ENS 49958
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ENS Event | |
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00:42 Mar 26, 2014 | |
Title | |
Event Description | The plant was stable at 85 percent power when off-gas flow started lowering. The operating crew entered the loss of vacuum off-normal procedure and commenced an emergency power reduction to attempt to slow/halt the loss of vacuum while attempting various prescribed actions in the off-normal procedure. When vacuum reached 24 in. Hg, a rapid plant shutdown was performed as prescribed in the off-normal procedure. Power was at 46 percent when a rapid plant shutdown was commenced with the mode switch placed in shutdown at 1942 CDT. All control rods fully inserted on the scram, no emergency core cooling system injected or was required, no safety/relief valve(s) lifted and all systems responded as expected on the scram. The plant will remain in mode 3 with normal makeup from the feedwater system and pressure control on the turbine bypass valves with the main condenser available as a heat sink. All vital and non-vital electrical busses are powered from reserve off-site sources and no emergency diesel generators started on the scram. The cause of the loss of vacuum is under investigation.
The licensee notified the NRC Resident Inspector. |
Where | |
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Clinton ![]() Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1.97 h-0.0821 days <br />-0.0117 weeks <br />-0.0027 months <br />) | |
Opened: | Dan Hunt 22:44 Mar 25, 2014 |
NRC Officer: | Donald Norwood |
Last Updated: | Mar 25, 2014 |
49958 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (46 %) |
After | Hot Shutdown (0 %) |
WEEKMONTHYEARENS 563282023-02-01T05:43:0001 February 2023 05:43:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Scram Due to Turbine Trip ENS 541972019-08-03T07:26:0003 August 2019 07:26:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge En Revision Imported Date 8/7/2019 ENS 536982018-10-28T05:00:00028 October 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram During a Reactor Shutdown ENS 531102017-12-09T19:48:0009 December 2017 19:48:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Manual Reactor Scram Due to Loss of Division 1 Ac Power to Numerous Components ENS 528002017-06-11T03:56:00011 June 2017 03:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Loss of Feedwater Heating ENS 527772017-05-31T01:38:00031 May 2017 01:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram ENS 499582014-03-26T00:42:00026 March 2014 00:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Loss of Condenser Vacuum ENS 496322013-12-13T23:57:00013 December 2013 23:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Feed Pump Swap ENS 496172013-12-09T02:27:0009 December 2013 02:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material Manual Scram Due to Loss of Division 1 480 Vac Power Causing Loss of Instrument Air to Containment and Scram Air Header ENS 489742013-04-26T13:55:00026 April 2013 13:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Rapidly Decreasing Level in the Ehc Oil Reservoir ENS 488122013-03-07T13:56:0007 March 2013 13:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram on Generator Trip/Turbine Trip ENS 474892011-11-29T23:28:00029 November 2011 23:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit Experienced an Automatic Reactor Scram During a Planned Shutdown ENS 454332009-10-15T10:37:00015 October 2009 10:37:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Reactor Recirculation Pump Trip ENS 439762008-02-11T04:07:00011 February 2008 04:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Scram Due to Increasing Reactor Vessel Level ENS 428072006-08-27T22:05:00027 August 2006 22:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Trip Due to Reactor High Water Level ENS 424302006-03-20T10:53:00020 March 2006 10:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Main Turbine Trip Caused Reactor Scram ENS 408682004-07-13T21:10:00013 July 2004 21:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to Possible Adverse Weather ENS 406042004-03-23T01:31:00023 March 2004 01:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Reactor Scram from 93% Power Due to Generator Trip ENS 403682003-12-02T22:58:0002 December 2003 22:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram Due to Low Reactor Water Feed Pump Suction Pressure 2023-02-01T05:43:00 | |
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