ML18347B207: Difference between revisions
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{{#Wiki_filter:consumers Power company | {{#Wiki_filter:consumers | ||
* Power company General Offices: 212 West Michigan Ave.nue, Jackson, Michigan 49201 | |||
* Area Code 517 788-0550 June 19, 1980 Mr James G Keppler Office of Inspection and Enforcement Region III U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 -LICENSE DPR | * Area Code 517 788-0550 June 19, 1980 Mr James G Keppler Office of Inspection and Enforcement Region III U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LICENSEEE EVENT REPORT 80-018 - SNUBBER FAILURE On the reverse side is Licensee Event Report 80-018 which is reportable under Technical Specification 6.9.2.B.2. | ||
Rog Senior Licensing Engineer CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector | Rog Senior Licensing Engineer CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector - Palisades | ||
-Palisades | :JUN 2 3 1880 | ||
:JUN 2 3 1880 PALISATIES PLANT NRC FORM 366 | |||
I During routine testing of hydraulic snubbers, the oil level in snubber- | PALISATIES PLANT NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7*771 LICENSEE EVENT REPORT CONTROL BLOCK: I I G) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6 | ||
Event reportable per T.S. 6.9.2.B.2 and 3.20. See LER I 80-14 thru 80-16 for similar occurrences. | [£:EJ I Ml IIPI AIL 111010 I 01- p 10 10 I 010 1-10101014 11111111101 7 B 9 LICENSEE CODE 14 ~5 LICENSE NUMBER 25 26 LICENSE TYPE 30. : 57 CAT 58 I 10 CON'T ITiiJ ~~~~~ L..!:JG) I o I 5 J o I o Io I 2 I 51 51(?)1 o I 5 12 12 I 8 I oKV I oI 61 1 19 I 8 I o IG) 7 B 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@ | ||
SYSTEr-...-. | -... [ill] I During routine testing of hydraulic snubbers, the oil level in snubber- | ||
~ I No. 2 was found to be less than zero, and the snubber was declared | |||
r::;::;., ATTACHMENT NPRD-< ON PLANT METHOD HOURS SUBMITTED FORM ,UB. | ~ inoperable. Event reportable per T.S. 6.9.2.B.2 and 3.20. See LER | ||
W@ W I o I 01 o I | ~ I 80-14 thru 80-16 for similar occurrences. | ||
The snubber o::ID jwill be disassembled to confirm the cause. ITEl 1 e 80 F,_C1L1-:-Y f:jQ\ STATUS 'i. POWER OTHER STATUS GE l.£l@ I b I 0 I 01@ ..... I | 80 SYSTEr-...-. CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCDDE SUB CODE I H1B I@ ~@) L1LJ@ Is I u IP Jo IR I Tl@ QLl@ Ll.J@ | ||
___ | 9 10 11 12 13 16 19 20 SEQUENTIAL OCCUR REN CE REPORT REVISION Q LEF.IRO CVENT YEAR REPORT NO. CODE TYPE ND. | ||
v REPORT NUMBER I 8 I 0I I I 10 111 81 1,..,...1 Io 13 I Li l.=l LQJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDDWt< r::;::;., ATTACHMENT NPRD-< PRIME COMP. COMPONENT TAKEN ACTI0'-1 ON PLANT METHOD HOURS ~ SUBMITTED FORM ,UB. SUPPLIER MANUFACTURER l.IJ@l.2.J@) | |||
33 3* | |||
(.;;;\ NUMBEP. (.;::;\TYPE DESCRIPTION DJ2J I 0 I 01 0 | W@ | ||
35 W I o I 36 37 01 o I o40I LIU@ 41 Lll§ 42 | |||
~@) | |||
[2JZ] I 01 OIOl@)L- | 43 IB 1211 10 47 | ||
7 B 9 11 12 ao LOSS Q< OR DAMAGE TO FACILITY 0 TYPE DESCRIPTION GTIJ U_j@ NA 7 B 9 10 so PUBLICITY r,;-.. NRC USE ONLY ISSUEDQ LN..16......._ | ' | ||
CAUSE DESCRIPTION AND CORR EC rive ACTIONS @ | |||
II II I I I I I I I I I 8 9 10 68 65 BO}} | [II§] 1The cause of fluid leakage is apparent seal degradation. The snubber o::ID jwill be disassembled to confirm the cause. | ||
ITEl 1 e 80 F,_C1L1-:-Y f:jQ\ METHOD OF r::;::;., | |||
STATUS 'i. POWER OTHER STATUS ~ DISCOVERY DISCOVERY DESCRIPTION '2Y GE l.£l@ I b I 0 I 01@I....._N_A_ _ _ ___. ~'2J>~I~S_u_rv~_e_i_l_l_a_n_c_e~T_e_s_t~~~~~~~~--' | |||
B 9 10 12 13 45 46 80 ACTIVITY C:JNTENT (.;.;\ | |||
RELEASED OF RELEASE AMONUl'jT OF ACTIVITY~ LOCATIOt< OF RELEASE @ | |||
8IJ ~@) ~@.._I_ _ _A_ _ _ ___, NA a 9 10 11 45 BO PERSONNEL EXPOSURES (.;;;\ | |||
NUMBEP. (.;::;\TYPE DESCRIPTION DJ2J I 0 I 01 0 '~@.___NA_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___. | |||
7 B 9 11 12 13 80 PERSONNEL INJURIES Q NUMBER DESCRIPTION~ | |||
[2JZ] I 01 OIOl@)L-_ _ _N_A_ _ _ _ _ _ _ _ _ _ _~----------~ | |||
7 B 9 11 12 ao LOSS Q< OR DAMAGE TO FACILITY 0 TYPE DESCRIPTION ~ | |||
GTIJ U_j@ NA 7 B 9 10 so PUBLICITY r,;-.. NRC USE ONLY ISSUEDQ DESCRIPTION~ | |||
~ LN..16.......__ _ _ _ __...N=----------------~ II II I I I I I I I I I 8 9 10 68 65 BO}} |
Revision as of 09:03, 20 October 2019
ML18347B207 | |
Person / Time | |
---|---|
Site: | Palisades |
Issue date: | 06/19/1980 |
From: | Huston R Consumers Power Co |
To: | James Keppler NRC/IE, NRC/RGN-III |
References | |
LER 80-018 | |
Download: ML18347B207 (2) | |
Text
consumers
- Area Code 517 788-0550 June 19, 1980 Mr James G Keppler Office of Inspection and Enforcement Region III U S Nuclear Regulatory Commission 799 Roosevelt Road Glen Ellyn, IL 60137 DOCKET 50-255 - LICENSE DPR PALISADES PLANT - LICENSEEE EVENT REPORT 80-018 - SNUBBER FAILURE On the reverse side is Licensee Event Report 80-018 which is reportable under Technical Specification 6.9.2.B.2.
Rog Senior Licensing Engineer CC Director, Office of Nuclear Reactor Regulation Director, Office of Inspection and Enforcement NRC Resident Inspector - Palisades
- JUN 2 3 1880
PALISATIES PLANT NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (7*771 LICENSEE EVENT REPORT CONTROL BLOCK: I I G) (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6
[£:EJ I Ml IIPI AIL 111010 I 01- p 10 10 I 010 1-10101014 11111111101 7 B 9 LICENSEE CODE 14 ~5 LICENSE NUMBER 25 26 LICENSE TYPE 30. : 57 CAT 58 I 10 CON'T ITiiJ ~~~~~ L..!:JG) I o I 5 J o I o Io I 2 I 51 51(?)1 o I 5 12 12 I 8 I oKV I oI 61 1 19 I 8 I o IG) 7 B 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE BO EVENT DESCRIPTION AND PROBABLE CONSEQUENCES@
-... [ill] I During routine testing of hydraulic snubbers, the oil level in snubber-
~ I No. 2 was found to be less than zero, and the snubber was declared
~ inoperable. Event reportable per T.S. 6.9.2.B.2 and 3.20. See LER
~ I 80-14 thru 80-16 for similar occurrences.
80 SYSTEr-...-. CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCDDE SUB CODE I H1B I@ ~@) L1LJ@ Is I u IP Jo IR I Tl@ QLl@ Ll.J@
9 10 11 12 13 16 19 20 SEQUENTIAL OCCUR REN CE REPORT REVISION Q LEF.IRO CVENT YEAR REPORT NO. CODE TYPE ND.
v REPORT NUMBER I 8 I 0I I I 10 111 81 1,..,...1 Io 13 I Li l.=l LQJ 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDDWt< r::;::;., ATTACHMENT NPRD-< PRIME COMP. COMPONENT TAKEN ACTI0'-1 ON PLANT METHOD HOURS ~ SUBMITTED FORM ,UB. SUPPLIER MANUFACTURER l.IJ@l.2.J@)
33 3*
W@
35 W I o I 36 37 01 o I o40I LIU@ 41 Lll§ 42
~@)
43 IB 1211 10 47
'
CAUSE DESCRIPTION AND CORR EC rive ACTIONS @
[II§] 1The cause of fluid leakage is apparent seal degradation. The snubber o::ID jwill be disassembled to confirm the cause.
ITEl 1 e 80 F,_C1L1-:-Y f:jQ\ METHOD OF r::;::;.,
STATUS 'i. POWER OTHER STATUS ~ DISCOVERY DISCOVERY DESCRIPTION '2Y GE l.£l@ I b I 0 I 01@I....._N_A_ _ _ ___. ~'2J>~I~S_u_rv~_e_i_l_l_a_n_c_e~T_e_s_t~~~~~~~~--'
B 9 10 12 13 45 46 80 ACTIVITY C:JNTENT (.;.;\
RELEASED OF RELEASE AMONUl'jT OF ACTIVITY~ LOCATIOt< OF RELEASE @
8IJ ~@) ~@.._I_ _ _A_ _ _ ___, NA a 9 10 11 45 BO PERSONNEL EXPOSURES (.;;;\
NUMBEP. (.;::;\TYPE DESCRIPTION DJ2J I 0 I 01 0 '~@.___NA_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___.
7 B 9 11 12 13 80 PERSONNEL INJURIES Q NUMBER DESCRIPTION~
[2JZ] I 01 OIOl@)L-_ _ _N_A_ _ _ _ _ _ _ _ _ _ _~----------~
7 B 9 11 12 ao LOSS Q< OR DAMAGE TO FACILITY 0 TYPE DESCRIPTION ~
GTIJ U_j@ NA 7 B 9 10 so PUBLICITY r,;-.. NRC USE ONLY ISSUEDQ DESCRIPTION~
~ LN..16.......__ _ _ _ __...N=----------------~ II II I I I I I I I I I 8 9 10 68 65 BO