor pressure vessel level swell resulted in reactor pressure vessel level being greater than 48 inches and rising. Per Clinton Power Station operating procedures, the 'A' Reactor Operator placed the mode switch to the 'shutdown' position initiating a manual reactor scram. All control rods inserted [fully]. CPS is currently stable in Mode 3. | | event text = On February 10, 2008, at approximately 2207 hours CST, the 'B' Reactor Recirculation pump tripped from fast speed to off. The resultant reactor pressure vessel level swell resulted in reactor pressure vessel level being greater than 48 inches and rising. Per Clinton Power Station operating procedures, the 'A' Reactor Operator placed the mode switch to the 'shutdown' position initiating a manual reactor scram. All control rods inserted [fully]. CPS is currently stable in Mode 3. | ||
Decay heat is being removed to the main condenser via the turbine bypass valves. Reactor level is being maintained using the motor driven reactor feedpump. No SRVs lifted during the transient. Licensee is in progress of restoring the electrical plant to a normal shutdown lineup. | Decay heat is being removed to the main condenser via the turbine bypass valves. Reactor level is being maintained using the motor driven reactor feedpump. No SRVs lifted during the transient. Licensee is in progress of restoring the electrical plant to a normal shutdown lineup. |
Latest revision as of 21:15, 1 March 2018
Where | |
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Clinton Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-2.32 h-0.0967 days <br />-0.0138 weeks <br />-0.00318 months <br />) | |
Opened: | Mike Reandeau 01:48 Feb 11, 2008 |
NRC Officer: | Jeff Rotton |
Last Updated: | Feb 13, 2008 |
43976 - NRC Website
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