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              y                                     UsesTSO STATSS
y
      '    f                           NUCLEAR REGULATORY COMMISSHM
UsesTSO STATSS
    .
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          f                                             Reescos as
NUCLEAR REGULATORY COMMISSHM
          g                                   tel e4ARIETTA STREET.N.W.
'
          *
f
                                              ATLANTA.G80A41A 30333
Reescos as
          *$
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              .....
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                                '
tel e4ARIETTA STREET.N.W.
                              .
*
          Report Nos.: 50-280/06-42 and 50-281/86-42
ATLANTA.G80A41A 30333
          Licensee: Virgirtia Electric and Power C'ompany
*$
                    Richmond, VA 23261
.....
          Docket Nos.: 50-280 and 50-281                           License Nos.: DPR-32 and DPR-37
'
          Facility Name: Surry 1 and 2
.
          Inspection Conducted: December 9,1986 - January 14, 1987
Report Nos.: 50-280/06-42 and 50-281/86-42
          Team Inspectors:   J. Caldwell
Licensee: Virgirtia Electric and Power C'ompany
                              M. A. Caruso
Richmond, VA 23261
                              W. T. Cooper
Docket Nos.: 50-280 and 50-281
                              8. R. Crowley
License Nos.:
                              J. T. Gilliland
DPR-32 and DPR-37
                              W. E. Holland
Facility Name: Surry 1 and 2
                              T. A. Peebles
Inspection Conducted: December 9,1986 - January 14, 1987
                              P. A. Taylor
Team Inspectors:
          Contributing Inspectors:     A. R. Herdt
J. Caldwell
                                      J. D. Ennis
M. A. Caruso
                                      P. M. Mad n
W. T. Cooper
                                      W. Ros
8. R. Crowley
          Approved by: _mm                  I /L n s
J. T. Gilliland
                      Vincent W. Panciera, Team ~ Lea' der'
W. E. Holland
                                                                    h ~
T. A. Peebles
                                                                                      a ~
P. A. Taylor
                                                                                              7
Contributing Inspectors:
                                                                                    /Date Sigried
A. R. Herdt
                      Division of Reactor Safety
J. D. Ennis
                                                      SL)l9tARY
P. M. Mad n
          Scope: This special, announced augmented inspection was conducted for the Surry
W. Ros
          Unit 2 feedwater pipe rupture event of December 9,1986. The areas inspected
Approved by:
          included the sequence of events, effects of failure, metallurgical aspects, items
I /L n s h
          contributing to the likelihood or severity of the event, licensee's response to
a
          the event, aspects that made handling the event more difficult, consideration of
7
          shutdown of Unit 1, investigation and corrective actions planned and safety
_mm
          considerations for station restart.
Vincent W. Panciera, Team ~ Lea' der'
          Results: One violation was identified (paragraph 11.a.(2)).
~
                                                                            .
/Date Sigried
                                                                    '
~
          0,g22Kg[[{ $$$$ go
Division of Reactor Safety
  -
SL)l9tARY
          o
Scope: This special, announced augmented inspection was conducted for the Surry
Unit 2 feedwater pipe rupture event of December 9,1986. The areas inspected
included the sequence of events, effects of failure, metallurgical aspects, items
contributing to the likelihood or severity of the event, licensee's response to
the event, aspects that made handling the event more difficult, consideration of
shutdown of Unit 1, investigation and corrective actions planned and safety
considerations for station restart.
Results: One violation was identified (paragraph 11.a.(2)).
.
0,g22Kg[[{ $$$$
go
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                                          REPORT DETAILS
REPORT DETAILS
                            .
.
        1. Persons Contacted
1.
                                                '
Persons Contacted
            Licensee Employees
'
            W. L. Stewart, Vice President, Nuclear Operations
Licensee Employees
            R. J. Hardwick, Corporate Manager for Licensing and Safety
W. L. Stewart, Vice President, Nuclear Operations
            R. F. Saunders, Surry Station Manager
R. J. Hardwick, Corporate Manager for Licensing and Safety
          *R. W. Calder, Nuclear Engineering Manager
R. F. Saunders, Surry Station Manager
          "H. L. Miller, Assistant Station Manager for Licensing and Safety
*R. W. Calder, Nuclear Engineering Manager
          *D. L. Benson, Assistant Station Manager for Operations and Maintenance
"H. L. Miller, Assistant Station Manager for Licensing and Safety
            J. M. McAvoy, System Metallurgist
*D. L. Benson, Assistant Station Manager for Operations and Maintenance
          *W. D. Craft, Licensing Coordinator
J. M. McAvoy, System Metallurgist
          *W. R. Benthall, Nuclear Specialist
*W. D. Craft, Licensing Coordinator
            Other licensee employees contacted included engineers, technicians,
*W. R. Benthall, Nuclear Specialist
            operators, mechanics, security members and office personnel.
Other licensee employees contacted included engineers, technicians,
            NRC Residen' Inspector
operators, mechanics, security members and office personnel.
          *W. Holland
NRC Residen' Inspector
          * Attended exit interview.
*W. Holland
                                                                                        .
* Attended exit interview.
        2. Exit Interview
.
            The inspection scope and findings were summarized on January 14, 1987, with
2.
            those persons indicated in paragraph 1 above. The inspectors described
Exit Interview
            the areas inspected and discussed in detail the inspection findings listed
The inspection scope and findings were summarized on January 14, 1987, with
            below.   No dissenting comments were received from the licensee.
those persons indicated in paragraph 1 above.
            Violation 50-281/86-42-02 - Inadequate Procedure for the Maintenance of the
The inspectors described
            Main Steam Trip Valve (paragraph 11.a.(2)).
the areas inspected and discussed in detail the inspection findings listed
                                                        ~
below.
            Inspector Followup Item 50-280, 281/86-42-01 - Clarification of Surface
No dissenting comments were received from the licensee.
            Preparation Methods in NOE Procedures (paragraph 8.e.).
Violation 50-281/86-42-02 - Inadequate Procedure for the Maintenance of the
            The licensee did not identify as proprietary any of the material provided
Main Steam Trip Valve (paragraph 11.a.(2)).
            to or reviewed by the inspectors during this inspection.
~
        3.   Licensee Action on Previous Enforcement Matters
Inspector Followup Item 50-280, 281/86-42-01 - Clarification of Surface
            This subject was not addressed in the inspection.
Preparation Methods in NOE Procedures (paragraph 8.e.).
        4. Unresolved Items
The licensee did not identify as proprietary any of the material provided
            Unresolved items were not identified during the inspection.
to or reviewed by the inspectors during this inspection.
L                                                         .-
3.
                    4
Licensee Action on Previous Enforcement Matters
                                                                                    0
This subject was not addressed in the inspection.
                              .
4.
Unresolved Items
Unresolved items were not identified during the inspection.
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      .     . ~ . --       .   --   .-       . _ _ - - _.- _   . . _ _ - -   . - . - _ _ _ -   - - ..   -
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                    5. Augmented Inspection Team (AIT) Activities
5.
:                     Shortly after the pipe rupture event, Region II was notified by the Surry
Augmented Inspection Team (AIT) Activities
                      Senior Resident Inspector (SRI) who was on site, and had proceeded to the
:
Shortly after the pipe rupture event, Region II was notified by the Surry
Senior Resident Inspector (SRI) who was on site, and had proceeded to the
y
y
                      control roong to assess the situation. The Regional personnel immediately
control roong to assess the situation. The Regional personnel immediately
1                     staffed the regional response center at about 2:45 p.m. NRC Headquarters
1
                      was then notified at approximately 3:00 p.m. that a main feedwater line pipe
staffed the regional response center at about 2:45 p.m.
                      rupture in the turbine building had occurred. An open line between the
NRC Headquarters
                      Surty site and the NRC Operations Center was maintained until early hours
was then notified at approximately 3:00 p.m. that a main feedwater line pipe
,                      of the next morning. About 3:30 p.m., a decision was made by Regional
rupture in the turbine building had occurred. An open line between the
;                     management to send an inspection team to the site. This team consisted of
Surty site and the NRC Operations Center was maintained until early hours
{                     Regional based personnel and the SRIs from North Anna and Surry. The team
of the next morning. About 3:30 p.m., a decision was made by Regional
,
;
management to send an inspection team to the site. This team consisted of
{
Regional based personnel and the SRIs from North Anna and Surry. The team
arrived on site about 9:30 p.m. on December 9, 1986. After a meeting with
:
:
                      arrived on site about 9:30 p.m. on December 9, 1986. After a meeting with
j
j                      plant management to assess the operational status of the unit, the team
plant management to assess the operational status of the unit, the team
!                     toured the damaged area of the turbine building in the vicinity of the feed-
!
l                     pump suction piping. During a meeting at 9:00 a.m. on December 10, 1986,
toured the damaged area of the turbine building in the vicinity of the feed-
                      with plant management, NRC inspection assignments were outlined. Virginia
l
pump suction piping.
During a meeting at 9:00 a.m. on December 10, 1986,
with plant management, NRC inspection assignments were outlined.
Virginia
Power agreed to provide any assistance required by the team.
In addition,
4
4
                      Power agreed to provide any assistance required by the team. In addition,
l
l                      the ground rules to be applied by the inspection team regarding quarantine
the ground rules to be applied by the inspection team regarding quarantine
!                     of equipment were discussed. Virginia Power agreed to seek NRC concurrence
!
of equipment were discussed. Virginia Power agreed to seek NRC concurrence
!
before any work was accomplished for restoration of systems. During the
'
morning of December 10, 1986, the team's status was upgraded to an Augmented
!
Inspection Team (AIT), and an engineer from the Office of Nuclear Reactor
l
Regulation, knowledgeable in water hammer phenomena, was assigned to the
l
team. The team conducted inspections during the remainder of the week
1
ending December 12, 1986, to ascertain the circumstances involved in the
j
accident. An executive summary was transmitted to the Region II office on
l
December 17, 1986.
This summary provided the significant facts concerning
:
the event. The AIT did not conclude its inspection at that time due to the
!
!
'                      before any work was accomplished for restoration of systems. During the
ongoing activities by the licensee to develop a root cause analysis, which
                      morning of December 10, 1986, the team's status was upgraded to an Augmented
I
!                      Inspection Team (AIT), and an engineer from the Office of Nuclear Reactor
required subsequent inspection activities. AIT activities continued during
l                      Regulation, knowledgeable in water hammer phenomena, was assigned to the
!
l                      team. The team conducted inspections during the remainder of the week
the weeks of December 22 and 29, 1986, and January 12, 1987. An AIT exit
1                      ending December 12, 1986, to ascertain the circumstances involved in the
l
j                      accident. An executive summary was transmitted to the Region II office on
meeting with plant management was held on January 14, 1987, after review of
l                      December 17, 1986.    This summary provided the significant facts concerning
:
:                      the event. The AIT did not conclude its inspection at that time due to the
the licensee's investigative report entitled "Surry Unit 2 Reactor Trip and
!                      ongoing activities by the licensee to develop a root cause analysis, which
!
I                     required subsequent inspection activities. AIT activities continued during
Feedwater Pipe Failure Report" and proposed corrective actions which were
!                     the weeks of December 22 and 29, 1986, and January 12, 1987. An AIT exit
j
l                     meeting with plant management was held on January 14, 1987, after review of
presented to the NRC on January 12, 1987,
:                     the licensee's investigative report entitled "Surry Unit 2 Reactor Trip and
in addition to the AIT inspection
!                     Feedwater Pipe Failure Report" and proposed corrective actions which were
i
j                     presented to the NRC on January 12, 1987, in addition to the AIT inspection
activities, inspectors knowledgeable in security, fire protection systems,
i                     activities, inspectors knowledgeable in security, fire protection systems,
l
l                     water chemistry and check valve design were assigned to review specific
water chemistry and check valve design were assigned to review specific
!                     concerns in these areas. Where applicable, their inspection findings have
!
i                     been incorporated into this AIT inspection report.
concerns in these areas. Where applicable, their inspection findings have
i
been incorporated into this AIT inspection report.
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t
6.
Overview of the Event
,
,
                  6.  Overview of the Event                                                      .
.
;
;
                      On December 9, 1986, with both units operating at 100 percent reactor power,
On December 9, 1986, with both units operating at 100 percent reactor power,
!                     a Unit 2 reactor trip followed by a main feedwater (MFW) line rupture
!
a Unit 2 reactor trip followed by a main feedwater (MFW) line rupture
:
:
                      occurred. Unit 2 had completed a refueling outage and returned to full
occurred. Unit 2 had completed a refueling outage and returned to full
I                     power operation on December 8, 1986.
I
!                     A low-low level in the C Steam Generator ($/G) caus6d a reactor trip and
power operation on December 8, 1986.
l                     start of the two motor driven auxiliary feedwater pumps.
!
                                                                              .'
A low-low level in the C Steam Generator ($/G) caus6d a reactor trip and
  e
l
                                                                                                          '
start of the two motor driven auxiliary feedwater pumps.
                                                                                                        . .
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The control room operators noted the S/G code safety valves lifting and
regulated S/G pressure through the atmospheric dump valves. Approximately
30 seconds after the trip the unit's electrical busses auto-transferred to
offsite power. A small steam release noise was heard followed by a very
loud noise approximately five seconds later.
A shift supervisor who was in the turbine building, realizing that a large
steam break had occurred, went to the control room and alerted the control
room watch. All secondary pumps (high pressure drain, condensate and main
feedwater) were secured, and the break was isolated. Water to the S/GS was
supplied by the auxiliary feedwater system.
The primary systems responded normally to the loss of load transient.
Reactor coolant temperature, pressure, and pressurizer level were stabilized
in the desired band.
A notification of unusual event was declared by the licensee at 2:27 p.m.
and was upgraded later to an ALERT in order to ensure accountability of all
station personnel.
The 18-inch suction line to the A main feedwater pump was subsequently
found to have ruptured at the elbow where the line connects to the 24-inch
condensate header.
In addition, station halon and cardox systems actuated because of water
short-circuiting control systems in the area. Control room habitability
was a concern prior to initiating control room ventilation because doors
were blocked open to allow better control room access without recognizing
that carbon dioxide had been discharged in the areas above. The carbon
dioxide was apparently coming into the control room from the hallway.
The
emergency was terminated at 4:23 p.m. after personnel accountability had
been established.
Eight individuals were injured due to the steam and water.
Four of the
injured subt.equently died. Two of the injured were treated and released.
Two individuals remained hospitalized. One, individual was later released.
Unit 2 was placed in cold shutdown at 7:04 a.m. hours on December 10, 1986.
7.
Sequence of Events
a.
Initial Plant Conditions Prior to the Unit 2 Event
Unit 2 had achieved stable 100 percent power operation on December 8,
1986, following a refueling outage.
Unit 1 was operating at 100
percent power.
Two major maintenance or surveillance activities were in progress:
the troubleshootin
coolant pump (RCP)g of a B train underfrequendy relay for a reactor
breaker, and the troubleshooting of an aux 111ary
.
.
,
!
9
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.
  .
e                                            3
        The control room operators noted the S/G code safety valves lifting and
        regulated S/G pressure through the atmospheric dump valves. Approximately
        30 seconds after the trip the unit's electrical busses auto-transferred to
        offsite power. A small steam release noise was heard followed by a very
        loud noise approximately five seconds later.
        A shift supervisor who was in the turbine building, realizing that a large
        steam break had occurred, went to the control room and alerted the control
        room watch. All secondary pumps (high pressure drain, condensate and main
        feedwater) were secured, and the break was isolated. Water to the S/GS was
        supplied by the auxiliary feedwater system.
        The primary systems responded normally to the loss of load transient.
        Reactor coolant temperature, pressure, and pressurizer level were stabilized
        in the desired band.
        A notification of unusual event was declared by the licensee at 2:27 p.m.
        and was upgraded later to an ALERT in order to ensure accountability of all
        station personnel.
        The 18-inch suction line to the A main feedwater pump was subsequently
        found to have ruptured at the elbow where the line connects to the 24-inch
        condensate header.
        In addition, station halon and cardox systems actuated because of water
        short-circuiting control systems in the area. Control room habitability
        was a concern prior to initiating control room ventilation because doors
        were blocked open to allow better control room access without recognizing
        that carbon dioxide had been discharged in the areas above. The carbon
        dioxide was apparently coming into the control room from the hallway. The
        emergency was terminated at 4:23 p.m. after personnel accountability had
        been established.
        Eight individuals were injured due to the steam and water. Four of the
        injured subt.equently died. Two of the injured were treated and released.
        Two individuals remained hospitalized. One, individual was later released.
        Unit 2 was placed in cold shutdown at 7:04 a.m. hours on December 10, 1986.
      7. Sequence of Events
        a.    Initial Plant Conditions Prior to the Unit 2 Event
              Unit 2 had achieved stable 100 percent power operation on December 8,
              1986, following a refueling outage. Unit 1 was operating at 100
              percent power.
              Two major maintenance or surveillance activities were in progress:
              the troubleshootin
              coolant pump (RCP)g    of a B
                                  breaker,  train
                                            and  theunderfrequendy
                                                    troubleshooting ofrelay for 111ary
                                                                        an aux  a reactor
                                                          .                  .
                                                        ,
                !
                                                                                        9
                                                                                          .


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                                        4
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        instrument air ccepressor. The first item had required the racking
instrument air ccepressor. The first item had required the racking
        in and closing of the B reactor trip bypass breaker. The A and B
in and closing of the B reactor trip bypass breaker. The A and B
        reactor trip breakers were still closed. The second item required
reactor trip breakers were still closed. The second item required
        the shutdown of the running auxiliary instrument air compressor and the
the shutdown of the running auxiliary instrument air compressor and the
        attempted start of the non-running auxiliary instrument air compressor.
attempted start of the non-running auxiliary instrument air compressor.
        The delay in starting the auxiliary instrument air compressor caused
The delay in starting the auxiliary instrument air compressor caused
        the instrument air pressure to decrease to approximately 78 psig,
the instrument air pressure to decrease to approximately 78 psig,
        instead of the normal 100 psig.
instead of the normal 100 psig.
        Some minor construction activity was occurring in the vicinity of the
Some minor construction activity was occurring in the vicinity of the
        main feedwater (MFW) pumps, such as installing insulation on piping.
main feedwater (MFW) pumps, such as installing insulation on piping.
        The unit's data gathering computer (Prodac 250) was out of service,
The unit's data gathering computer (Prodac 250) was out of service,
        but reactor trip information was available from a sequence of events
but reactor trip information was available from a sequence of events
        (SOE) alarm printer and a newly installed Emergency Response Facility
(SOE) alarm printer and a newly installed Emergency Response Facility
        Computer (ERFC). The SOE alarm printer prints information continuously
Computer (ERFC).
        on a millisecond basis, but is limited in scope to alarms. The ERFC
The SOE alarm printer prints information continuously
        displays s'y stem parameters, but only updates in fifteen second incre-
on a millisecond basis, but is limited in scope to alarms. The ERFC
        ments and samples the parameters at different times. The ERFC is
displays s' stem parameters, but only updates in fifteen second incre-
        intended for a broader picture than the SOE alarm printer. Interviews
y
        with the Shift Supervisor and Control Room Operators (CRO) were used
ments and samples the parameters at different times.
        to correlate times and to fill in gaps of the event.
The ERFC is
        The SOE alarm printer time of the reactor trip was 1420:03(RT00)and
intended for a broader picture than the SOE alarm printer.
        the ERFC time of the reactor trip was between 1421:15-:30 and has been
Interviews
        correlated to be 1421:15. Therefore, the SOE information will be
with the Shift Supervisor and Control Room Operators (CRO) were used
        addressed in increments per the ERFC clock with specifics referred to
to correlate times and to fill in gaps of the event.
        as seconds of time from the RT per the SOE alarm printer.
The SOE alarm printer time of the reactor trip was 1420:03(RT00)and
        Other sequence of events information was developed by the licensee,
the ERFC time of the reactor trip was between 1421:15-:30 and has been
        using security alarm computer data, interviews with additional person-
correlated to be 1421:15. Therefore, the SOE information will be
        nel, and time motion studies. This information correlates with this
addressed in increments per the ERFC clock with specifics referred to
        SOE data.
as seconds of time from the RT per the SOE alarm printer.
      b. Secondary System Conditions Prior To The Event
Other sequence of events information was developed by the licensee,
        Both MFV pumps were operating with a suction pressure of 370 psig, a
using security alarm computer data, interviews with additional person-
        discharge pressure of 1040 psig and a temperature of 374 degrees F.
nel, and time motion studies.
        The condensate system was operating normally with one of two high pres-
This information correlates with this
        sure heater drain pumps, two of two low pressure heater drain pumps,
SOE data.
        and two of three condensate pumps running. The full flow condensate
b.
        polishing system and all feedwater h9aters were in service.       .
Secondary System Conditions Prior To The Event
      c. Plant Conditions and Personnel Actions During The Event
Both MFV pumps were operating with a suction pressure of 370 psig, a
        1421:(00-15) ERFC time
discharge pressure of 1040 psig and a temperature of 374 degrees F.
        The first indication of a problem occurred at RT -03 when the Unit 2
The condensate system was operating normally with one of two high pres-
        control room received an annunciator alarm for!the B steam generator
sure heater drain pumps, two of two low pressure heater drain pumps,
        (S/G) as MFV flow was less than steam flow. This indication and the
and two of three condensate pumps running.
                                                  .'
The full flow condensate
          '
polishing system and all feedwater h9aters were in service.
.
c.
Plant Conditions and Personnel Actions During The Event
1421:(00-15) ERFC time
The first indication of a problem occurred at RT -03 when the Unit 2
control room received an annunciator alarm for!the B steam generator
(S/G) as MFV flow was less than steam flow.
This indication and the
.'
'
.
.
                                                                              O i
O
i


  .'
.'
  ,
5
                                    5
,
    subsequent alarm on the A S/G indicated that the C main steam trip
subsequent alarm on the A S/G indicated that the C main steam trip
    valve (MSTV) had inadvertently closed. The closure of the MSTV caused
valve (MSTV) had inadvertently closed. The closure of the MSTV caused
    the steam flow from the other S/Gs to begin to increase by 50 percent
the steam flow from the other S/Gs to begin to increase by 50 percent
    and caused the mismatch alarm, since the MFW flow to the S/Gs had not
and caused the mismatch alarm, since the MFW flow to the S/Gs had not
    yet responded.                   .
yet responded.
    A direct indication of the C MSTV closing was not received as the
.
    valve-closed limit switches did not function properly. However,
A direct indication of the C MSTV closing was not received as the
    indication and alarm that the valve was not fully open was available to
valve-closed limit switches did not function properly. However,
    the CRO.
indication and alarm that the valve was not fully open was available to
    The closure of the C MSTV caused MFW pressure downstream of the C MFW
the CRO.
    flow control valve (FCV) to increase from 865 psig to 970 psig with
The closure of the C MSTV caused MFW pressure downstream of the C MFW
    the A and B MFW pressures initially stable at 845 and 835 psig,
flow control valve (FCV) to increase from 865 psig to 970 psig with
    respectively..                                                         -
the A and B MFW pressures initially stable at 845 and 835 psig,
    The other steam generator MSTVs closed shortly afterward due to the
respectively..
    higher than normal steam flow in those lines caused by the continuing
-
    100 percent demand of the main turbine. The MSTVs are reverse seated
The other steam generator MSTVs closed shortly afterward due to the
    check valves held open against the steam flow by air operated pistons.
higher than normal steam flow in those lines caused by the continuing
    As the MSTV discs are partially in the steam flow path, an increase
100 percent demand of the main turbine. The MSTVs are reverse seated
    in steam flow places more closing force on the disc. All three MSTVs
check valves held open against the steam flow by air operated pistons.
    closed and seated properly and steam flow was stopped.
As the MSTV discs are partially in the steam flow path, an increase
    1421:(15-30)
in steam flow places more closing force on the disc. All three MSTVs
    A low-low S/G 1evel annunciator signal which was received for C S/G and
closed and seated properly and steam flow was stopped.
    was the initiating signal for the reactor trip at 1421:15 (RT 00) and
1421:(15-30)
    for the starting of the two motor driven auxiliary feedwater pumps.
A low-low S/G 1evel annunciator signal which was received for C S/G and
    The reactor trip resulted in a trip of the main turbine generator. The
was the initiating signal for the reactor trip at 1421:15 (RT 00) and
    stopping of steam flow to the main turbine by the MSTVs closing caused
for the starting of the two motor driven auxiliary feedwater pumps.
    the S/G pressures to increase. As C MSTV had closed first, its pres-
The reactor trip resulted in a trip of the main turbine generator.
    sure increased first. This increase in pressure collapsed the bubbles
The
    in its S/G which caused the level to decrease to the reactor trip low-
stopping of steam flow to the main turbine by the MSTVs closing caused
    Iow level setpoint.
the S/G pressures to increase. As C MSTV had closed first, its pres-
    At RT +03, the CR0 manually tripped th'e reactor. One control rod
sure increased first. This increase in pressure collapsed the bubbles
    (M-10) indicated that it had inserted from 228 steps to 35 steps.
in its S/G which caused the level to decrease to the reactor trip low-
    Reactor power was verified to have decreased to normal post-trip decay
Iow level setpoint.
At RT +03, the CR0 manually tripped th'e reactor. One control rod
(M-10) indicated that it had inserted from 228 steps to 35 steps.
Reactor power was verified to have decreased to normal post-trip decay
l
l
    values.
values.
    At RT +04, the CRO, noting that the S/G code safety valves were
At RT +04, the CRO, noting that the S/G code safety valves were
    lif ting, took the S/G Power Operated Relief Valves (PORV) out of manual
lif ting, took the S/G Power Operated Relief Valves (PORV) out of manual
    and began to regulate S/G pressure through this atmospheric dump mode.
and began to regulate S/G pressure through this atmospheric dump mode.
    S/G pressures had increased from their initta) values of 820, 814 and
S/G pressures had increased from their initta) values of 820, 814 and
!
!
I
1
1
                                                    I
i
i                                              *               .
*
                                              ,
.
                                                                          '
,
!
!
l                                                                             -
'
l
-


                  ~
~
              .
.
                .
.
              -
6
                                                                                      6
-
                                                      815 psig and were 936, 979, and 1055 psig.* The S/G pressures all
815 psig and were 936, 979, and 1055 psig.* The S/G pressures all
                                                        responded to the individual MSTV closings, and since C MSTV had been
responded to the individual MSTV closings, and since C MSTV had been
                                                      closed longest, it caused the C S/G to reach the highest pressure.
closed longest, it caused the C S/G to reach the highest pressure.
                                                        The AFW flows were greatest to the S/G with the least pressure. AFW
The AFW flows were greatest to the S/G with the least pressure. AFW
                                                        flow was 344, 300 and 98 gpa.   .
flow was 344, 300 and 98 gpa.
                                                        Pressure downstream of the MFW FCVs increased to 1054, 1042 and
.
                                                        1090 psig.
Pressure downstream of the MFW FCVs increased to 1054, 1042 and
                                                        1421:(30 -45)
1090 psig.
                                                        Pressure downstream of the MFW FCVs decreased to 1008, 1015 and
1421:(30 -45)
                                                        1028 psig. S/G pressures were 1028, 1013, and 1055 psig. The C S/G
Pressure downstream of the MFW FCVs decreased to 1008, 1015 and
                                                        PORV was being used to control primary temperature and C S/G pressure
1028 psig. S/G pressures were 1028, 1013, and 1055 psig. The C S/G
                                                        remained constant.
PORV was being used to control primary temperature and C S/G pressure
                                                        Low-low levels occurred in the A and B S/Gs in response to their
remained constant.
                                                        increasing pressure which caused the automatic initiation of the third
Low-low levels occurred in the A and B S/Gs in response to their
                                                        auxiliary feedwater pump. The steam inlet valve to the turbine driven
increasing pressure which caused the automatic initiation of the third
                                                        auxiliary feedwater pump opened and the pump started. S/G 1evels as
auxiliary feedwater pump.
                                                      a percent of wide range instrumentation were 74, 73 and 75 versus
The steam inlet valve to the turbine driven
                                                        a normal operating level of 84 percent. AFW flow was 337, 317 and
auxiliary feedwater pump opened and the pump started.
                                                        109 gpm.
S/G 1evels as
                                                        1421:(45-1422:00)                                                                     .
a percent of wide range instrumentation were 74, 73 and 75 versus
                                                        The three MFW FCVs received an automatic signal to close and in a few
a normal operating level of 84 percent. AFW flow was 337, 317 and
                                                        seconds were closed. This signal is generated to minimize primary
109 gpm.
                                                        system cooldown following a reactor trip and is generated when the
1421:(45-1422:00)
                                                        primary temperature decreases to less than 554 degrees F. The MFW pump
.
                                                        recirculation valves (FCV-FW-250A and 2508) for A and 8 MFW pumps auto-
The three MFW FCVs received an automatic signal to close and in a few
                                                      opened a few seconds later. Each recire valve opens when flow from its
seconds were closed. This signal is generated to minimize primary
                                                      MFW pump decreases to less than 2800 gpm.
system cooldown following a reactor trip and is generated when the
                                                        Pressure downstream of the MFW FCVs increased on A to 1059 and
primary temperature decreases to less than 554 degrees F.
                                                      decreased on B and C to 812 and 949 psig. Pressure in the S/Gs
The MFW pump
                                                        remained constant at 1028, 1013 and 1065 psig. The A MFW FCV may have
recirculation valves (FCV-FW-250A and 2508) for A and 8 MFW pumps auto-
                                                      been slightly slow in closing, and as the discharge pressure of the
opened a few seconds later. Each recire valve opens when flow from its
                                                      MFW pumps was increasing to its high of 1290 psig, the pressure down-
MFW pump decreases to less than 2800 gpm.
                                                        stream of the A MFW FCV would have increased.
Pressure downstream of the MFW FCVs increased on A to 1059 and
                                                      The unit's electrical busses auto-transferred to offsite power at
decreased on B and C to 812 and 949 psig. Pressure in the S/Gs
                                                        RT +32, when the main generator, as is normal, auto-transferred on
remained constant at 1028, 1013 and 1065 psig. The A MFW FCV may have
                                                        a 30-second delay signal following a main turbine generator trip.
been slightly slow in closing, and as the discharge pressure of the
MFW pumps was increasing to its high of 1290 psig, the pressure down-
stream of the A MFW FCV would have increased.
The unit's electrical busses auto-transferred to offsite power at
RT +32, when the main generator, as is normal, auto-transferred on
a 30-second delay signal following a main turbine generator trip.
1
1
                                                    *When pressures, flows, etc., are listed in sequence, the order refers
*When pressures, flows, etc., are listed in sequence, the order refers
                                                        respectively to the A, 8, and C steam generatob.
respectively to the A, 8, and C steam generatob.
'
'
                                                                                                                  .
.
                                                                                                              ,
,
d
d
  u
u
    . . - . _
. . - . _
                    _ _ . . . _ - . _________._._._--.__ - ,._ ______._ _ _.- _
_ _ . . . _ - . _________._._._--.__ - ,._ ______._ _ _.- _
                                                          _
__m,
                                                                                          __m, - _ . _ _ - _ _ _ _ _ _-- - .. _ -.. , . -. -
- _ . _ _ - _ _ _ _ _ _--
-
.. _ -.. , .
-.
-
_


  .'
.'
    '
'
  .-                                       7
.-
        Five seconds later at RT +37, a small steam release was seen and heard
7
        in the vicinity of the A MFW pump and the first point heater steam-side
Five seconds later at RT +37, a small steam release was seen and heard
        safety relief.
in the vicinity of the A MFW pump and the first point heater steam-side
        1422:(00 -15)                     .
safety relief.
                .,           .
1422:(00 -15)
        Pressure downstream of the MFW FCVs decreased to 445 psig which
.
        indicates that the downstream MFW check valves were operating and the
.,
        pressure of the water in the lines was decreasing to its saturation
.
        pressure. The S/G pressures decreased to 997, 1003 and 1020 psig and
Pressure downstream of the MFW FCVs decreased to 445 psig which
        levels remained in the 74 percent range. The AFW flow was 342, 317 and
indicates that the downstream MFW check valves were operating and the
        98 gps. The MFW pump discharge pressure reached a peak of 1290 psig
pressure of the water in the lines was decreasing to its saturation
        and the suction pressure rose to 550-600 psig as the condensata pumps
pressure. The S/G pressures decreased to 997, 1003 and 1020 psig and
        responded to the minimal recirculation flow conditions.
levels remained in the 74 percent range.
        The noise of a small steam release was followed at approximately RT +42
The AFW flow was 342, 317 and
        by a very loud noise from the vicinity of the MFW pump suction piping.
98 gps. The MFW pump discharge pressure reached a peak of 1290 psig
        The primary system responded normally to the loss of load transient.
and the suction pressure rose to 550-600 psig as the condensata pumps
        Reactor coolant system temperature was stabilized at 552 degrees F and
responded to the minimal recirculation flow conditions.
        pressurizer level was recovered as it reached the low level setpoint.
The noise of a small steam release was followed at approximately RT +42
        Reactor coolant system pressure decreased from 2235 to 2015 psig in
by a very loud noise from the vicinity of the MFW pump suction piping.
        response to the cooldown.
The primary system responded normally to the loss of load transient.
        The probable time for the piping break appears to have occurred at
Reactor coolant system temperature was stabilized at 552 degrees F and
        RT +42.   The break occurred in an elbow where the 24-inch MFW suction
pressurizer level was recovered as it reached the low level setpoint.
        header splits off at a tee to an 18-inch branch line in an elbow toward
Reactor coolant system pressure decreased from 2235 to 2015 psig in
        the suction of the A MFW pump. About ten feet farther down the 24-inch
response to the cooldown.
        header toward the suction of the 8 MFW pump is where the high pressure
The probable time for the piping break appears to have occurred at
        heater drain pumps' discharge flow is combined with the condensate
RT +42.
      , flow.
The break occurred in an elbow where the 24-inch MFW suction
        Approximately 15 seconds after the large pipe rupture, at RT +57, the A
header splits off at a tee to an 18-inch branch line in an elbow toward
the suction of the A MFW pump. About ten feet farther down the 24-inch
header toward the suction of the 8 MFW pump is where the high pressure
heater drain pumps' discharge flow is combined with the condensate
flow.
,
Approximately 15 seconds after the large pipe rupture, at RT +57, the A
MFW pump tripped due to low suction pressure. The time delay relays
,
,
'
'
        MFW pump tripped due to low suction pressure. The time delay relays
which operate in conjunction with a suction pressure of less than
        which operate in conjunction with a suction pressure of less than
55 psig were found set at 15 seconds,V pump rectre valve indicated that
                                                  and the SOE alarm printer agrees
and the SOE alarm printer agrees
        55 psig
with the time of pump trip. The B MF
        with       wereoffound
it closed while the A rectre valve remained open, as it should have,
              the time   pump set
                                  trip.atThe
                                          15Bseconds,V
                                              MF        pump rectre valve indicated that
,
,
        it closed while the A rectre valve remained open, as it should have,
i
i
        for 60 seconds after the pump trip. A reason for the 8 recirc valve
for 60 seconds after the pump trip. A reason for the 8 recirc valve
r        closing is that the B MFW pump continued to run and the flow in that
closing is that the B MFW pump continued to run and the flow in that
l       line increased to greater than the rectre re-setpoint of 4000 GPM.
r
,        This increase in flow was caused by a backward flow path through-the
l
;       tripped A MFW pump. It was later found that this pump's discharge
line increased to greater than the rectre re-setpoint of 4000 GPM.
j       check valve was disabled. The 8 MFW pump continued to run for 23
This increase in flow was caused by a backward flow path through-the
l       seconds.
,
;
tripped A MFW pump.
It was later found that this pump's discharge
j
check valve was disabled. The 8 MFW pump continued to run for 23
l
seconds.
;
;
!
!
                                                          !
!
                                                  .'
.'
          &
&
                                                                                O
O
                                                                                      t
t


            -
-
        .
.
          .
.
        -
8
                                              8
-
              1422:(15-30)
1422:(15-30)
              An operations supervisor was in the turbine building observing construc-
An operations supervisor was in the turbine building observing construc-
              tion activity around the MFW pumps. He heard and saw the large steam
tion activity around the MFW pumps. He heard and saw the large steam
              break, And immediately ran to the control room to alert the operators.
break, And immediately ran to the control room to alert the operators.
              He also' told them that people had been injured. The shift supervisor
He also' told them that people had been injured. The shift supervisor
              then ordered that all secondary pumps be secured.
then ordered that all secondary pumps be secured.
              1422:(30-45)
1422:(30-45)
              When the CR0s began to secure the secondary pumps, the B MFW pump
When the CR0s began to secure the secondary pumps, the B MFW pump
              was found " auto-off" with its yellow disagreement light on, which
was found " auto-off" with its yellow disagreement light on, which
              occurred at RT +81, or about 1422:36. Its time delay relays were also
occurred at RT +81, or about 1422:36. Its time delay relays were also
i
found set at 15 seconds. Therefore, its trip point of 70 psig was
              found set at 15 seconds. Therefore, its trip point of 70 psig was
i
              reached at RT 66 or about 24 seconds after the break. The high pres -
reached at RT 66 or about 24 seconds after the break.
              sure heater drain pump was running and had to be turned off, and both
The high pres -
              low pressure heater drain pumps had tripped. After all secondary pumps
sure heater drain pump was running and had to be turned off, and both
              were secured, the steam release stopped.
low pressure heater drain pumps had tripped. After all secondary pumps
              The ERFC and SOE alarm printer agreed with the operators on the above
were secured, the steam release stopped.
              time sequence.
The ERFC and SOE alarm printer agreed with the operators on the above
              1424
time sequence.
              The CR0 noted that primary temperature was stable at about 550
1424
              degrees F.
The CR0 noted that primary temperature was stable at about 550
degrees F.
'
The NRC Senior Resident Inspector arrived in the Control Room.
!
1425
The CR0 secured the B RCP to avoid adding heat to the reactor coolant
system. Plant conditions were stable with RCS temperature being
l
maintained at approximately 540 degrees F by releasing decay heat
through the C S/G power operated relief valve (PORV).
'
'
              The NRC Senior Resident Inspector arrived in the Control Room.
1427
!            1425
An Unusual Event was declared.
              The CR0 secured the B RCP to avoid adding heat to the reactor coolant
1430
              system. Plant conditions were stable with RCS temperature being
l
l            maintained at approximately 540 degrees F by releasing decay heat
Ground and air ambulances were called.
              through the C S/G power operated relief valve (PORV).
The CR0 changed the normal suction of the charging pumps to refueling
                                                      '
water storage tank.
              1427
The B and C S/G low-low level alarms cleared and the steam driven APW
              An Unusual Event was declared.
pump was secured.
              1430
!
l             Ground and air ambulances were called.
The Regional response center called the c,ontrol room.
              The CR0 changed the normal suction of the charging pumps to refueling
,
              water storage tank.
,
              The B and C S/G low-low level alarms cleared and the steam driven APW
b en
              pump was secured.                               !
              The Regional response center called the c,ontrol room.     ,
                                                        ,
  b en


                      _.                                             _
_.
        ~
_
    .
~
      ,
.
    .
,
                            ,           9
9
          1440
.
          An Alert was declared to assist in personnel accountability.
,
          1445                           .
1440
                    _
An Alert was declared to assist in personnel accountability.
          The CR0 secured the A RCP.
1445
          The Shift Supervisor noted that the condenser still had a vacuum and as
'
          there was no steam for the main turbine gland seal, opened the vacuum
          breaker.
          State and local authorities were notified of the Alert.
          1500
          NRC Operations Center was notified of the Alert.
          Reactor coolant system temperature was 530 degrees F, pressurizer level
          was 25 percent, and pressurizer pressure was 2160 psig.
          1506
          The CR0 secured B auxiliary motor driven feedwater pump.
          1514
'
          The CR0 began emergency boration to cold shutdown concentration as part
          of the normal post trip procedure.
          1518
.
.
_
The CR0 secured the A RCP.
The Shift Supervisor noted that the condenser still had a vacuum and as
there was no steam for the main turbine gland seal, opened the vacuum
'
'
          Personnel accountability initiated.
breaker.
I         1535
State and local authorities were notified of the Alert.
i         The corporate Emergency Response Cente'r was activated.
1500
          1539
NRC Operations Center was notified of the Alert.
          The CR0 secured emergency boration.
Reactor coolant system temperature was 530 degrees F, pressurizer level
was 25 percent, and pressurizer pressure was 2160 psig.
1506
The CR0 secured B auxiliary motor driven feedwater pump.
1514
The CR0 began emergency boration to cold shutdown concentration as part
'
of the normal post trip procedure.
1518
.
'
Personnel accountability initiated.
I
1535
i
The corporate Emergency Response Cente'r was activated.
1539
The CR0 secured emergency boration.
i
i
!
!
          1548
1548
          Personnel accountability completed.
Personnel accountability completed.
          1625
1625
          The Alert was terminated. The control rod (M410) which had indicated
The Alert was terminated. The control rod (M410) which had indicated
          that it inserted only to 35 steps now was noted to indicate fully
that it inserted only to 35 steps now was noted to indicate fully
          inserted.
inserted.
                                                  .'
.'
  -
-
!
!


            ..-                                   .             . - -           -
..-
                                                                                      - . .                 .                     . - _ .
.
                  -
. - -
                      .
-
.
.
                  .
.
                -
.
                                                                                              10
. - _
:
.
                                                          1821
-
                                                          Cooldown at 50 degrees F per hour was initiated.
-
.
.
.
10
-
:
1821
Cooldown at 50 degrees F per hour was initiated.
2130
,
.
,
,
                                                        2130          ,                        .
                                                                        <
t
t
<
NRC team arrived on site.
,
0355 December 10, 1986
Unit placed on residual heat removal system with ter.perature at
350 degrees F and pressure at 450 psig.
0704
i
The unit achieved cold shutdown conditions.
'
8.
Effects of Fai1'ure
!
a.
Pipe Rupture
The rupture of the 18-inch A MFW suction pipe occurred on a 90 degree
!
elbow at a point about one foot from where the suction pipa joins the
condensate supply header.
The point at which the break occurred
,
,
                                                        NRC team arrived on site.
relative to the main feedwater pump is indicated on Figure 1, which is
                                                        0355 December 10, 1986
                                                        Unit placed on residual heat removal system with ter.perature at
                                                          350 degrees F and pressure at 450 psig.
                                                        0704
i                                                        The unit achieved cold shutdown conditions.
                                                                            '
                                    8.      Effects of Fai1'ure
!                                            a.          Pipe Rupture
                                                        The rupture of the 18-inch A MFW suction pipe occurred on a 90 degree
!                                                        elbow at a point about one foot from where the suction pipa joins the
'
'
,                                                      condensate supply header.          The point at which the break occurred
a picture of the identical undamaged Unit 1 piping configuration.
                                                          relative to the main feedwater pump is indicated on Figure 1, which is
Figure 2 shows the rupture location from the condensate supply header
                                                        a picture of the identical undamaged Unit 1 piping configuration.
side.
                                                          Figure 2 shows the rupture location from the condensate supply header
Figure 2 clearly indicates that the rupture was a catastrophic,
,
,
                                                        side. Figure 2 clearly indicates that the rupture was a catastrophic,
;
;                                                        360 degree circumferential break. Figure 3 shows the broken pipe from
360 degree circumferential break.
;                                                       the MFW pump suction side.
Figure 3 shows the broken pipe from
;
the MFW pump suction side.
!
!
                                            b.           Pipe Whip
b.
Pipe Whip
i
i
                                                        Observation of the damaged A MFW pump suction piping indicated sig-
Observation of the damaged A MFW pump suction piping indicated sig-
                                                        nificant movement of the piping following the rupture. The piping,
nificant movement of the piping following the rupture. The piping,
                                                        attached to the pump suction, dropped and rotated away from the break
attached to the pump suction, dropped and rotated away from the break
point, pivoting on the elbow near the pump suction. Although the
,
,
;
;
                                                        point, pivoting on the elbow near the pump suction. Although the
piping came to rest against a prtion of the B MFW pump discharge
                                                        piping came to rest against a prtion of the B MFW pump discharge
l
l                                                       piping it did not appear to have damaged it significantly.
piping it did not appear to have damaged it significantly.
!                                                         Inspection of the area following the event also revealed that one
!
                                                        piece of suction piping had ripped off and was blown some distanca from
Inspection of the area following the event also revealed that one
'
piece of suction piping had ripped off and was blown some distanca from
                                                        the break point. The piece was about two feet by three feet in size.
'
                                                        It appears that the joint between the' suction pipe and condensate
the break point. The piece was about two feet by three feet in size.
                                                        supply header provided lateral support of the suction piping assembly
It appears that the joint between the' suction pipe and condensate
                                                          including the suction isolation valve. The loss of this support along
supply header provided lateral support of the suction piping assembly
including the suction isolation valve. The loss of this support along
with the weight distribution of the suction pipe assembly probably
,
,
                                                        with the weight distribution of the suction pipe assembly probably
contributed to the pivot and rotation of the assembly.
It is also
i
i
                                                        contributed to the pivot and rotation of the assembly. It is also
;
;
likely that back flow by the B MFW pump througli the damaged A MFW
'
'
                                                          likely that back flow by the B MFW pump througli the damaged A MFW
pump discharge check valve and out the broken suction pipe contributed
                                                        pump discharge check valve and out the broken suction pipe contributed
to pipe whip motion of the feed pump suct, ion pipe.
                                                        to pipe whip motion of the feed pump suct, ion pipe.
                                                                                                          *
l
l
*
'
'
                                                            ,
,
          ~
l
l                                                                        .
~
                                                                                                                                  .
.
  ---,--r--         - , , - -m-r--   ..,,ew   ,----+-+--m                   ,-m- w
.
---,--r--
- , , - -m-r--
..,,ew
,----+-+--m
,-m-
w
w-*----
**v*we*--w
-
*:-"--' - " * * " * * - - * ' ' " " * * " " " "


        ~
~
    .
.
      .
.
    .
11
                                              11
.
          c. Personnel Injury
c.
            Those injured were eight contractor employees who were working in
Personnel Injury
            the general area, but not on the affected pipe itself. Six of these
Those injured were eight contractor employees who were working in
            individuals were hospitalized f.or treatment of severe burns. Three
the general area, but not on the affected pipe itself. Six of these
            were evacuated directly from the site by helicopter, and three others
individuals were hospitalized f.or treatment of severe burns. Three
            were taken off site by ambulance. The other two, who were less
were evacuated directly from the site by helicopter, and three others
            severely injured, were treated at a clinic and released.
were taken off site by ambulance. The other two, who were less
            One of those hospitalized died the afternoon of the following day and
severely injured, were treated at a clinic and released.
            another victim died two days after the accident. Two others. died
One of those hospitalized died the afternoon of the following day and
            several days later. The others remained in serious to critical condi-
another victim died two days after the accident. Two others. died
            tion. One of the two hospitalized improved and was later released,
several days later. The others remained in serious to critical condi-
            but the other was still in serious condition more than a month after
tion. One of the two hospitalized improved and was later released,
            the accident.
but the other was still in serious condition more than a month after
            These contractor personnel were employed by Daniel Construction Company
the accident.
            of Greenville, South Carolina, and by Insulation Specialties Inc.,     of
These contractor personnel were employed by Daniel Construction Company
            Hopewell, Virginia. They were doing instrument line relocation and
of Greenville, South Carolina, and by Insulation Specialties
            pipe insulation work,
Inc., of
          d. Plant Cooldown
Hopewell, Virginia. They were doing instrument line relocation and
            The loss of the suction, piping to the A MFW pump and subsequent steam
pipe insulation work,
            release had no adverse effects on the plant cooldown. The MSTVs had
d.
            closed as had the MFW FCVs before the pipe rupture. These actions           -
Plant Cooldown
            isolated the S/Gs from the rupture. The normal cooldown mode for a
The loss of the suction, piping to the A MFW pump and subsequent steam
            MSTV closure event is steam release by the code safeties, and S/G PORVs
release had no adverse effects on the plant cooldown. The MSTVs had
            and continued feedwater flow from the auxiliary feedwater system.
closed as had the MFW FCVs before the pipe rupture. These actions
          e. Employee Concerns
-
            On December 11, 1986, a former employee at Surry (a carpenter)
isolated the S/Gs from the rupture.
The normal cooldown mode for a
MSTV closure event is steam release by the code safeties, and S/G PORVs
and continued feedwater flow from the auxiliary feedwater system.
e.
Employee Concerns
On December 11, 1986, a former employee at Surry (a carpenter)
contacted the NRC and expressed concern about grinding activities at
,
,
            contacted the NRC and expressed concern about grinding activities at
}
}            Surry. The employee said that during June 1986, he and four other
Surry. The employee said that during June 1986, he and four other
            carpenters were directed to grind on p,ipe in the containment building.
'
'
            He stated that his foreman advised his crew that they were carpenters
carpenters were directed to grind on p,ipe in the containment building.
;           and not qualified to perform this work activity. They were terminated
He stated that his foreman advised his crew that they were carpenters
            for refusing to do the work. A case was filed with the Department of
;
;           Labor (DOL). The employee did not know the current status of his DOL
and not qualified to perform this work activity. They were terminated
;           issue. The employee stated that the group of carpenters who remained
for refusing to do the work. A case was filed with the Department of
i            did perform grinding activities at various locations, including in the
;
l            turbine building. He did not know if they actually performed gririding
Labor (DOL).
The employee did not know the current status of his DOL
;
issue. The employee stated that the group of carpenters who remained
i
i
            on the pipe that ruptured but wanted the NRC to determine if the pipe
did perform grinding activities at various locations, including in the
            rupture was connected with the carpenters' grinding work.
l
J           As discussed in paragraph 9 below, preliminary investigations show
turbine building. He did not know if they actually performed gririding
!           that the pipe rupture was caused by a corrosion / erosion mechanism on
i
i           the inside surface of the pipe. It is clear tfhat the rupture was not
on the pipe that ruptured but wanted the NRC to determine if the pipe
!           related to grinding on the outside of the pipe.
rupture was connected with the carpenters' grinding work.
                                                        ,'
J
  w
As discussed in paragraph 9 below, preliminary investigations show
                                                                                      n
!
that the pipe rupture was caused by a corrosion / erosion mechanism on
i
the inside surface of the pipe.
It is clear tfhat the rupture was not
!
related to grinding on the outside of the pipe.
,'
w
n


        .
.
    .
.
      .
.
    *
12
                                          12
*
          As further followup to the employee's concern, the inspector discussed
As further followup to the employee's concern, the inspector discussed
          grinding practices at the site with licensee officials. The licensee
grinding practices at the site with licensee officials. The licensee
          was aware of the employee's concern based on the individual's DOL case
was aware of the employee's concern based on the individual's DOL case
          in June 1986, and the employee's contacts with the news media after the
in June 1986, and the employee's contacts with the news media after the
          pipe rupture. The licensee stated that the work to which the former
pipe rupture. The licensee stated that the work to which the former
          employee-referred was buffing or cleaning pipe welds in preparation for
employee-referred was buffing or cleaning pipe welds in preparation for
          non-destructive examination (NDE) and was not grinding. The licensee's
non-destructive examination (NDE) and was not grinding. The licensee's
          representative said their practice had always been to use carpenters or
representative said their practice had always been to use carpenters or
          laborers to help pipe fitters clean or buff pipe welds in preparation
laborers to help pipe fitters clean or buff pipe welds in preparation
          for NDE. The carpenters or laborers worked under direction of the pipe
for NDE. The carpenters or laborers worked under direction of the pipe
          fitters and were never allowed to grind pipe.
fitters and were never allowed to grind pipe.
          The inspectors interviewed both the foreman who had terminated the
The inspectors interviewed both the foreman who had terminated the
          carpenters in June, and a carpenter who was on shift at the time the
carpenters in June, and a carpenter who was on shift at the time the
          other carpenters were terminated. Both agreed with the Itcensee's
other carpenters were terminated. Both agreed with the Itcensee's
          statements about carpenters being used only for cleaning or buffing
statements about carpenters being used only for cleaning or buffing
          pipe welds in preparation for NDE. They both also stated that the
pipe welds in preparation for NDE. They both also stated that the
          issue was that the carpenters who were terminated wanted pipe fitters'
issue was that the carpenters who were terminated wanted pipe fitters'
          pay. When they refused to buff pipe without pipe fitters' pay, they
pay. When they refused to buff pipe without pipe fitters' pay, they
          were terminated. The foreman was the same foreman, who the concerned
were terminated. The foreman was the same foreman, who the concerned
          employee stated, had advised his crew that they were carpenters and not
employee stated, had advised his crew that they were carpenters and not
          qualified to perform this work activity. During the interview, the
qualified to perform this work activity. During the interview, the
          foreman stated that, at the time of the termination he advised the
foreman stated that, at the time of the termination he advised the
          carpenters only that the work they were requested to perform (buffing
carpenters only that the work they were requested to perform (buffing
          pipe welds) was not outside their work classification.
pipe welds) was not outside their work classification.
          The inspectors also reviewed U. S. 00L letter dated November 21, 1986,
The inspectors also reviewed U. S. 00L letter dated November 21, 1986,
          relative to the employee's concern. The letter states in part:
relative to the employee's concern.
                "
The letter states in part:
                  ... it is our conclusion that your allegations are unprovable
" ... it is our conclusion that your allegations are unprovable
                for the following reason: Your termination, although officially
for the following reason: Your termination, although officially
                recorded as involuntary, arose from a refusal to accept a work
recorded as involuntary, arose from a refusal to accept a work
                assignment arising from previous and ongoing personal and
assignment arising from previous and ongoing personal and
                jurisdiction disputes with supervisor (s). These disputes were
jurisdiction disputes with supervisor (s). These disputes were
                unrelated to any safety and health issue."
unrelated to any safety and health issue."
                                                      ~
~
          The inspector also reviewed the licens e's program for control of
The inspector also reviewed the licens e's program for control of
!        grinding on pipe. During fabrication of piping systems, grinding
!
!
          is controlled by Volume 2 of the Corporate Welding Manual including
grinding on pipe. During fabrication of piping systems, grinding
          Procedure P-101, Revision 2, " General Piping and Pressure Vessel
is controlled by Volume 2 of the Corporate Welding Manual including
,        Welding Procedure," and Attachment A to P-101, " Weld Grinding Standard
!
Procedure P-101, Revision 2, " General Piping and Pressure Vessel
Welding Procedure," and Attachment A to P-101, " Weld Grinding Standard
,
and Techniques." For NDE, surface preparation is covered by NDE proce-
'
'
          and Techniques." For NDE, surface preparation is covered by NDE proce-
dures. The inspectors reviewed a number of NDE procedures from the
*
*
          dures. The inspectors reviewed a number of NDE procedures from the
NDE Manual and found that the procedures specify the surface condition
          NDE Manual and found that the procedures specify the surface condition
i
i         required but do not always clearly specify the method of surface
required but do not always clearly specify the method of surface
i        preparation required to obtain the surface condition. NDE Procedure       .
preparation required to obtain the surface condition. NDE Procedure
          NDE-3.1, Revision 3, Preparation, Issue and Control of Nondestructive
i
          Examination Procedures, requires in paragraph 4.3.2.5 that NDE proce-
NDE-3.1, Revision 3, Preparation, Issue and Control of Nondestructive
          dure list all actions which should be completeif prior to implementing
.
          the procedure, such as surface condition and preparation, temperature
Examination Procedures, requires in paragraph 4.3.2.5 that NDE proce-
j         of parts, etc.     The licensee agreed to ev,aluate NDE procedures and
dure list all actions which should be completeif prior to implementing
  -
the procedure, such as surface condition and preparation, temperature
;                                                                                ,
j
\
of parts, etc.
The licensee agreed to ev,aluate NDE procedures and
;
-
,
\\
[
[


                            -- - -         .     -       - -       -.             -     ---.
-- - -
          -
.
-
- -
-.
-
---.
-
.
.
j
13
*
.
.
      .
determine if clarification is needed in specifying required surface
        *
j      .
                                                          13
-
-
                    determine if clarification is needed in specifying required surface
preparation methods. Pending review of the licensee's evaluation,
                    preparation methods. Pending review of the licensee's evaluation,
!
!
                    Inspector Followup Item 280, 281/86-42-01, Clarification of Surface
Inspector Followup Item 280, 281/86-42-01, Clarification of Surface
                    Preparation Methods in NOE Procedures, is identified.
Preparation Methods in NOE Procedures, is identified.
                                                                          -
-
                                                            .
4
                            4
.
            9. Metallurgical Aspects
9.
                As noted in paragraph 8.a. above, the 18-inch suction line to the A main
Metallurgical Aspects
i               feed pump failed catastrophically completely severing the line from the
As noted in paragraph 8.a. above, the 18-inch suction line to the A main
i
feed pump failed catastrophically completely severing the line from the
!
!
                24-inch header (see Figures 1, 2 and 3). The failure occurred in an 18-inch
24-inch header (see Figures 1, 2 and 3). The failure occurred in an 18-inch
                90 degree elbow approximately one foot downstream of a tee in the 24-inch                             >
90 degree elbow approximately one foot downstream of a tee in the 24-inch
                header. The suction line was completely separated and dislocated from the
>
                header. Immediately after the failure, the licensee initiated a comprehen-
header. The suction line was completely separated and dislocated from the
                sive analysis to determine the reasons for the failure and the necessary
header.
                corrective actions. The following summarizes the licensee's analysis:                     -
Immediately after the failure, the licensee initiated a comprehen-
                a.   Initial Observations
sive analysis to determine the reasons for the failure and the necessary
corrective actions. The following summarizes the licensee's analysis:
-
a.
Initial Observations
.
.
]                   The failed 18-inch suction line was fabricated from ASTM A-106,
]
The failed 18-inch suction line was fabricated from ASTM A-106,
Grade B, Extra Strong carbon steel seamless pipe and ASTM A-234,
'
'
                    Grade B, Extra Strong carbon steel seamless pipe and ASTM A-234,
:                    Grade B, Extra Strong, WP8 carbon steel wrought fittings with a
j                    nominal wall thickness of 0.500 inches.
:
:
Grade B, Extra Strong, WP8 carbon steel wrought fittings with a
j
nominal wall thickness of 0.500 inches.
:
When the 18-inch elbow failed, a fragment approximately two feet by
4
4
                    When the 18-inch elbow failed, a fragment approximately two feet by
three feet was ejected from the outside of the elbow.
,                    three feet was ejected from the outside of the elbow. The free end of
The free end of
j                   the severed line was displaced in a horizontal direction approximately
,
                    6.5 feet and was wedged against the bottom of the B main feed pump
j
                    discharge line. During the displacement, the A suction line rotated
the severed line was displaced in a horizontal direction approximately
                    around the point of connection at the inlet to the pump, severely                         ,
6.5 feet and was wedged against the bottom of the B main feed pump
;                    deforming that portion of the line. The failed elbow, the short
discharge line. During the displacement, the A suction line rotated
                    section of pipe between the elbow and the 24-inch header, and a short
around the point of connection at the inlet to the pump, severely
'
,
                    section of pipe downstream of the elbow were removed for a detailed
'
i                   study. The three parts were re-assembled as close as possible to
deforming that portion of the line. The failed elbow, the short
:                   understand better the failure origination point and the sequence of
;
l                   the failure after origination. The licensee performed a field
section of pipe between the elbow and the 24-inch header, and a short
i                   metallurgical investigation of the fai, led elbow as detailed below.
section of pipe downstream of the elbow were removed for a detailed
!                   (1) The investigation consisted of the following:
i
                          -
study. The three parts were re-assembled as close as possible to
                                      Visual inspection of the system failure location.
:
                          -
understand better the failure origination point and the sequence of
                                      Removal of the fractured elbow from the suction line.      .
l
                          -
the failure after origination. The licensee performed a field
                                      Visual 5X magnification evaluation and photography of
i
                                      fracture surfaces, and elbow surface conditions.
metallurgical investigation of the fai, led elbow as detailed below.
                                                                                                                '
!
                          -
(1) The investigation consisted of the following:
                                      Ultrasonic wall thickness measurements, on a two-inch grid
Visual inspection of the system failure location.
                                      pattern, of the failed elbow.
-
                                                                    ,'
Removal of the fractured elbow from the suction line.
  sem
-
                                    .
.
                                                                                                  -,------m._     ~ ,
Visual 5X magnification evaluation and photography of
-
fracture surfaces, and elbow surface conditions.
'
Ultrasonic wall thickness measurements, on a two-inch grid
-
pattern, of the failed elbow.
,'
sem
.
-,------m._
~ ,


                                                                                                                              .
.
    O
O
        -
-
    .                                                                                            14
14
                          -
.
                                Metallurgical replicas taken on the elbow at several surface
Metallurgical replicas taken on the elbow at several surface
                                locations.
-
                          -
locations.
                                Mechanical measurements of elbow thickness.
Mechanical measurements of elbow thickness.
                  (2) Th'e_ investigation resulted in the following observations:
-
                          -
(2) Th'e_ investigation resulted in the following observations:
                                Visual inspection of the inside surface of the elbow revealed
Visual inspection of the inside surface of the elbow revealed
                                a dimpled surface appearance, generally thinned wall and a
-
                                number of localized very thin areas. The localized thin
a dimpled surface appearance, generally thinned wall and a
                                areas were small in area, usually less than one inch across,
number of localized very thin areas. The localized thin
                                with remaining wall thickness as small as 1/16-inch. The
areas were small in area, usually less than one inch across,
                                areas were fairly smooth and blended smoothly into the
with remaining wall thickness as small as 1/16-inch. The
                                surrounding material. Ultrasonic thickness measurements
areas were fairly smooth and blended smoothly into the
                                showed the wall thinning to be a gradual sloping change over'
surrounding material.
                                most of the surface of the elbow. The general thickness of
Ultrasonic thickness measurements
                                the elbow varied from 0.120 inches to 0.390 inches. The
showed the wall thinning to be a gradual sloping change over'
                                short section of upstream pipe varied in thickness from
most of the surface of the elbow. The general thickness of
                                0.150 inches to 0.450 inches. Near the elbow, thickness
the elbow varied from 0.120 inches to 0.390 inches. The
                                measurements on the section of downstream pipe revealed
short section of upstream pipe varied in thickness from
                                thicknesses from 0.295 inches to 0.405 inches. The wall
0.150 inches to 0.450 inches. Near the elbow, thickness
                                thickness of pipe a short distance downstream of the elbow
measurements on the section of downstream pipe revealed
                                was within manufacturer's tolerance.
thicknesses from 0.295 inches to 0.405 inches. The wall
                                As noted above, the nominal wall thickness should have been
thickness of pipe a short distance downstream of the elbow
                                0.500 inches.
was within manufacturer's tolerance.
                          -
As noted above, the nominal wall thickness should have been
                                Field metallurgical replicas taken on the surface of the
0.500 inches.
                                elbow revealed a microstructure typical of ASTM A-106 Grade 8
Field metallurgical replicas taken on the surface of the
                                material with no signs of strain.
-
                          -
elbow revealed a microstructure typical of ASTM A-106 Grade 8
                                The fracture surface was typical of a ductile tearing mode
material with no signs of strain.
                                failure. Tears, which appeared to be fracture origination
The fracture surface was typical of a ductile tearing mode
                                points, were noted at two localized thin cavity areas of the
-
                                fracture. Small defects, indicative of laps, laminations
failure. Tears, which appeared to be fracture origination
                                and inclusions, typical for A-106, Grade B, materials, were
points, were noted at two localized thin cavity areas of the
                                noted at the fracture surface. One of these small defects
fracture.
                                was noted at one of the thin overload tear areas and could
Small defects, indicative of laps, laminations
j                               have been the start of the fracture.
and inclusions, typical for A-106, Grade B, materials, were
l                 (3) The licensee's analysis revealed the following probable scenario
noted at the fracture surface. One of these small defects
!                         for the pipe failure:
was noted at one of the thin overload tear areas and could
                                                                                                                                                                ,
j
                          -
have been the start of the fracture.
                                The pipe failed because of a thinned wall. A corrosion /
l
l                               erosion mechanism is the probable cause of the wall loss.
(3) The licensee's analysis revealed the following probable scenario
l                               Wall loss by this mechanism occurs by a gouging out pattern                                                                         _
!
                                on the carbon steel surface under the action of a flowing
for the pipe failure:
,
The pipe failed because of a thinned wall. A corrosion /
-
l
erosion mechanism is the probable cause of the wall loss.
l
Wall loss by this mechanism occurs by a gouging out pattern
_
on the carbon steel surface under the action of a flowing
medium and an electrochemical action. This phenomenon has
i
i
                                medium and an electrochemical action. This phenomenon has                                                                            .
.
                                been well documented for two phase fIow such as extraction                                                                           ,
been well documented for two phase fIow such as extraction
                                steam systems. The licensee has an inspection procedure
,
                                documented for monitoring the t,hickness of its two phase
steam systems. The licensee has an inspection procedure
                                                                                                                                      .
documented for monitoring the t,hickness of its two phase
  .
.
                                                                                                                                                                  O
.
      ..- . . - -   . .- .
O
                        .
..- . . - -
                                    , - _ _ . . . _ - - - . . , - - , , , , , . . . _ _ . - , , - - , , _ . . . . . . , _ . . . - . _   _.., --.--,,-, - _ .--
. . .
, - _ _ . . . _ - - - . . , - - , , , , , . . . _ _ . - , , - - , , _ . . . . . . , _ . . . - . _
_.., --.--,,-, - _ .--
- .


                                                              .
.
                    O
O
                      .
.
                    -
-
                                                                                                15
15
                                                systems (see Surry Administrative Procedure SUAD-M-33,
systems (see Surry Administrative Procedure SUAD-M-33,
                                                No. ADM-89.13. " Secondary Piping Inspections"). However,
No. ADM-89.13. " Secondary Piping Inspections").
                                                for single phase flow in systems, such as feedwater and
However,
                                                condensate, the problem had not been recognized. The only
for single phase flow in systems, such as feedwater and
                                            ,
condensate, the problem had not been recognized. The only
                                              '
place where the phenomenon has been documented in a single
                                                place where the phenomenon has been documented in a single
,
                                                phase flow system is in the steam generator feed ring
'
                                                J-tubes. The design geometry of the failed elbow in the
phase flow system is in the steam generator feed ring
                                                feedwater suction line is similar to the design geometry of
J-tubes. The design geometry of the failed elbow in the
                                                the feed ring J-tubes. Both consist of a header or large
feedwater suction line is similar to the design geometry of
                                                diameter pipe and a right angle discharge pipe with a 90 or
the feed ring J-tubes. Both consist of a header or large
                                                ISO degree turn. The licensee concluded that the turbulent
diameter pipe and a right angle discharge pipe with a 90 or
                                                flow created by the geometry and the low oxygen feedwater
ISO degree turn. The licensee concluded that the turbulent
                                                probably contributed to the corrosion / erosion thinning of the
flow created by the geometry and the low oxygen feedwater
                                                pipe wall.
probably contributed to the corrosion / erosion thinning of the
                                          -
pipe wall.
                                                Because of the thinned wall (as low as 0.048-inches in a
Because of the thinned wall (as low as 0.048-inches in a
                                                localized area and 0.100-inch over a more general area),
-
                                                ' local membrane stresses were near yield at system pressure
localized area and 0.100-inch over a more general area),
                                                and temperature of 367 psig and 374 degrees F, respectively.
' local membrane stresses were near yield at system pressure
                                                The system underwent an upward pressure transient (see para-
and temperature of 367 psig and 374 degrees F, respectively.
                                                graph 7.c. above) resulting in a localized tensile overload
The system underwent an upward pressure transient (see para-
                                                failure in a thin wall cavity. Using the ASME Code minimum
graph 7.c. above) resulting in a localized tensile overload
                                                wall equation, and assuming an internal pipe pressure of
failure in a thin wall cavity. Using the ASME Code minimum
                                                600 psig, a temperature of 370 degrees F, and an ultimate
wall equation, and assuming an internal pipe pressure of
                                                strength of 60,000 psi, results in a calculated burst thick-
600 psig, a temperature of 370 degrees F, and an ultimate
strength of 60,000 psi, results in a calculated burst thick-
ness of 0.090 inches and a yield thickness of 0.173 inches.
,
,
Therefore, with a local cavity thickness of 0.048 inches,
'
'
                                                ness of 0.090 inches and a yield thickness of 0.173 inches.
l
                                                Therefore, with a local cavity thickness of 0.048 inches,
a general thickness of 0.100-inch, and a upward pressure
l                                                a general thickness of 0.100-inch, and a upward pressure
I
I                                               transient, the material easily exceeded its burst strength.
transient, the material easily exceeded its burst strength.
                                                The initial tensile overload tear was considered to have
The initial tensile overload tear was considered to have
                                                arrested and not to have developed into an unstable tearing
arrested and not to have developed into an unstable tearing
                                                mode. Water flashing to steam was heard by station person-
mode. Water flashing to steam was heard by station person-
                                                nel. As water continued to flash to steam for a few seconds
nel. As water continued to flash to steam for a few seconds
                                                and pressure continued to increase in the elbow, an unstable
and pressure continued to increase in the elbow, an unstable
                                                tear developed in a second t,hin walled area. The pipe then
tear developed in a second t,hin walled area. The pipe then
                                                ruptured, ejecting the fragment from the elbow.
ruptured, ejecting the fragment from the elbow.
:                           b.       Metallurgical Analysis
:
                                    (1) VEPCO
b.
                                          VEPC0 has hired Failure Analysis Associates (FAA) to perform a
Metallurgical Analysis
                                          complete metallurgical analysis of the failed elbow. The
(1) VEPCO
                                          following is a summary of the work to be performed and the
VEPC0 has hired Failure Analysis Associates (FAA) to perform a
complete metallurgical analysis of the failed elbow.
The
following is a summary of the work to be performed and the
.
.
                                          preliminary results as of January 14, 1987:
preliminary results as of January 14, 1987:
l
l
l
l                                          (a) Phase 1 - Scheduled for completion a, bout February 1, 1987
(a) Phase 1 - Scheduled for completion a, bout February 1, 1987
                                                -
Tensile Tests
                                                              Tensile Tests
-
                                                                                                                      .' -
.'
                                      >
-
          _
>
                                                                                                                          ,
_
  , _ , . . . - - -     --.   . . -               .,- - --,         . - - - - - - . , - - - - - , - - - - - - - ~ ~
,
, _ , . . . - - -
--.
. . -
.,- - --,
. - - - - - - . , - - - - - , - - - - - - - ~ ~
- - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -


      . .
. .
    .
.
  O
O
  .-                                   16
.-
                      Tee, elbow and across the weld tested. Results
16
                      complete. Acceptable to specifications.
Tee, elbow and across the weld tested. Results
                  -
complete. Acceptable to specifications.
                      Charpy Impact Tests
Charpy Impact Tests
            '
-
              ~
Elbow tested. Small specimens used due to thickness of
                      Elbow tested. Small specimens used due to thickness of
'
                      material. Results appear to be satisfactory. Complete
~
                      curve will be generated to correlate results with full
material.
                      size specimens.
Results appear to be satisfactory. Complete
                -
curve will be generated to correlate results with full
                      Hardness Tests
size specimens.
                      Elbow base material, elbow heat affected zone (HAZ),
Hardness Tests
                      tee base material, tee HAZ and weld material tested.
-
                      Results complete and appear to be satisfactory.
Elbow base material, elbow heat affected zone (HAZ),
                -
tee base material, tee HAZ and weld material tested.
                      Chemistry
Results complete and appear to be satisfactory.
                      Elbow base material, tee base material, and weld
Chemistry
                      material tested. Results complete and appear to be
-
                      satisfactory. Trace elements are almost nonexistent.
Elbow base material, tee base material, and weld
                -
material tested. Results complete and appear to be
                      Micro and Macro Examinations
satisfactory. Trace elements are almost nonexistent.
                      Work partially complete. At 50X, inside surface
Micro and Macro Examinations
                      dimpled, outside surface smooth.   Structure typical         -
-
                      Pearlite / Ferrite.
Work partially complete. At 50X, inside surface
                -
dimpled, outside surface smooth.
                      Scanning Electron Microscope Examination
Structure typical
                      Started.
-
                -
Pearlite / Ferrite.
                      Oxide Layer Micro Probe Study
Scanning Electron Microscope Examination
                      Started.
-
          (b) Phase 2 - Scheduled for compietion about the end of February,
Started.
                1987.
Oxide Layer Micro Probe Study
-
Started.
(b) Phase 2 - Scheduled for compietion about the end of February,
1987.
l
l
l
l
                -
Finite Element Analysis
                      Finite Element Analysis
-
                -
Basic Stress Analysis
                      Basic Stress Analysis
-
                                                                            -
-.
                                                                            .
Complete.
                      Complete.   Primary stresses 8500 psi, secondary thermal
Primary stresses 8500 psi, secondary thermal
stresses 5000 psi. Code allowable 15,000 psi primary,
,
,
                      stresses 5000 psi. Code allowable 15,000 psi primary,
j
j                      22,500 psi primary plus secondary.                       _
22,500 psi primary plus secondary.
_
,
,
i
i
                                                  *
*
                                                .
.
i
i
                                                                              g
g
'
'
                                                                                  .
.
                          -               - --     _-- -
, ,
-
,
- --
_-- -
,--- , - , , - , . , - - , - -
, - - - -


                                                                            . _ _       . _ .                                                                       . . _ . .           _ ._     _ _
. _ _
        '
. _ .
    .
.
      ~
. _ .
    -
.
                                                                                                                                17
_ ._
_ _
'
.
~
17
-
f
f
                                                          (c) Phase 3 - Scheduled for completion about mid-March,1987.
(c) Phase 3 - Scheduled for completion about mid-March,1987.
                                                                                  -
Establish J-Resistance Curves tad perform detailed
                                                                                        Establish J-Resistance Curves tad perform detailed
-
fracture mechanics analysis.
,
,
                                                                                        fracture mechanics analysis.
!
                                                                                                                                        '
'
                                                                !
_
                                                                    _                  Contract is being finalized. FAA will have basic
Contract is being finalized.
                                                                                        contract. Material Engineering Associates (MEA) will
FAA will have basic
                                                                                        be used as a subcontractor.
contract. Material Engineering Associates (MEA) will
I
be used as a subcontractor.
                                  (2) NRC
I
                                                          The NRC has hired Brookhaven National Laboratories to perform an
(2) NRC
                                                          independent metallurgical analysis of the failed elbow. The
The NRC has hired Brookhaven National Laboratories to perform an
                                                          tests being conducted are essentially the same as the VEPCO
independent metallurgical analysis of the failed elbow. The
                                                          Phase 1 tests. Tests are scheduled for completion about the same
tests being conducted are essentially the same as the VEPCO
                                                          time as the VEPCO Phase 1 tests.
Phase 1 tests. Tests are scheduled for completion about the same
                      10. Chemistry - Corrosion
time as the VEPCO Phase 1 tests.
                          a.       Introduction
10.
                                  A Region II chemistry specialist / inspector visited the Surry site
Chemistry - Corrosion
                                  on December 22-23, 1986 to examine the sections of the feedwater
a.
                                  suction lines from both units that had been exposed by the licensee
Introduction
                                  subsequent to the rupture in Unit 2. The inspector also reviewed
A Region II chemistry specialist / inspector visited the Surry site
                                  chemistry data that had been documented since the startup of Unit 2
on December 22-23, 1986 to examine the sections of the feedwater
                                  in 1973 to assess the chemistry control of the secondary water system
suction lines from both units that had been exposed by the licensee
                                  during the operational history of this unit. Based on the information
subsequent to the rupture in Unit 2.
                                  that is summarized below, the inspector evaluated the licensee's
The inspector also reviewed
chemistry data that had been documented since the startup of Unit 2
in 1973 to assess the chemistry control of the secondary water system
during the operational history of this unit. Based on the information
that is summarized below, the inspector evaluated the licensee's
preliminary theory that the pipe rupture was the result of extensive
-
-
'
'
                                  preliminary theory that the pipe rupture was the result of extensive
erosion / corrosion of the 18-inch suction line to a feedwater pump,
                                  erosion / corrosion of the 18-inch suction line to a feedwater pump,
:
:                                 especially in the vicinity of the intersection of this pipe and the
especially in the vicinity of the intersection of this pipe and the
i
i
                                  feedwater header.
feedwater header.
                          b.       Inspection
b.
                                                                                                                                                                    "
Inspection
                                  (1) Visual Inspection
(1) Visual Inspection
!                                                         (a) Unit 1 - On December 21, 1986, the licensee had cut out
"
!
(a) Unit 1 - On December 21, 1986, the licensee had cut out
:
:
the suction line to A feedwater pump from, and including,
'
'
                                                                                  the suction line to A feedwater pump from, and including,
the junction with the feedwater header to, and including, the
                                                                                  the junction with the feedwater header to, and including, the
isolation valve. The upstream portions of this pipe had been
                                                                                  isolation valve. The upstream portions of this pipe had been
further separated and stored indoors while the downstream
                                                                                  further separated and stored indoors while the downstream
segments had been stored in'the open overnight.
                                                                                  segments had been stored in'the open overnight.
The most significant observations were as follows:
                                                                                  The most significant observations were as follows:
An adhesive black film, conside, red to be Fe 034
                                                                                  -
-
                                                                                        An adhesive black film, conside, red to be Fe 034
'
i                                                                                        (magnetite), covered the inner ' surface of the junction
(magnetite), covered the inner ' surface of the junction
                                                                                        segment (i.e., approximately four feet of the header and
i
segment (i.e., approximately four feet of the header and
the 18-inch pipe past the. initial 90* bend) except in a
'
'
                                                                                        the 18-inch pipe past the. initial 90* bend) except in a
                                        '
, .-
, .-
                                                                                                                                                                                                  9
9
          . . . , _ _.     . _ . _ _ _ . . _ _ . , _ _ _ . _ _ _ _ _ . _ _                     - _ . _ _ _ . , _ . , _ _ - . . - . _ . _ , _ , , _ _ _ _ _ . - .             _ _ - . _     -_       _ _ _ , , _ . - .
. . . , _ _.
. _ . _ _ _ . . _ _ . , _ _ _ . _ _ _ _ _ . _ _
- _ . _ _ _ . , _ . , _ _ - . . - . _ . _ , _ , , _ _ _ _ _ . - .
_ _ - . _
-_
_ _ _ , , _ . - .


      *
*
  .,
.,
    *
*
  .
18
                                                                  18
.
                                          limited region in the lower part of the 90' bend. A
limited region in the lower part of the 90' bend. A
                                  -
-
                                          similar patch of black oxide was located on the surface
similar patch of black oxide was located on the surface
                                          of the second bend. Although there were small areas of
of the second bend. Although there were small areas of
.                                         black oxide in the other portions of the suction line,
.
                          ,
black oxide in the other portions of the suction line,
                          *
most inner surfaces were covered with a thin layer of
                                          most inner surfaces were covered with a thin layer of
,
                                _
_
                                          red powder that was assumed to be Fe O2 3 (hematite).
red powder that was assumed to be Fe O2 3 (hematite).
                                  -
*
                                          The weld bead that formed the inner junction of the
The weld bead that formed the inner junction of the
                                          header and 18-inch pipe had been worn smooth on the
-
                                          downstream side, and significant (approximately
header and 18-inch pipe had been worn smooth on the
                                          one quarter-inch) amounts of weld metal had been lost.
downstream side, and significant (approximately
                                  -
one quarter-inch) amounts of weld metal had been lost.
                                          The weld bead joining the upstream segment of the
The weld bead joining the upstream segment of the
                                          18-inch pipe to the first elbow had also been worn
-
                                          smooth except in the quadrant approximating the outer   *
18-inch pipe to the first elbow had also been worn
                                          portion of the bend in the elbow.
smooth except in the quadrant approximating the outer
                                  -
portion of the bend in the elbow.
                                          The weld discussed above also exhibited a scallop shaped
*
                                          depression that indicated a limited region of signifi-
The weld discussed above also exhibited a scallop shaped
                                          cant loss of metal. This gouged area was located
-
                                          in both the weld bead and adjacent pipe approximately
depression that indicated a limited region of signifi-
                                          90 degrees from the direction of flow in the header.
cant loss of metal.
                                  -
This gouged area was located
                                          An indication of a scratch or gauged area, approximately
in both the weld bead and adjacent pipe approximately
                                          0.5 inch x 12 inches was observed in the isolated black
90 degrees from the direction of flow in the header.
                                          region on the top (horizontal) side of the second elbow
An indication of a scratch or gauged area, approximately
                                          from the header.
-
                    (b) Unit 2 - After tne 18-inch suction line ruptured the licensee
0.5 inch x 12 inches was observed in the isolated black
                                  had cut out this line at the tee weld at the header and five
region on the top (horizontal) side of the second elbow
                                  feet downstream of the first elbow from the header. The
from the header.
                                  section of pipe that was removed included the failed region
(b) Unit 2 - After tne 18-inch suction line ruptured the licensee
                                  and the 2-ft. x 3-ft. hole formed by the expulsion of the
had cut out this line at the tee weld at the header and five
!                                 weakest section of the first elbow.
feet downstream of the first elbow from the header. The
                                  The exposed openings in the header and the 18-inch suction
section of pipe that was removed included the failed region
                                    line had been capped with plastic for protection against
and the 2-ft. x 3-ft. hole formed by the expulsion of the
                                  dust.
!
                                  The most significant observations relating to the feedwater
weakest section of the first elbow.
                                  header and the remaining section of the suction pipe are
The exposed openings in the header and the 18-inch suction
                                    listed below:
line had been capped with plastic for protection against
                                  -
dust.
                                          Approximately one inch *of water remained at the bottom
The most significant observations relating to the feedwater
(                                         of the header, and evidence of fresh rusting was
header and the remaining section of the suction pipe are
                                          observed beneath the water.
listed below:
Approximately one inch *of water remained at the bottom
-
(
of the header, and evidence of fresh rusting was
observed beneath the water.
I
I
                                                                            !
!
                                                                        '
'
                                                                      ,
,
                                                                                                Q
Q
        , - . . . - , . - - .             , . . - , , , . , , .
,
-
. . . -
, . - - .
, . . - , , , . , , .
w
-w
---y-,


        *
*
    .
.
      *
*
    ,                                    19
19
                      -
,
                            The entire length of the header from the upstream
The entire length of the header from the upstream
                            elbow to the most distant section downstream that
-
                            was visible with a flashlight was coated with red
elbow to the most distant section downstream that
                            iron oxide. The layer of oxide was not deep,
was visible with a flashlight was coated with red
                ,          however, and appeared as a film over roughened iron
iron oxide. The layer of oxide was not deep,
                  +
however, and appeared as a film over roughened iron
                    _       and was easily wiped off.
,
                      -
_
                            The nearest elbow on the header upstream from the
and was easily wiped off.
                            opening was black in color.
+
                      -
The nearest elbow on the header upstream from the
                            The downstream region of the inside bead of the weld
-
                            head that held the 18-inch pipe to the header was gouged
opening was black in color.
                            out in the same manner and location as observed in
The downstream region of the inside bead of the weld
                            Unit 1. Also, as in Unit 1, this weld bead had been
-
                            worn smooth with the pipe except on part of the upstream
head that held the 18-inch pipe to the header was gouged
                            side.
out in the same manner and location as observed in
                      -
Unit 1.
                            A concave area of approximately two inches in diameter
Also, as in Unit 1, this weld bead had been
                            had been formed immediately below the weld in the
worn smooth with the pipe except on part of the upstream
                            remaining stub of the 18-inch pipe.
side.
                      -
A concave area of approximately two inches in diameter
                            The inner surface of the initial foot of the downstream
-
                            run of the suction pipe was red in color while the
had been formed immediately below the weld in the
                            remainder of the visible portions were black. The line
remaining stub of the 18-inch pipe.
                            of demarcation was very sharp.
The inner surface of the initial foot of the downstream
                (c) Evidence of thinning
-
                      The licensee had completed detailed ultrasonic tests of the
run of the suction pipe was red in color while the
                      Unit 1 suction line to A pump so that profiles of pipe
remainder of the visible portions were black. The line
                      thickness were available to the inspector. These profiles
of demarcation was very sharp.
                      and visual evidence of thinning at the ends of cut out
(c) Evidence of thinning
                      sections of this 18-inch pipe showed clearly that widespread
The licensee had completed detailed ultrasonic tests of the
                      wastage had occurred from the header to several (approxi-
Unit 1 suction line to A pump so that profiles of pipe
                      mately 5) feet downstream of the first elbow from the header.
thickness were available to the inspector. These profiles
                      However, the thinning was no,t evident from the inner surfaces
and visual evidence of thinning at the ends of cut out
                      of the pipe beer.use the loss of metal had been very uniform,
sections of this 18-inch pipe showed clearly that widespread
                      as if polished with coarse emery cloth, even where the pipes
wastage had occurred from the header to several (approxi-
                      were red in color. The degradation of the welds at the tee
mately 5) feet downstream of the first elbow from the header.
                      junction and the single gouged region in each unit were the
However, the thinning was no,t evident from the inner surfaces
                      only obvious indications of metal having been removed in a
of the pipe beer.use the loss of metal had been very uniform,
                      non-uniform fashion.
as if polished with coarse emery cloth, even where the pipes
          (2) Audit of Chemistry Records                                       ,
were red in color. The degradation of the welds at the tee
                The inspector reviewed archived documentation of daily analyses of
junction and the single gouged region in each unit were the
                the condensate, feedwater, and reactor coolant from the startup of
only obvious indications of metal having been removed in a
                Unit 2 (March 1973) until the unit was sh,utdown in February 1979.
non-uniform fashion.
                                                      ,'
(2) Audit of Chemistry Records
,
The inspector reviewed archived documentation of daily analyses of
the condensate, feedwater, and reactor coolant from the startup of
Unit 2 (March 1973) until the unit was sh,utdown in February 1979.
,'
+o
+o
  -                                                                                 - - - - - - - - , . ,
-
.- --.
- - - . . - - . - . . _ , - - - . . -
. - - -
- - -
. - - - - - ,
.,
~ . - - - - . - - - . , . _
- - - - - - - - , . ,


                                          .                                                 -. .
.
                    .
-.
              .
.
                  '
.
            .
.
                                                                                      20
'
                              Through previous inspections, the inspector was already familiar
20
                          '
.
                              with the licensee's chemistry control subsequent to the replace-
Through previous inspections, the inspector was already familiar
                              ment of the steam generators in Unit 2; i.e., from 1980 to the
with the licensee's chemistry control subsequent to the replace-
                              present time.
'
                                                                                          '
ment of the steam generators in Unit 2; i.e., from 1980 to the
                                    4
present time.
                              As'_one of the first nuclear power plants constructed in the United
4
                              States, both units at Surry began operation with a chemistry
'
                              control program that included the use of hydrazine to control the
As'_one of the first nuclear power plants constructed in the United
:                             detrimental effect of dissolved oxygen - as an oxidant of carbon
States, both units at Surry began operation with a chemistry
                              steel pipe. For two years the licensee also had added phosphate
control program that included the use of hydrazine to control the
                              salts to the feedwater to control pH and to prevent attack of the
:
                              carbon steel by hydrogen ions. In 1975 the phosphate control
detrimental effect of dissolved oxygen - as an oxidant of carbon
steel pipe.
For two years the licensee also had added phosphate
salts to the feedwater to control pH and to prevent attack of the
carbon steel by hydrogen ions.
In 1975 the phosphate control
l
l
                              program had been discarded in favor of the use of ammonia in an
program had been discarded in favor of the use of ammonia in an
                              effort to minimize or eliminate denting of the tubes in the steam
effort to minimize or eliminate denting of the tubes in the steam
                              generator. During part of 1976-1977 cyclohexamine had been also -
generator. During part of 1976-1977 cyclohexamine had been also -
                              added for pH control but was soon replaced by the use of morpho-
added for pH control but was soon replaced by the use of morpho-
                              l i ne.. When the units started up after replacement of the steam
l i ne..
                              generators, the licensee, following the recommendation of the
When the units started up after replacement of the steam
                              Steam Generators Owners Group (SG0G), based the chemistry control
generators, the licensee, following the recommendation of the
                              on all-volatile-chemical treatment (AVT) with hydrazine and ammonia.
Steam Generators Owners Group (SG0G), based the chemistry control
on all-volatile-chemical treatment (AVT) with hydrazine and ammonia.
Because of the original design of the Surry units (copper-alloy
'
'
                              Because of the original design of the Surry units (copper-alloy
condenser tubes, absence of a condensate cleanup system, copper-
                              condenser tubes, absence of a condensate cleanup system, copper-
alloy feedwater heater tubes) and the relatively high salinity of
                              alloy feedwater heater tubes) and the relatively high salinity of
the condenser cooling water, control of secondary water chemistry
                              the condenser cooling water, control of secondary water chemistry
had been difficult, as indicated by the following examples:
                              had been difficult, as indicated by the following examples:
l
l
                              -
Intrusions of chloride ions in concentrations of tens of
                                            Intrusions of chloride ions in concentrations of tens of
-
parts per million (ppm) occurred several times in 1973,
i
i
                                            parts per million (ppm) occurred several times in 1973,
I
I                                          1975, 1977, and 1978 as the result of condenser tube
1975, 1977, and 1978 as the result of condenser tube
                                            failures. (The current upper limit recommended by the SGOG
failures.
                                            to prevent corrosive attack of iron pipe is 20 parts per
(The current upper limit recommended by the SGOG
                                            billion (ppb)).
to prevent corrosive attack of iron pipe is 20 parts per
          '                   -
billion (ppb)).
                                            During four weeks in 1975 the pH of the feedwater remained
'
                                            below a value 8, and thus ingreased the vulnerability of
During four weeks in 1975 the pH of the feedwater remained
                                            carbon steel pipe to corrosion by hydrogen ions (acid).           The
-
                                            SGOG recommends that the pH of the feedwater be maintained
below a value 8, and thus ingreased the vulnerability of
                                            between 8.8-9.2 in ferrous / copper systems such as were
carbon steel pipe to corrosion by hydrogen ions (acid).
                                            present in the Surry units prior to 1980.           In systems that
The
                                            do not contain copper components, the SGOG recommends that
SGOG recommends that the pH of the feedwater be maintained
                                            the feedwater be maintained in a more basic condition (pH
between 8.8-9.2 in ferrous / copper systems such as were
                                            of 9.3 to 9.6) to increase the electrochemical stability'of
present in the Surry units prior to 1980.
                                            iron in water and to minimize the dissolution of iron through
In systems that
                                            reaction with hydrogen ions (acids).
do not contain copper components, the SGOG recommends that
                              -
the feedwater be maintained in a more basic condition (pH
                                            During the period when cyclohexamine was used, the pH of
of 9.3 to 9.6) to increase the electrochemical stability'of
                                            the feedwater exceeded 9.5 and, occasionally even 10.0.
iron in water and to minimize the dissolution of iron through
                                            Although the higher pH benefited the! reduction of iron
reaction with hydrogen ions (acids).
                                            corrosion, it also caused accelerated corrosion of the
During the period when cyclohexamine was used, the pH of
                                            copper-bearing alloys in the co,ndenser and feedwater heater
-
                            '
the feedwater exceeded 9.5 and, occasionally even 10.0.
    .
Although the higher pH benefited the! reduction of iron
  . - --,~._,_____-_,,,,_     . - _ . _ -         _ _ _ ...__ _ __ , - _ . __ _ _ -_.-
corrosion, it also caused accelerated corrosion of the
copper-bearing alloys in the co,ndenser and feedwater heater
'
.
. - --,~._,_____-_,,,,_
. - _ . _ -
_ _ _ ...__ _ __ , - _ . __ _ _ -_.-
, . - . ,
- . _ . - , _ _ _ . . . , _ , _ _ _ _ _ _


                                                                          . .- .-             .
. .- .-
        .
.
    .
.
      .
.
    -
.
                                                                                                21
21
                                                      tubes. Inasmuch as copper ions in solution exacerbate
-
                                                    .several forms of chemical corrosion of carbon steel and alloy
tubes.
                                                      600 (Inconel), the SGOG recommends that the concentration of
Inasmuch as copper ions in solution exacerbate
                                                      copper in feedwater be kept below 2 ppb. The presence of
.several forms of chemical corrosion of carbon steel and alloy
                                                ,    higher concentrations of copper in the feedwater of the Surry
600 (Inconel), the SGOG recommends that the concentration of
                                                  _  units before 1980 was considered to be a major cause of the
copper in feedwater be kept below 2 ppb. The presence of
                                                      degradation of the original inconel steam generator tubes.
higher concentrations of copper in the feedwater of the Surry
                                                      The licensee replaced the copper alloy condenser tubes with
,
                                                      titanium during the steam generator replacement outage but is
units before 1980 was considered to be a major cause of the
                                                      only now planning the replacement of the feedwater heater
_
                                                      tubes with non-copper alloys.
degradation of the original inconel steam generator tubes.
                                            -
The licensee replaced the copper alloy condenser tubes with
                                                      Throughout the operational history of Unit 2 the licensee had
titanium during the steam generator replacement outage but is
                                                      observed the concentration of oxygen in the condensate and
only now planning the replacement of the feedwater heater
                                                      feedwater to have been less than the limit detectable by the
tubes with non-copper alloys.
                                                      most sensitive analytical instrumentation (except during 10
Throughout the operational history of Unit 2 the licensee had
                                                      days in 1975 when, because of seal failures, the concentra-
-
                                                      tion of oxygen increased to approximately 20 ppb.) The
observed the concentration of oxygen in the condensate and
                                                      inspector considered that the lowest detectable limit had
feedwater to have been less than the limit detectable by the
                                                      been 0-10 ppb during this period - which is consistent with
most sensitive analytical instrumentation (except during 10
                                                      the limiting concentration, 5 ppb, currently recommended by
days in 1975 when, because of seal failures, the concentra-
                                                      the SGOG. Control of oxygen had been maintained by the
tion of oxygen increased to approximately 20 ppb.) The
                                                      addition of hydrazine; however, during much of the early
inspector considered that the lowest detectable limit had
                                                      operating history the residual concentration of hydrazine had
been 0-10 ppb during this period - which is consistent with
                                                      been close to the detectable limits (approximately 5 ppb).
the limiting concentration, 5 ppb, currently recommended by
                                                      Currently the licensee adds sufficient hydrazine to ensure   -
the SGOG. Control of oxygen had been maintained by the
                                                      that the residual is greater than 20 ppb, as recommended by
addition of hydrazine; however, during much of the early
                                                      the SGOG, so that oxygen is quantitatively reduced and elimi-
operating history the residual concentration of hydrazine had
                                                      nated as an oxidant.
been close to the detectable limits (approximately 5 ppb).
                          (3) Conclusions
Currently the licensee adds sufficient hydrazine to ensure
l                                            The tee and upper elbow of the 18-inch pipe to the A feedwater
-
that the residual is greater than 20 ppb, as recommended by
the SGOG, so that oxygen is quantitatively reduced and elimi-
nated as an oxidant.
(3) Conclusions
l
l
                                            pump in both Surry units were visually observed to have been
The tee and upper elbow of the 18-inch pipe to the A feedwater
!                                           degraded through extensive thinning and severe, but localized,
l
(                                           gouging. However, the interrelationship between the roles of
pump in both Surry units were visually observed to have been
l                                           corrosion and erosion was not clear. The degree to which the
!
I                                             feedwater pipe had been protected against general corrosion by a
degraded through extensive thinning and severe, but localized,
                                              film of magnetite was difficult to establish because the pipes
(
                                            had been opened and exposed to moist air. Although general
gouging. However, the interrelationship between the roles of
                                            corrosion, as well as more localized forms of chemical attack,
l
                                            may have been aggravated by the occasional presence of corrosive
corrosion and erosion was not clear. The degree to which the
                                              impurities in the feedwater during the initial seven years of
I
                                              plant operation, there was no visual or ultrasonic evidence to
feedwater pipe had been protected against general corrosion by a
                                              support this speculation. A more comprehensive analysis of this
film of magnetite was difficult to establish because the pipes
                                              subject is presented in the Appendix to this report.
had been opened and exposed to moist air. Although general
                                                                                                      !
corrosion, as well as more localized forms of chemical attack,
                                                                                                    .-
may have been aggravated by the occasional presence of corrosive
  .
impurities in the feedwater during the initial seven years of
plant operation, there was no visual or ultrasonic evidence to
support this speculation. A more comprehensive analysis of this
subject is presented in the Appendix to this report.
!
.-
.
,
,
        , . - . . , - - .-
, . - . . , - - .
                          _ . _ . , - - , .       - .--,-,.,-.--,-.---.-_-------- --_- .-- ,
_ . _ . , - - , .
- .--,-,.,-.--,-.---.-_-------- --_- .-- ,
... ..---
-
-


                                                                                                                                                              -
-
                        *
*
                    .
.
                      .
.
                    *
*
                                                                                                        22
22
                          11.   Items Which Could Have Contributed to the Likelihood or Severity of the
11.
                                  Event
Items Which Could Have Contributed to the Likelihood or Severity of the
,                                a.     General
Event
                                                                                                              '
a.
                                          The inspectors reviewed system operating procedures, system maintenance
General
                                          history and the operating status of selected systems to determine those
,
                                          factors which contributed to the closure of the C steam generator
'
                                          main steam trip valve (MSTV TV-MS-201C) and the subsequent reactor trip
The inspectors reviewed system operating procedures, system maintenance
                                          and feedwater pipe ruture.
history and the operating status of selected systems to determine those
                                          (1). Plant Service Air / Instrument Air System (SA/IA)
factors which contributed to the closure of the C steam generator
                                                    The inspectors reviewed control room logs, interviewed control
main steam trip valve (MSTV TV-MS-201C) and the subsequent reactor trip
and feedwater pipe ruture.
(1). Plant Service Air / Instrument Air System (SA/IA)
The inspectors reviewed control room logs, interviewed control
i
i
                                                    room operators and examined equipment in the plant associated
room operators and examined equipment in the plant associated
                                                    with SA/IA system. This system supplies air to the air operated
with SA/IA system.
                                                    MSTVs. The air pressure supplied to the air operated cylinders
This system supplies air to the air operated
                                                    associated with each MSTV holds the MSTV open during normal plant
MSTVs. The air pressure supplied to the air operated cylinders
                                                    operation. The air pressure is automatically vented off the
associated with each MSTV holds the MSTV open during normal plant
                                                    operating cylinders following a trip signal or manually vented by
operation. The air pressure is automatically vented off the
                                                    the operator action. The MSTV will then shut, assisted by the
operating cylinders following a trip signal or manually vented by
                                                    steam flow acting on the value disc. Prior to the reactor trip,
the operator action. The MSTV will then shut, assisted by the
                                                    the operating status of the SA/IA system was as follows:
steam flow acting on the value disc. Prior to the reactor trip,
,
the operating status of the SA/IA system was as follows:
                                                    SA/IA blue auxiliary air compressor was in operation; the three
,
                                                    turbine building air compressors were in automatic mode, one was
SA/IA blue auxiliary air compressor was in operation; the three
                                                    off; one of the condensate polisher air compressors was floating
turbine building air compressors were in automatic mode, one was
i                                                   on the SA/IA system. System pressure indications as observed from
off; one of the condensate polisher air compressors was floating
                                                    the control room was approximately 100 psig (normal operating
i
                                                    range is 95-110 psig).
on the SA/IA system.
System pressure indications as observed from
the control room was approximately 100 psig (normal operating
range is 95-110 psig).
I
I
                                                    Planned maintenance was being performed on the SA/IA grey
Planned maintenance was being performed on the SA/IA grey
                                                    auxiliary compressor which consisted of the installation of a new
auxiliary compressor which consisted of the installation of a new
                                                    temperature sensing element. Following this maintenance, the grey
temperature sensing element.
                                                    compressor was scheduled to be placed in service. Both the blue
Following this maintenance, the grey
                                                    and grey air compressors share a. single power source. In order to
compressor was scheduled to be placed in service. Both the blue
                                                    position the transfer switch from the operating blue compressor to                                                       '
and grey air compressors share a. single power source.
                                                    the grey compressor, the electrical power supply is required to be
In order to
                                                    deenergized. Control room operators were aware of these operations
position the transfer switch from the operating blue compressor to
                                                    and were adjusting air flow from the condensate polisher air
'
                                                    system. System pressure decreased to approximately 85 psig as both
the grey compressor, the electrical power supply is required to be
                                                    blue and grey compressors were deenergized.
deenergized. Control room operators were aware of these operations
                                                    At the time of the reactor trip, control room operators noted that
and were adjusting air flow from the condensate polisher air
                                                    SA/IA system pressure was approximately 78 psig.                                                           Subsequent to
system. System pressure decreased to approximately 85 psig as both
                                                    the reactor trip, the blue air compressor was placed back into
blue and grey compressors were deenergized.
                                                    service.
At the time of the reactor trip, control room operators noted that
                                                                                                                                                            !
SA/IA system pressure was approximately 78 psig.
!                                                                                                                                             ,'
Subsequent to
            .
the reactor trip, the blue air compressor was placed back into
                                                                                                                                                                            _
service.
  _ , _ _ _ . . - -       _
!
                              _ .. . ,m_       . - _ _ . _ - . . _ . , - - - . - . . , , - - - - - - . - - , . - - - . - - _ - - _ _ _ . - - - - - . . - -
!
,'
.
_
_ , _ _ _ . . - -
_
_ .. . ,m_
. - _ _ . _ - .
. _ .
, - - - . - . . , , - - - - - - . - - , . - - - . - - _ - - _ _ _ . - - - - - . . - -
-
.
- - - - -


              _ _ _ _ _   _ ___                                   _ _ _ _   _______ _           _                   _ __   _ _ _ . _
_ _ _ _ _
                        '
_
            .
___
                  .
_
            '
_ _ _
                                                                            23
_______ _
                                                                                                                                          1
_
                                  Discussions with control room operators indicated that operating                                       ;
_ __
,                                  experience has shown that SA/IA receiver pressure has decreased as
_ _ _ .
'                                  low as 55 psig without any MSTV closing. As noted by this
_
                                  event, the only MSTV to close as a result of the lower instrument
'
                                  air pressure was the C MSTV.
.
                                                                                                                                          I
.
,                                The inspectors reviewed operating procedures for the SA/IA system.
'
                                  Discussions were also held with operators to determine adherence
23
                                  to procedures; no problems were identified.
Discussions with control room operators indicated that operating
'                                During December 15-19, 1986, the licensee tested and opened for
;
                                  inspection the C steam generator MSTV. The detailed inspection
experience has shown that SA/IA receiver pressure has decreased as
                                  and testing of the valve and the results are discussed in a
,
                                  separate paragraph in this report. The problem discovered during                                     ,
low as 55 psig without any MSTV closing. As noted by this
                                  this inspection, however, showed that the valve disc operator                           -
'
event, the only MSTV to close as a result of the lower instrument
air pressure was the C MSTV.
I
The inspectors reviewed operating procedures for the SA/IA system.
,
Discussions were also held with operators to determine adherence
to procedures; no problems were identified.
During December 15-19, 1986, the licensee tested and opened for
'
inspection the C steam generator MSTV.
The detailed inspection
and testing of the valve and the results are discussed in a
separate paragraph in this report. The problem discovered during
,
this inspection, however, showed that the valve disc operator
-
assembly had previously been assembled incorrectly and permitted
.
.
                                  assembly had previously been assembled incorrectly and permitted
the~ valve disc to be positioned in the steam flow path at an
                                  the~ valve disc to be positioned in the steam flow path at an
:
:
                                  angle greater than that allowed by design. This condition,
angle greater than that allowed by design. This condition,
j                                 coupled with the drop in SA/IA system air pressure prior to the
j
                                  reactor trip, appeared to have allowed rapid closure of the MSTV
coupled with the drop in SA/IA system air pressure prior to the
                                  by steam flow forces.                                                                                 '
reactor trip, appeared to have allowed rapid closure of the MSTV
by steam flow forces.
'
'
                                  Following the event, soap bubble air leak testing of instrument
Following the event, soap bubble air leak testing of instrument
                                  air piping and components to the C MSTV was conducted under
'
                                  normal system pressure condition. No significant leakage was
air piping and components to the C MSTV was conducted under
                                  identified that would have affected MSTV air operated cylinder
normal system pressure condition. No significant leakage was
identified that would have affected MSTV air operated cylinder
operation.
,
,
                                  operation.
(2) C Main Steam Trip Valve (MSTV).
                            (2) C Main Steam Trip Valve (MSTV).
The action which initiated the reactor trip and subsequent
                                  The action which initiated the reactor trip and subsequent
feedwater rupture was the inadvertent closing of the C MSTV.
i                                  feedwater rupture was the inadvertent closing of the C MSTV.
i
I                                A review of the maintenance history indicated this valve was
I
I
                                  overhauled during the most recent refueling outage in November
A review of the maintenance history indicated this valve was
overhauled during the most recent refueling outage in November
I
1986. On November 27, 1986, following the overhaul, the valve
i
i
i
i
                                  1986. On November 27, 1986, following the overhaul, the valve
position limit switch was adjusted and the valve was cold-cycled
'
'
                                  position limit switch was adjusted and the valve was cold-cycled
satisfactorily per Periodic Test 14.2.
                                  satisfactorily per Periodic Test 14.2.                 On November 29, 1986, with
On November 29, 1986, with
                                  Unit 2 in hot standby, the C MSTV was again cycled, and the
Unit 2 in hot standby, the C MSTV was again cycled, and the
                                  valve failed to open fully. The reactor operator generated a Work
valve failed to open fully. The reactor operator generated a Work
                                  Order 046251, which indicated that the C MSTV was binding and
Order 046251, which indicated that the C MSTV was binding and
                                  capable of only partially opening. That same day, November 29,
capable of only partially opening. That same day, November 29,
                                  1986, it was determined that the cause of the C MSTV was nots
1986, it was determined that the cause of the C MSTV was nots
                                  fully opening because of water in the valve. The next operating
fully opening because of water in the valve. The next operating
                                  shift drained the water and successfully cycled the valve on                                           '
shift drained the water and successfully cycled the valve on
                                  November 30, 1986. However, Work Order 046251 remained open
'
                                  because the valve appeared to operate somewhat differently from
November 30, 1986. However, Work Order 046251 remained open
                                  the other MSTVs, even though it met its intended safety function
because the valve appeared to operate somewhat differently from
                                  as required by Technical Specifications.
the other MSTVs, even though it met its intended safety function
                                                                                            '
as required by Technical Specifications.
                                                                                            .
'
                                                                                        e
.
        =
e
  _. . _ _ _ _ _ _                      . _ _ _ _ _ _ _ _ _ _ _ -_                                  _ _ _ _. _ ._ _ _
=
. .    
.
-
.
.


                                                                                                                                    ___         _ _ _ - _ _ , _ _ .
___
            .
_ _ _ -
    .
_ _ , _ _ .
          .
.
    .
.
                                                                                24
.
                                              Following the event and the initial AIT inspection, the C MSTV
24
.
Following the event and the initial AIT inspection, the C MSTV
was released to the licensee for inspection and testing. The
,
,
                                              was released to the licensee for inspection and testing. The
licensee developed a detailed testing and inspection program
                                              licensee developed a detailed testing and inspection program
to determine the cause of the valve's inadvertent closure.
                                              to determine the cause of the valve's inadvertent closure.
The results of this program are as follows:
                                              The results of this program are as follows:
Prior to disassembly, the valve was cycled and determined
                                                    Prior to disassembly, the valve was cycled and determined
to only open approximately 62 degrees. Normal full open
                                                    to only open approximately 62 degrees. Normal full open
position should be 80 +2 degrees.
                                                    position should be 80 +2 degrees. Disassembly of the valve
Disassembly of the valve
                                                    revealed the valve cover had been installed one stud or
revealed the valve cover had been installed one stud or
                                                    approximately 15 degrees off. This cover has a stop tube
approximately 15 degrees off.
                                                    welded to it which normally limits valve disc travel to 80
This cover has a stop tube
                                                    +2 degrees when going full open. With the cover installed
welded to it which normally limits valve disc travel to 80
                                                    approximately 15 degrees off, the stop tube was positioned
+2 degrees when going full open. With the cover installed
                                                    such that it limited the disc travel to only 62 degrees which
approximately 15 degrees off, the stop tube was positioned
                                                    left the disc approximately 25% from the full open position,
such that it limited the disc travel to only 62 degrees which
                                                    exposing the disc to the closing force of main steam flow.
left the disc approximately 25% from the full open position,
                                                    This pragram also revealed that the radius lever had been
exposing the disc to the closing force of main steam flow.
i                                                   installed on the rock shaft one spline tooth off, which would
This pragram also revealed that the radius lever had been
i
installed on the rock shaft one spline tooth off, which would
!
!
                                                    have limited valve travel to 75 degrees had it not been for
have limited valve travel to 75 degrees had it not been for
                                                    the valve cover misalignment. This also would leave a
the valve cover misalignment.
                                                    portion of the disc exposed to the closing force of the steam
This also would leave a
                                                    flow. The misalignment of the radius lever also contributed
portion of the disc exposed to the closing force of the steam
                                                    to the failure of the C MSTV closed limit switch to indicate
flow.
                                                    that the valve had closed. During testing, the licensee
The misalignment of the radius lever also contributed
                                                    determined that placement of the radius lever up one spline
to the failure of the C MSTV closed limit switch to indicate
                                                    tooth prevented the limit switch from fully engaging in the
that the valve had closed. During testing, the licensee
                                                    closed position. A maintenance history review revealed that
determined that placement of the radius lever up one spline
l                                                   the limit switch was adjusted before the valve was retested
tooth prevented the limit switch from fully engaging in the
                                                    after maintenance. This adjustment appeared to be on the
closed position. A maintenance history review revealed that
l
the limit switch was adjusted before the valve was retested
after maintenance. This adjustment appeared to be on the
i
i
lower limit switch, but a complete determination of what was
'
'
                                                    lower limit switch, but a complete determination of what was
actually adjusted could not be made dua to lack of documenta-
                                                    actually adjusted could not be made dua to lack of documenta-
tion. The operation of the closed limit switch was deter-
                                                    tion. The operation of the closed limit switch was deter-
mined to be intermittent. During the cold and hot cycle, the
                                                    mined to be intermittent. During the cold and hot cycle, the
switch was depressed enough ,to actuate. But during and
                                                    switch was depressed enough ,to actuate. But during and
following the event, the switch, even though engaged, was not
                                                    following the event, the switch, even though engaged, was not
depressed enough to actuate, although only slight additional
                                                    depressed enough to actuate, although only slight additional
movement caused the closed limit switch to actuate.
                                                    movement caused the closed limit switch to actuate.
Several observations can be made based on the licensee's inves-
                                              Several observations can be made based on the licensee's inves-
tigation into the C MSTV closure.
                                              tigation into the C MSTV closure. The maintenance procedure
The maintenance procedure
                                              MMP-C-MS-002 used for overhaul of C MSTV was not correctTy '
MMP-C-MS-002 used for overhaul of C MSTV was not correctTy '
                                              followed. The procedure was inadequate in that it did not
followed.
                                              prevent, nor did the post maintenance testing discover the
The procedure was inadequate in that it did not
                                              improper assembly of the C MSTV. The licensee failed to
prevent, nor did the post maintenance testing discover the
                                              document all the non-routine work associated with this valve
improper assembly of the C MSTV. The licensee failed to
                                              overhaul. A review of MMP-C-MS-002 shows that step 5.4.8 which
document all the non-routine work associated with this valve
                                              reinstalls the radius levers does not prdvide adequate instruc-
overhaul. A review of MMP-C-MS-002 shows that step 5.4.8 which
                                              tions to maintenance personnel or quality control (QC) inspectors
reinstalls the radius levers does not prdvide adequate instruc-
                                                                                                                            *
tions to maintenance personnel or quality control (QC) inspectors
                                                                                                                        .
*
  ~~
.
                                                                                                                                                                      .
~~
      __     __ _ _ _ _ . _ _ _ _ _ . _ __ =       _ . _ - . - _ , , _ . _ . _
.
                                                          -
__
                                                                                _ _ . - _ _ _ , , _ . _ _ _ , _ _ . - _ _ - _ _ _ _ . , . _ , ,                     - - _ _ _ - . - , , _
.
.
=
_ . _ - . - _ , , _ . _ . _
_ _ . - _ _ _ , , _ . _ _ _ , _ _ . - _ _ - _ _ _ _ . , . _ , ,
-
- _ _ _ - . - , , _
-


      '
'
  .
.
    .
.
  -
25
                                      25
-
            as to the proper reinstallation alignment. Investigation by the
as to the proper reinstallation alignment.
            licensee revealed that the maintenance person reinstalling the
Investigation by the
            valve decided, based on comments from a QC inspector, to reinstall                                   ,
licensee revealed that the maintenance person reinstalling the
            the radius lever up one spline tooth from the previous installa-
valve decided, based on comments from a QC inspector, to reinstall
            ti,on. This decision was made without any documentation or
,
            engineering review. This decision alone resulted in limiting
the radius lever up one spline tooth from the previous installa-
            valve travel to only 75 degrees exposing the disc to steam flow
ti,on. This decision was made without any documentation or
            and appears to be the cause of the failure of the closed limit
engineering review. This decision alone resulted in limiting
            switch to operate.
valve travel to only 75 degrees exposing the disc to steam flow
            Step 5.4.12 required the QC inspector to check and record the arc
and appears to be the cause of the failure of the closed limit
            of valve travel. The recorded data was 80 degrees - although
switch to operate.
            the licensee determined after the event that it was only 75
Step 5.4.12 required the QC inspector to check and record the arc
            degrees. The inaccurate documentation appears to be a result of
of valve travel. The recorded data was 80 degrees - although
            the QC inspector performing this verification by visual check                                       <
the licensee determined after the event that it was only 75
            only. Since the step calls for a quantitative result, the step
degrees. The inaccurate documentation appears to be a result of
            should have required that some type of instrumentation be used to
the QC inspector performing this verification by visual check
            determine the arc of the valve travel. Also, the QC inspector
<
            should not have documented it as 80 degrees unless there was a
only. Since the step calls for a quantitative result, the step
            means of precise verification.
should have required that some type of instrumentation be used to
            Although Step 5.4.15 required replacement of the valve cover, the
determine the arc of the valve travel. Also, the QC inspector
            step does not mention anything about cover alignment; specifi-
should not have documented it as 80 degrees unless there was a
            cally, there is no mention of any problem that cculd result from
means of precise verification.
            cover misalignment. This would have illustrated the importance of
Although Step 5.4.15 required replacement of the valve cover, the
            proper alignment. The inadequacy of the step resulted in the
step does not mention anything about cover alignment; specifi-
            misalignment of the cover, preventing full travel of the valve
cally, there is no mention of any problem that cculd result from
            disc, and leaving the disc exposed to the closing force of steam
cover misalignment. This would have illustrated the importance of
            flow.
proper alignment. The inadequacy of the step resulted in the
            Finally, step 6.3 requires a post maintenance test be performed
misalignment of the cover, preventing full travel of the valve
            which only tested the operation of the valve based on the open and
disc, and leaving the disc exposed to the closing force of steam
            closed limit switches. This test, PT-14.2, does not verify full
flow.
            valve disc travel, and therefore was not adequate to verify proper
Finally, step 6.3 requires a post maintenance test be performed
            valve reassembly. However, it should be noted that the test was
which only tested the operation of the valve based on the open and
            adequate to verify the safety function of the valve which is to
closed limit switches. This test, PT-14.2, does not verify full
            close. Also this test was used to verify that the valve was in
valve disc travel, and therefore was not adequate to verify proper
            compliance with Technical Specifications.
valve reassembly. However, it should be noted that the test was
            The fact that the C MSTV was reassembled so that the disc was
adequate to verify the safety function of the valve which is to
            always exposed to the closing forces steam flow, coupled with the
close. Also this test was used to verify that the valve was in
compliance with Technical Specifications.
The fact that the C MSTV was reassembled so that the disc was
always exposed to the closing forces steam flow, coupled with the
;
;
low air pressure, resulted in the inadvertent closure of the C
'
'
            low air pressure, resulted in the inadvertent closure of the C
MSTV.
            MSTV.   This inadvertent closure of the C MSTV resulted in a
This inadvertent closure of the C MSTV resulted in a
            reactor scram but did not contribute to or cause the rupture of
reactor scram but did not contribute to or cause the rupture of
            the main feed piping. This rupture would have happened during any
the main feed piping. This rupture would have happened during any
            normal pressure transient of the feedwater system. Even though
normal pressure transient of the feedwater system. Even though
:           the inadvertent closure of the C MSTV did not cause the feed
:
!           line rupture and the safety function of t,he valve along with
the inadvertent closure of the C MSTV did not cause the feed
                                                    -
!
                                                  .
line rupture and the safety function of t,he valve along with
          3
-
                                                                                                              9
.
        .                                               - - - - . - - . - _ . - - . _ , _ - - . . - - . - _.       .
3
9
--
.
-
.
-
-.
,-.
-. .,
.-
- - - - . - - . - _ . - - . _ , _ - - . . - - . - _.
.


                                                      _ . __
_ . __
            *
*
    .
.
          '
'
    .
26
                                                              26
.
                          compliance witti Technical Specifications were verified, the
compliance witti Technical Specifications were verified, the
                          fact.that the valve was reassembled in such a way that it resulted
fact.that the valve was reassembled in such a way that it resulted
                          in an inadvertent reactor scram and a challenge to the unit's
in an inadvertent reactor scram and a challenge to the unit's
                          safety system is still a significant problem.
safety system is still a significant problem.
                          TkchnicalSpecification6.'4.Arequiresthatdetailedwritten
TkchnicalSpecification6.'4.Arequiresthatdetailedwritten
                          procedures with appropriate check-off lists and instructions shall
procedures with appropriate check-off lists and instructions shall
                          be provided for preventive or corrective maintenance operation
be provided for preventive or corrective maintenance operation
                          which would have an effect on the safety of the reactor. The
which would have an effect on the safety of the reactor. The
                          failure of the licensee to fully follow procedures, provide
failure of the licensee to fully follow procedures, provide
                          adequate instruction for and document the performance of maintence
adequate instruction for and document the performance of maintence
                          operations involved in the performance of the procedure to over-
operations involved in the performance of the procedure to over-
                          haul the C MSTV will be identified as Violation 50-281/86-42-02.
haul the C MSTV will be identified as Violation 50-281/86-42-02.
                    (3) Feedwater Pump Discharge Check Valve (No. 2-N-127)
(3) Feedwater Pump Discharge Check Valve (No. 2-N-127)
                          Dur,ing the initial investigation of the feedwater pipe rupture
Dur,ing the initial investigation of the feedwater pipe rupture
                          event, an abnormal pressure transient of the A MN pump suction
event, an abnormal pressure transient of the A MN pump suction
                          piping was suspected to be the cause of the rupture. For such a
piping was suspected to be the cause of the rupture. For such a
                          pressure transient to occur, the A MN pump discharge check
pressure transient to occur, the A MN pump discharge check
                          valve (2-N-127) would have had to be permitted flow in the
valve (2-N-127) would have had to be permitted flow in the
                          reverse direction. Since this was a potential cause of the pipe
reverse direction.
                          rupture, a review of the maintenance history and an internal
Since this was a potential cause of the pipe
                          inspection was conducted on the check valve (2-N-127).
rupture, a review of the maintenance history and an internal
                          A review of the maintenance history on this particular check valve       -
inspection was conducted on the check valve (2-N-127).
                          revealed that the valve was scheduled to be inspected in late
A review of the maintenance history on this particular check valve
  '
-
                          1984. The licensee decided not to inspect the valve, based
revealed that the valve was scheduled to be inspected in late
                          on a satisfactory inspection perforced on a Unit 1 feed pump
1984. The licensee decided not to inspect the valve, based
                          discharge system check valve and on the operational history of the
'
                          valve. It should also be noted that during the startup prior to
on a satisfactory inspection perforced on a Unit 1 feed pump
                          this event, the B main feed pump was operated with the A main
discharge system check valve and on the operational history of the
                          feed pump secured. There was no mention of a problem with high
valve.
                          feed pump suction pressures, and the A main feed pump was
It should also be noted that during the startup prior to
                          started successfully on December 5, 1986.
this event, the B main feed pump was operated with the A main
                          The licensee disassembled 2-N-12'7 after the event.           Inspection
feed pump secured.
                          of the internals showed the disc was not fully seated. One of the
There was no mention of a problem with high
                          two hinge pins was missing, and the valve seat was displaced. The
feed pump suction pressures, and the A main feed pump was
                          condition of the check valve at the time of the inspection would
started successfully on December 5, 1986.
                          have allowed for flow in the reverse direction. The licensee has
The licensee disassembled 2-N-12'7 after the event.
                          been able to determine, based on the operation of the A and B
Inspection
                          main feed pumps, that reverse flow tarough the A main feed p~ ump
of the internals showed the disc was not fully seated. One of the
                          did not occur at the time of the' event. As discussed in the
two hinge pins was missing, and the valve seat was displaced. The
                          sequence of events paragraph that the A main feed pump was still
condition of the check valve at the time of the inspection would
                          operating after pipe rupture.         Therefore, flow past the check
have allowed for flow in the reverse direction. The licensee has
                          valve into A feed pump suction piping could not have occurred
been able to determine, based on the operation of the A and B
                          prior to the pipe rupture. This conclusion strengthens the
main feed pumps, that reverse flow tarough the A main feed p~ ump
                          supposition that the feed water pipe ruptfured during a normal
did not occur at the time of the' event. As discussed in the
                          pressure transient and that back flow past the chec' valve did
sequence of events paragraph that the A main feed pump was still
                          not cause a pressure spike which resulted in the pipe rupture.
operating after pipe rupture.
                                                                                                  .
Therefore, flow past the check
valve into A feed pump suction piping could not have occurred
prior to the pipe rupture. This conclusion strengthens the
supposition that the feed water pipe ruptfured during a normal
pressure transient and that back flow past the chec' valve did
not cause a pressure spike which resulted in the pipe rupture.
.
t
t
      - .     -.       ,_     , _ - - . . . - _   ,
- .
                .-7                            -   ,_
-.
.-7
,_
, _ - - . . . - _
,
,_
_--,_c._
.,.,,_._.,r___.-
--
.
-
- - -
- . . - - _ . - _ _ , , - _ . _ _ _ . - - -
--
-


                                                      __     _         _
__
      -
_
  .
_
    *
-
  .
.
                                            27
*
                However, the condition of the check valve would have contributed
27
                to the amount of feed water which exited the feed line break
.
                and possibly the extent of the pipe whip after the event. The
However, the condition of the check valve would have contributed
                  licensee has inspected the other Unit 1 and Unit 2 feed pump
to the amount of feed water which exited the feed line break
                ch;eck valves and discovered additional discrepancies (see para-
and possibly the extent of the pipe whip after the event.
                graph 15.c.). The condition of each of these valves at the time
The
                of inspection was such that they would have performed properly and
licensee has inspected the other Unit 1 and Unit 2 feed pump
                not allowed significant reverse flow.
ch;eck valves and discovered additional discrepancies (see para-
            (4) Feedwater System Maintenance History
graph 15.c.).
                A review of recent feed water system maintenance history did not
The condition of each of these valves at the time
                  reveal any identified problems with the A or B main feed pump
of inspection was such that they would have performed properly and
                  suction piping. The licensee has identified some problems with
not allowed significant reverse flow.
                the feed water system such as pin hole leaks which were associated
(4) Feedwater System Maintenance History
A review of recent feed water system maintenance history did not
reveal any identified problems with the A or B main feed pump
suction piping.
The licensee has identified some problems with
the feed water system such as pin hole leaks which were associated
with erosion, but these problems were located in the feed water
'
'
                with erosion, but these problems were located in the feed water
pump, discharge recirculation piping. While the licensee did not
                pump, discharge recirculation piping. While the licensee did not
have a program to inspect the feedwater piping for thickness, it
                have a program to inspect the feedwater piping for thickness, it
does have a formal ultrasonic inspection program to determine
                does have a formal ultrasonic inspection program to determine
thickness for the following secondary system areas:
                  thickness for the following secondary system areas:
Turbine Exhaust Cross Under Piping
                -
-
                        Turbine Exhaust Cross Under Piping
1st and 2nd Point Extraction System
                -
-
                        1st and 2nd Point Extraction System
3rd and 4th Point Extraction System
                -
-
                        3rd and 4th Point Extraction System
Moisture Separation Drain Liner
                -
-
                        Moisture Separation Drain Liner
Moisture Separator Reheater Inlet Piping
                -
-
                        Moisture Separator Reheater Inlet Piping
- (5) Safety System Equipment Review
        - (5) Safety System Equipment Review
!
!               A discussion with the Superintendent of Operations and a review of
A discussion with the Superintendent of Operations and a review of
i
i
                  pertinent documents - i.e., plan of the day, the tagging log, the
pertinent documents - i.e., plan of the day, the tagging log, the
                  reactor operator's log, the shift. supervisor's log and the minimum
reactor operator's log, the shift. supervisor's log and the minimum
                equipment list for criticality and power operation checklist--
equipment list for criticality and power operation checklist--
                  indicated that all safety-related equipment required to support
indicated that all safety-related equipment required to support
                  unit operation was operable.   The only safety-related equipment
unit operation was operable.
                  problems indentified prior to the event were (1) the inoperability
The only safety-related equipment
                of one of the three charging pumps (only two are required to be
problems indentified prior to the event were (1) the inoperability
                  operable by technical specifications); and (2) a service water
of one of the three charging pumps (only two are required to be
                  pump which was operable but listed in an alert condition.       '
operable by technical specifications); and (2) a service water
                  During the event, all safety systems responded as required.
pump which was operable but listed in an alert condition.
                These systems include the operation of the reactor protection
'
During the event, all safety systems responded as required.
These systems include the operation of the reactor protection
system (RPS), the steam generator safety relief valves and the
a
a
'
'
                  system (RPS), the steam generator safety relief valves and the
auxiliary feedwater system. The secondary power-operated relief
                  auxiliary feedwater system. The secondary power-operated relief
-
                                                            -
.
                                                          .
Q
                                                                                    Q
.e>-ww-
                                                                                      .e>-ww- w---- - - - v-v--
w----
- - -
v-v--


        _       _ _ .     _     _     __             . _ _ _ _       _ _     . .       -
_
                                                                                                  . _ _ __ _ .- _ ._
_ _ .
              *
_
          .
_
            *
__
          .
. _ _ _ _
_
_
.
.
-
. _ _ __ _ .- _ ._
*
.
*
.
'
'
                                                                      28
28
                                          valves (PORVs) were in the manual mode of operation. The opera-
valves (PORVs) were in the manual mode of operation. The opera-
                                          tors.took manual control of the secondary PORVs to control steam
tors.took manual control of the secondary PORVs to control steam
                                          generator pressure, allowing the secondary relief valves to shut
generator pressure, allowing the secondary relief valves to shut
                                          and to control the removal of decay heat in the primary plant.
and to control the removal of decay heat in the primary plant.
                                            _
_
                                                                                                                    ,
,
;                                          The only equipment which did not respond as required was (1)
The only equipment which did not respond as required was (1)
;
.
control rod (M-10) which indicated 35 steps for a short time
'
'
.
following the reactor trip before indicating fully inserted;
                                          control rod (M-10) which indicated 35 steps for a short time
!
                                          following the reactor trip before indicating fully inserted;
(2) the fire protection system which spuriously initiated as
*
*
!                                        (2) the fire protection system which spuriously initiated as
discussed in paragraph 13; (3) the instrumentation which failed
                                          discussed in paragraph 13; (3) the instrumentation which failed
to indicate closure of the C MSTV as discussed in paragraph
,
,
                                          to indicate closure of the C MSTV as discussed in paragraph
:
:
11.a.(2); and (4) the security door card readers which failed as
6
6
                                          11.a.(2); and (4) the security door card readers which failed as
discussed in paragraph 13.b.
                                          discussed in paragraph 13.b.
t
t                           b.     Review of Maintenance Activities Being Performed Prior to the Event
b.
                                  Discussions with licensee personnel and review of the maintenance
Review of Maintenance Activities Being Performed Prior to the Event
:                                 activities being conducted prior to the event did not indicate any
Discussions with licensee personnel and review of the maintenance
]'                                 maintenance activities which would have contributed to the initiation
:
                                  or resulted in the feed water pipe rupture. Maintenance activities
activities being conducted prior to the event did not indicate any
j                                 being conducted by the individuals who were injured were unrelated to
]'
l                                 the feed water system rupture and would not have contributed to the
maintenance activities which would have contributed to the initiation
                                  cause of the event.
or resulted in the feed water pipe rupture. Maintenance activities
j
being conducted by the individuals who were injured were unrelated to
l
the feed water system rupture and would not have contributed to the
cause of the event.
i
i
                      12.   Licensee's Response to the Event
12.
Licensee's Response to the Event
4
4
                            a.     Operator Response
a.
                                  The response of the operators to the initial reactor trip and later
Operator Response
                                  pipe rupture was excellent. The break was isolated rapidly. The only
The response of the operators to the initial reactor trip and later
!                                 problem that occurred was a control rod gave an indication of not
pipe rupture was excellent. The break was isolated rapidly. The only
i                                  being fully inserted by 35 steps. Emergency procedures were followed
!
i                                  quickly and orderly to assure adequate shutdown margin. It should be
problem that occurred was a control rod gave an indication of not
                                  noted that the licensee has conducted tests with the plant in a cold
                                  condition, but has been unable to duplicate this rod position
i
i
'                                  anomaly. The licensee intends to conduct additional testing during
being fully inserted by 35 steps.
                                  startup.
Emergency procedures were followed
                            b.     Emergency Response
i
                                  The inspectors discussed various aspects of the licensee's response
quickly and orderly to assure adequate shutdown margin.
                                                                                                            ~
It should be
                                  to the feedwater pipe rupture with licensee employees. The first
noted that the licensee has conducted tests with the plant in a cold
                                  person responding to the accident was a senior instrument technician
condition, but has been unable to duplicate this rod position
                                  who had been perfor'ning quarterly calibrations on security equipment.
i
                                  He responded to a station security call for first aid assistance to the
anomaly. The licensee intends to conduct additional testing during
                                  Unit 2 truck bay. Upon arrival, one injured employee was observed
'
                                  leaving the accident area. The technician escorted the individual to
startup.
                                  the high level intake structure and set up a triage area. Three                   .
b.
                                  additional personnel subsequently exited the decident area and were               '
Emergency Response
                                                                                .
The inspectors discussed various aspects of the licensee's response
                                                                              .
~
  6 .n
to the feedwater pipe rupture with licensee employees.
The first
person responding to the accident was a senior instrument technician
who had been perfor'ning quarterly calibrations on security equipment.
He responded to a station security call for first aid assistance to the
Unit 2 truck bay.
Upon arrival, one injured employee was observed
leaving the accident area. The technician escorted the individual to
the high level intake structure and set up a triage area. Three
additional personnel subsequently exited the decident area and were
.
'
.
.
6 .n
- - - . - . -
- - , - - - - . , . .
,
.


                          _     _ _ _ _ . _ _ _ _ _ _                       _ _ _ _ _ _ _ _ _ _ __               _     ___     _- _ _
_
                                                                                                                                        l
_ _ _ _ . _ _ _ _ _ _
        .
_ _ _ _ _ _ _ _ _ _ __
    .
_
      .
___
    -
_- _
                                                                          29
_
l
.
.
.
29
-
.
.
i
i
                                      given first aid by the team that was present. The technician unsuc-
given first aid by the team that was present. The technician unsuc-
                                      cessfully attempted to contact the Unit 2 Control Room using a security
cessfully attempted to contact the Unit 2 Control Room using a security
                                        radio. The technician then proceeded to the maintenance services area
radio. The technician then proceeded to the maintenance services area
                                        to call for assistance. Upon arrival, the technician discovered two
to call for assistance. Upon arrival, the technician discovered two
                                      additional accident victims. The technician used the plant page system
additional accident victims. The technician used the plant page system
                                                                                                                                        ,
j
                                                        '
,
                                                                                                                                        j
'
                                        to notify the control room who called in offsite medical support,                               i
to notify the control room who called in offsite medical support,
                                        including two medical evacuation helicopters and two local rescue
                                        squads.
                                      The licensee prepared the victims for transport and moved them to the
                                        licensee's heliport, located behind the training building. The three
i
i
                                      most seriously injured personnel were air evacuated to hospital burn
including two medical evacuation helicopters and two local rescue
                                        units while three were transported by ambulance.
squads.
                                        Licensee personnel interviewed following the event have stated that                     <     !
The licensee prepared the victims for transport and moved them to the
,                                      the site's emergency team functioned extremely well and was well
licensee's heliport, located behind the training building.
The three
most seriously injured personnel were air evacuated to hospital burn
i
units while three were transported by ambulance.
Licensee personnel interviewed following the event have stated that
!
<
the site's emergency team functioned extremely well and was well
,
-
-
                                      coordinated. Further, licensee representatives have stated that the
coordinated.
i                                     Alert was declared so that a personnel accountability could be made
Further, licensee representatives have stated that the
i                                     because it was not kncwn at the time of the event how many people
i
                                        had been in the area when the feedwater pipe ruptured.
Alert was declared so that a personnel accountability could be made
i
because it was not kncwn at the time of the event how many people
had been in the area when the feedwater pipe ruptured.
The inspector reviewed the actions required by the licensee's emergency
.
.
                                      The inspector reviewed the actions required by the licensee's emergency
plan and determined that the actions taken by the licensee were in
                                      plan and determined that the actions taken by the licensee were in
accordance with the actions specified in the plan.
4
4
                                      accordance with the actions specified in the plan.
!
!                              c.       Emergency Information Activities
c.
Emergency Information Activities
'
'
                                      The accident spurred extensive interest from the media in the immediate
The accident spurred extensive interest from the media in the immediate
                                      plant area, throughout Virginia,=and-nationwide. Virginia Power issued - -
plant area, throughout Virginia,=and-nationwide. Virginia Power issued - -
                                        its first press release slightly more than an hour after the declara-
its first press release slightly more than an hour after the declara-
!                                       tion of the alert.     This initial announcement was followed by several
!
                                      others later in the day and into the evening.                     Follow-up announcements
tion of the alert.
                                      were issued the next few days. In accordance with the company emer-
This initial announcement was followed by several
                                      gency information policy, Virginia Power began steps to open the
others later in the day and into the evening.
                                        near-site media center in the Surry, Virginia, Community Center.
Follow-up announcements
were issued the next few days.
In accordance with the company emer-
gency information policy, Virginia Power began steps to open the
4
4
!                                    Because the Alert was cancelled before,the media center was fully
near-site media center in the Surry, Virginia, Community Center.
l                                     operational, reporters were briefed at the emergency operations
Because the Alert was cancelled before,the media center was fully
!
l
operational, reporters were briefed at the emergency operations
!
!
                                        facility at the site. Virginia Power also opened its main media center
facility at the site. Virginia Power also opened its main media center
i                                     at company headquarters in Richmond and issued information from there
i
                                        for several days thereafter.
at company headquarters in Richmond and issued information from there
                                      The day after the accident press conferences were held at noon at.the
for several days thereafter.
                                      on-site training facility and at the Richmond media center. An NRC
The day after the accident press conferences were held at noon at.the
l                                     public affairs officer went to the site with the Augmented Inspection
on-site training facility and at the Richmond media center. An NRC
i                                     Team. He answered telephone media inquiries from the resident
l
                                        inspector's office and participated in three press conferences with
public affairs officer went to the site with the Augmented Inspection
;                                     Virginia Power. NRC also responded to inquiries received by the public
i
                                      affairs offices in the Region II office and in, Headquarters.
Team. He answered telephone media inquiries from the resident
inspector's office and participated in three press conferences with
;
Virginia Power. NRC also responded to inquiries received by the public
affairs offices in the Region II office and in, Headquarters.
;
;
1                                                                                                     .             .
1
'
.
                                                                                                    .
.
  -
'
.
-
,
,
,
                                                                                                                              ,
-----.,,n---,-,_,.--
          -----.,,n---,-,_,.--                           -,,
-,,
--~n
, - - . - - , , , . - . , - - -
- - - - - - - - - - - . -
---


        '
'
    .
.
      .
.
    .
30
                                                      30
.
                  In addition to written announcements, news briefings, and answers to
In addition to written announcements, news briefings, and answers to
                  telephone inquiries, Virginia Power also made available to reporters
telephone inquiries, Virginia Power also made available to reporters
                  both videotapes and still pictures of the accident scene.
both videotapes and still pictures of the accident scene.
                  Both NRC and Virginia Power continued for several weeks to respond to
Both NRC and Virginia Power continued for several weeks to respond to
                  media 'imquiries about the accident and the followup investigations. A
media 'imquiries about the accident and the followup investigations. A
                  briefing of NRC by Virginia Power on January 12, 1987, attracted media
briefing of NRC by Virginia Power on January 12, 1987, attracted media
                  coverage, as did a technical meeting convened in NRC Headquarters on
coverage, as did a technical meeting convened in NRC Headquarters on
                  January 15. Virginia Power on January 22 held a special media briefing
January 15.
                  on the results of its investigation. NRC received numerous requests
Virginia Power on January 22 held a special media briefing
                  from reporters and for copies of the AIT report.
on the results of its investigation. NRC received numerous requests
          13. Aspects That Made Handling The Event More Difficult
from reporters and for copies of the AIT report.
              a. Security System / Personnel Actions
13. Aspects That Made Handling The Event More Difficult
                  (1) At,the time the pipe ruptured, water and steam saturated a
a.
                        security card reader located approximately fifty feet from the
Security System / Personnel Actions
                        break point and shorted out the entire plant card reader system.
(1) At,the time the pipe ruptured, water and steam saturated a
                        As a result, key-cards would not open plant doors. Security
security card reader located approximately fifty feet from the
                        personnel responded to the control room and provided access
break point and shorted out the entire plant card reader system.
                        control while doors into the control room were opened for easy
As a result, key-cards would not open plant doors.
                        access and to improve control room ventilation. Guards admitted
Security
                        personnel on the basis of personal recognition. The Senior
personnel responded to the control room and provided access
                        Resident Inspector reported observing that plant management and
control while doors into the control room were opened for easy
                        operations personnel were immediately admitted by the guards and
access and to improve control room ventilation. Guards admitted
                        nonessential personnel were excluded. The card reader system
personnel on the basis of personal recognition. The Senior
                        returned to service approximately 20 minutes after the pipe break
Resident Inspector reported observing that plant management and
                        and functioned normally thereafter. An operator reported being
operations personnel were immediately admitted by the guards and
                        delayed in the stairway outside the control room as a result of
nonessential personnel were excluded. The card reader system
I                       the card reader failure. Due to the hot water conditions on the
returned to service approximately 20 minutes after the pipe break
                        turbine building basement floor and the discharge of Halon fire
and functioned normally thereafter. An operator reported being
                        suppression system in the emergency switchgear rooms below the
delayed in the stairway outside the control room as a result of
!                       control room and the carbon dioxide fire suppression system in the
I
                        cable tray rooms above the control room, the operator had no safe
the card reader failure. Due to the hot water conditions on the
                        way to exit the stairway other than the control room itself. The
turbine building basement floor and the discharge of Halon fire
l                        operator was admitted to the control room by someone opening the
suppression system in the emergency switchgear rooms below the
l                        door from inside the control room. The licensee is considering                      *
!
!                        installing electronic override switches which would permit the
control room and the carbon dioxide fire suppression system in the
(                        opening of electronically locked doors in emergency situations.
cable tray rooms above the control room, the operator had no safe
way to exit the stairway other than the control room itself. The
l
l
l                        Plant management personnel reported that security provided fast
operator was admitted to the control room by someone opening the
                        and excellent support during the emergency.
                                                                                      '
                  (2) The security radio repeater is. located in cable tray room 1
                        (turbine building elevation 45), which is equipped with a Cardox
                        fire suppression system. As a result of steam infiltrating
                        various electrical systems this Cardox system was activated and
                        the full volume of Cardox was discharged!into the room. The
                        security repeater, located approximately five feet from a Cardox
                        discharge nozzle, failed and was la,ter found to be covered with a
  .
l
l
                            ._- ___ _ -__     _ _ _ _ - _
door from inside the control room. The licensee is considering
                                                                . ___ _.. _ -___-_.-.     - _ _ _ _ - - _ _
*
!
installing electronic override switches which would permit the
(
opening of electronically locked doors in emergency situations.
l
l
Plant management personnel reported that security provided fast
and excellent support during the emergency.
'
(2) The security radio repeater is. located in cable tray room 1
(turbine building elevation 45), which is equipped with a Cardox
fire suppression system. As a result of steam infiltrating
various electrical systems this Cardox system was activated and
the full volume of Cardox was discharged!into the room. The
security repeater, located approximately five feet from a Cardox
discharge nozzle, failed and was la,ter found to be covered with a
.
l
._- ___ _
-__
_ _ _ _ -
_
.
..
-
- .-.
- _ _ _ _ - - _ _


                            -                                                               _ - - _ . .   -               --
-
          *
_ - - _
      .
. .
      .'                                       31
-
                    thick layer of ice. As a result, security communications were
--
                    limited to the non-repeater or " simplex" mode. Since the hand-
*
                    held security radios have only four watts of transmitting power,
.
  ,
.'
  '
31
                    some communications clarity was lost between units inside
thick layer of ice. As a result, security communications were
                    buildings. Loss of the radio repeater may also have prevented
limited to the non-repeater or " simplex" mode.
                    cohtact with the Unit 2 control room by the first responder as
Since the hand-
                    described in paragraph 12.b.
held security radios have only four watts of transmitting power,
              (3) A truck carrying water coolers containing ice was the only
some communications clarity was lost between units inside
                    vehicle admitted to the protected area during the emergency.
,
                    While the truck was processed expeditiously, it was not processed
'
                    as an emergency vehicle, which would have allowed its immediate
buildings. Loss of the radio repeater may also have prevented
                    entry. This resulted from the lack of information available to
cohtact with the Unit 2 control room by the first responder as
                    security personnel at the vehicle gate about the exact nature
described in paragraph 12.b.
                    of the emergency and lack of understanding that the truck was
(3) A truck carrying water coolers containing ice was the only
                    bringing in ice and ice water for use in treating the burn
vehicle admitted to the protected area during the emergency.
                    v i ct,i m s . The licensee has recognized the importance of ensuring
While the truck was processed expeditiously, it was not processed
                    that personnel functioning in a supporting role know what is
as an emergency vehicle, which would have allowed its immediate
                    happening so they may better understand and, therefore, better
entry. This resulted from the lack of information available to
                    respond to tasks they are given or situations as they arise.
security personnel at the vehicle gate about the exact nature
              (4) One security badge /keycard was temporarfly lost during the
of the emergency and lack of understanding that the truck was
                    emergency. Badges were retrieved from five victims before they
bringing in ice and ice water for use in treating the burn
                    were transported from the site, but the badge on one individual
v i ct,i m s . The licensee has recognized the importance of ensuring
                    was overlooked. As part of the personnel accountability process,
that personnel functioning in a supporting role know what is
                    security realized that one badge, belonging to one of the                                                   -
happening so they may better understand and, therefore, better
                    victims, was unaccounted for. That badge was deleted from the
respond to tasks they are given or situations as they arise.
                    access control computer and computer records were checked to
(4) One security badge /keycard was temporarfly lost during the
                    ensure that the badge had not been.used since the accident.                                         The
emergency.
                    individual's wife found the badge on his shirt at the hospital
Badges were retrieved from five victims before they
                    and the badge was returned to the plant the morning following
were transported from the site, but the badge on one individual
                    the accident.
was overlooked. As part of the personnel accountability process,
'
security realized that one badge, belonging to one of the
              (5) At the time of the pipe break, two security shifts were on duty,
-
                    which permitted security to provide a great deal of manpower to
victims, was unaccounted for. That badge was deleted from the
                    support the plant. The inspector, determined that one security
access control computer and computer records were checked to
                    shift could have provided the manpower to perform the actions
ensure that the badge had not been.used since the accident.
                    taken by security during this event. The security force, however,
The
individual's wife found the badge on his shirt at the hospital
and the badge was returned to the plant the morning following
the accident.
'
(5) At the time of the pipe break, two security shifts were on duty,
which permitted security to provide a great deal of manpower to
support the plant. The inspector, determined that one security
shift could have provided the manpower to perform the actions
taken by security during this event.
The security force, however,
:
:
would have had to suspend all routine activities if only one
'
'
                    would have had to suspend all routine activities if only one
shift had been available.
                    shift had been available.
.
(6) The Surry security organization has examined its performance
'
'
.
and identified ten areas in which improvements can and should be
              (6) The Surry security organization has examined its performance
made.
                    and identified ten areas in which improvements can and should be
Recommendations in these areas were submitted to both
                    made.     Recommendations in these areas were submitted to both
security and plant management for evaluation and possible
                    security and plant management for evaluation and possible
implementation on December 19, 1986.
                    implementation on December 19, 1986.
b.
            b. Fire Protection System Actuations and Main Control Room Habitability
Fire Protection System Actuations and Main Control Room Habitability
                                                                                          l
l
              Within minutes of the feedwater pipe rupture event in the Unit 2
Within minutes of the feedwater pipe rupture event in the Unit 2
              turbine building, portions of the Unit 2 turbine building sprinkler
turbine building, portions of the Unit 2 turbine building sprinkler
I
I
              system actuated.     Sixty-two sprinkler hea'ds opened in the immediate
system actuated.
    .
Sixty-two sprinkler hea'ds opened in the immediate
                                                            - - _ - , . - - .- - - - - _ _             --
.
                                                                                                              . . _ _ - _
- - _ - , . - - .- - - - - _ _
. . _ _ - _
.
--


  -           . - . - - - -.       ~.   . - -   . -   - . - - - - - - - - . -                   _ - -   .
-
            , -
. - . - - - -.
        ,
~.
.
- -
. -
- . - - - - - - - - . -
_ - -
.
, -
,
4
4
!
!
          -
-
        ,
32
                                                                32
,
i
i
i                             area of the feedwater pipe rupture due to the high heat levels                   !
i
area of the feedwater pipe rupture due to the high heat levels
3
3
'                              associated with the event. As they opened, these sprinkler heads
associated with the event. As they opened, these sprinkler heads
'                             immediately began discharging water to cool the turbine building
'
                              atmosphere.
immediately began discharging water to cool the turbine building
'
atmosphere.
,
,
!                             As a result of the sprinkler wa'ter and feedwater discharge, the carbon
!
                              dioxide and the Halon fire suppression system control panels were
As a result of the sprinkler wa'ter and feedwater discharge, the carbon
                              affected. The carbon dioxide fire suppression system control panels
dioxide and the Halon fire suppression system control panels were
;                             for both Units 1 and 2 cable tray rooms are located near the Unit 2
affected. The carbon dioxide fire suppression system control panels
i                             cable tray room access door along the column line 9 wall on elevation
;
j                             45'-0". The sprinkler water discharge from the sprinkler heads
for both Units 1 and 2 cable tray rooms are located near the Unit 2
                              directly over and adjacent to these panels intruded into the carbon
i
                                                                                                                ,
cable tray room access door along the column line 9 wall on elevation
j
45'-0".
The sprinkler water discharge from the sprinkler heads
1
1
                                                                                                                '
,
directly over and adjacent to these panels intruded into the carbon
'
dioxide fire suppression system control panels through multiple open
;
;
                              dioxide fire suppression system control panels through multiple open
i
i
conduit ends which extend from the panels to the cable tray raceway
'
'
                              conduit ends which extend from the panels to the cable tray raceway
above. As a result, the water intrusion into these panels caused the -
                              above. As a result, the water intrusion into these panels caused the -
time limit switches to short-circuit in the closed position. When
                              time limit switches to short-circuit in the closed position. When
!
!
                              these switches closed the carbon dioxide fire suppression systems, at
these switches closed the carbon dioxide fire suppression systems, at
i                             approximately 2:32 p.m. (12 minutes into the event) the Robertshaw fire
i
l                             protection panel / printer in the main control room recorded the initial
approximately 2:32 p.m. (12 minutes into the event) the Robertshaw fire
                              discharge of the Unit 2 cable tray room carbon dioxide fire suppression
l
j                             system. In addition, at approximately 2:34 p. m. (14 minutes into the
protection panel / printer in the main control room recorded the initial
l'
discharge of the Unit 2 cable tray room carbon dioxide fire suppression
                              event) the Robertshaw panel recorded the second discharge of carbon
j
'
system.
                              dioxide into the Unit 2 cable tray room. It should be noted that the
In addition, at approximately 2:34 p. m. (14 minutes into the
                              bulk of carbon dioxide discharge was in the Unit I cable tray room,
l
event) the Robertshaw panel recorded the second discharge of carbon
'
dioxide into the Unit 2 cable tray room.
It should be noted that the
bulk of carbon dioxide discharge was in the Unit I cable tray room,
'
which was noticed by the licensee's loss prevention staff who c'onducted
-
-
                              which was noticed by the licensee's loss prevention staff who c'onducted
i
i
the personnel search and initiated the venting of carbon dioxide from
'
'
                              the personnel search and initiated the venting of carbon dioxide from
the cable tray rooms. The Robertshaw fire protection panel / printer did
                              the cable tray rooms. The Robertshaw fire protection panel / printer did
;
;
                              not register a Unit I discharge throughout the duration of the pipe
not register a Unit I discharge throughout the duration of the pipe
rupture event. Thus, as a result of the water affecting the time
.
.
                              rupture event. Thus, as a result of the water affecting the time
limit switches in the carbon dioxide control panels, the discharge
!
!
                              limit switches in the carbon dioxide control panels, the discharge
timers did not function as designed. As a result, a total of 17 tons
                              timers did not function as designed. As a result, a total of 17 tons
.
.                             of carbon dioxide was discharged into the cable tray rooms,
of carbon dioxide was discharged into the cable tray rooms,
i
i
'
'
                              In addition, the Halon fire suppression system protecting Units 1
In addition, the Halon fire suppression system protecting Units 1
l                             and 2 emergency switchgear rooms on elevation 9'-6" actuated at approx-
l
and 2 emergency switchgear rooms on elevation 9'-6" actuated at approx-
imately 3:02 p.m. (42 minutes into the, event as documented by the
;
;
                              imately 3:02 p.m. (42 minutes into the, event as documented by the
!
!                              Robertshaw panel printer). The Halon system actuation was caused
Robertshaw panel printer). The Halon system actuation was caused
j                             by sprinkler water discharge and feedwater runoff which flowed under
j
;                             the elevation 27'-0" fire door No. 30 installed in the column line 9
by sprinkler water discharge and feedwater runoff which flowed under
;                             wall. The water runoff cascaded down the column line 9 wall, which
;
the elevation 27'-0" fire door No. 30 installed in the column line 9
;
wall. The water runoff cascaded down the column line 9 wall, which
:
:
                              separates Units 1 and 2 turbine buildings, on the Unit 1 side, entered
separates Units 1 and 2 turbine buildings, on the Unit 1 side, entered
                              a Halon system conduit through a conduit fitting which had the fitting
a Halon system conduit through a conduit fitting which had the fitting
                              cover plate removed at the time of the event. The specific conduit
cover plate removed at the time of the event.
3                              fitting is located directly below the open grating floor on the Unit 1
The specific conduit
fitting is located directly below the open grating floor on the Unit 1
3
side of the elevation 27'-0" column line 9 wall fire door No. 30. The
;
;
                              side of the elevation 27'-0" column line 9 wall fire door No. 30. The
l
l                              runoff water which entered the subject conduit flowed through the
runoff water which entered the subject conduit flowed through the
j                             conduit and into Halon control panel 1-FPH-CP-1 located on the Unit 1
j
J                             side of the column line 9 wall on elevation 9'-6". This water intru-
conduit and into Halon control panel 1-FPH-CP-1 located on the Unit 1
!                             sion caused short-circuiting of the time limit!, battery charger and the
J
side of the column line 9 wall on elevation 9'-6".
This water intru-
!
sion caused short-circuiting of the time limit!, battery charger and the
t
t
                                                                                    *
*
                                                                                  .
.
    4=
4=
                                                                                                            .
.


                                                                                                            -   - -
-
          '
- -
      .
-
        .
'
      .                                                       33
.
                      dual zone modules. With the shorting of the dual zone modules, which
.
                      are associated with the manual remote actuation circuit located in
33
                      the control room, the Halon system actuated discharging 7 percent to                                 i
.
                      10 percent Halon concentration into the emergency switchgear rooms.                                   !
dual zone modules. With the shorting of the dual zone modules, which
                                                                  '
are associated with the manual remote actuation circuit located in
                      Since H'alon extinguishing agent is heavier than air, thi, discharge
the control room, the Halon system actuated discharging 7 percent to
                      into the emergency switchgear rooms on elevation 9'-6" had essentially
i
                      no effect on the habitability of the main control room. Upon the
10 percent Halon concentration into the emergency switchgear rooms.
                      initial discharge of the emergency switchgear Halon fire suppression                                 i
!
                      system some Halon leakage into the main control room through floor
Since H'alon extinguishing agent is heavier than air, thi, discharge
                      penetrations in the Unit I computer room and through the control room
'
                      emergency air bottle discharge piping was noticed. However, it should
into the emergency switchgear rooms on elevation 9'-6" had essentially
                      be noted that these concentrations of Halon which resulted from the
no effect on the habitability of the main control room. Upon the
                      emergency switchgear room discharge would not have put the control room
initial discharge of the emergency switchgear Halon fire suppression
                      personnel at risk.
i
                      Upon verification of the carbon dioxide system discharge by the main
system some Halon leakage into the main control room through floor
                      control room personnel, two nembers of the licensee's loss prevention
penetrations in the Unit I computer room and through the control room
                      staff entered the cable tray rooms with self contained breathing
emergency air bottle discharge piping was noticed. However, it should
                      apparatus to conduct a search for personnel. As a part of this search,
be noted that these concentrations of Halon which resulted from the
                      measures were tsken to vent the carbon dioxide from the cable tray                                   ,
emergency switchgear room discharge would not have put the control room
                      rooms by opening the doors to the Units 1 and 2 mechanical equipment                                 '
personnel at risk.
                      rooms and the respective cable tray room access doors located on
Upon verification of the carbon dioxide system discharge by the main
                      elevation 45'-0" of the Units 1 and 2 turbine buildings.                 In addition,
control room personnel, two nembers of the licensee's loss prevention
                      while the carbon dioxide was being vented from the cable tray rooms,
staff entered the cable tray rooms with self contained breathing
                      the main control room annex door in the turbine building / control room
apparatus to conduct a search for personnel. As a part of this search,
                      complex wall and the main control room door separating the annex from
measures were tsken to vent the carbon dioxide from the cable tray
                      the main control room were blocked open. Thus, carbon dioxide being
,
                      heavier than air, flowed down from elevation 45'-0" to elevation 27'-0"
rooms by opening the doors to the Units 1 and 2 mechanical equipment
                      and into the main control room annex and the main control room through                               ,
'
                      the open doors. In addition, during the time the carbon dioxide was
rooms and the respective cable tray room access doors located on
                      being vented from the cable tray rooms, the main control room exhaust
elevation 45'-0" of the Units 1 and 2 turbine buildings.
;                    fan (1-VS-F-15) was operating. The operation of this fan created e
In addition,
i                     negative pressure in the main control room and the main control room
while the carbon dioxide was being vented from the cable tray rooms,
                      annex thus, causing the vented carbon dioxide to be drawn into the
the main control room annex door in the turbine building / control room
                      control room complex.                         ,
complex wall and the main control room door separating the annex from
                                                                                                                            i
the main control room were blocked open. Thus, carbon dioxide being
heavier than air, flowed down from elevation 45'-0" to elevation 27'-0"
and into the main control room annex and the main control room through
,
the open doors.
In addition, during the time the carbon dioxide was
being vented from the cable tray rooms, the main control room exhaust
fan (1-VS-F-15) was operating.
The operation of this fan created e
;
i
negative pressure in the main control room and the main control room
annex thus, causing the vented carbon dioxide to be drawn into the
control room complex.
i
,
1
1
'                    Presence of carbon dioxide in the control room can also be attributed                                 i
l
                      to the fact that at the time of the event control room ventilation                                   L
Presence of carbon dioxide in the control room can also be attributed
                ~
i
                      unit 1-VS-AC4 was out of service for design modifications and that a                                 l
'
                      temporary unit which obtained its makeup air from mechanical equipment
to the fact that at the time of the event control room ventilation
,                   room I was in service. Therefore, when carbon dioxide vented from the                                 !
L
l                     respective cable tray room came into the mechanical equipment room',
~
l                     this allowed the te.nporary control room HVAC fan unit to draw the gas                               r
unit 1-VS-AC4 was out of service for design modifications and that a
l
temporary unit which obtained its makeup air from mechanical equipment
,
room I was in service. Therefore, when carbon dioxide vented from the
!
l
respective cable tray room came into the mechanical equipment room',
l
this allowed the te.nporary control room HVAC fan unit to draw the gas
r
into the control room ventilation system.
I
I
                      into the control room ventilation system.
Control room personnel in the main control room annex and near the
                      Control room personnel in the main control room annex and near the
1
1                     main control room door experienced shortness of breath, dizziness and
main control room door experienced shortness of breath, dizziness and
                      nausea. But it should be noted that once theyl recognized that carbon                                 :
nausea. But it should be noted that once theyl recognized that carbon
                      dioxide was present the control room operators took the appropriate                                   '
:
                      corrective actions and initiated control , room emergency air supply
'
                        '
dioxide was present the control room operators took the appropriate
  .-
corrective actions and initiated control , room emergency air supply
                                                                                                          ,
'
I--~~..     _ _ - _ _    m , _.- - - ...__,,_..._,_-m.__.~...       _ _ _ _ . _ . , _ , _ - _               ,
.-
                                                                                                                    . m_-.
,
I - - ~ ~ . .
-
m
, _.- - -
...__,,_..._,_-m.__.~...
.
.
, _ , _ - _
,
.
m_-.


                        _.       .__. __         _                           . _ . _ .           _.     ..
_.
              '
.__. __
          .
_
            .
. _ . _ .
          .
_.
                                                                                              34
..
                              fans 1-VSF-41 and 2-VSF-41. The starting of these fans placed the main
                              control room at a higher pressure than the turbine building. This
'
'
                              action assisted in diluting and exhausting the existing carbon dioxide
.
                              levels and kept any additional carbon dioxide from infiltrating into
.
                              themajncontrolroom.                                               .
34
                              As a result of the spurious fire protection system actuations associ-
.
                              ated with the feedwater pipe break event, the licensee has proposed
fans 1-VSF-41 and 2-VSF-41. The starting of these fans placed the main
                              the following carbon dioxide /Halon fire protection system modifica-
control room at a higher pressure than the turbine building.
                              tions:
This
                              (1) Seal the open ends of all conduits leading to the carbon dioxide
action assisted in diluting and exhausting the existing carbon dioxide
                                            system control panels throughout the plant.
'
                              (2) Replace all components within both the Unit 1 and Unit 2 cable
levels and kept any additional carbon dioxide from infiltrating into
                                            tray room carbon dioxide control panels that show visible signs
themajncontrolroom.
q                                           of corrosion.
.
As a result of the spurious fire protection system actuations associ-
ated with the feedwater pipe break event, the licensee has proposed
the following carbon dioxide /Halon fire protection system modifica-
tions:
(1) Seal the open ends of all conduits leading to the carbon dioxide
system control panels throughout the plant.
(2) Replace all components within both the Unit 1 and Unit 2 cable
tray room carbon dioxide control panels that show visible signs
q
of corrosion.
.
.
!
!
                              (3) Fully test both systems to confirm proper system operation.
(3) Fully test both systems to confirm proper system operation.
1
1
l                             (4) Seal the Unit I control panel. A 1-1/2-inch hole and a 1 inch
l
                                            hole exist in the right side wall near the bottom of the panel.
(4) Seal the Unit I control panel. A 1-1/2-inch hole and a 1 inch
                              (5) Replace missing 2-inch conduit cover under the elevation 27'-0"
hole exist in the right side wall near the bottom of the panel.
(5) Replace missing 2-inch conduit cover under the elevation 27'-0"
turbine building column line 9 wall platform and walk down all
,
,
'
'
                                            turbine building column line 9 wall platform and walk down all
other conduits to ensure that covers to conduit, pull boxes, and
                                            other conduits to ensure that covers to conduit, pull boxes, and
junction boxes are in place and properly sealed.
                                            junction boxes are in place and properly sealed.
i
i
                              (6) Repair door seal on the Halon control panel and relocate
(6) Repair door seal on the Halon control panel and relocate
!                                           identification sign,
!
identification sign,
i
i
!
!
                              (7) Replace all existing Halon panel modules which are no longer
(7) Replace all existing Halon panel modules which are no longer
i                                           manufactured and upgrade these modules to current state-of-the-art
i
                                            equipment
manufactured and upgrade these modules to current state-of-the-art
equipment
<
<
j                             (8) Perform functional tests of the H.alon system for both units 1
j
                                            and 2 emergency switchgear rooms to ensure proper operation.
(8) Perform functional tests of the H.alon system for both units 1
                              (9) Replace Halon system check valves in discharge lines or replace
and 2 emergency switchgear rooms to ensure proper operation.
j                                           rubber seals.
(9) Replace Halon system check valves in discharge lines or replace
l                         (10) Have all Halon cylinder heads replaced or reworked to ensure,
j
,                                          bottles will not leak and that seals are in good condition.
rubber seals.
                          (11) Have Halon bottles filled and placed in discharge header.
l
                          (12) Have Halon pressure switch covers and solenoid covers removed and
(10) Have all Halon cylinder heads replaced or reworked to ensure,
bottles will not leak and that seals are in good condition.
,
(11) Have Halon bottles filled and placed in discharge header.
(12) Have Halon pressure switch covers and solenoid covers removed and
I
I
                                            inspect for corrosion or water damage. ,
inspect for corrosion or water damage.
                                                                                                        .
,
                                                                                                      .
.
                                  4
.
  ..
4
l
l
'.                                                                                                               *
..
I                                                                                                                                     <
'.
    -- - -       . - _.     . _ . -_. - . .               - . - - - _ . _ - - . - - _ _ _ . .               .. -   _ _ _ . _ _ _ _ -
*
I
<
-- - -
. - _.
.
. - . - . .
- . - - -
.
- - . - -
. .
.. -
.
-


          ..           .                   ,.     - .           _   -   . - - - - -
..
                                                                                                -
.
    '
,.
  .
- .
  ,-                                                 35
_
                  Based on our review of the above modifications, it appears that upon
-
                  their completion the probabilities of spurious cable tray room carbon
. - - - - -
                  dioxide and emergency switchgear room fire suppression system actua-
-
                  tions due to water / steam intrusion will be greatly reduced. However,
'
                    it is our recommendation that the licensee, in addition to implementing
.
                  the abo,ve proposed modifications, consider the following with respect
,-
                  to ensurthg control room habitability and personnel safety:
35
                  -
Based on our review of the above modifications, it appears that upon
                          Install a wintergreen odorizer on the Units 1 and 2 cable tray
their completion the probabilities of spurious cable tray room carbon
                          room carbon dioxide system,
dioxide and emergency switchgear room fire suppression system actua-
                  -
tions due to water / steam intrusion will be greatly reduced. However,
                          Install a permanent oxygen analyzer with a control room audible
it is our recommendation that the licensee, in addition to implementing
                          alarm in the main control room annex,
the abo,ve proposed modifications, consider the following with respect
                  -
to ensurthg control room habitability and personnel safety:
                          Develop a procedure which will require the control room operators-
Install a wintergreen odorizer on the Units 1 and 2 cable tray
'                          to pressurize the control room in the event of a gaseous fire
-
                          suppression system actuation in either the cable tray room or the
room carbon dioxide system,
                          emerge.ncy switchgear rooms, and
Install a permanent oxygen analyzer with a control room audible
                  -
-
                          Install predischarge visual and audible warning devices near the
alarm in the main control room annex,
                          Units 1 and 2 cable tray room doors and inside the cable tray
Develop a procedure which will require the control room operators-
                          rooms which will activate to alert personnel prior to a carbon
-
                          dioxide system discharge.
l
to pressurize the control room in the event of a gaseous fire
'
suppression system actuation in either the cable tray room or the
emerge.ncy switchgear rooms, and
Install predischarge visual and audible warning devices near the
-
Units 1 and 2 cable tray room doors and inside the cable tray
rooms which will activate to alert personnel prior to a carbon
dioxide system discharge.
c.
Other System Interactions
,
,
              c.  Other System Interactions
.
.
i                 There does not appear to have been other significant system interac-
i
                  tions which impeded the safe shutdown of the plant. All shutdown
There does not appear to have been other significant system interac-
                  systems responded as designed, and an orderly plant cooldown was
tions which impeded the safe shutdown of the plant. All shutdown
                  accomplished.
systems responded as designed, and an orderly plant cooldown was
accomplished.
l
l
14. Consideration of Shut Down of Unit 1
At 12:30 p.m. on December 10, licensee management decided to shut down Surry
Unit 1 and operation of the unit was placed on power ramp down at 5:30 p.m.
The unit was subsequently cooled down and pl, aced on residual heat removal
and is currently in a cold shutdown condition.
The decision to shut down the unit was based on preliminary findings
resulting from the Unit 2 main feed pump suction pipe rupture. These
findings indicated that there might have been significant thinning of the
l
l
l      14. Consideration of Shut Down of Unit 1
pipe wall due to a corrosion / erosion mechanism not fully understood at the
              At 12:30 p.m. on December 10, licensee management decided to shut down Surry
time. The shutdown plan included inspections of selected Unit 1 piping.to
              Unit 1 and operation of the unit was placed on power ramp down at 5:30 p.m.
ascertain its condition with regard to pipe wall thinning.
              The unit was subsequently cooled down and pl, aced on residual heat removal
Subsequent ultrasonic examination of the identical elbow that failed in
              and is currently in a cold shutdown condition.
Unit 2 revealed similar but not as severe pipe wall thinning.
              The decision to shut down the unit was based on preliminary findings
!
              resulting from the Unit 2 main feed pump suction pipe rupture. These
*
              findings indicated that there might have been significant thinning of the
.
l            pipe wall due to a corrosion / erosion mechanism not fully understood at the
O
              time. The shutdown plan included inspections of selected Unit 1 piping.to
O
              ascertain its condition with regard to pipe wall thinning.
e
              Subsequent ultrasonic examination of the identical elbow that failed in
              Unit 2 revealed similar but not as severe pipe wall thinning.
                                                                    !
                                                                *
                                                              .
                      O
                                                                                          O
                                                                                              e


    -             . _                 .-                 . _ .-                                             .-                                                   - .                       - . - -
-
              .
. _
      .
.-
            .
. _ .-
      -
.-
                                                                                                                      36
-
                                    The licensee gave priority to Unit 1 inspection and hardware replacement in
.
                                    parallel with its investigation to determine the root cause of the Unit 2
- . - -
                                    pipe rupture. This was done in order to facilitate restart of Unit 1.
.
                          15.     Investigatipns and Corrective Actions Taken
.
                                                                                ~
.
                                    a.               Initial Activity
36
                                                      The licensee agreed to a quarantine of all equipment and systems
-
,                                                    which could be significant to the ongoing investigation of the event.
The licensee gave priority to Unit 1 inspection and hardware replacement in
                                                      Consequently, all activities undertaken with regard to restoration work
parallel with its investigation to determine the root cause of the Unit 2
                                                      or investigations were done with the concurrence of the NRC team on
pipe rupture. This was done in order to facilitate restart of Unit 1.
                                                      site. During the first week following the event, . concurrence was given
15.
                                                      for some turbine generator work on the turbine deck which was not
Investigatipns and Corrective Actions Taken
                                                      relevant to the investigation and work involving cleanup and restora--
~
                                                      tion of the damaged area. The following equipment was inspected:
a.
,                                                    (1) A main feed pump suction indication in the control room pegged at
Initial Activity
                                                                        1000 psi. The pressure transmitter associated with this indica-
The licensee agreed to a quarantine of all equipment and systems
                                                                        tion was inspected to determine operability. Subsequently, it
which could be significant to the ongoing investigation of the event.
                                                                        was determined that the transmitter housing was 1/3 full of water
,
                                                                        and it appeared that the electrical portion of the transmitter
Consequently, all activities undertaken with regard to restoration work
                                                                        was not operable due to shorting.
or investigations were done with the concurrence of the NRC team on
                                                      (2) A calibration and circuit check was performed on pressure cutoff
site. During the first week following the event, . concurrence was given
                                                                        switch for the high pressure heater drain pump. This was done to                                                                         -
for some turbine generator work on the turbine deck which was not
                                                                        determine if the section of line leading from the HP heater drain
relevant to the investigation and work involving cleanup and restora--
                                                                        pump discharge to the condensate header had been pressurized to
tion of the damaged area. The following equipment was inspected:
                                                                        at least 600 psi. The switch was designed to cut off the pump if
(1) A main feed pump suction indication in the control room pegged at
'
,
                                                                        a 600 psi pressure was exceeded. The switch was calibrated and
1000 psi. The pressure transmitter associated with this indica-
                                                                        found to be operable indicating that a line pressure of greater
tion was inspected to determine operability.
l                                                                       than 600 psi was not present.
Subsequently, it
                                                                                                                                                                      5
was determined that the transmitter housing was 1/3 full of water
                                                    On December 16, 1986, this quarantine was lifted.
and it appeared that the electrical portion of the transmitter
l                                   b.               Piping Systems                                                           ,
was not operable due to shorting.
;                                                    Based on the failure of Surry Unit 2 main feedwater pump suction line
(2) A calibration and circuit check was performed on pressure cutoff
switch for the high pressure heater drain pump. This was done to
-
determine if the section of line leading from the HP heater drain
pump discharge to the condensate header had been pressurized to
at least 600 psi. The switch was designed to cut off the pump if
a 600 psi pressure was exceeded. The switch was calibrated and
found to be operable indicating that a line pressure of greater
'
l
than 600 psi was not present.
5
On December 16, 1986, this quarantine was lifted.
l
b.
Piping Systems
,
Based on the failure of Surry Unit 2 main feedwater pump suction line
;
and the fact that the Surry Unit 1 suction line design was similar to
,
,
                                                      and the fact that the Surry Unit 1 suction line design was similar to
Surry Unit 2, the licensee decided to shut down Surry Unit I and
-
-
                                                      Surry Unit 2, the licensee decided to shut down Surry Unit I and
;
;                                                    inspect the main feedwater pump suction line. The Surry Unit 1
inspect the main feedwater pump suction line. The Surry Unit 1
,                                                    suction line was found to have reduced wall thicknesses similar to
suction line was found to have reduced wall thicknesses similar to
i                                                     Surry Unit 2. When pipe wall thinning was found in Surry Unit 1,'
,
l                                                     the licensee decided to inspect similar piping at North Anna Unit 1.
i
                                                    Approximately 4900 ultrasonic inspections were made on North Anna
Surry Unit 2.
;                                                   Unit 1 piping. No measurements indicated pipe wall thickness below
When pipe wall thinning was found in Surry Unit 1,'
l
the licensee decided to inspect similar piping at North Anna Unit 1.
Approximately 4900 ultrasonic inspections were made on North Anna
;
Unit 1 piping. No measurements indicated pipe wall thickness below
the required minimum. The feedwater pump suction piping and header
,
,
                                                      the required minimum. The feedwater pump suction piping and header
wall thicknesses were within original pipe manufacturing specifica-
                                                    wall thicknesses were within original pipe manufacturing specifica-
l
l                                                     tions, and the high pressure drain pump dischdrge piping was no more
tions, and the high pressure drain pump dischdrge piping was no more
                                                      than 15 percent below the original specifications.
than 15 percent below the original specifications.
                                                                                                                                  .'
.'
                                                                                                                                                                                                                    l
l
                                                        #
#
  .
.
f
f
        , - - * - - - - -   ,m-., . - - , - - - . , , . , - , - ~ , - - , - - - - - - - - - - - ,,,,,--,,,--,-+.-,.m.   _ _ , ,   --
, - - * - - - - -
                                                                                                                                        . - - - - - - , , - -, , ,,  - - - - . , . - - - - - - - + - ---s------
,m-.,
. - - , - - - . , , . , - , - ~ , - - , - - - - - - - - - - -
,,,,,--,,,--,-+.-,.m.
_ _ , ,
. - - - - - - , , - - ,
- - - - . , . - - - - - - - + -
---s------
--
,
,,


      .
.
  .
.
    .
.
  -
37
                                        37
-
        As a result of finding thinned pipe at both units, the licensee
As a result of finding thinned pipe at both units, the licensee
        initiated a pipe wall thickness measuring inspection program to
initiated a pipe wall thickness measuring inspection program to
        define the extent of pipe wall thinning at Surry Units 1 and 2.       The
define the extent of pipe wall thinning at Surry Units 1 and 2.
        following summarizes the criteria for the program, the acceptance
The
        criteria, and the inspection results to date.
following summarizes the criteria for the program, the acceptance
        (1) Corrosion / Erosion Parameters
criteria, and the inspection results to date.
                In the review to determine the parameters affecting corrosion /
(1) Corrosion / Erosion Parameters
              erosion, the licensee found limited data available from industry
In the review to determine the parameters affecting corrosion /
              experience with bulk single phase corrosion / erosion. The
erosion, the licensee found limited data available from industry
              available literature correlates single phase corrosion / erosion to
experience with bulk single phase corrosion / erosion. The
              two phase wet steam corrosion / erosion.   The parameters that
available literature correlates single phase corrosion / erosion to
              appear to affect corrosion / erosion in single phase flow are:
two phase wet steam corrosion / erosion.
                                                                                  .
The parameters that
              -
appear to affect corrosion / erosion in single phase flow are:
                      Material         -
.
                                          Phenomenon occurs in carbon steels. The
Material
                                          resistance to corrosion / erosion
Phenomenon occurs in carbon steels. The
                    '
-
                                          increases with alloying.
-
              -
resistance to corrosion / erosion
                      Fluid Velocities - High fluid velocities increase
'
                                          corrosion / erosion.
increases with alloying.
              -
Fluid Velocities - High fluid velocities increase
                      Temperature     -
-
                                          Corrosion / erosion takes place batween
corrosion / erosion.
                                          195 and 440*F.
Temperature
              -
Corrosion / erosion takes place batween
                      High Water Purity- Corrosion / erosion.affected by oxygen
-
                                          content.
-
              These parameters and the corrosion / erosion process relate to the
195 and 440*F.
              rate of buildup and removal of the protective magnitite (Fe34  0)
High Water Purity- Corrosion / erosion.affected by oxygen
              layer.
-
              Based on the above information, the licensee established the
content.
              following criteria to select systems to be inspected:
These parameters and the corrosion / erosion process relate to the
              -
rate of buildup and removal of the protective magnitite (Fe 0 )
                    System handles water or steam
34
              -
layer.
                      System piping is carbon steel
Based on the above information, the licensee established the
              -
following criteria to select systems to be inspected:
                      System temperature is greater than 195"F
System handles water or steam
              -
-
                      System is deoxygenated (low ppb range)
System piping is carbon steel
              As added verification of these criteria, the licensee also
-
              included in the program specific locations within systems outside
System temperature is greater than 195"F
              the criteria, including safety-related systems, such as, the'
-
              auxiliary feedwater system (oxygenated and less than 195*F),
System is deoxygenated (low ppb range)
              charging system (stainless steel) and condensate system prior to
-
              the point heater (less than 195*F).
As added verification of these criteria, the licensee also
        (2) Rating Scheme
included in the program specific locations within systems outside
              Within a system, a rating scheme, based oh temperature, velocity,
the criteria, including safety-related systems, such as, the'
              and geometry, was used to identify potentially high corrosion /
auxiliary feedwater system (oxygenated and less than 195*F),
              erosion wear regions.                 ..                 .
charging system (stainless steel) and condensate system prior to
                                                    ,
the point heater (less than 195*F).
(2) Rating Scheme
Within a system, a rating scheme, based oh temperature, velocity,
and geometry, was used to identify potentially high corrosion /
erosion wear regions.
..
.
,
.-
.-
                              9
9


            .
.
        .
.
          *
*
        .                                         38
38
                        After consideration of the above criteria and rating scheme, the
.
                        licensee decided to inspect components beyond those identified
After consideration of the above criteria and rating scheme, the
                        as priority by the rating scheme. In addition to the components
licensee decided to inspect components beyond those identified
                        picked for the auxiliary feedwater system, charging system, and
as priority by the rating scheme.
                        condensate system to the 4th point heater, the following compo-
In addition to the components
                        nents were included in the wall thickness inspection program for
picked for the auxiliary feedwater system, charging system, and
                        both Surry 1 and Surry 2:
condensate system to the 4th point heater, the following compo-
                        -
nents were included in the wall thickness inspection program for
                              Every fitting and selected locations on straight pipe from
both Surry 1 and Surry 2:
                              the inlet of the 4th point heaters to the feedwater pumps
Every fitting and selected locations on straight pipe from
                              and from the feedwater pumps to the feedwater regulating
-
                              valves.
the inlet of the 4th point heaters to the feedwater pumps
                        -
and from the feedwater pumps to the feedwater regulating
                              Selected locations along sweeps and straight lengths of pipes
valves.
                              from the feedwater regulating valves to the containment for'
Selected locations along sweeps and straight lengths of pipes
                              loops A, B and C. There were no priority points in these
-
                              sections of pipe using the rating scheme.
from the feedwater regulating valves to the containment for'
                        -
loops A, B and C.
                              High priority points on B feedwater loops from the contain-
There were no priority points in these
                              ment to the steam generator. The points picked were
sections of pipe using the rating scheme.
                              representative of similar configurations in loops A and C
High priority points on B feedwater loops from the contain-
                              and also included some unusual configurations.
-
                    (3) Acceptance Criteria
ment to the steam generator. The points picked were
                        The licensee developed an acceptance criteria to provide guidance
representative of similar configurations in loops A and C
                        in determining whether a fitting or section of pipe needed to be
and also included some unusual configurations.
                        replaced immediately, replaced at some future time in its operat-
(3) Acceptance Criteria
                        ing life, or monitored by inspection during its operating life.
The licensee developed an acceptance criteria to provide guidance
                        The acceptance criteria were based on the existing wall thickness,
in determining whether a fitting or section of pipe needed to be
                        as measured by the inspection program, the calculated corrosion
replaced immediately, replaced at some future time in its operat-
                        wear rate, and the Code minimum required wall thickness. The
ing life, or monitored by inspection during its operating life.
                        wear rate was calculated by dividing the wear to date (assumed
The acceptance criteria were based on the existing wall thickness,
                        to be the nominal specification thickness plus manufacturer's
as measured by the inspection program, the calculated corrosion
                        tolerance minus the existing as measured thickness) by the number
wear rate, and the Code minimum required wall thickness. The
                        of years of operating history.       ,
wear rate was calculated by dividing the wear to date (assumed
                        The following acceptance categories were defined:
to be the nominal specification thickness plus manufacturer's
                        (a)   Immediate Replacement     -
tolerance minus the existing as measured thickness) by the number
                                                                Existing thickness below
of years of operating history.
                                                                minimum Code or below 0.100
,
                                                                inches.                   ,
The following acceptance categories were defined:
                        (b) Engineering Evaluation         -
(a)
                                                                Existing thickness greater
Immediate Replacement
                                                                than Code minimum but
Existing thickness below
                                                                calculated (based on wear
-
                                                                rate) to still be acceptable
minimum Code or below 0.100
                                                                at the time to next outage
inches.
                                                                plus I/2 year.
,
                                                                .'
(b) Engineering Evaluation
_ -. . . .     . .-
Existing thickness greater
-
than Code minimum but
calculated (based on wear
rate) to still be acceptable
at the time to next outage
plus I/2 year.
.'
_ -. . . .
. .-
.
. _ , , . _ . _ _ _ _ _ . _ . , , - _ _ _ . _ . . _ , , . - , _ _ _ _ _ - _ . _ _ _ _ _ _ - . . _ .
_ _ , , _ _ _ ,
, - . _ . . , _ _ _ . . , _ , . . . . . . , _ . _ _


                .
    *
.
.
                                                                                  39
*
  *
.
39
*
.
.
              (c) Potential Next Outage                                               -
(c) Potential Next Outage
                                                                                                Existing thickness greater than
Existing thickness greater than
                        Replacement                                                             acceptable thicknest at time to
-
                                                                                                next outage plus 1/2 year but
Replacement
                                                                                                less than acceptable thickness
acceptable thicknest at time to
                ,                                                                    ,          at time to next two outages
next outage plus 1/2 year but
                a
less than acceptable thickness
                                                                                                plus 1/2 year. Inspect at
at time to next two outages
                    _
,
                                                                                                next outage.
,
              (d) Each Outage Inspection                                               -
plus 1/2 year.
                                                                                                Existing thickness greater
Inspect at
                                                                                                than acceptable thickness at
a
                                                                                                time to next two outages plus
_
                                                                                                1/2 year but less than
next outage.
                                                                                                acceptable to next three
(d) Each Outage Inspection
                                                                                                outages plus one year.
Existing thickness greater
                                                                                                                                ,
-
              (e) Place Component in                                                   -
than acceptable thickness at
                                                                                                Existing thickness greater
time to next two outages plus
                        Station's Inspection                                                     than acceptable thickness at
1/2 year but less than
                        Program                                                                 time to next three outages
acceptable to next three
                                                                                                plus one year.
outages plus one year.
        (4) Summary of Inspection Results and Replacement as of January 8,
,
              1987
(e) Place Component in
                                                                                                      Unit 1         Unit 2
Existing thickness greater
              Components to be Inspected                                                               588           588
-
              Inspection Requests Issued                                                 - - - -
Station's Inspection
                                                                                                        515-           208
than acceptable thickness at
              Inspections Complete                                                                     427           150
Program
              Components Designated for Immediate                                                       48               7
time to next three outages
                  Replacement
plus one year.
              Components Designated for Potential                                                         8               4
(4) Summary of Inspection Results and Replacement as of January 8,
                  Replacement at Next Refueling Outage
1987
              Components Designated for Inspection                                                       40               8
Unit 1
                  at Next Refueling Outage
Unit 2
              Components Removed                                                                         38               7
Components to be Inspected
              Components Installed                                                                       8               0
588
      b. Main Steam Trip Valve
588
        Because of deficiencies found in the Unit 2 C MSTV (see paragraph
Inspection Requests Issued
        11.a.(2), the licensee inspected the internals of the remaining Unit 2
- - - -
        MSTV and the three Unit 1 MSTVs.                                             No assembly deficiencies were found.
515-
        In addition, each pair,of air actuating cylinders for each valve was
208
        rebuilt.
Inspections Complete
                                                                                                .'
427
                                                                                                                              9
150
                                    _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ . . _ _ _
Components Designated for Immediate
48
7
Replacement
Components Designated for Potential
8
4
Replacement at Next Refueling Outage
Components Designated for Inspection
40
8
at Next Refueling Outage
Components Removed
38
7
Components Installed
8
0
b.
Main Steam Trip Valve
Because of deficiencies found in the Unit 2 C MSTV (see paragraph
11.a.(2), the licensee inspected the internals of the remaining Unit 2
MSTV and the three Unit 1 MSTVs.
No assembly deficiencies were found.
In addition, each pair,of air actuating cylinders for each valve was
rebuilt.
.'
9
_ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ . . _ _ _


              .                                 .           __                                _                       __.
.
          ~
.
      .
_ _
                                                                                                    '
_
        .
__.
      -
~
                                                                                40
.
                                        c.   Main Feed Pump Discharge Check Valve
'
                                                            '
.
                                              The remaining three main feed pump discharge check valves were
40
                                                inspected. The results were as follows:                                       ,
-
                                                      5
c.
                                              Unit 2 8 Check Valve    -
Main Feed Pump Discharge Check Valve
                                                                          Both c' lamp assemblies had loose bolts and the
'
                                                                          lock wires for these bolts were missing. The
The remaining three main feed pump discharge check valves were
                                                                          lock plates exhibited some erosion but the
inspected. The results were as follows:
;                                                                         disc / seat assembly was not displaced.
,
5
Both c' lamp assemblies had loose bolts and the
Unit 2 8 Check Valve
-
lock wires for these bolts were missing. The
lock plates exhibited some erosion but the
;
disc / seat assembly was not displaced.
t
t
                                              Unit 1 B Check Valve     -
Unit 1 B Check Valve
                                                                          Both clamp assemblies had loose bolts and the
Both clamp assemblies had loose bolts and the
                                                                          lock wires for these bolts were missing. The
-
                                                                          lock plates exhibited extensive erosion but
lock wires for these bolts were missing. The
                                                                          the disc / seat assembly was not displaced.
lock plates exhibited extensive erosion but
                                                                          The left side hinge pin was missing.
the disc / seat assembly was not displaced.
                                              Unit 1 A Check Valve - No defects found.         This valve was overhauled
The left side hinge pin was missing.
;                                                         -
Unit 1 A Check Valve - No defects found.
                                                                          in May 1986.
This valve was overhauled
;
-
in May 1986.
'
The check valves will be modified as follows:
(1) New hinge pins will be installed that are secured in place by a
lock pin which is welded in place.
The lock pin will project
through a hole in the hinge pin. This modification will be
completed prior to startup of the units.
(2) The clamp assembly which holds the seat to the valve body will be
eliminated by welding the disc / seat assembly onto the valve body.
"
This modification required a material change. Due to the unavail-
;
ability of this material, the modification will be made at the
l
next scheduled outage of sufficient duration when the material is
available or during the next refueling outage.
(3) The check valves will be periodically inspected in accordance
with an inspection plan to be developed by the licensee.
'
'
                                              The check valves will be modified as follows:
16. Safety Considerations for Station Restart
                                              (1) New hinge pins will be installed that are secured in place by a
By letter dated January 14, 1987', the licensee submitted a report entitled
                                                    lock pin which is welded in place. The lock pin will project
"Surry Unit 2 Reactor Trip and Feedwater Pipe Failure." This report
                                                    through a hole in the hinge pin. This modification will be
provides detailed information on the December 9, 1986 event and a recovery
                                                    completed prior to startup of the units.
plan and corrective actions for NRC review and concurrence prior to station
                                              (2) The clamp assembly which holds the seat to the valve body will be
restart.
                                                    eliminated by welding the disc / seat assembly onto the valve body.      "
The AIT has reviewed this report and has conducted an independent inspection
                                                    This modification required a material change. Due to the unavail-
effort which provides the bases for our concurrence with the licensee's
;                                                    ability of this material, the modification will be made at the
restart plan.
l                                                    next scheduled outage of sufficient duration when the material is
I
                                                    available or during the next refueling outage.
*
                                              (3) The check valves will be periodically inspected in accordance
.
                                                    with an inspection plan to be developed by the licensee.
ee.
                                                                                          '
.. ~ . . - _ _ _ _ _ , , . _ .
                            16. Safety Considerations for Station Restart
_,, _ _ , . - _
                                        By letter dated January 14, 1987', the licensee submitted a report entitled
. .__.- ,
                                        "Surry Unit 2 Reactor Trip and Feedwater Pipe Failure." This report
_ , . _ _ _ . . _ _ _ _ _ _ _ . - _
                                        provides detailed information on the December 9, 1986 event and a recovery
-
                                        plan and corrective actions for NRC review and concurrence prior to station
.
                                        restart.
- . .
                                        The AIT has reviewed this report and has conducted an independent inspection
. .
                                        effort which provides the bases for our concurrence with the licensee's
.
                                        restart plan.
-.
                                                                                                  I
. .
                                                                                              *
                                                                                            .
  ee.
          .. ~ . . - _ _ _ _ _ , , . _ .


                    _       _             _                             _               _       _           _     _ _     .
_
              .
_
  >   .
_
            .                                                                                                                     ,
_
      -
_
                                                                                      41                                          '
_
                            The Itcensee's report outlines a program which has been implemented for
_
                              initial inspection, hardware replacement and periodic inspection of the
_ _
                            main feed and condensate piping systems.                       This program provides for
.
                            development of a model which is believed to predict the erosion-corrosion
.
                            mechanism and the rate of pipe wall thinning in a conservative manner. The
>
                              licensee, ush g this model, developed an inspection / replacement program
.
                            for various fittings in the feed / condensate systems. This program defines
.
                            conservative acceptance criteria for the fitting replacement which predict
,
                            the time that would elapse before minimum allowable wall thickness would
41
                            occur (see Section 15.b). In addition, a periodic inspection program has
-
                            been established. The periodic inspections would provide information to
'
                            continually reaffirm or modify the model. Thus, the present inspection /
The Itcensee's report outlines a program which has been implemented for
                            replacement program would permit a satisfactory knowledge of the present
initial inspection, hardware replacement and periodic inspection of the
                            state of the plant's condensate /feedwater systems. Future inspections
main feed and condensate piping systems.
                            together with the current information would continually provide assurance
This program provides for
j                           that the loss of wall thickness is not occurring at the rate which could
development of a model which is believed to predict the erosion-corrosion
                            result-in prem.ature failure. These actions provide additional confidence in
mechanism and the rate of pipe wall thinning in a conservative manner. The
                            the startup and permits the carrying out of a conservative inspection
licensee, ush g this model, developed an inspection / replacement program
                            program which adequately defines weak points in the feed and condensate
for various fittings in the feed / condensate systems. This program defines
                            systems.
conservative acceptance criteria for the fitting replacement which predict
l                         This replacement / inspection program is an interim measure to be utilized
the time that would elapse before minimum allowable wall thickness would
                          as more information_is developed with regard to the mechanism of erosion /
occur (see Section 15.b).
In addition, a periodic inspection program has
been established. The periodic inspections would provide information to
continually reaffirm or modify the model. Thus, the present inspection /
replacement program would permit a satisfactory knowledge of the present
state of the plant's condensate /feedwater systems. Future inspections
together with the current information would continually provide assurance
j
that the loss of wall thickness is not occurring at the rate which could
result-in prem.ature failure. These actions provide additional confidence in
the startup and permits the carrying out of a conservative inspection
program which adequately defines weak points in the feed and condensate
systems.
l
This replacement / inspection program is an interim measure to be utilized
as more information_is developed with regard to the mechanism of erosion /
;
;
corrosion. The licensee intends to develop a long range program of correc-
'
'
                          corrosion. The licensee intends to develop a long range program of correc-
tive action that includes geometry as well as material changes to the feed
                            tive action that includes geometry as well as material changes to the feed
and condensate systems.
                          and condensate systems.                                                                               *
*
                            Inspection performed on the other single phase systems in the plant showed.                         -
Inspection performed on the other single phase systems in the plant showed.
                          no indication of the type of failure experienced in the feed / condensate
-
                            system (i.e., wall thinning due to corrosion / erosions). In addition, the
no indication of the type of failure experienced in the feed / condensate
                            licensee will continue the inspection program previously developed for two-
system (i.e., wall thinning due to corrosion / erosions).
                          phase flow systems.
In addition, the
                          The AIT has also reviewed the licensee's corrective actions with regard to
licensee will continue the inspection program previously developed for two-
                          the MSTV maintenance procedures and the proposed short-term and longer term
phase flow systems.
                          hardware improvements for the main feed pump discharge check valves, and
The AIT has also reviewed the licensee's corrective actions with regard to
                          concludes that the licensee actions are satisfactory.
the MSTV maintenance procedures and the proposed short-term and longer term
                          In addition, as a result of the AIT inspection and re. view of the licensee's
hardware improvements for the main feed pump discharge check valves, and
                          program, the following conclusions and findings were developed.
concludes that the licensee actions are satisfactory.
                          a.       Sequence of Events
In addition, as a result of the AIT inspection and re. view of the licensee's
                                                                                                                          .
program, the following conclusions and findings were developed.
                                    The inspectors performed an independent evaluation of the event
a.
                                    scenario, including the sequence of events and their cause of the
Sequence of Events
                                    events. The inspectors' conclusions are that the reactor primary
.
                                    system and all safety-related components reacted properly to a loss of
The inspectors performed an independent evaluation of the event
                                    load transient initiated by the closure of one of the main steam trip
scenario, including the sequence of events and their cause of the
                                    valves. The pipe rupture occurred before the bain feedwater discharge
events. The inspectors' conclusions are that the reactor primary
l                                                                                             ;
system and all safety-related components reacted properly to a loss of
                                      >
load transient initiated by the closure of one of the main steam trip
    _
valves. The pipe rupture occurred before the bain feedwater discharge
                                                                                                                            9
l
        - , - . - -   ..-,c-------         - ., - - - - . - - - - - ---,- ,- _ _ ----               .. -- - .
;
>
_
9
- , - . - -
..-,c-------
- ., - - - - . - - - - - ---,- ,- _ _ ----
.. -- - .
-- - -
-


      .                                                     -                                                                                   _.
.
          .
-
    .
_.
                                                                    *
.
        .
.
    -
*
                                                                                      42
.
                                check valve could malfunction. The only contribution to the event was
42
                                that the malfunction of the MFW pump discharge check valve caused
-
                                  steam / water to be discharged from the break. We concur with the
check valve could malfunction. The only contribution to the event was
;                                 licensee's evaluation of the sequence of events.
that the malfunction of the MFW pump discharge check valve caused
                                                                                              '
steam / water to be discharged from the break. We concur with the
                  b.             WaterbammerOccurrence
;
                                  Inspection of the Surry Unit 2 condensate and feedwater piping
licensee's evaluation of the sequence of events.
                                conducted following the pipe rupture event did not indicate that
b.
                                feedwater system water hammer occurred during the event. Reviews of
WaterbammerOccurrence
                                PWR operating experience regarding water hammer in feedwater systems
'
                                  indicate that severe water hammer loads usually result in extreme
Inspection of the Surry Unit 2 condensate and feedwater piping
                                damage to pipe nanger supports and instrumentation and are usually
conducted following the pipe rupture event did not indicate that
                                the result of feedwater control valve instability. The Surry Unit 2
feedwater system water hammer occurred during the event. Reviews of
                                feedwater piping from the containment penetration back through the A
PWR operating experience regarding water hammer in feedwater systems
                                main feedwater pump, haater drain pump and condensate pumps have been
indicate that severe water hammer loads usually result in extreme
                                inspected by the team, and there is no indication of this type of
damage to pipe nanger supports and instrumentation and are usually
                                damage anywhere but in the vicinity of the rupture. Inspection by
the result of feedwater control valve instability. The Surry Unit 2
                                the licensee has also indicated no such damage. In addition to this,
feedwater piping from the containment penetration back through the A
                                measurements of pressure between the steam generator and feedwater
main feedwater pump, haater drain pump and condensate pumps have been
                                control valves indicate there was no leakage from the steam generator
inspected by the team, and there is no indication of this type of
                                back through the feedwater system.
damage anywhere but in the vicinity of the rupture.
                  c.             Metallurgical
Inspection by
                                The pipe rupture occurred due to severe pipe wall thinning. The
the licensee has also indicated no such damage.
                                general thinning condition appears to have been caused by a corrosion /
In addition to this,
                                erosion mechanism with thinner localized areas related to high
measurements of pressure between the steam generator and feedwater
                                turbulent flow. The fracture appeared to have originated at one of the
control valves indicate there was no leakage from the steam generator
                                local severely thinned areas. The licensee's preliminary metallurgical
back through the feedwater system.
                                analysis indicated that the material met all specification require-
c.
                                ments. Additional tests are in process by the licensee and the NRC to
Metallurgical
                                fully define all material properties. The licensee has outlined an
The pipe rupture occurred due to severe pipe wall thinning. The
                                inspection program for the feedwater and condensate piping systems,
general thinning condition appears to have been caused by a corrosion /
                                based on conservatively predicting the corrosion / erosion mechanism and
erosion mechanism with thinner localized areas related to high
                                the rate of wall thinning which should, ensure that the wall thickness
turbulent flow. The fracture appeared to have originated at one of the
                                is monitored adequately to preclude premature failure. The licensee's
local severely thinned areas. The licensee's preliminary metallurgical
                                results and inspection program are outlined in their report, "Surry
analysis indicated that the material met all specification require-
                                Unit 2 reactor trip and feedwater pipe failure" submitted by letter
ments. Additional tests are in process by the licensee and the NRC to
                                dated January 14, 1987. We concur that the report covers the metallur-
fully define all material properties. The licensee has outlined an
                                gical aspects of the problem adequately,
inspection program for the feedwater and condensate piping systems,
                  d.             Chemistry
based on conservatively predicting the corrosion / erosion mechanism and
                                                                                                                                            '
the rate of wall thinning which should, ensure that the wall thickness
                                The methodology used to control secondary water chemistry to prevent
is monitored adequately to preclude premature failure. The licensee's
                                localized corrosion of stea:n generator components (as recommended by
results and inspection program are outlined in their report, "Surry
                                the Steam Generator Owners Group) may result in " aggressive" water
Unit 2 reactor trip and feedwater pipe failure" submitted by letter
                                chemistry conditions that favor general corros, ion of carbon steel.
dated January 14, 1987. We concur that the report covers the metallur-
gical aspects of the problem adequately,
d.
Chemistry
'
The methodology used to control secondary water chemistry to prevent
localized corrosion of stea:n generator components (as recommended by
the Steam Generator Owners Group) may result in " aggressive" water
chemistry conditions that favor general corros, ion of carbon steel.
I
I
I                                                                                                                                     ;
I
                                                                                                                                          -
-
                                    *
;
  .
*
                                                                                                                                              *
.
            . _ . ,_.._,____._x         _ .__.._____,__ ._.   ,_,.. _ ,_________.___ ,.___ ,_. _.,___, . _____.__ __.__ - ._._____._ _.~_
*
. _ .
,_.._,____._x
_ .__.._____,__ ._.
,_,.. _ ,_________.___ ,.___ ,_. _.,___, . _____.__ __.__ - ._._____._ _.~_


                                                                            ._   _ .-                                 . _ -                 _                       _ .           ._ .
._
                  .
_ .-
          .
. _ -
                .
_
          *
_ .
                                                                                                                  43
._ .
.
                                                          The formation and retentien of an adhesive film of magnetite on the
                                                          inner surfaces of carbon steel pipe, in regions of single phase and
                                                          turbulent flow, may be affected by variables other than regeneration
                                                        by oxygen.
                                                                                                                    '
                                          e.            Emergen'cy Preparedness
                                                          The facility's emergency organization responded to the pipe rupture
                                                          event in a commendable manner. The plant staff worked together effi-
                                                          ciently to minimize personnel injuries and to mitigate the consequences
                                                          of the event. Offsite support requested for the injured personnel
                                                          responded to the call for assistance expeditiously to transport the
                                                          injured personnel to area medical facilities.                                          Verbatim compliance
.
.
                                                        with the actions specified in the Emergency Plan appears to have been
.
;.                                                       exercised by the plant staff in responding to the event.                                                                 <
.
;                                           f.           Public Information
*
43
The formation and retentien of an adhesive film of magnetite on the
.
inner surfaces of carbon steel pipe, in regions of single phase and
turbulent flow, may be affected by variables other than regeneration
by oxygen.
Emergen'cy Preparedness
'
e.
The facility's emergency organization responded to the pipe rupture
event in a commendable manner. The plant staff worked together effi-
ciently to minimize personnel injuries and to mitigate the consequences
of the event. Offsite support requested for the injured personnel
responded to the call for assistance expeditiously to transport the
injured personnel to area medical facilities.
Verbatim compliance
with the actions specified in the Emergency Plan appears to have been
.
;.
exercised by the plant staff in responding to the event.
<
;
f.
Public Information
Virginia Power implemented an aggressive and candid program to inform
<
<
                                                          Virginia Power implemented an aggressive and candid program to inform
'
'
                                                          news agencies - and, through them, the public - of the basic facts
news agencies - and, through them, the public - of the basic facts
                                                          concerning the accident and of continually updated findings as the
concerning the accident and of continually updated findings as the
                                                          Company's own investigation went forward.                               Key ranking company execu-
Company's own investigation went forward.
                                                          tive spent an unusual amount of time in briefing reporters in several
Key ranking company execu-
;                                                       news conferences.             Reporters were taken on several tours for a first-
tive spent an unusual amount of time in briefing reporters in several
  !                                                       hand look at the accident area and at pieces of the broken pipe.
;
news conferences.
Reporters were taken on several tours for a first-
!
hand look at the accident area and at pieces of the broken pipe.
I
I
!                                         g.             Plant Systems
!
                                                          (1) The inspectors reviewed the' licensee's program for determining
g.
                                                                        the cause of the C MSTV closure and also the failure of the MFW
Plant Systems
                                                                        pump discharge check valve to fully close during the event. The
(1) The inspectors reviewed the' licensee's program for determining
                                                                        licensee's technical evaluation and the corrective actions taken
the cause of the C MSTV closure and also the failure of the MFW
                                                                        to restore the above components to normal operation were deter-
pump discharge check valve to fully close during the event. The
                                                                        mined to be comprehensive and acceptable.
licensee's technical evaluation and the corrective actions taken
                                                          (2) An apparent violation of Maintenance Procedure MMP-C-MS-002 which
to restore the above components to normal operation were deter-
                                                                        initially overhauled the C MSTV wits identified. This procedure
mined to be comprehensive and acceptable.
                                                                        lacked detailed instructions, was not fully followed and did not
(2) An apparent violation of Maintenance Procedure MMP-C-MS-002 which
                                                                        provide adequate documentation to show the repair of the MSTV
initially overhauled the C MSTV wits identified. This procedure
                                                                        was accomplished in a quality manner. The licensee was informed
lacked detailed instructions, was not fully followed and did not
                                                                        that similar problems may exist with other system maintenance
provide adequate documentation to show the repair of the MSTV
                                                                        procedures and licensee review should be conducted.                                                   ,
was accomplished in a quality manner. The licensee was informed
                                                          (3) The inadequate maintenance performed on the C MSTV did not prevent
that similar problems may exist with other system maintenance
                                                                        the valve from performing its safety function or cause it to be in
procedures and licensee review should be conducted.
,
(3) The inadequate maintenance performed on the C MSTV did not prevent
the valve from performing its safety function or cause it to be in
l
l
                                                                        noncompliance with Technical Specifications.
noncompliance with Technical Specifications.
                                                          (4) The reactor trip was a direct result of the improper overhaul of
(4) The reactor trip was a direct result of the improper overhaul of
                                                                        the C MSTV in conjunction with the lower than normal instrument
the C MSTV in conjunction with the lower than normal instrument
,
,
air pressure.
However, the MFW line rupture was not caused by
l
l
                                                                        air pressure.    However, the MFW line rupture was not caused by
the MSTV closure but occurred due to the normal pressure transient
                                                                        the MSTV closure but occurred due to the normal pressure transient
'
                                                                        which followed the reactor trip.                     ;
which followed the reactor trip.
                                                                                                                              '
;
                                                              '
'
    ,_
,_
                                                                                                                                                                                ,
,
    , - , . - - - - - . - - , - - , - - - . - - - - - , - - . . - , - ~ , .                   - - - - - - - - - ,               - - - - . . - ~ - - - - - - - - ~ ~ - - - - -
, - , . - - - - - . - - , - - , - - - . - - - - - , - - . . - , - ~ , .
                                                                                                                                                    -
- - - - - - - - - ,
                                                                                                                                                                                          - - - -
- - - - . . - ~ - - - - - - - - ~ ~ - - - - -
- - - -
-


                        .
.
              .
.
                      ~
~
              -
44
                                                                      44
-
                                                        .
.
                                (5) The maintenance performed on the C MSTV indicated several cases
(5) The maintenance performed on the C MSTV indicated several cases
                                              where anomalies were resolved without either proper documentation,
where anomalies were resolved without either proper documentation,
                                              notification of supervision or engineering review. Examples are
notification of supervision or engineering review.
                                              the changing of the radius levers on the rock shafts and the
Examples are
                                              need to adjust the MSTV lijnit switch following maintenance. Had
the changing of the radius levers on the rock shafts and the
                                              these problems received the proper attention and evaluation, the
need to adjust the MSTV lijnit switch following maintenance. Had
                                              improper reassembly of the C MSTV could have been identified
these problems received the proper attention and evaluation, the
improper reassembly of the C MSTV could have been identified
.
before causing a reactor trip and a challenge to the reactor
'
'
.
safety systems.
                                              before causing a reactor trip and a challenge to the reactor
(6) The post maintenance test used to check the operation of the
                                              safety systems.
MSTVs following maintenance only verified their safety function
                                (6) The post maintenance test used to check the operation of the
and compliance with Technical Specification. Additional testing
                                              MSTVs following maintenance only verified their safety function
should have been required to verify full are travel of the valve
                                              and compliance with Technical Specification. Additional testing
,
,
disc and therefore proper reassembly of the valve would have been
                                              should have been required to verify full are travel of the valve
confirmed.
                                              disc and therefore proper reassembly of the valve would have been
h.
                                              confirmed.
Security
                          h.   Security
The actions of security personnel during the event provided prompt
                                The actions of security personnel during the event provided prompt
personnel access to sensitive operational areas including the control
                                personnel access to sensitive operational areas including the control
room. As a result of evaluating the security aspects of the event,
                                room. As a result of evaluating the security aspects of the event,
the licensee is considering additional training and hardware changes
                                the licensee is considering additional training and hardware changes
to further facilitate emergency access to restricted areas.
                                to further facilitate emergency access to restricted areas.
1.
                          1.   Fire Protection
Fire Protection
4
As a result of the feedwater pipe rupture event in the Surry Unit 2
                                As a result of the feedwater pipe rupture event in the Surry Unit 2
4
                                turbine building, Units 1 and 2 cable tray room carbon dioxide fire
turbine building, Units 1 and 2 cable tray room carbon dioxide fire
                                suppression systems and emergency switchgear room Halon fire suppres-
suppression systems and emergency switchgear room Halon fire suppres-
                                sion systems spuriously actuated causing control room habitability
sion systems spuriously actuated causing control room habitability
                                problems during the event. Based on our review, we conclude that the
problems during the event. Based on our review, we conclude that the
l
l
                                licensee's staff has properly analyzed what caused the spurious fire
licensee's staff has properly analyzed what caused the spurious fire
!
!
protection system actuations and has initiated modifications to the
'
'
                                protection system actuations and has initiated modifications to the
subject fire suppression systems which will greatly reduce the prob-
                                subject fire suppression systems which will greatly reduce the prob-
abilities that these systems will spur,iously operate due to water / steam
,                                abilities that these systems will spur,iously operate due to water / steam
,
j                               intrusion. In addition, it should be noted that once carbon dioxide
j
intrusion. In addition, it should be noted that once carbon dioxide
!
!
                                leakage into the control room was recognized, the licensee's control
leakage into the control room was recognized, the licensee's control
                                room operations staff initiated prompt corrective actions to maintain
room operations staff initiated prompt corrective actions to maintain
                                control room habitability. However, with respect to ensuring control
control room habitability. However, with respect to ensuring control
                                room habitability and personnel safety we recommend that the licensee
room habitability and personnel safety we recommend that the licensee
                                consider the following:
consider the following:
                                -
The installation of a wintergreen odorizer on the Units 1 and 2
                                            The installation of a wintergreen odorizer on the Units 1 and 2
-
                                              cable tray room carbon dioxide system,
cable tray room carbon dioxide system,
                                -
The installation of a permanent carbon dioxide analyzer with a
                                            The installation of a permanent carbon dioxide analyzer with a
-
                                              control room audible alarm in the main co,ntrol room annex,
control room audible alarm in the main co,ntrol room annex,
                                                                                  .'
.'
    4
4
  ,- - _ _ _. .. _ -_ _ _   __     .._,.___m...,_,
,- - _ _ _. .. _ -_ _ _
__
.._,.___m...,_,
, _ . _ _ _ _ , - _ _ _ , . _ , . . , _ .
_ _ . _ , _ _ - _ . . _ _ _ . . _ _ _ . . .
_
_


                                                                                                                                                                                      l
l
                .
.
      .
.
              *                                                                                                                                                                        '
'
    .
*
                                                                          45
45
                                                                                                                                                                                      i
.
                                                                                                                                                                                      !
i
                              -
The development of a procedure which will require the control
                                      The development of a procedure which will require the control
-
                                      room operators to pressurize the control room in the event of a
room operators to pressurize the control room in the event of a
                                      gaseous fire suppression system actuation in either the cable
gaseous fire suppression system actuation in either the cable
                                      tray room or the emergency switchgear rooms, and                                                                                                 '
tray room or the emergency switchgear rooms, and
                                                                                                                                                                                      ,
'
                              -
                                      Th'e_ installation of predischarge visual and audible warning
                                      devices near the Units 1 and 2 cable tray room doors and inside
                                      the cable tray rooms which will activate to alert personnel prior
                                      to a carbon dioxide system discharge.
                                                                                                                                                                                  a
                                            .
                                                                                O
,
,
I                                                                                 .*
Th'e_ installation of predischarge visual and audible warning
                                                                                  *
-
devices near the Units 1 and 2 cable tray room doors and inside
the cable tray rooms which will activate to alert personnel prior
to a carbon dioxide system discharge.
a
.
O
,
I
. *
*
i
i
,
,
  w
w
                                                                                                                                                                            e
e
                                                                                                                                                                                    .
.
    . -.- , -     , - - - - --   .n ,   ,     y .,, - .,-. - . ,, .-- - ,   ,       ,- ,en,- n--- , _ ---, -w,-_.,-- - - - - . - - -- _ - - - , - - - - - . _ - _ . _ _ _ . - -
. -.- , -
, - - - - --
.n
,
,
y
.,, - .,-. - .
,, .-- - ,
,
,-
,en,-
n--- , _ ---,
-w,-_.,--
- - - - . - - -- _ - - - , - - - - - . _ - _ . _ _ _ . - -


                    .         _ _ _                 -_. .   .               _     ._. _ . _ - _ _       -. .
.
                    .
_ _ _
                .
-_.
                  ~
.
                .
.
t
_
                                                            APPENDIX
._. _ . _ - _
                                            .
_
  ,
-.
                                          CHEMISTRY-CORROSION CONSIDERATION OF THE SURRY
.
                                                UNIT 2 FEEDWATER P.IPE RUPTURE EVENT
.
                        1. Fundamentals of Generalized Corrosion
.
                            Although the eventual rupture of the 18-inch suction pipe may have been
~
                            initiated at a point on the upper-inside region of the first elbow down-
.
                            stream of the header, both visual evidence and ultrasonic measurements
t
APPENDIX
.
CHEMISTRY-CORROSION CONSIDERATION OF THE SURRY
,
,
                            showed that generalized wastage of the pipe, with resulting thinning from
UNIT 2 FEEDWATER P.IPE RUPTURE EVENT
                            the nominal 0.5-inch wall thickness, had been the obvious precursor to the
1.
                            pipe failure. Because of the uniform nature of the thinning there was no
Fundamentals of Generalized Corrosion
                            evidence of other types of mechanical or chemical attack.
Although the eventual rupture of the 18-inch suction pipe may have been
                            Generalized thinning of iron surfaces is considered to be caused by erosion /
initiated at a point on the upper-inside region of the first elbow down-
:'
stream of the header, both visual evidence and ultrasonic measurements
                            corrosion processes, with either process being dominant. The potential for
showed that generalized wastage of the pipe, with resulting thinning from
                            mechanical and hydraulic erosion is greatest in regions of turbulence and
,
                            non-single phase flow and is enhanced by increased flow and temperature.
the nominal 0.5-inch wall thickness, had been the obvious precursor to the
                            Consequently, erosion mechanisms can be expected in the regions of the
pipe failure.
                            tee junction of the feedwater header and suction pipe, and, to a lesser
Because of the uniform nature of the thinning there was no
                            degree, in the elbow regions of the suction pipe. The role of corrosion,
evidence of other types of mechanical or chemical attack.
                            specifically in the Surry feedwater system, is more speculative because of
Generalized thinning of iron surfaces is considered to be caused by erosion /
                            the multiple chemical reactions that might have occurred during the thirteen         -
:
                            years of normal and abnormal chemistry control. The licensee has tenta-
corrosion processes, with either process being dominant.
                            tively assumed that general corrosion occurred because the carbon steel
The potential for
!                           pipes had been in contact with ' aggressive' (low dissolved oxygen) water.
'
'                          Removal of iron from a carbon steel pipe is thought to occur through
mechanical and hydraulic erosion is greatest in regions of turbulence and
                            oxidation processes that establish a corrosion electropotential between
non-single phase flow and is enhanced by increased flow and temperature.
Consequently, erosion mechanisms can be expected in the regions of the
tee junction of the feedwater header and suction pipe, and, to a lesser
degree, in the elbow regions of the suction pipe. The role of corrosion,
specifically in the Surry feedwater system, is more speculative because of
the multiple chemical reactions that might have occurred during the thirteen
-
years of normal and abnormal chemistry control. The licensee has tenta-
tively assumed that general corrosion occurred because the carbon steel
!
pipes had been in contact with ' aggressive' (low dissolved oxygen) water.
Removal of iron from a carbon steel pipe is thought to occur through
'
oxidation processes that establish a corrosion electropotential between
i
i
                            metallic iron (as an anode) and an oxidant in the water layer adjacent
metallic iron (as an anode) and an oxidant in the water layer adjacent
;                           to the metal surface (cathode). Depending on the magnitude of the corrosion
;
i                          potential the oxidant in feedwater could have been hydrogen tons, cupric or
to the metal surface (cathode). Depending on the magnitude of the corrosion
                            cuprous ions, or oxygen. All of these cathodic reactions are enhanced by
potential the oxidant in feedwater could have been hydrogen tons, cupric or
j                           the presence of chloride ions.
i
l                           In stagnant water systems the ferrous ions (Fe++) generated at the metal /
cuprous ions, or oxygen. All of these cathodic reactions are enhanced by
j
the presence of chloride ions.
l
In stagnant water systems the ferrous ions (Fe++) generated at the metal /
water interface are amenable to further oxidation by dissolved oxygen to
l
j
produce insoluble iron oxides such as Fe 02 3 (hematite) and Fe 03 4 (magnetite)
l
l
                            water interface are amenable to further oxidation by dissolved oxygen to
as well as other, less stable, hydrous oxides of iron.
j                          produce insoluble iron oxides such as Fe 02 3 (hematite) and Fe 03 4 (magnetite)
The formation of
l                          as well as other, less stable, hydrous oxides of iron.       The formation of
magnetite also can occur in the absence of. measurable amounts of dissolved
                            magnetite also can occur in the absence of. measurable amounts of dissolved
t
t
                            oxygen. One mechanism that has been prop ~osed is further electrochemical
oxygen. One mechanism that has been prop ~osed is further electrochemical
                            reaction of hydrogen ions (H+) and the trace concentrations of soluble
reaction of hydrogen ions (H+) and the trace concentrations of soluble
                            ferrous hydroxide in the aqueous layer adjacent to the metal surface.
ferrous hydroxide in the aqueous layer adjacent to the metal surface.
                            The formation of magnetite rather than hematite is favored by increased
The formation of magnetite rather than hematite is favored by increased
[                           temperature (especially between 300-350 degrees F) ,and again under stagnant
[
                            conditions. Under optimum conditions, a non-porous', adhesive film of
temperature (especially between 300-350 degrees F) ,and again under stagnant
                            magnetite forms on iron or steel surface. The film eventually terminates
conditions. Under optimum conditions, a non-porous', adhesive film of
                                                                              '
magnetite forms on iron or steel surface. The film eventually terminates
                                                                            ;
';
                                                                                                                    .
.
          * eo
* eo
    , , - -           r
, , - -
r
,
,,n,,,,,-----,--,--,--,-,--,r,-
,~,c,-..--~n
,-,.~.-------.->_.-,~w--,-,-~---.,,-,----,n~
- - - , .


        .
.
      .
.
              Appendix                                                                 2
Appendix
                                    further removal of iron by electrochemical attack by eliminating the anodic
2
                                    reactor (Fe*+ Fe++). The oxide is in chemical equilibrium with the adjacent
further removal of iron by electrochemical attack by eliminating the anodic
                                  water and will degrade if the equilibrium is impacted by chemical and/or
reactor (Fe*+ Fe++).
                                    hydraulic factors.
The oxide is in chemical equilibrium with the adjacent
              2.                   Role of Pass'ivity and Corrosion in the Thinning of the Feedwater Pipes
water and will degrade if the equilibrium is impacted by chemical and/or
                                                                                                                                  a
hydraulic factors.
                                    a.                 Observations
2.
                                                        As the result of his visual inspection the inspector could not
Role of Pass'ivity and Corrosion in the Thinning of the Feedwater Pipes
                                                        establish the extent to which the chemistry of the feedwater abetted
a
                                                        the thinning process or provided protection against the continuous
a.
                                                        removal of iron from regions of turbulence and single phase flow.
Observations
                                                        The appearance of the pipe in Unit 1 was significantly different from
As the result of his visual inspection the inspector could not
                                                        Unit 2; however the extent of thinning was similar in both units, but <
establish the extent to which the chemistry of the feedwater abetted
                                                        it was less severe in Unit 1. The presence of.a thin layer of red
the thinning process or provided protection against the continuous
                                                        hematite in.the region of the rupture in Unit 2 can be attributed
removal of iron from regions of turbulence and single phase flow.
                                                        to removal of any previous magnetite film during the expulsion of
The appearance of the pipe in Unit 1 was significantly different from
                                                        water / steam followed by inflow of moist air while the pipes were hot.
Unit 2; however the extent of thinning was similar in both units, but <
                                                        Upstream and downstream of the rupture the pipes appeared to have
it was less severe in Unit 1.
                                                          retained a magnetite film.
The presence of.a thin layer of red
                                                        The appearance of the pipe in Unit I was considered to be more repre-
hematite in.the region of the rupture in Unit 2 can be attributed
                                                          sentative of the true condition of the inner surface of the feedwater
to removal of any previous magnetite film during the expulsion of
                                                          system during plant operation, although most the suction line had been
water / steam followed by inflow of moist air while the pipes were hot.
                                                          exposed to air for 24 to 48 hours before being insps:ted. However,
Upstream and downstream of the rupture the pipes appeared to have
                                                          this unit was shut down normally and the pipes drained at ambient
retained a magnetite film.
                                                          temperature before the pipes were cut u Such conditions.are less
The appearance of the pipe in Unit I was considered to be more repre-
                                                          conducive to conversion of magnetite to hematite.
sentative of the true condition of the inner surface of the feedwater
                                                          The most significant nbservation was that in Unit 1 the suction pipe
system during plant operation, although most the suction line had been
                                                          tee with the header and the first elbow had a black coloration although
exposed to air for 24 to 48 hours before being insps:ted. However,
this unit was shut down normally and the pipes drained at ambient
temperature before the pipes were cut u Such conditions.are less
conducive to conversion of magnetite to hematite.
The most significant nbservation was that in Unit 1 the suction pipe
tee with the header and the first elbow had a black coloration although
extensive thinning had occurred.
Conversely, downstream sections of
,
,
l                                                        extensive thinning had occurred. Conversely, downstream sections of
                                                          the suction lines that experienced much less thinning had a thin layer
                                                          of red, non passivating, hematite.
                                                                                                  '
                                        b.                Effect of Chemical Variables
                                                          The role of chemistry control, especially before the original steam
                                                          generators were replaced, is also not clear. The very large amounts of
                                                            iron oxide sludge that has been periodically removed from all of the
!                                                          steam generators throughout the thirteen years of operation is proof
                                                            that wastage was occurring. However, this oxide sludge is thought'to
                                                            have originated predominantly in the high pressure pipes of the second-
                                                            ary water system which have been subjected to both dry and moisture
l
l
                                                            laden steam.
the suction lines that experienced much less thinning had a thin layer
of red, non passivating, hematite.
b.
Effect of Chemical Variables
'
The role of chemistry control, especially before the original steam
generators were replaced, is also not clear. The very large amounts of
iron oxide sludge that has been periodically removed from all of the
steam generators throughout the thirteen years of operation is proof
!
that wastage was occurring. However, this oxide sludge is thought'to
have originated predominantly in the high pressure pipes of the second-
ary water system which have been subjected to both dry and moisture
l
laden steam.
l
l
                                                                                                          !
!
                                                                                                    l
l
    -
-
  -     - - - - _ - - - , , _ _ _ _ , _ _ , , _ _ _ , _             , _ _ _ _ _ _ _
-
- - - - _ - - - , , _ _ _ _ , _ _ , , _ _ _ , _
, _ _ _ _ _
_
_


      .
.
    .
.
    *
*
                      Appendix                                                                                                         3
Appendix
                                                    During the last four years the deposition of sludge in the steam
3
                                                    generators had decreased considerably, a phenomenon that has been
During the last four years the deposition of sludge in the steam
                                                    attributed to higher purity condensate and feedwater and to AVT
generators had decreased considerably, a phenomenon that has been
                                                    chemistry control following the criteria of the Steam Generators
attributed to higher purity condensate and feedwater and to AVT
                                                  Owners Group (SGOG).                                                                   .
chemistry control following the criteria of the Steam Generators
                                                    Before 1980 several relatively brief periods of inleakage of James
Owners Group (SGOG).
                                                    River water upset chemistry control and allowed ppe amounts of chloride
.
                                                    to enter the secondary water system. Consequently, stress corrosion of
Before 1980 several relatively brief periods of inleakage of James
                                                    carbon steel and inconel components of the steam generator occurred as
River water upset chemistry control and allowed ppe amounts of chloride
                                                  well as denting of the inconel steam generator tubes through formation
to enter the secondary water system. Consequently, stress corrosion of
                                                    of magnetite in the tube / tube sheet regions. The effect of these
carbon steel and inconel components of the steam generator occurred as
                                                    transients on the general wastage of carbon steel pipe is not obvious.
well as denting of the inconel steam generator tubes through formation
                                                  The licensee's tentative scenario stresses the capability of pure,
of magnetite in the tube / tube sheet regions. The effect of these
                                                  deaerated water to attack carbon steel:
transients on the general wastage of carbon steel pipe is not obvious.
                                                                              '
The licensee's tentative scenario stresses the capability of pure,
deaerated water to attack carbon steel:
!
!
                                                                                              Fe*+ Fe*+ + 2e-
'
                                                                                2e-           +2H+ + 20H" + H                           2 + 20H'_
Fe*+ Fe*+ + 2e-
                                                                                                                                                                ~                      -
2e-
                                                                                              Fe* (solid) + 2H+ + 20H + Fe++ + 20H +H 2 (gas)
+2H+ + 20H" + H + 20H'_
                                                  The trace amount of Fe (OH)2 is continuously removed from the region of
2
                                                    formation before it can be further converted (oxidized) to adhesive and
Fe* (solid) + 2H+ + 20H + Fe++ + 20H
                                                    passivating magnetite.
+H
                                                  (1) Effect of pH
(gas)
l                                                                 It is the purpose of pH control, however to minimize this
~
1                                                                mechanism of attack by reducing the concentration of hydrogen
-
                                                                  ions. During the first seven years of operation the licensee
2
                                                                  controlled pH with several chemicals;                                                                      i.e., sodium phosphate,
The trace amount of Fe (OH)2 is continuously removed from the region of
                                                                  cyclohexamine, morpho 11ne, and ammonia, and the pH of the feed-
formation before it can be further converted (oxidized) to adhesive and
                                                                water and condensate varied from less than 8 (conducive to general
passivating magnetite.
                                                                  corrosion of iron) to greater tha,n 10 (not conducive to general
(1) Effect of pH
                                                                  corrosion of iron - although conducive to loss of copper from
l
                                                                  condense and feedwater tubes.) Since startup after the steam
It is the purpose of pH control, however to minimize this
                                                                  generator replacement outages the pH has been maintained between
                                                                  8.8 and 9.2, as recommended by the SGOG, as a compromise range to
                                                                minimize the corrosion of copper and iron in both the low and high
                                                                  pressure lines in the secondary system.
                                                  (2) Effect of Dissolved Oxygen
                                                                The licensee, as well as various investigators of corrosion
                                                                mechanisms, considers very low concentrations of oxygen to be
,                                                                detrimental to control of generalized thinning of carbon steel.
1
1
                                                                  In steady state conditions diffusion of dxygen to the metal -
mechanism of attack by reducing the concentration of hydrogen
                                                                water interface aids in the initial formation of magnetite and its
ions. During the first seven years of operation the licensee
                                                                continued replacement. Under such conditions redLcing agents are
controlled pH with several chemicals;
                                                      '
i.e., sodium phosphate,
  --
cyclohexamine, morpho 11ne, and ammonia, and the pH of the feed-
      -- . - , . _ , - - - . . , , - - , - - - , , . - - - - - - - , - - - - - - - - - - - - - - - - - - - - - - - - - - - , - - - - - , - - - - - - - - - - - - - - - - - -
water and condensate varied from less than 8 (conducive to general
corrosion of iron) to greater tha,n 10 (not conducive to general
corrosion of iron - although conducive to loss of copper from
condense and feedwater tubes.) Since startup after the steam
generator replacement outages the pH has been maintained between
8.8 and 9.2, as recommended by the SGOG, as a compromise range to
minimize the corrosion of copper and iron in both the low and high
pressure lines in the secondary system.
(2) Effect of Dissolved Oxygen
The licensee, as well as various investigators of corrosion
mechanisms, considers very low concentrations of oxygen to be
detrimental to control of generalized thinning of carbon steel.
,
1
In steady state conditions diffusion of dxygen to the metal -
water interface aids in the initial formation of magnetite and its
continued replacement. Under such conditions redLcing agents are
'
--
-- . - , . _ , - - - . . , , - - , - - - , , . - - - - - - - , - - - - - - - - - - - - - - - - - - - - - - - - - - - , - - - - - , - - - - - - - - - - - - - - - - - -


                                _ _ , - _ -                               .__                       -
_ _ , - _ -
          ,
.__
      ..
-
          '
,
        *                    Appendix                                                         4
..
                                                          harmful since they tend to reverse the formation of ferrous ton
'
                                                          through the reactions written above. However, this argument must
Appendix
                                                          be balanced against the cathodic attack of oxygen on iron (if the
4
                                                          iron surface is not isolated by impervious Fe 03 4 (magnetite).
*
                                                            8
harmful since they tend to reverse the formation of ferrous ton
                                                          In' a dynamic environment, such as in the feedwater pipe, all
through the reactions written above. However, this argument must
                                                              .
be balanced against the cathodic attack of oxygen on iron (if the
                                                          equilibria are changed because of the high probability that the
iron surface is not isolated by impervious Fe 03 4 (magnetite).
                                                          products of electrochemical reactions will be removed immediately.
8
                            3.             Conclusions
In' a dynamic environment, such as in the feedwater pipe, all
                                            On the basis of current technology and the understanding of the mechanisms
.
                                            of localized corrosion, the damage experienced by the or'31nal steam
equilibria are changed because of the high probability that the
                                            generator tubes during the initial seven years of plant operation is
products of electrochemical reactions will be removed immediately.
                                            understandable. However, the inspector has not been able to correlate the -
3.
                                            cause of steam generator tube denting to the generalized thinning of the A
Conclusions
                                            feedwater suct, ion pipe. Also, the inspector has not been convinced that the
On the basis of current technology and the understanding of the mechanisms
                                            feedwater system was ever coated completely with magnetite, or if it were,
of localized corrosion, the damage experienced by the or'31nal steam
                                            that the magnetite protected the pipe from erosion / corrosion. It is evident
generator tubes during the initial seven years of plant operation is
                                            that thinning occurred in regions of hydraulic turbulence, and consequently
understandable. However, the inspector has not been able to correlate the -
                                            erosion appears to have been the dominant cause of thinning.
cause of steam generator tube denting to the generalized thinning of the A
                                            The degree to which generalized corrosion mechanisms abetted the transfer of
feedwater suct, ion pipe. Also, the inspector has not been convinced that the
:                                           metallic or ionic iron from the pipe surface has not been established.
feedwater system was ever coated completely with magnetite, or if it were,
that the magnetite protected the pipe from erosion / corrosion.
It is evident
that thinning occurred in regions of hydraulic turbulence, and consequently
erosion appears to have been the dominant cause of thinning.
The degree to which generalized corrosion mechanisms abetted the transfer of
:
metallic or ionic iron from the pipe surface has not been established.
;
;
.
.
                                                                                                              .
.
                                                                                                                                I
I
:
:
                                                                                                                  .                       .
.
_
.
1                                                       ,
_
  "
1
!                                                                                                                                                      g
,
!
"
g
<
<
  ,n.-     -- , , - - , , ,-               ,,,r,_n.,,,         ,,-n__-_     nn,- n.- -.,_,n   ,n . , - - - ,   ,-n. , .n.,,--..n-.,-- --.,,.----n.- ,,,,.---,,.m--. , - _ , .
,n.-
-- , , - - , , ,-
,,,r,_n.,,,
,,-n__-_
nn,-
n.-
-.,_,n
,n
. , - - - ,
,-n.
,
.n.,,--..n-.,--
--.,,.----n.-
,,,,.---,,.m--.
, - _ , .


  ___.___ ____         _ _ _ . _ _ _ _ _ _ _ _ _ _ _ ___ _ __ _ _ _ _                                       _                                  ..                                                                                             -- -
___.___ ____
                                                                                                                                                                    '
_ _ _ . _ _ _ _ _ _ _ _ _ _ _ ___ _ __ _ _ _ _
                                                                                                          .,e eemf                                * ':
..
                                                                                                                                                          ;;                            , ;;                                                                  *
-- -
                                                                                                                              ~
_
                                                                                                                                                                <                                             -
~
                            .
'
                                                                                                , . .                                                                   : .,              ,
* ':
                                                                          ,
<
                                                                                                                                        ,
.
                                                                                                                                                                                                                                                                  '
, . .
                                                                  .                                       .                                                                                                                            1
,
                  '
;;
                                                                                                                                                                                                                                        \
.,
                                                                                                                                                                                                .
, ;;
                                                                                                                                                                  g'__.
-
                                                      /
*
                -
.,e eemf
                                                                                                                                                4
:
                                                                                                                                                                                                                  ,
,
                                                          s                                  ;           :-
,
                                                                                                                                          -
                                                                                                                                                                                  ^
                                                                                                                                                                                                  ,
                                                                                                                                                                                                  f        .
                                                                                                                                                                      ~                            <
                                                                                                                                                                                                                                                ,
                                                                                                e
                                                                                                                                                                Y                                , ~,              '
                                                                                                                                                                                                                                                                ,
                                                                                  _
                                                                                                                                                                                                                    ,-, .
                                                                                                                                                                                                                        .
                                                                                                                                                                                                                    a+s
                                                                                                                                                                  g        .
                                                                                                                                                                                                                '
1
1
                                                                                                                                                                        7[                             '
'
I                                                                                                                  -
.
                                                                                                                        -
\\
                                                                                                                                                        '
.
                                                                                                                                                                  %                       '
'
                                                                                                                                                                                              ,               [                                          _7
.
                                                                                                                                                                                                                                                            .
/
              -
s
                                    -
;
:-
-
g'__.
-
4
,
,
,
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f
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.
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e
,
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. .
l
l
                                                                                  ,
- :
                                                                                        ,  .
.
                                                                                              3,. g                                                                                                                                                  ,
' ,
                                  g                                    '
\\
                                                                                                        . .          l      .
.
                                                                                                                                                            :
'
                                                                                                                                                              '
'
                                                                                                                                                                                          -:          .                 ' ,
-
                                                                                                                                                                                                                              . >                  .<
.<
                                                                                                                                                                                                                                                      \
.
                                                                                                      .v
.o
                                                                                                                                                                                                                                -
.v
                                                    ...,       .                                .o                                                      ,
:
                                                            , . <                                                               .
. >
                                                                                                                                                      ,
...,
                                                                                    .
,
                                                                                                                                                                                        ,
, . <
                                                                                                                                                                                                                                  '
.
                                                                                            *    i                                                 /                                  /
,
                                                                      .. , .j .
,
                                                                                                    p.-
'
                                                                                                    .
.
                                                                                                              .
/
                                                                                                                  ,
i
                                                                                                                                                  -
/
                                                                                                                                                                                    ,
.
                                                                                                                                                                                                                                  .
.. , .j
                                                                                                                                                                                                                                  3
p.-
                                                                                '
.
                                                                                        w                      -
,
                                                                                                                                            ,.
-
                                                                                                                                                                                                                            '
,
                                                                                      :  'M                                             /,                                     ,'                                               ,
3
                                                                                                                                                                                                                                                    ,   ,_
*
                                                                                                                                                                                                                                      ,   ,
.
                                            :                                                                                         .
.
                                                                                                                                                                                ,
w
                                                                                                                                                                                                                                            4
-
                                                                                                                                    '
,.
                                                                            '                                                                                                                            '
'
                                                                                                                                  ,                                         .                                                       .
'
                                        '                                                                                                                                                     ,
'M
                                                                                                                                                                                                                                              '                 i
/,
                                                                                                                                                                                                                          ,
,'
:
,
,
,_
,
,
:
.
,
'
'
'
4
,
.
.
'
'
i
,
,
;
;
                                                                                                                                                                                                                                                          *
*
l
l
i                     "B"                                                                             "A"                 Location                       24" Condensate
i
l                   MFW Pump                                                                   MFW Pump               of Rupture                           Supply Header
"B"
                                                                                                                      in "A" Suction
"A"
                                                                                                                            Pipe
Location
                                                                                                                                                                                                                                                                .
24" Condensate
                                                                                                                                            Figure 1
l
                                                                                                                                                                                          __      __
MFW Pump
MFW Pump
of Rupture
Supply Header
in "A" Suction
Pipe
.
Figure 1


                                                                                                                                                                                  . _ - _ _ _ _ _ _                                 ._ _ _ _ _ _ _ .
. _ - _ _ _ _ _ _
<                                                                                                                                                                                                                                                         l
._ _ _ _ _ _ _ .
                                                      - '
<
                                                              ;
l
                                                                                    ..                      l-
.
                                                                                                                  .
t
                                                                                                                            77 7      -
77 7
                                                                                                                                          -
.
                                                                                                                                                -        *
,
                                                                                                                                                            .
- '
                                                                                                                                                                              g
l-
                                                                                                                                                                                                                                                      ,
-
                                                                                                                                                                                                                                                          t
-
                                                                      ,.
-
;                                                                   .     . <,3 /                           .e-                                             .              .
*
            .
g
                                                                                                                                                      <c                       (,
;
                                                                                                                                                  ..
,.
                                                                                                                                                                                  ;
..
                                                          .
;
                                                                                                                                                  y.:
.
                                                                                                        y
. <,3
                                                                                                                        -
/
                                                                                                              .1
.e-
.
.
<c
(
.
,
..
;
.
y.:
','
y
.1
-
;
;
                                                        ','
l
          '
._
                                                                l                 ~
T
                                                                                      ._
g
                                                                                            T*              i              g       --
'
                                                                                                                                              '
--
                              -
'
                                        &*                       -
i
                                                                    f-
&*
                                                                          ~
f-
                                                                                      s         .
~
                                                                                                      .
*
                                                                                                            l
s
                                                                                                            :
.
                                                                                                                                                                                                                                                          _
l
                                                                                                                                                                                                                                                          :
_
                                                                .
-
                                                                        4                                                                                       _.
-
                                                                                                                                                                                                                                                          !
:
                                                                                                                                                                                                                                                          .
:
                                                            '
~
                                                                                            %
.
                                          ?                                       r               >
.
                                                                                                                            s     -
4
                                                                                                                                                                                                      \                                                   ,.
!
                                                                                                  -
_.
                                                      . , , . .                      ~'$ ~                                  %                                                                                           >
.
                                                                                                                                                                                                                                ~ l}                       i
%
                                ! . ' , ,,
'
l                                  ,
?
                                    ...
r
                                        * ' *                                -       -
>
                f                   .,.     l.                                                                                                                           ,
s
                                                                                                                                                                                                                                                          i
-
                                e J _ summme-
\\
                                                                                          -
,.
                                                                                                                                            '
-
                                          M 'W!9 M                                                                                                                                                                 , _ . ,
~'$
                                                                                                                                                                                                ',
%
                                                                                                                                                                                                    <
~ l}
                                                                                                                                                            .               .
i
                                                                                                                                                    -
>
                  -                                                           .
~
                                                                                                                                                                                                                            _..
. , , . .
                                                                                                                                                                                                                              .
l
                  "B"                                                             "A'"                   Location       24" Condensate
! . ' , ,,
              MFW Pump                                                   MFW Pump                     of Rupture         Supply Header
,
                                                                                                    in "A" Suction
* ' *
                                                                                                            Pipe
...
                                                                                                                                                                                                                                                            i
-
                                                                                                                    Figure 1
-
  _ _ _ .       . _ - - - . .               . . _ . -.                                   .   -__
f
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7. a '
                                                                                                                                                                                                                                                                fj
,
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,
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\\.
                                                                                                                                                                                                                                                          ~
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        f._                   \.           -
ci
                                                                                                                                                            ,
e
                                                                                                                                                                                                                      4
'
                                                                                                                                                                                                                                                        ,,_,,
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                                                                                  y
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                                                                                                  . -
                                                                                                                                      - *;
                                                                                                                                                    m
                                                                                                                                                                                                                                                -
                                                                                                                                                                                                                                                          ,
                                        .
                                                                                                'E,'<
                                                                                                .  -                                        '_- '
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f
                                                                                      &;*                 h                     f ff             Q       Q ',\
\\
                                                                            '
'E,'<
                                                                                .if?b                                       b               ' ';                     ,
_ t. '_- '
                                                                                q E O.tk
-
                                                                                                                                                                            ~'
m
                                                                                                                                        p,?e
. -
                                                                                ,                                                                                                                                                                    Aq,7
,, ,
                                                                                  ,m,.                                  4uc         g^ 4 :,
&;*
                          .,
h
                                                                                        $.W;f h                                                                                                                                                       p];q j&
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s\\
                                                                        "hkh                                                                                                                                                                    IM
.
                    -
m
                                                                                                                              m          .
-
                                                                                                                                                                                A-                                                              s\
.
                                                                                                                                                                                                                                                                  .
Al
                                                                                                                        Al
.
                                                                                  , wen,.c.e4In f
A-
                                                                                                        .
, wen,.c.e4In f
                                                                      *                                                                                                   '
'
                          '
*
                                      2h
2h
                                                                                                                                                                                                                                                                      -
'
--
-


                                                    - - - . _ _ _ _ _ _ . _ _ _ .
- - - . _ _ _ _ _ _ . _ _ _ .
    O
O
                                                                                  r>       -
r>
            ,.
-
                              7          _ YNY;$%@                                               gv., y g                                                                            ,; bj
NY;$%@ gv., y
                                y        e
,.
                                                i%?Q *
7
                            J;Jgg           ty;,..                                               + ;; 4                                                     g.g 7. t y9               ''
_ Y
                                  ~.  ..    4;l, ,.                                          l    *
bj
                                                                                                          '
i%?Q *
                                                                                                            ~- O'"klR                                     f '" , . .'
g
                                                                                                                                                                        !id
,;
                ~.                   N sy ,og ,
e
                                                                                                ''
y
                                                                                                    --
J;Jgg
                                                                                                                  ,.;f:;,
ty;,..
                                                                                                                      :~                     . ,, ,
+ ;; 4
                                                                                                                                                          n                   e
g.g 7. t y9
                                                                                                                                                                                        ,
''
                                                                                                                  t      -          . ;; 3                           t,          .
O'"klR
                                              a ':.L .                                                                     '
f '" , . .'
                                                                                                                                    ~.5' ; .jf           f.I;q)?2'"
!id
                    -     .
'
                                                b y-
~.
                                                  .-
4;l, ,.
                                                                                                                . . ,
l
                                                                                                            j;;L ,
*
                                                                                                                            -
~-
                                                                                                                              . =y
..
                                                                                                                                      .y              .  1'
,.;f:;,
                                                                                                                                                              s, g
''
                                                                                                                                                                  -
N s ,og ,
                                                                                                                                                                                  .
:~
                                                                                                                                                                                  ,7
--
                                                                                                                                                  'hNfI;f.; .t ';; bl. }R
,
                                                1
y
                  ~
. , ,
                                                  OA'F '                                                      '{, J. .,[[? N
,
                                                                                                                                                                        yp;,g.,
~.
                                          -
e
                                                                                                                                                            .
n
                                                                                                      ,
t,
                                                                                                - ',                  ..
f.I;q)?2'"
                                                                                                        i ~
. ;; 3
                    ,
L
                                                                                                                                                                                            _
t
                                                                                          .
-
    -                                                                                   ..
a ':. .
                                                              ,,
.
                                                  -
'
                                                                                                                                                                                          e
. =y ~.5'
    [-                                                     ' -
;
                                                                  ~
.jf
                                                                                                                                                        ,
s, g
                                                                                                                                                                    -
-
                                                                                                                                                                            7             a
.
    !-
b y-
    ,x .
. . ,
                                                            e.                                                                             ,.                           j                m
-
                                            s,              ~.                                                                                                       }
.y
                                                                                                                                                                      #
.
                                              #                           .
-
                                                                                                                                                                        *'
OA'F '
                                                    ia%
'{, J. .,[[? N
                                      f
'hNfI;f.; .t '; bl. }R
                                          ( '' $                               s
j;;L ,
                                  f'
.
                                                                        h
1'
                                '
-
                                                                    D
,7
                                                                  .+;               ,
1
                                                                              i,
.-
                                                                      ,,
~
                                                          ?:
;
                                                  ;.               ,
.
                                                                                                  %
yp;,g.,
                      I                                             .
- ',
                                                  $
,
                                                    ay
..
                                                                                                                '
i ~
                ,.';   ,                  Fl$
,
                      cg w ~                                                                                                                                 [
_
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                                                                                                                                          .
-
                                                                                                                              .
..
                    .
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                                                                                                                            _
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- _ _ _ _ . _ . . . _ _ _ . _ _ . _ _.
                                                                                                                                                                                                                                                            e
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                                                                                                                                                                                                                -e       -
-e
            em                                                 w-                                             . . . . .
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l                                                                                                             .             ,
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                                                                                                          '
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. . . . .
                                                                              _
l
                                                                                                                                4                       '                                                                                                     f
.
l                                                                                                               s                                                                                                            ..
,
                                                                                                                                                                                                                              ,
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.
                                                                                                                                                                                                                                ~
-
                                                                                                                                                                                                                                  . _ -t
'
                                                                                                                                                                                                                                                    -  '
,
,                         .
.
                                                                                                                                                                                                                      .
. . . .
                                                                                                                                                                                                                                    ....'
i
                                                                                                                                                                                                                                          -
.
                                                                                                                                                  .
-
i                                                                                                                                                                                                                                             *-
I
                                                                                                                                                      '..
                                                                                                                                                              ~
                                                                                                                                                                                    Ruptured 'A" MFW Suction Pipe
l'                                        '
                                                                                                                                      g\                            ,~
                                                                                                                                                                        *        ' fiesting Against "B" MFW Pump
                                                                                                                                                %                                        Discharge Pipe. (Post Rupture                                '
              .
                                                                                                                                      .
                                                                                                                                                              4                                  Configuration)
                                                                          .                                                                                        -
                                                                                                                                                                  *
                                                                                                                                                                                                                        .                    e    ,
                                                                                ,
                                                                                                                                                                                                                                  -
'
'
                i..' 4.,                      ..                    ._
'..
                                                                                  .
*-
                                                                                                                        &                'e                                                                      -
                    .
                #
                                      h,[        ,, ' ,
                                                            '
                                                                                  ~.                                                                                                                                                                      ,
                                                          e'                          <:
                                              '
                        : '          ,
                                                                                                ,  .
                                                                                    '
                                                                                                                                                    /
                                                                                                                                                                                      *                      %
                                                                                                                                              ,
                                                                          -
                                                                                          .
                                                                                                            =
                                                                                                                                                .        .
                                        '
                                                                                            '
                                                                                                        '      :                                                                  ~      - -
                          -                .
                                                                                  4                  .
                                                                                                                                              .
                                                                                                                                                .                                                .
                                                                                                                                                    >
1                                                                                                                  .
                                                                                                                            .                        *           '                  -
                                                                                                                                                                                                            -
-
,
                                                                                        .
                                                                                                    e                                                                                                          .-         ,
                                                                                          *                                              -
                                                                                                                                                                                                                                                  ,
l                                                                  8                e.          e.        /
I                                                                                                                  g Y              f                                          ,
                                                                                                                              >                                                                ,
l
l
                                                                                                                                                                          .
g\\
                                                                                                                                                                                            )     M
~
                                                                                                                                          .-                                 .
Ruptured 'A" MFW Suction Pipe
(
l'
'
,~
' fiesting Against "B" MFW Pump
*
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Discharge Pipe. (Post Rupture
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Figure 3
i
'
'
                                _. .                                                                                                                       ._             _                           .--
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    a ...,m.,.-maa_   _-_a_.Au___.h._a__-2       .  _____m-   a     .a--_.-.,44   4_am___2,_____s.           ma   _ _         . .__             . _ _ _ _ _ _ .     4 .___..am .mam._ __ _,, m2,.m _ ,.,
a
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                                                              *
                                                                                                                    *
                                                                                                                                                    ,
                                          ,                  ..                                                                  9
                                                              -
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Latest revision as of 13:36, 23 May 2025

Augmented Insp Repts 50-280/86-42 & 50-281/86-42 on 861209- 870114.Violation Noted:Failure to Fully Follow Procedures, Provide Adequate Instruction for & Document Performance of Maint Operations
ML20211C516
Person / Time
Site: Surry  Dominion icon.png
Issue date: 02/10/1987
From: Panciera V
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20211C439 List:
References
50-280-86-42, 50-281-86-42, NUDOCS 8702200119
Download: ML20211C516 (53)


See also: IR 05000280/1986042

Text

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..... ' . Report Nos.: 50-280/06-42 and 50-281/86-42 Licensee: Virgirtia Electric and Power C'ompany Richmond, VA 23261 Docket Nos.: 50-280 and 50-281 License Nos.: DPR-32 and DPR-37 Facility Name: Surry 1 and 2 Inspection Conducted: December 9,1986 - January 14, 1987 Team Inspectors: J. Caldwell M. A. Caruso W. T. Cooper 8. R. Crowley J. T. Gilliland W. E. Holland T. A. Peebles P. A. Taylor Contributing Inspectors: A. R. Herdt J. D. Ennis P. M. Mad n W. Ros Approved by: I /L n s h a 7 _mm Vincent W. Panciera, Team ~ Lea' der' ~ /Date Sigried ~ Division of Reactor Safety SL)l9tARY Scope: This special, announced augmented inspection was conducted for the Surry Unit 2 feedwater pipe rupture event of December 9,1986. The areas inspected included the sequence of events, effects of failure, metallurgical aspects, items contributing to the likelihood or severity of the event, licensee's response to the event, aspects that made handling the event more difficult, consideration of shutdown of Unit 1, investigation and corrective actions planned and safety considerations for station restart. Results: One violation was identified (paragraph 11.a.(2)). . 0,g22Kg[[{ $$$$ go ' o - t

' . ' . REPORT DETAILS . 1. Persons Contacted ' Licensee Employees W. L. Stewart, Vice President, Nuclear Operations R. J. Hardwick, Corporate Manager for Licensing and Safety R. F. Saunders, Surry Station Manager

  • R. W. Calder, Nuclear Engineering Manager

"H. L. Miller, Assistant Station Manager for Licensing and Safety

  • D. L. Benson, Assistant Station Manager for Operations and Maintenance

J. M. McAvoy, System Metallurgist

  • W. D. Craft, Licensing Coordinator
  • W. R. Benthall, Nuclear Specialist

Other licensee employees contacted included engineers, technicians, operators, mechanics, security members and office personnel. NRC Residen' Inspector

  • W. Holland
  • Attended exit interview.

. 2. Exit Interview The inspection scope and findings were summarized on January 14, 1987, with those persons indicated in paragraph 1 above. The inspectors described the areas inspected and discussed in detail the inspection findings listed below. No dissenting comments were received from the licensee. Violation 50-281/86-42-02 - Inadequate Procedure for the Maintenance of the Main Steam Trip Valve (paragraph 11.a.(2)). ~ Inspector Followup Item 50-280, 281/86-42-01 - Clarification of Surface Preparation Methods in NOE Procedures (paragraph 8.e.). The licensee did not identify as proprietary any of the material provided to or reviewed by the inspectors during this inspection. 3. Licensee Action on Previous Enforcement Matters This subject was not addressed in the inspection. 4. Unresolved Items Unresolved items were not identified during the inspection. L .- 4 0 .

. . ~ . -- . -- .- . _ _ - - _.- _ . . _ _ - - . - . - _ _ _ - - - .. - ' . b 2 = 4 - 5. Augmented Inspection Team (AIT) Activities

Shortly after the pipe rupture event, Region II was notified by the Surry Senior Resident Inspector (SRI) who was on site, and had proceeded to the y control roong to assess the situation. The Regional personnel immediately 1 staffed the regional response center at about 2:45 p.m. NRC Headquarters was then notified at approximately 3:00 p.m. that a main feedwater line pipe rupture in the turbine building had occurred. An open line between the Surty site and the NRC Operations Center was maintained until early hours of the next morning. About 3:30 p.m., a decision was made by Regional ,

management to send an inspection team to the site. This team consisted of { Regional based personnel and the SRIs from North Anna and Surry. The team arrived on site about 9:30 p.m. on December 9, 1986. After a meeting with

j plant management to assess the operational status of the unit, the team ! toured the damaged area of the turbine building in the vicinity of the feed- l pump suction piping. During a meeting at 9:00 a.m. on December 10, 1986, with plant management, NRC inspection assignments were outlined. Virginia Power agreed to provide any assistance required by the team. In addition, 4 l the ground rules to be applied by the inspection team regarding quarantine ! of equipment were discussed. Virginia Power agreed to seek NRC concurrence ! before any work was accomplished for restoration of systems. During the ' morning of December 10, 1986, the team's status was upgraded to an Augmented ! Inspection Team (AIT), and an engineer from the Office of Nuclear Reactor l Regulation, knowledgeable in water hammer phenomena, was assigned to the l team. The team conducted inspections during the remainder of the week 1 ending December 12, 1986, to ascertain the circumstances involved in the j accident. An executive summary was transmitted to the Region II office on l December 17, 1986. This summary provided the significant facts concerning

the event. The AIT did not conclude its inspection at that time due to the ! ongoing activities by the licensee to develop a root cause analysis, which I required subsequent inspection activities. AIT activities continued during ! the weeks of December 22 and 29, 1986, and January 12, 1987. An AIT exit l meeting with plant management was held on January 14, 1987, after review of

the licensee's investigative report entitled "Surry Unit 2 Reactor Trip and ! Feedwater Pipe Failure Report" and proposed corrective actions which were j presented to the NRC on January 12, 1987, in addition to the AIT inspection i activities, inspectors knowledgeable in security, fire protection systems, l water chemistry and check valve design were assigned to review specific ! concerns in these areas. Where applicable, their inspection findings have i been incorporated into this AIT inspection report. t 6. Overview of the Event , .

On December 9, 1986, with both units operating at 100 percent reactor power, ! a Unit 2 reactor trip followed by a main feedwater (MFW) line rupture

occurred. Unit 2 had completed a refueling outage and returned to full I power operation on December 8, 1986. ! A low-low level in the C Steam Generator ($/G) caus6d a reactor trip and l start of the two motor driven auxiliary feedwater pumps. .' e ' . . I

' . . e 3 The control room operators noted the S/G code safety valves lifting and regulated S/G pressure through the atmospheric dump valves. Approximately 30 seconds after the trip the unit's electrical busses auto-transferred to offsite power. A small steam release noise was heard followed by a very loud noise approximately five seconds later. A shift supervisor who was in the turbine building, realizing that a large steam break had occurred, went to the control room and alerted the control room watch. All secondary pumps (high pressure drain, condensate and main feedwater) were secured, and the break was isolated. Water to the S/GS was supplied by the auxiliary feedwater system. The primary systems responded normally to the loss of load transient. Reactor coolant temperature, pressure, and pressurizer level were stabilized in the desired band. A notification of unusual event was declared by the licensee at 2:27 p.m. and was upgraded later to an ALERT in order to ensure accountability of all station personnel. The 18-inch suction line to the A main feedwater pump was subsequently found to have ruptured at the elbow where the line connects to the 24-inch condensate header. In addition, station halon and cardox systems actuated because of water short-circuiting control systems in the area. Control room habitability was a concern prior to initiating control room ventilation because doors were blocked open to allow better control room access without recognizing that carbon dioxide had been discharged in the areas above. The carbon dioxide was apparently coming into the control room from the hallway. The emergency was terminated at 4:23 p.m. after personnel accountability had been established. Eight individuals were injured due to the steam and water. Four of the injured subt.equently died. Two of the injured were treated and released. Two individuals remained hospitalized. One, individual was later released. Unit 2 was placed in cold shutdown at 7:04 a.m. hours on December 10, 1986. 7. Sequence of Events a. Initial Plant Conditions Prior to the Unit 2 Event Unit 2 had achieved stable 100 percent power operation on December 8, 1986, following a refueling outage. Unit 1 was operating at 100 percent power. Two major maintenance or surveillance activities were in progress: the troubleshootin coolant pump (RCP)g of a B train underfrequendy relay for a reactor breaker, and the troubleshooting of an aux 111ary . . , ! 9 .

.' . ' 4 instrument air ccepressor. The first item had required the racking in and closing of the B reactor trip bypass breaker. The A and B reactor trip breakers were still closed. The second item required the shutdown of the running auxiliary instrument air compressor and the attempted start of the non-running auxiliary instrument air compressor. The delay in starting the auxiliary instrument air compressor caused the instrument air pressure to decrease to approximately 78 psig, instead of the normal 100 psig. Some minor construction activity was occurring in the vicinity of the main feedwater (MFW) pumps, such as installing insulation on piping. The unit's data gathering computer (Prodac 250) was out of service, but reactor trip information was available from a sequence of events (SOE) alarm printer and a newly installed Emergency Response Facility Computer (ERFC). The SOE alarm printer prints information continuously on a millisecond basis, but is limited in scope to alarms. The ERFC displays s' stem parameters, but only updates in fifteen second incre- y ments and samples the parameters at different times. The ERFC is intended for a broader picture than the SOE alarm printer. Interviews with the Shift Supervisor and Control Room Operators (CRO) were used to correlate times and to fill in gaps of the event. The SOE alarm printer time of the reactor trip was 1420:03(RT00)and the ERFC time of the reactor trip was between 1421:15-:30 and has been correlated to be 1421:15. Therefore, the SOE information will be addressed in increments per the ERFC clock with specifics referred to as seconds of time from the RT per the SOE alarm printer. Other sequence of events information was developed by the licensee, using security alarm computer data, interviews with additional person- nel, and time motion studies. This information correlates with this SOE data. b. Secondary System Conditions Prior To The Event Both MFV pumps were operating with a suction pressure of 370 psig, a discharge pressure of 1040 psig and a temperature of 374 degrees F. The condensate system was operating normally with one of two high pres- sure heater drain pumps, two of two low pressure heater drain pumps, and two of three condensate pumps running. The full flow condensate polishing system and all feedwater h9aters were in service. . c. Plant Conditions and Personnel Actions During The Event 1421:(00-15) ERFC time The first indication of a problem occurred at RT -03 when the Unit 2 control room received an annunciator alarm for!the B steam generator (S/G) as MFV flow was less than steam flow. This indication and the .' ' . O i

.' 5 , subsequent alarm on the A S/G indicated that the C main steam trip valve (MSTV) had inadvertently closed. The closure of the MSTV caused the steam flow from the other S/Gs to begin to increase by 50 percent and caused the mismatch alarm, since the MFW flow to the S/Gs had not yet responded. . A direct indication of the C MSTV closing was not received as the valve-closed limit switches did not function properly. However, indication and alarm that the valve was not fully open was available to the CRO. The closure of the C MSTV caused MFW pressure downstream of the C MFW flow control valve (FCV) to increase from 865 psig to 970 psig with the A and B MFW pressures initially stable at 845 and 835 psig, respectively.. - The other steam generator MSTVs closed shortly afterward due to the higher than normal steam flow in those lines caused by the continuing 100 percent demand of the main turbine. The MSTVs are reverse seated check valves held open against the steam flow by air operated pistons. As the MSTV discs are partially in the steam flow path, an increase in steam flow places more closing force on the disc. All three MSTVs closed and seated properly and steam flow was stopped. 1421:(15-30) A low-low S/G 1evel annunciator signal which was received for C S/G and was the initiating signal for the reactor trip at 1421:15 (RT 00) and for the starting of the two motor driven auxiliary feedwater pumps. The reactor trip resulted in a trip of the main turbine generator. The stopping of steam flow to the main turbine by the MSTVs closing caused the S/G pressures to increase. As C MSTV had closed first, its pres- sure increased first. This increase in pressure collapsed the bubbles in its S/G which caused the level to decrease to the reactor trip low- Iow level setpoint. At RT +03, the CR0 manually tripped th'e reactor. One control rod (M-10) indicated that it had inserted from 228 steps to 35 steps. Reactor power was verified to have decreased to normal post-trip decay l values. At RT +04, the CRO, noting that the S/G code safety valves were lif ting, took the S/G Power Operated Relief Valves (PORV) out of manual and began to regulate S/G pressure through this atmospheric dump mode. S/G pressures had increased from their initta) values of 820, 814 and ! I 1 i

. , ! ' l -

~ . . 6 - 815 psig and were 936, 979, and 1055 psig.* The S/G pressures all responded to the individual MSTV closings, and since C MSTV had been closed longest, it caused the C S/G to reach the highest pressure. The AFW flows were greatest to the S/G with the least pressure. AFW flow was 344, 300 and 98 gpa. . Pressure downstream of the MFW FCVs increased to 1054, 1042 and 1090 psig. 1421:(30 -45) Pressure downstream of the MFW FCVs decreased to 1008, 1015 and 1028 psig. S/G pressures were 1028, 1013, and 1055 psig. The C S/G PORV was being used to control primary temperature and C S/G pressure remained constant. Low-low levels occurred in the A and B S/Gs in response to their increasing pressure which caused the automatic initiation of the third auxiliary feedwater pump. The steam inlet valve to the turbine driven auxiliary feedwater pump opened and the pump started. S/G 1evels as a percent of wide range instrumentation were 74, 73 and 75 versus a normal operating level of 84 percent. AFW flow was 337, 317 and 109 gpm. 1421:(45-1422:00) . The three MFW FCVs received an automatic signal to close and in a few seconds were closed. This signal is generated to minimize primary system cooldown following a reactor trip and is generated when the primary temperature decreases to less than 554 degrees F. The MFW pump recirculation valves (FCV-FW-250A and 2508) for A and 8 MFW pumps auto- opened a few seconds later. Each recire valve opens when flow from its MFW pump decreases to less than 2800 gpm. Pressure downstream of the MFW FCVs increased on A to 1059 and decreased on B and C to 812 and 949 psig. Pressure in the S/Gs remained constant at 1028, 1013 and 1065 psig. The A MFW FCV may have been slightly slow in closing, and as the discharge pressure of the MFW pumps was increasing to its high of 1290 psig, the pressure down- stream of the A MFW FCV would have increased. The unit's electrical busses auto-transferred to offsite power at RT +32, when the main generator, as is normal, auto-transferred on a 30-second delay signal following a main turbine generator trip. 1

  • When pressures, flows, etc., are listed in sequence, the order refers

respectively to the A, 8, and C steam generatob. ' . , d u . . - . _ _ _ . . . _ - . _________._._._--.__ - ,._ ______._ _ _.- _ __m, - _ . _ _ - _ _ _ _ _ _-- - .. _ -.. , . -. - _

.' ' .- 7 Five seconds later at RT +37, a small steam release was seen and heard in the vicinity of the A MFW pump and the first point heater steam-side safety relief. 1422:(00 -15) . ., . Pressure downstream of the MFW FCVs decreased to 445 psig which indicates that the downstream MFW check valves were operating and the pressure of the water in the lines was decreasing to its saturation pressure. The S/G pressures decreased to 997, 1003 and 1020 psig and levels remained in the 74 percent range. The AFW flow was 342, 317 and 98 gps. The MFW pump discharge pressure reached a peak of 1290 psig and the suction pressure rose to 550-600 psig as the condensata pumps responded to the minimal recirculation flow conditions. The noise of a small steam release was followed at approximately RT +42 by a very loud noise from the vicinity of the MFW pump suction piping. The primary system responded normally to the loss of load transient. Reactor coolant system temperature was stabilized at 552 degrees F and pressurizer level was recovered as it reached the low level setpoint. Reactor coolant system pressure decreased from 2235 to 2015 psig in response to the cooldown. The probable time for the piping break appears to have occurred at RT +42. The break occurred in an elbow where the 24-inch MFW suction header splits off at a tee to an 18-inch branch line in an elbow toward the suction of the A MFW pump. About ten feet farther down the 24-inch header toward the suction of the 8 MFW pump is where the high pressure heater drain pumps' discharge flow is combined with the condensate flow. , Approximately 15 seconds after the large pipe rupture, at RT +57, the A MFW pump tripped due to low suction pressure. The time delay relays , ' which operate in conjunction with a suction pressure of less than 55 psig were found set at 15 seconds,V pump rectre valve indicated that and the SOE alarm printer agrees with the time of pump trip. The B MF it closed while the A rectre valve remained open, as it should have, , i for 60 seconds after the pump trip. A reason for the 8 recirc valve closing is that the B MFW pump continued to run and the flow in that r l line increased to greater than the rectre re-setpoint of 4000 GPM. This increase in flow was caused by a backward flow path through-the ,

tripped A MFW pump. It was later found that this pump's discharge j check valve was disabled. The 8 MFW pump continued to run for 23 l seconds.

! ! .' & O t

- . . 8 - 1422:(15-30) An operations supervisor was in the turbine building observing construc- tion activity around the MFW pumps. He heard and saw the large steam break, And immediately ran to the control room to alert the operators. He also' told them that people had been injured. The shift supervisor then ordered that all secondary pumps be secured. 1422:(30-45) When the CR0s began to secure the secondary pumps, the B MFW pump was found " auto-off" with its yellow disagreement light on, which occurred at RT +81, or about 1422:36. Its time delay relays were also found set at 15 seconds. Therefore, its trip point of 70 psig was i reached at RT 66 or about 24 seconds after the break. The high pres - sure heater drain pump was running and had to be turned off, and both low pressure heater drain pumps had tripped. After all secondary pumps were secured, the steam release stopped. The ERFC and SOE alarm printer agreed with the operators on the above time sequence. 1424 The CR0 noted that primary temperature was stable at about 550 degrees F. ' The NRC Senior Resident Inspector arrived in the Control Room. ! 1425 The CR0 secured the B RCP to avoid adding heat to the reactor coolant system. Plant conditions were stable with RCS temperature being l maintained at approximately 540 degrees F by releasing decay heat through the C S/G power operated relief valve (PORV). ' 1427 An Unusual Event was declared. 1430 l Ground and air ambulances were called. The CR0 changed the normal suction of the charging pumps to refueling water storage tank. The B and C S/G low-low level alarms cleared and the steam driven APW pump was secured. ! The Regional response center called the c,ontrol room. , , b en

_. _ ~ . , 9 . , 1440 An Alert was declared to assist in personnel accountability. 1445 . _ The CR0 secured the A RCP. The Shift Supervisor noted that the condenser still had a vacuum and as there was no steam for the main turbine gland seal, opened the vacuum ' breaker. State and local authorities were notified of the Alert. 1500 NRC Operations Center was notified of the Alert. Reactor coolant system temperature was 530 degrees F, pressurizer level was 25 percent, and pressurizer pressure was 2160 psig. 1506 The CR0 secured B auxiliary motor driven feedwater pump. 1514 The CR0 began emergency boration to cold shutdown concentration as part ' of the normal post trip procedure. 1518 . ' Personnel accountability initiated. I 1535 i The corporate Emergency Response Cente'r was activated. 1539 The CR0 secured emergency boration. i ! 1548 Personnel accountability completed. 1625 The Alert was terminated. The control rod (M410) which had indicated that it inserted only to 35 steps now was noted to indicate fully inserted. .' - !

..- . . - - - . . . . - _ . - - . . . 10 -

1821 Cooldown at 50 degrees F per hour was initiated. 2130 , . , t < NRC team arrived on site. , 0355 December 10, 1986 Unit placed on residual heat removal system with ter.perature at 350 degrees F and pressure at 450 psig. 0704 i The unit achieved cold shutdown conditions. ' 8. Effects of Fai1'ure ! a. Pipe Rupture The rupture of the 18-inch A MFW suction pipe occurred on a 90 degree ! elbow at a point about one foot from where the suction pipa joins the condensate supply header. The point at which the break occurred , relative to the main feedwater pump is indicated on Figure 1, which is ' a picture of the identical undamaged Unit 1 piping configuration. Figure 2 shows the rupture location from the condensate supply header side. Figure 2 clearly indicates that the rupture was a catastrophic, ,

360 degree circumferential break. Figure 3 shows the broken pipe from

the MFW pump suction side. ! b. Pipe Whip i Observation of the damaged A MFW pump suction piping indicated sig- nificant movement of the piping following the rupture. The piping, attached to the pump suction, dropped and rotated away from the break point, pivoting on the elbow near the pump suction. Although the ,

piping came to rest against a prtion of the B MFW pump discharge l piping it did not appear to have damaged it significantly. ! Inspection of the area following the event also revealed that one piece of suction piping had ripped off and was blown some distanca from ' the break point. The piece was about two feet by three feet in size. It appears that the joint between the' suction pipe and condensate supply header provided lateral support of the suction piping assembly including the suction isolation valve. The loss of this support along with the weight distribution of the suction pipe assembly probably , contributed to the pivot and rotation of the assembly. It is also i

likely that back flow by the B MFW pump througli the damaged A MFW ' pump discharge check valve and out the broken suction pipe contributed to pipe whip motion of the feed pump suct, ion pipe. l

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~ . . 11 . c. Personnel Injury Those injured were eight contractor employees who were working in the general area, but not on the affected pipe itself. Six of these individuals were hospitalized f.or treatment of severe burns. Three were evacuated directly from the site by helicopter, and three others were taken off site by ambulance. The other two, who were less severely injured, were treated at a clinic and released. One of those hospitalized died the afternoon of the following day and another victim died two days after the accident. Two others. died several days later. The others remained in serious to critical condi- tion. One of the two hospitalized improved and was later released, but the other was still in serious condition more than a month after the accident. These contractor personnel were employed by Daniel Construction Company of Greenville, South Carolina, and by Insulation Specialties Inc., of Hopewell, Virginia. They were doing instrument line relocation and pipe insulation work, d. Plant Cooldown The loss of the suction, piping to the A MFW pump and subsequent steam release had no adverse effects on the plant cooldown. The MSTVs had closed as had the MFW FCVs before the pipe rupture. These actions - isolated the S/Gs from the rupture. The normal cooldown mode for a MSTV closure event is steam release by the code safeties, and S/G PORVs and continued feedwater flow from the auxiliary feedwater system. e. Employee Concerns On December 11, 1986, a former employee at Surry (a carpenter) contacted the NRC and expressed concern about grinding activities at , } Surry. The employee said that during June 1986, he and four other ' carpenters were directed to grind on p,ipe in the containment building. He stated that his foreman advised his crew that they were carpenters

and not qualified to perform this work activity. They were terminated for refusing to do the work. A case was filed with the Department of

Labor (DOL). The employee did not know the current status of his DOL

issue. The employee stated that the group of carpenters who remained i did perform grinding activities at various locations, including in the l turbine building. He did not know if they actually performed gririding i on the pipe that ruptured but wanted the NRC to determine if the pipe rupture was connected with the carpenters' grinding work. J As discussed in paragraph 9 below, preliminary investigations show ! that the pipe rupture was caused by a corrosion / erosion mechanism on i the inside surface of the pipe. It is clear tfhat the rupture was not ! related to grinding on the outside of the pipe. ,' w n

. . . 12

As further followup to the employee's concern, the inspector discussed grinding practices at the site with licensee officials. The licensee was aware of the employee's concern based on the individual's DOL case in June 1986, and the employee's contacts with the news media after the pipe rupture. The licensee stated that the work to which the former employee-referred was buffing or cleaning pipe welds in preparation for non-destructive examination (NDE) and was not grinding. The licensee's representative said their practice had always been to use carpenters or laborers to help pipe fitters clean or buff pipe welds in preparation for NDE. The carpenters or laborers worked under direction of the pipe fitters and were never allowed to grind pipe. The inspectors interviewed both the foreman who had terminated the carpenters in June, and a carpenter who was on shift at the time the other carpenters were terminated. Both agreed with the Itcensee's statements about carpenters being used only for cleaning or buffing pipe welds in preparation for NDE. They both also stated that the issue was that the carpenters who were terminated wanted pipe fitters' pay. When they refused to buff pipe without pipe fitters' pay, they were terminated. The foreman was the same foreman, who the concerned employee stated, had advised his crew that they were carpenters and not qualified to perform this work activity. During the interview, the foreman stated that, at the time of the termination he advised the carpenters only that the work they were requested to perform (buffing pipe welds) was not outside their work classification. The inspectors also reviewed U. S. 00L letter dated November 21, 1986, relative to the employee's concern. The letter states in part: " ... it is our conclusion that your allegations are unprovable for the following reason: Your termination, although officially recorded as involuntary, arose from a refusal to accept a work assignment arising from previous and ongoing personal and jurisdiction disputes with supervisor (s). These disputes were unrelated to any safety and health issue." ~ The inspector also reviewed the licens e's program for control of ! grinding on pipe. During fabrication of piping systems, grinding is controlled by Volume 2 of the Corporate Welding Manual including ! Procedure P-101, Revision 2, " General Piping and Pressure Vessel Welding Procedure," and Attachment A to P-101, " Weld Grinding Standard , and Techniques." For NDE, surface preparation is covered by NDE proce- ' dures. The inspectors reviewed a number of NDE procedures from the

NDE Manual and found that the procedures specify the surface condition i required but do not always clearly specify the method of surface preparation required to obtain the surface condition. NDE Procedure i NDE-3.1, Revision 3, Preparation, Issue and Control of Nondestructive . Examination Procedures, requires in paragraph 4.3.2.5 that NDE proce- dure list all actions which should be completeif prior to implementing the procedure, such as surface condition and preparation, temperature j of parts, etc. The licensee agreed to ev,aluate NDE procedures and

- , \\ [

-- - - . - - - -. - ---. - . . j 13

. determine if clarification is needed in specifying required surface - preparation methods. Pending review of the licensee's evaluation, ! Inspector Followup Item 280, 281/86-42-01, Clarification of Surface Preparation Methods in NOE Procedures, is identified. - 4 . 9. Metallurgical Aspects As noted in paragraph 8.a. above, the 18-inch suction line to the A main i feed pump failed catastrophically completely severing the line from the ! 24-inch header (see Figures 1, 2 and 3). The failure occurred in an 18-inch 90 degree elbow approximately one foot downstream of a tee in the 24-inch > header. The suction line was completely separated and dislocated from the header. Immediately after the failure, the licensee initiated a comprehen- sive analysis to determine the reasons for the failure and the necessary corrective actions. The following summarizes the licensee's analysis: - a. Initial Observations . ] The failed 18-inch suction line was fabricated from ASTM A-106, Grade B, Extra Strong carbon steel seamless pipe and ASTM A-234, '

Grade B, Extra Strong, WP8 carbon steel wrought fittings with a j nominal wall thickness of 0.500 inches.

When the 18-inch elbow failed, a fragment approximately two feet by 4 three feet was ejected from the outside of the elbow. The free end of , j the severed line was displaced in a horizontal direction approximately 6.5 feet and was wedged against the bottom of the B main feed pump discharge line. During the displacement, the A suction line rotated around the point of connection at the inlet to the pump, severely , ' deforming that portion of the line. The failed elbow, the short

section of pipe between the elbow and the 24-inch header, and a short section of pipe downstream of the elbow were removed for a detailed i study. The three parts were re-assembled as close as possible to

understand better the failure origination point and the sequence of l the failure after origination. The licensee performed a field i metallurgical investigation of the fai, led elbow as detailed below. ! (1) The investigation consisted of the following: Visual inspection of the system failure location. - Removal of the fractured elbow from the suction line. - . Visual 5X magnification evaluation and photography of - fracture surfaces, and elbow surface conditions. ' Ultrasonic wall thickness measurements, on a two-inch grid - pattern, of the failed elbow. ,' sem . -,------m._ ~ ,

. O - 14 . Metallurgical replicas taken on the elbow at several surface - locations. Mechanical measurements of elbow thickness. - (2) Th'e_ investigation resulted in the following observations: Visual inspection of the inside surface of the elbow revealed - a dimpled surface appearance, generally thinned wall and a number of localized very thin areas. The localized thin areas were small in area, usually less than one inch across, with remaining wall thickness as small as 1/16-inch. The areas were fairly smooth and blended smoothly into the surrounding material. Ultrasonic thickness measurements showed the wall thinning to be a gradual sloping change over' most of the surface of the elbow. The general thickness of the elbow varied from 0.120 inches to 0.390 inches. The short section of upstream pipe varied in thickness from 0.150 inches to 0.450 inches. Near the elbow, thickness measurements on the section of downstream pipe revealed thicknesses from 0.295 inches to 0.405 inches. The wall thickness of pipe a short distance downstream of the elbow was within manufacturer's tolerance. As noted above, the nominal wall thickness should have been 0.500 inches. Field metallurgical replicas taken on the surface of the - elbow revealed a microstructure typical of ASTM A-106 Grade 8 material with no signs of strain. The fracture surface was typical of a ductile tearing mode - failure. Tears, which appeared to be fracture origination points, were noted at two localized thin cavity areas of the fracture. Small defects, indicative of laps, laminations and inclusions, typical for A-106, Grade B, materials, were noted at the fracture surface. One of these small defects was noted at one of the thin overload tear areas and could j have been the start of the fracture. l (3) The licensee's analysis revealed the following probable scenario ! for the pipe failure: , The pipe failed because of a thinned wall. A corrosion / - l erosion mechanism is the probable cause of the wall loss. l Wall loss by this mechanism occurs by a gouging out pattern _ on the carbon steel surface under the action of a flowing medium and an electrochemical action. This phenomenon has i . been well documented for two phase fIow such as extraction , steam systems. The licensee has an inspection procedure documented for monitoring the t,hickness of its two phase . . O ..- . . - - . . . , - _ _ . . . _ - - - . . , - - , , , , , . . . _ _ . - , , - - , , _ . . . . . . , _ . . . - . _ _.., --.--,,-, - _ .-- - .

. O . - 15 systems (see Surry Administrative Procedure SUAD-M-33, No. ADM-89.13. " Secondary Piping Inspections"). However, for single phase flow in systems, such as feedwater and condensate, the problem had not been recognized. The only place where the phenomenon has been documented in a single , ' phase flow system is in the steam generator feed ring J-tubes. The design geometry of the failed elbow in the feedwater suction line is similar to the design geometry of the feed ring J-tubes. Both consist of a header or large diameter pipe and a right angle discharge pipe with a 90 or ISO degree turn. The licensee concluded that the turbulent flow created by the geometry and the low oxygen feedwater probably contributed to the corrosion / erosion thinning of the pipe wall. Because of the thinned wall (as low as 0.048-inches in a - localized area and 0.100-inch over a more general area), ' local membrane stresses were near yield at system pressure and temperature of 367 psig and 374 degrees F, respectively. The system underwent an upward pressure transient (see para- graph 7.c. above) resulting in a localized tensile overload failure in a thin wall cavity. Using the ASME Code minimum wall equation, and assuming an internal pipe pressure of 600 psig, a temperature of 370 degrees F, and an ultimate strength of 60,000 psi, results in a calculated burst thick- ness of 0.090 inches and a yield thickness of 0.173 inches. , Therefore, with a local cavity thickness of 0.048 inches, ' l a general thickness of 0.100-inch, and a upward pressure I transient, the material easily exceeded its burst strength. The initial tensile overload tear was considered to have arrested and not to have developed into an unstable tearing mode. Water flashing to steam was heard by station person- nel. As water continued to flash to steam for a few seconds and pressure continued to increase in the elbow, an unstable tear developed in a second t,hin walled area. The pipe then ruptured, ejecting the fragment from the elbow.

b. Metallurgical Analysis (1) VEPCO VEPC0 has hired Failure Analysis Associates (FAA) to perform a complete metallurgical analysis of the failed elbow. The following is a summary of the work to be performed and the . preliminary results as of January 14, 1987: l l (a) Phase 1 - Scheduled for completion a, bout February 1, 1987 Tensile Tests - .' - > _ , , _ , . . . - - - --. . . - .,- - --, . - - - - - - . , - - - - - , - - - - - - - ~ ~ - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -

. . . O .- 16 Tee, elbow and across the weld tested. Results complete. Acceptable to specifications. Charpy Impact Tests - Elbow tested. Small specimens used due to thickness of ' ~ material. Results appear to be satisfactory. Complete curve will be generated to correlate results with full size specimens. Hardness Tests - Elbow base material, elbow heat affected zone (HAZ), tee base material, tee HAZ and weld material tested. Results complete and appear to be satisfactory. Chemistry - Elbow base material, tee base material, and weld material tested. Results complete and appear to be satisfactory. Trace elements are almost nonexistent. Micro and Macro Examinations - Work partially complete. At 50X, inside surface dimpled, outside surface smooth. Structure typical - Pearlite / Ferrite. Scanning Electron Microscope Examination - Started. Oxide Layer Micro Probe Study - Started. (b) Phase 2 - Scheduled for compietion about the end of February, 1987. l l Finite Element Analysis - Basic Stress Analysis - -. Complete. Primary stresses 8500 psi, secondary thermal stresses 5000 psi. Code allowable 15,000 psi primary, , j 22,500 psi primary plus secondary. _ , i

. i g ' . , , - , - -- _-- - ,--- , - , , - , . , - - , - - , - - - -

. _ _ . _ . . . _ . . _ ._ _ _ ' . ~ 17 - f (c) Phase 3 - Scheduled for completion about mid-March,1987. Establish J-Resistance Curves tad perform detailed - fracture mechanics analysis. , ! ' _ Contract is being finalized. FAA will have basic contract. Material Engineering Associates (MEA) will be used as a subcontractor. I (2) NRC The NRC has hired Brookhaven National Laboratories to perform an independent metallurgical analysis of the failed elbow. The tests being conducted are essentially the same as the VEPCO Phase 1 tests. Tests are scheduled for completion about the same time as the VEPCO Phase 1 tests. 10. Chemistry - Corrosion a. Introduction A Region II chemistry specialist / inspector visited the Surry site on December 22-23, 1986 to examine the sections of the feedwater suction lines from both units that had been exposed by the licensee subsequent to the rupture in Unit 2. The inspector also reviewed chemistry data that had been documented since the startup of Unit 2 in 1973 to assess the chemistry control of the secondary water system during the operational history of this unit. Based on the information that is summarized below, the inspector evaluated the licensee's preliminary theory that the pipe rupture was the result of extensive - ' erosion / corrosion of the 18-inch suction line to a feedwater pump,

especially in the vicinity of the intersection of this pipe and the i feedwater header. b. Inspection (1) Visual Inspection " ! (a) Unit 1 - On December 21, 1986, the licensee had cut out

the suction line to A feedwater pump from, and including, ' the junction with the feedwater header to, and including, the isolation valve. The upstream portions of this pipe had been further separated and stored indoors while the downstream segments had been stored in'the open overnight. The most significant observations were as follows: An adhesive black film, conside, red to be Fe 034 - ' (magnetite), covered the inner ' surface of the junction i segment (i.e., approximately four feet of the header and the 18-inch pipe past the. initial 90* bend) except in a ' , .- 9 . . . , _ _. . _ . _ _ _ . . _ _ . , _ _ _ . _ _ _ _ _ . _ _ - _ . _ _ _ . , _ . , _ _ - . . - . _ . _ , _ , , _ _ _ _ _ . - . _ _ - . _ -_ _ _ _ , , _ . - .

.,

18 . limited region in the lower part of the 90' bend. A - similar patch of black oxide was located on the surface of the second bend. Although there were small areas of . black oxide in the other portions of the suction line, most inner surfaces were covered with a thin layer of , _ red powder that was assumed to be Fe O2 3 (hematite).

The weld bead that formed the inner junction of the - header and 18-inch pipe had been worn smooth on the downstream side, and significant (approximately one quarter-inch) amounts of weld metal had been lost. The weld bead joining the upstream segment of the - 18-inch pipe to the first elbow had also been worn smooth except in the quadrant approximating the outer portion of the bend in the elbow.

The weld discussed above also exhibited a scallop shaped - depression that indicated a limited region of signifi- cant loss of metal. This gouged area was located in both the weld bead and adjacent pipe approximately 90 degrees from the direction of flow in the header. An indication of a scratch or gauged area, approximately - 0.5 inch x 12 inches was observed in the isolated black region on the top (horizontal) side of the second elbow from the header. (b) Unit 2 - After tne 18-inch suction line ruptured the licensee had cut out this line at the tee weld at the header and five feet downstream of the first elbow from the header. The section of pipe that was removed included the failed region and the 2-ft. x 3-ft. hole formed by the expulsion of the ! weakest section of the first elbow. The exposed openings in the header and the 18-inch suction line had been capped with plastic for protection against dust. The most significant observations relating to the feedwater header and the remaining section of the suction pipe are listed below: Approximately one inch *of water remained at the bottom - ( of the header, and evidence of fresh rusting was observed beneath the water. I ! ' , Q , - . . . - , . - - . , . . - , , , . , , . w -w ---y-,

.

19 , The entire length of the header from the upstream - elbow to the most distant section downstream that was visible with a flashlight was coated with red iron oxide. The layer of oxide was not deep, however, and appeared as a film over roughened iron , _ and was easily wiped off. + The nearest elbow on the header upstream from the - opening was black in color. The downstream region of the inside bead of the weld - head that held the 18-inch pipe to the header was gouged out in the same manner and location as observed in Unit 1. Also, as in Unit 1, this weld bead had been worn smooth with the pipe except on part of the upstream side. A concave area of approximately two inches in diameter - had been formed immediately below the weld in the remaining stub of the 18-inch pipe. The inner surface of the initial foot of the downstream - run of the suction pipe was red in color while the remainder of the visible portions were black. The line of demarcation was very sharp. (c) Evidence of thinning The licensee had completed detailed ultrasonic tests of the Unit 1 suction line to A pump so that profiles of pipe thickness were available to the inspector. These profiles and visual evidence of thinning at the ends of cut out sections of this 18-inch pipe showed clearly that widespread wastage had occurred from the header to several (approxi- mately 5) feet downstream of the first elbow from the header. However, the thinning was no,t evident from the inner surfaces of the pipe beer.use the loss of metal had been very uniform, as if polished with coarse emery cloth, even where the pipes were red in color. The degradation of the welds at the tee junction and the single gouged region in each unit were the only obvious indications of metal having been removed in a non-uniform fashion. (2) Audit of Chemistry Records , The inspector reviewed archived documentation of daily analyses of the condensate, feedwater, and reactor coolant from the startup of Unit 2 (March 1973) until the unit was sh,utdown in February 1979. ,' +o - .- --. - - - . . - - . - . . _ , - - - . . - . - - - - - - . - - - - - , ., ~ . - - - - . - - - . , . _ - - - - - - - - , . ,

. -. . . . ' 20 . Through previous inspections, the inspector was already familiar with the licensee's chemistry control subsequent to the replace- ' ment of the steam generators in Unit 2; i.e., from 1980 to the present time. 4 ' As'_one of the first nuclear power plants constructed in the United States, both units at Surry began operation with a chemistry control program that included the use of hydrazine to control the

detrimental effect of dissolved oxygen - as an oxidant of carbon steel pipe. For two years the licensee also had added phosphate salts to the feedwater to control pH and to prevent attack of the carbon steel by hydrogen ions. In 1975 the phosphate control l program had been discarded in favor of the use of ammonia in an effort to minimize or eliminate denting of the tubes in the steam generator. During part of 1976-1977 cyclohexamine had been also - added for pH control but was soon replaced by the use of morpho- l i ne.. When the units started up after replacement of the steam generators, the licensee, following the recommendation of the Steam Generators Owners Group (SG0G), based the chemistry control on all-volatile-chemical treatment (AVT) with hydrazine and ammonia. Because of the original design of the Surry units (copper-alloy ' condenser tubes, absence of a condensate cleanup system, copper- alloy feedwater heater tubes) and the relatively high salinity of the condenser cooling water, control of secondary water chemistry had been difficult, as indicated by the following examples: l Intrusions of chloride ions in concentrations of tens of - parts per million (ppm) occurred several times in 1973, i I 1975, 1977, and 1978 as the result of condenser tube failures. (The current upper limit recommended by the SGOG to prevent corrosive attack of iron pipe is 20 parts per billion (ppb)). ' During four weeks in 1975 the pH of the feedwater remained - below a value 8, and thus ingreased the vulnerability of carbon steel pipe to corrosion by hydrogen ions (acid). The SGOG recommends that the pH of the feedwater be maintained between 8.8-9.2 in ferrous / copper systems such as were present in the Surry units prior to 1980. In systems that do not contain copper components, the SGOG recommends that the feedwater be maintained in a more basic condition (pH of 9.3 to 9.6) to increase the electrochemical stability'of iron in water and to minimize the dissolution of iron through reaction with hydrogen ions (acids). During the period when cyclohexamine was used, the pH of - the feedwater exceeded 9.5 and, occasionally even 10.0. Although the higher pH benefited the! reduction of iron corrosion, it also caused accelerated corrosion of the copper-bearing alloys in the co,ndenser and feedwater heater ' . . - --,~._,_____-_,,,,_ . - _ . _ - _ _ _ ...__ _ __ , - _ . __ _ _ -_.- , . - . , - . _ . - , _ _ _ . . . , _ , _ _ _ _ _ _

. .- .- . . . . 21 - tubes. Inasmuch as copper ions in solution exacerbate .several forms of chemical corrosion of carbon steel and alloy 600 (Inconel), the SGOG recommends that the concentration of copper in feedwater be kept below 2 ppb. The presence of higher concentrations of copper in the feedwater of the Surry , units before 1980 was considered to be a major cause of the _ degradation of the original inconel steam generator tubes. The licensee replaced the copper alloy condenser tubes with titanium during the steam generator replacement outage but is only now planning the replacement of the feedwater heater tubes with non-copper alloys. Throughout the operational history of Unit 2 the licensee had - observed the concentration of oxygen in the condensate and feedwater to have been less than the limit detectable by the most sensitive analytical instrumentation (except during 10 days in 1975 when, because of seal failures, the concentra- tion of oxygen increased to approximately 20 ppb.) The inspector considered that the lowest detectable limit had been 0-10 ppb during this period - which is consistent with the limiting concentration, 5 ppb, currently recommended by the SGOG. Control of oxygen had been maintained by the addition of hydrazine; however, during much of the early operating history the residual concentration of hydrazine had been close to the detectable limits (approximately 5 ppb). Currently the licensee adds sufficient hydrazine to ensure - that the residual is greater than 20 ppb, as recommended by the SGOG, so that oxygen is quantitatively reduced and elimi- nated as an oxidant. (3) Conclusions l The tee and upper elbow of the 18-inch pipe to the A feedwater l pump in both Surry units were visually observed to have been ! degraded through extensive thinning and severe, but localized, ( gouging. However, the interrelationship between the roles of l corrosion and erosion was not clear. The degree to which the I feedwater pipe had been protected against general corrosion by a film of magnetite was difficult to establish because the pipes had been opened and exposed to moist air. Although general corrosion, as well as more localized forms of chemical attack, may have been aggravated by the occasional presence of corrosive impurities in the feedwater during the initial seven years of plant operation, there was no visual or ultrasonic evidence to support this speculation. A more comprehensive analysis of this subject is presented in the Appendix to this report. ! .- . , , . - . . , - - . _ . _ . , - - , . - .--,-,.,-.--,-.---.-_-------- --_- .-- , ... ..--- - -

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22 11. Items Which Could Have Contributed to the Likelihood or Severity of the Event a. General , ' The inspectors reviewed system operating procedures, system maintenance history and the operating status of selected systems to determine those factors which contributed to the closure of the C steam generator main steam trip valve (MSTV TV-MS-201C) and the subsequent reactor trip and feedwater pipe ruture. (1). Plant Service Air / Instrument Air System (SA/IA) The inspectors reviewed control room logs, interviewed control i room operators and examined equipment in the plant associated with SA/IA system. This system supplies air to the air operated MSTVs. The air pressure supplied to the air operated cylinders associated with each MSTV holds the MSTV open during normal plant operation. The air pressure is automatically vented off the operating cylinders following a trip signal or manually vented by the operator action. The MSTV will then shut, assisted by the steam flow acting on the value disc. Prior to the reactor trip, the operating status of the SA/IA system was as follows: , SA/IA blue auxiliary air compressor was in operation; the three turbine building air compressors were in automatic mode, one was off; one of the condensate polisher air compressors was floating i on the SA/IA system. System pressure indications as observed from the control room was approximately 100 psig (normal operating range is 95-110 psig). I Planned maintenance was being performed on the SA/IA grey auxiliary compressor which consisted of the installation of a new temperature sensing element. Following this maintenance, the grey compressor was scheduled to be placed in service. Both the blue and grey air compressors share a. single power source. In order to position the transfer switch from the operating blue compressor to ' the grey compressor, the electrical power supply is required to be deenergized. Control room operators were aware of these operations and were adjusting air flow from the condensate polisher air system. System pressure decreased to approximately 85 psig as both blue and grey compressors were deenergized. At the time of the reactor trip, control room operators noted that SA/IA system pressure was approximately 78 psig. Subsequent to the reactor trip, the blue air compressor was placed back into service. ! ! ,' . _ _ , _ _ _ . . - - _ _ .. . ,m_ . - _ _ . _ - . . _ . , - - - . - . . , , - - - - - - . - - , . - - - . - - _ - - _ _ _ . - - - - - . . - - - . - - - - -

_ _ _ _ _ _ ___ _ _ _ _ _______ _ _ _ __ _ _ _ . _ ' . . ' 23 Discussions with control room operators indicated that operating

experience has shown that SA/IA receiver pressure has decreased as , low as 55 psig without any MSTV closing. As noted by this ' event, the only MSTV to close as a result of the lower instrument air pressure was the C MSTV. I The inspectors reviewed operating procedures for the SA/IA system. , Discussions were also held with operators to determine adherence to procedures; no problems were identified. During December 15-19, 1986, the licensee tested and opened for ' inspection the C steam generator MSTV. The detailed inspection and testing of the valve and the results are discussed in a separate paragraph in this report. The problem discovered during , this inspection, however, showed that the valve disc operator - assembly had previously been assembled incorrectly and permitted . the~ valve disc to be positioned in the steam flow path at an

angle greater than that allowed by design. This condition, j coupled with the drop in SA/IA system air pressure prior to the reactor trip, appeared to have allowed rapid closure of the MSTV by steam flow forces. ' Following the event, soap bubble air leak testing of instrument ' air piping and components to the C MSTV was conducted under normal system pressure condition. No significant leakage was identified that would have affected MSTV air operated cylinder operation. , (2) C Main Steam Trip Valve (MSTV). The action which initiated the reactor trip and subsequent feedwater rupture was the inadvertent closing of the C MSTV. i I A review of the maintenance history indicated this valve was overhauled during the most recent refueling outage in November I 1986. On November 27, 1986, following the overhaul, the valve i i position limit switch was adjusted and the valve was cold-cycled ' satisfactorily per Periodic Test 14.2. On November 29, 1986, with Unit 2 in hot standby, the C MSTV was again cycled, and the valve failed to open fully. The reactor operator generated a Work Order 046251, which indicated that the C MSTV was binding and capable of only partially opening. That same day, November 29, 1986, it was determined that the cause of the C MSTV was nots fully opening because of water in the valve. The next operating shift drained the water and successfully cycled the valve on ' November 30, 1986. However, Work Order 046251 remained open because the valve appeared to operate somewhat differently from the other MSTVs, even though it met its intended safety function as required by Technical Specifications. ' . e = . . . - . .

___ _ _ _ - _ _ , _ _ . . . . 24 . Following the event and the initial AIT inspection, the C MSTV was released to the licensee for inspection and testing. The , licensee developed a detailed testing and inspection program to determine the cause of the valve's inadvertent closure. The results of this program are as follows: Prior to disassembly, the valve was cycled and determined to only open approximately 62 degrees. Normal full open position should be 80 +2 degrees. Disassembly of the valve revealed the valve cover had been installed one stud or approximately 15 degrees off. This cover has a stop tube welded to it which normally limits valve disc travel to 80 +2 degrees when going full open. With the cover installed approximately 15 degrees off, the stop tube was positioned such that it limited the disc travel to only 62 degrees which left the disc approximately 25% from the full open position, exposing the disc to the closing force of main steam flow. This pragram also revealed that the radius lever had been i installed on the rock shaft one spline tooth off, which would ! have limited valve travel to 75 degrees had it not been for the valve cover misalignment. This also would leave a portion of the disc exposed to the closing force of the steam flow. The misalignment of the radius lever also contributed to the failure of the C MSTV closed limit switch to indicate that the valve had closed. During testing, the licensee determined that placement of the radius lever up one spline tooth prevented the limit switch from fully engaging in the closed position. A maintenance history review revealed that l the limit switch was adjusted before the valve was retested after maintenance. This adjustment appeared to be on the i lower limit switch, but a complete determination of what was ' actually adjusted could not be made dua to lack of documenta- tion. The operation of the closed limit switch was deter- mined to be intermittent. During the cold and hot cycle, the switch was depressed enough ,to actuate. But during and following the event, the switch, even though engaged, was not depressed enough to actuate, although only slight additional movement caused the closed limit switch to actuate. Several observations can be made based on the licensee's inves- tigation into the C MSTV closure. The maintenance procedure MMP-C-MS-002 used for overhaul of C MSTV was not correctTy ' followed. The procedure was inadequate in that it did not prevent, nor did the post maintenance testing discover the improper assembly of the C MSTV. The licensee failed to document all the non-routine work associated with this valve overhaul. A review of MMP-C-MS-002 shows that step 5.4.8 which reinstalls the radius levers does not prdvide adequate instruc- tions to maintenance personnel or quality control (QC) inspectors

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' . . 25 - as to the proper reinstallation alignment. Investigation by the licensee revealed that the maintenance person reinstalling the valve decided, based on comments from a QC inspector, to reinstall , the radius lever up one spline tooth from the previous installa- ti,on. This decision was made without any documentation or engineering review. This decision alone resulted in limiting valve travel to only 75 degrees exposing the disc to steam flow and appears to be the cause of the failure of the closed limit switch to operate. Step 5.4.12 required the QC inspector to check and record the arc of valve travel. The recorded data was 80 degrees - although the licensee determined after the event that it was only 75 degrees. The inaccurate documentation appears to be a result of the QC inspector performing this verification by visual check < only. Since the step calls for a quantitative result, the step should have required that some type of instrumentation be used to determine the arc of the valve travel. Also, the QC inspector should not have documented it as 80 degrees unless there was a means of precise verification. Although Step 5.4.15 required replacement of the valve cover, the step does not mention anything about cover alignment; specifi- cally, there is no mention of any problem that cculd result from cover misalignment. This would have illustrated the importance of proper alignment. The inadequacy of the step resulted in the misalignment of the cover, preventing full travel of the valve disc, and leaving the disc exposed to the closing force of steam flow. Finally, step 6.3 requires a post maintenance test be performed which only tested the operation of the valve based on the open and closed limit switches. This test, PT-14.2, does not verify full valve disc travel, and therefore was not adequate to verify proper valve reassembly. However, it should be noted that the test was adequate to verify the safety function of the valve which is to close. Also this test was used to verify that the valve was in compliance with Technical Specifications. The fact that the C MSTV was reassembled so that the disc was always exposed to the closing forces steam flow, coupled with the

low air pressure, resulted in the inadvertent closure of the C ' MSTV. This inadvertent closure of the C MSTV resulted in a reactor scram but did not contribute to or cause the rupture of the main feed piping. This rupture would have happened during any normal pressure transient of the feedwater system. Even though

the inadvertent closure of the C MSTV did not cause the feed ! line rupture and the safety function of t,he valve along with - . 3 9 -- . - . - -. ,-. -. ., .- - - - - . - - . - _ . - - . _ , _ - - . . - - . - _. .

_ . __

. ' 26 . compliance witti Technical Specifications were verified, the fact.that the valve was reassembled in such a way that it resulted in an inadvertent reactor scram and a challenge to the unit's safety system is still a significant problem. TkchnicalSpecification6.'4.Arequiresthatdetailedwritten procedures with appropriate check-off lists and instructions shall be provided for preventive or corrective maintenance operation which would have an effect on the safety of the reactor. The failure of the licensee to fully follow procedures, provide adequate instruction for and document the performance of maintence operations involved in the performance of the procedure to over- haul the C MSTV will be identified as Violation 50-281/86-42-02. (3) Feedwater Pump Discharge Check Valve (No. 2-N-127) Dur,ing the initial investigation of the feedwater pipe rupture event, an abnormal pressure transient of the A MN pump suction piping was suspected to be the cause of the rupture. For such a pressure transient to occur, the A MN pump discharge check valve (2-N-127) would have had to be permitted flow in the reverse direction. Since this was a potential cause of the pipe rupture, a review of the maintenance history and an internal inspection was conducted on the check valve (2-N-127). A review of the maintenance history on this particular check valve - revealed that the valve was scheduled to be inspected in late 1984. The licensee decided not to inspect the valve, based ' on a satisfactory inspection perforced on a Unit 1 feed pump discharge system check valve and on the operational history of the valve. It should also be noted that during the startup prior to this event, the B main feed pump was operated with the A main feed pump secured. There was no mention of a problem with high feed pump suction pressures, and the A main feed pump was started successfully on December 5, 1986. The licensee disassembled 2-N-12'7 after the event. Inspection of the internals showed the disc was not fully seated. One of the two hinge pins was missing, and the valve seat was displaced. The condition of the check valve at the time of the inspection would have allowed for flow in the reverse direction. The licensee has been able to determine, based on the operation of the A and B main feed pumps, that reverse flow tarough the A main feed p~ ump did not occur at the time of the' event. As discussed in the sequence of events paragraph that the A main feed pump was still operating after pipe rupture. Therefore, flow past the check valve into A feed pump suction piping could not have occurred prior to the pipe rupture. This conclusion strengthens the supposition that the feed water pipe ruptfured during a normal pressure transient and that back flow past the chec' valve did not cause a pressure spike which resulted in the pipe rupture. . t - . -. .-7 ,_ , _ - - . . . - _ , ,_ _--,_c._ .,.,,_._.,r___.- -- . - - - - - . . - - _ . - _ _ , , - _ . _ _ _ . - - - -- -

__ _ _ - .

27 . However, the condition of the check valve would have contributed to the amount of feed water which exited the feed line break and possibly the extent of the pipe whip after the event. The licensee has inspected the other Unit 1 and Unit 2 feed pump ch;eck valves and discovered additional discrepancies (see para- graph 15.c.). The condition of each of these valves at the time of inspection was such that they would have performed properly and not allowed significant reverse flow. (4) Feedwater System Maintenance History A review of recent feed water system maintenance history did not reveal any identified problems with the A or B main feed pump suction piping. The licensee has identified some problems with the feed water system such as pin hole leaks which were associated with erosion, but these problems were located in the feed water ' pump, discharge recirculation piping. While the licensee did not have a program to inspect the feedwater piping for thickness, it does have a formal ultrasonic inspection program to determine thickness for the following secondary system areas: Turbine Exhaust Cross Under Piping - 1st and 2nd Point Extraction System - 3rd and 4th Point Extraction System - Moisture Separation Drain Liner - Moisture Separator Reheater Inlet Piping - - (5) Safety System Equipment Review ! A discussion with the Superintendent of Operations and a review of i pertinent documents - i.e., plan of the day, the tagging log, the reactor operator's log, the shift. supervisor's log and the minimum equipment list for criticality and power operation checklist-- indicated that all safety-related equipment required to support unit operation was operable. The only safety-related equipment problems indentified prior to the event were (1) the inoperability of one of the three charging pumps (only two are required to be operable by technical specifications); and (2) a service water pump which was operable but listed in an alert condition. ' During the event, all safety systems responded as required. These systems include the operation of the reactor protection system (RPS), the steam generator safety relief valves and the a ' auxiliary feedwater system. The secondary power-operated relief - . Q .e>-ww- w---- - - - v-v--

_ _ _ . _ _ __ . _ _ _ _ _ _ . . - . _ _ __ _ .- _ ._

.

. ' 28 valves (PORVs) were in the manual mode of operation. The opera- tors.took manual control of the secondary PORVs to control steam generator pressure, allowing the secondary relief valves to shut and to control the removal of decay heat in the primary plant. _ , The only equipment which did not respond as required was (1)

. control rod (M-10) which indicated 35 steps for a short time ' following the reactor trip before indicating fully inserted; ! (2) the fire protection system which spuriously initiated as

discussed in paragraph 13; (3) the instrumentation which failed to indicate closure of the C MSTV as discussed in paragraph ,

11.a.(2); and (4) the security door card readers which failed as 6 discussed in paragraph 13.b. t b. Review of Maintenance Activities Being Performed Prior to the Event Discussions with licensee personnel and review of the maintenance

activities being conducted prior to the event did not indicate any ]' maintenance activities which would have contributed to the initiation or resulted in the feed water pipe rupture. Maintenance activities j being conducted by the individuals who were injured were unrelated to l the feed water system rupture and would not have contributed to the cause of the event. i 12. Licensee's Response to the Event 4 a. Operator Response The response of the operators to the initial reactor trip and later pipe rupture was excellent. The break was isolated rapidly. The only ! problem that occurred was a control rod gave an indication of not i being fully inserted by 35 steps. Emergency procedures were followed i quickly and orderly to assure adequate shutdown margin. It should be noted that the licensee has conducted tests with the plant in a cold condition, but has been unable to duplicate this rod position i anomaly. The licensee intends to conduct additional testing during ' startup. b. Emergency Response The inspectors discussed various aspects of the licensee's response ~ to the feedwater pipe rupture with licensee employees. The first person responding to the accident was a senior instrument technician who had been perfor'ning quarterly calibrations on security equipment. He responded to a station security call for first aid assistance to the Unit 2 truck bay. Upon arrival, one injured employee was observed leaving the accident area. The technician escorted the individual to the high level intake structure and set up a triage area. Three additional personnel subsequently exited the decident area and were . ' . . 6 .n - - - . - . - - - , - - - - . , . . , .

_ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ __ _ ___ _- _ _ l . . . 29 - . i given first aid by the team that was present. The technician unsuc- cessfully attempted to contact the Unit 2 Control Room using a security radio. The technician then proceeded to the maintenance services area to call for assistance. Upon arrival, the technician discovered two additional accident victims. The technician used the plant page system j , ' to notify the control room who called in offsite medical support, i including two medical evacuation helicopters and two local rescue squads. The licensee prepared the victims for transport and moved them to the licensee's heliport, located behind the training building. The three most seriously injured personnel were air evacuated to hospital burn i units while three were transported by ambulance. Licensee personnel interviewed following the event have stated that ! < the site's emergency team functioned extremely well and was well , - coordinated. Further, licensee representatives have stated that the i Alert was declared so that a personnel accountability could be made i because it was not kncwn at the time of the event how many people had been in the area when the feedwater pipe ruptured. The inspector reviewed the actions required by the licensee's emergency . plan and determined that the actions taken by the licensee were in accordance with the actions specified in the plan. 4 ! c. Emergency Information Activities ' The accident spurred extensive interest from the media in the immediate plant area, throughout Virginia,=and-nationwide. Virginia Power issued - - its first press release slightly more than an hour after the declara- ! tion of the alert. This initial announcement was followed by several others later in the day and into the evening. Follow-up announcements were issued the next few days. In accordance with the company emer- gency information policy, Virginia Power began steps to open the 4 near-site media center in the Surry, Virginia, Community Center. Because the Alert was cancelled before,the media center was fully ! l operational, reporters were briefed at the emergency operations ! facility at the site. Virginia Power also opened its main media center i at company headquarters in Richmond and issued information from there for several days thereafter. The day after the accident press conferences were held at noon at.the on-site training facility and at the Richmond media center. An NRC l public affairs officer went to the site with the Augmented Inspection i Team. He answered telephone media inquiries from the resident inspector's office and participated in three press conferences with

Virginia Power. NRC also responded to inquiries received by the public affairs offices in the Region II office and in, Headquarters.

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' . . 30 . In addition to written announcements, news briefings, and answers to telephone inquiries, Virginia Power also made available to reporters both videotapes and still pictures of the accident scene. Both NRC and Virginia Power continued for several weeks to respond to media 'imquiries about the accident and the followup investigations. A briefing of NRC by Virginia Power on January 12, 1987, attracted media coverage, as did a technical meeting convened in NRC Headquarters on January 15. Virginia Power on January 22 held a special media briefing on the results of its investigation. NRC received numerous requests from reporters and for copies of the AIT report. 13. Aspects That Made Handling The Event More Difficult a. Security System / Personnel Actions (1) At,the time the pipe ruptured, water and steam saturated a security card reader located approximately fifty feet from the break point and shorted out the entire plant card reader system. As a result, key-cards would not open plant doors. Security personnel responded to the control room and provided access control while doors into the control room were opened for easy access and to improve control room ventilation. Guards admitted personnel on the basis of personal recognition. The Senior Resident Inspector reported observing that plant management and operations personnel were immediately admitted by the guards and nonessential personnel were excluded. The card reader system returned to service approximately 20 minutes after the pipe break and functioned normally thereafter. An operator reported being delayed in the stairway outside the control room as a result of I the card reader failure. Due to the hot water conditions on the turbine building basement floor and the discharge of Halon fire suppression system in the emergency switchgear rooms below the ! control room and the carbon dioxide fire suppression system in the cable tray rooms above the control room, the operator had no safe way to exit the stairway other than the control room itself. The l operator was admitted to the control room by someone opening the l door from inside the control room. The licensee is considering

! installing electronic override switches which would permit the ( opening of electronically locked doors in emergency situations. l l Plant management personnel reported that security provided fast and excellent support during the emergency. ' (2) The security radio repeater is. located in cable tray room 1 (turbine building elevation 45), which is equipped with a Cardox fire suppression system. As a result of steam infiltrating various electrical systems this Cardox system was activated and the full volume of Cardox was discharged!into the room. The security repeater, located approximately five feet from a Cardox discharge nozzle, failed and was la,ter found to be covered with a . l ._- ___ _ -__ _ _ _ _ - _ . .. - - .-. - _ _ _ _ - - _ _

- _ - - _ . . - --

. .' 31 thick layer of ice. As a result, security communications were limited to the non-repeater or " simplex" mode. Since the hand- held security radios have only four watts of transmitting power, some communications clarity was lost between units inside , ' buildings. Loss of the radio repeater may also have prevented cohtact with the Unit 2 control room by the first responder as described in paragraph 12.b. (3) A truck carrying water coolers containing ice was the only vehicle admitted to the protected area during the emergency. While the truck was processed expeditiously, it was not processed as an emergency vehicle, which would have allowed its immediate entry. This resulted from the lack of information available to security personnel at the vehicle gate about the exact nature of the emergency and lack of understanding that the truck was bringing in ice and ice water for use in treating the burn v i ct,i m s . The licensee has recognized the importance of ensuring that personnel functioning in a supporting role know what is happening so they may better understand and, therefore, better respond to tasks they are given or situations as they arise. (4) One security badge /keycard was temporarfly lost during the emergency. Badges were retrieved from five victims before they were transported from the site, but the badge on one individual was overlooked. As part of the personnel accountability process, security realized that one badge, belonging to one of the - victims, was unaccounted for. That badge was deleted from the access control computer and computer records were checked to ensure that the badge had not been.used since the accident. The individual's wife found the badge on his shirt at the hospital and the badge was returned to the plant the morning following the accident. ' (5) At the time of the pipe break, two security shifts were on duty, which permitted security to provide a great deal of manpower to support the plant. The inspector, determined that one security shift could have provided the manpower to perform the actions taken by security during this event. The security force, however,

would have had to suspend all routine activities if only one ' shift had been available. . (6) The Surry security organization has examined its performance ' and identified ten areas in which improvements can and should be made. Recommendations in these areas were submitted to both security and plant management for evaluation and possible implementation on December 19, 1986. b. Fire Protection System Actuations and Main Control Room Habitability l Within minutes of the feedwater pipe rupture event in the Unit 2 turbine building, portions of the Unit 2 turbine building sprinkler I system actuated. Sixty-two sprinkler hea'ds opened in the immediate . - - _ - , . - - .- - - - - _ _ . . _ _ - _ . --

- . - . - - - -. ~. . - - . - - . - - - - - - - - . - _ - - . , - , 4 ! - 32 , i i area of the feedwater pipe rupture due to the high heat levels 3 associated with the event. As they opened, these sprinkler heads ' immediately began discharging water to cool the turbine building ' atmosphere. , ! As a result of the sprinkler wa'ter and feedwater discharge, the carbon dioxide and the Halon fire suppression system control panels were affected. The carbon dioxide fire suppression system control panels

for both Units 1 and 2 cable tray rooms are located near the Unit 2 i cable tray room access door along the column line 9 wall on elevation j 45'-0". The sprinkler water discharge from the sprinkler heads 1 , directly over and adjacent to these panels intruded into the carbon ' dioxide fire suppression system control panels through multiple open

i conduit ends which extend from the panels to the cable tray raceway ' above. As a result, the water intrusion into these panels caused the - time limit switches to short-circuit in the closed position. When ! these switches closed the carbon dioxide fire suppression systems, at i approximately 2:32 p.m. (12 minutes into the event) the Robertshaw fire l protection panel / printer in the main control room recorded the initial discharge of the Unit 2 cable tray room carbon dioxide fire suppression j system. In addition, at approximately 2:34 p. m. (14 minutes into the l event) the Robertshaw panel recorded the second discharge of carbon ' dioxide into the Unit 2 cable tray room. It should be noted that the bulk of carbon dioxide discharge was in the Unit I cable tray room, ' which was noticed by the licensee's loss prevention staff who c'onducted - i the personnel search and initiated the venting of carbon dioxide from ' the cable tray rooms. The Robertshaw fire protection panel / printer did

not register a Unit I discharge throughout the duration of the pipe rupture event. Thus, as a result of the water affecting the time . limit switches in the carbon dioxide control panels, the discharge ! timers did not function as designed. As a result, a total of 17 tons . of carbon dioxide was discharged into the cable tray rooms, i ' In addition, the Halon fire suppression system protecting Units 1 l and 2 emergency switchgear rooms on elevation 9'-6" actuated at approx- imately 3:02 p.m. (42 minutes into the, event as documented by the

! Robertshaw panel printer). The Halon system actuation was caused j by sprinkler water discharge and feedwater runoff which flowed under

the elevation 27'-0" fire door No. 30 installed in the column line 9

wall. The water runoff cascaded down the column line 9 wall, which

separates Units 1 and 2 turbine buildings, on the Unit 1 side, entered a Halon system conduit through a conduit fitting which had the fitting cover plate removed at the time of the event. The specific conduit fitting is located directly below the open grating floor on the Unit 1 3 side of the elevation 27'-0" column line 9 wall fire door No. 30. The

l runoff water which entered the subject conduit flowed through the j conduit and into Halon control panel 1-FPH-CP-1 located on the Unit 1 J side of the column line 9 wall on elevation 9'-6". This water intru- ! sion caused short-circuiting of the time limit!, battery charger and the t

. 4= .

- - - - ' . . 33 . dual zone modules. With the shorting of the dual zone modules, which are associated with the manual remote actuation circuit located in the control room, the Halon system actuated discharging 7 percent to i 10 percent Halon concentration into the emergency switchgear rooms. ! Since H'alon extinguishing agent is heavier than air, thi, discharge ' into the emergency switchgear rooms on elevation 9'-6" had essentially no effect on the habitability of the main control room. Upon the initial discharge of the emergency switchgear Halon fire suppression i system some Halon leakage into the main control room through floor penetrations in the Unit I computer room and through the control room emergency air bottle discharge piping was noticed. However, it should be noted that these concentrations of Halon which resulted from the emergency switchgear room discharge would not have put the control room personnel at risk. Upon verification of the carbon dioxide system discharge by the main control room personnel, two nembers of the licensee's loss prevention staff entered the cable tray rooms with self contained breathing apparatus to conduct a search for personnel. As a part of this search, measures were tsken to vent the carbon dioxide from the cable tray , rooms by opening the doors to the Units 1 and 2 mechanical equipment ' rooms and the respective cable tray room access doors located on elevation 45'-0" of the Units 1 and 2 turbine buildings. In addition, while the carbon dioxide was being vented from the cable tray rooms, the main control room annex door in the turbine building / control room complex wall and the main control room door separating the annex from the main control room were blocked open. Thus, carbon dioxide being heavier than air, flowed down from elevation 45'-0" to elevation 27'-0" and into the main control room annex and the main control room through , the open doors. In addition, during the time the carbon dioxide was being vented from the cable tray rooms, the main control room exhaust fan (1-VS-F-15) was operating. The operation of this fan created e

i negative pressure in the main control room and the main control room annex thus, causing the vented carbon dioxide to be drawn into the control room complex. i , 1 l Presence of carbon dioxide in the control room can also be attributed i ' to the fact that at the time of the event control room ventilation L ~ unit 1-VS-AC4 was out of service for design modifications and that a l temporary unit which obtained its makeup air from mechanical equipment , room I was in service. Therefore, when carbon dioxide vented from the ! l respective cable tray room came into the mechanical equipment room', l this allowed the te.nporary control room HVAC fan unit to draw the gas r into the control room ventilation system. I Control room personnel in the main control room annex and near the 1 main control room door experienced shortness of breath, dizziness and nausea. But it should be noted that once theyl recognized that carbon

' dioxide was present the control room operators took the appropriate corrective actions and initiated control , room emergency air supply ' .- , I - - ~ ~ . . - m , _.- - - ...__,,_..._,_-m.__.~... . . , _ , _ - _ , . m_-.

_. .__. __ _ . _ . _ . _. .. ' . . 34 . fans 1-VSF-41 and 2-VSF-41. The starting of these fans placed the main control room at a higher pressure than the turbine building. This action assisted in diluting and exhausting the existing carbon dioxide ' levels and kept any additional carbon dioxide from infiltrating into themajncontrolroom. . As a result of the spurious fire protection system actuations associ- ated with the feedwater pipe break event, the licensee has proposed the following carbon dioxide /Halon fire protection system modifica- tions: (1) Seal the open ends of all conduits leading to the carbon dioxide system control panels throughout the plant. (2) Replace all components within both the Unit 1 and Unit 2 cable tray room carbon dioxide control panels that show visible signs q of corrosion. . ! (3) Fully test both systems to confirm proper system operation. 1 l (4) Seal the Unit I control panel. A 1-1/2-inch hole and a 1 inch hole exist in the right side wall near the bottom of the panel. (5) Replace missing 2-inch conduit cover under the elevation 27'-0" turbine building column line 9 wall platform and walk down all , ' other conduits to ensure that covers to conduit, pull boxes, and junction boxes are in place and properly sealed. i (6) Repair door seal on the Halon control panel and relocate ! identification sign, i ! (7) Replace all existing Halon panel modules which are no longer i manufactured and upgrade these modules to current state-of-the-art equipment < j (8) Perform functional tests of the H.alon system for both units 1 and 2 emergency switchgear rooms to ensure proper operation. (9) Replace Halon system check valves in discharge lines or replace j rubber seals. l (10) Have all Halon cylinder heads replaced or reworked to ensure, bottles will not leak and that seals are in good condition. , (11) Have Halon bottles filled and placed in discharge header. (12) Have Halon pressure switch covers and solenoid covers removed and I inspect for corrosion or water damage. , . . 4 l .. '.

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.. . ,. - . _ - . - - - - - - ' . ,- 35 Based on our review of the above modifications, it appears that upon their completion the probabilities of spurious cable tray room carbon dioxide and emergency switchgear room fire suppression system actua- tions due to water / steam intrusion will be greatly reduced. However, it is our recommendation that the licensee, in addition to implementing the abo,ve proposed modifications, consider the following with respect to ensurthg control room habitability and personnel safety: Install a wintergreen odorizer on the Units 1 and 2 cable tray - room carbon dioxide system, Install a permanent oxygen analyzer with a control room audible - alarm in the main control room annex, Develop a procedure which will require the control room operators- - l to pressurize the control room in the event of a gaseous fire ' suppression system actuation in either the cable tray room or the emerge.ncy switchgear rooms, and Install predischarge visual and audible warning devices near the - Units 1 and 2 cable tray room doors and inside the cable tray rooms which will activate to alert personnel prior to a carbon dioxide system discharge. c. Other System Interactions , . i There does not appear to have been other significant system interac- tions which impeded the safe shutdown of the plant. All shutdown systems responded as designed, and an orderly plant cooldown was accomplished. l l 14. Consideration of Shut Down of Unit 1 At 12:30 p.m. on December 10, licensee management decided to shut down Surry Unit 1 and operation of the unit was placed on power ramp down at 5:30 p.m. The unit was subsequently cooled down and pl, aced on residual heat removal and is currently in a cold shutdown condition. The decision to shut down the unit was based on preliminary findings resulting from the Unit 2 main feed pump suction pipe rupture. These findings indicated that there might have been significant thinning of the l pipe wall due to a corrosion / erosion mechanism not fully understood at the time. The shutdown plan included inspections of selected Unit 1 piping.to ascertain its condition with regard to pipe wall thinning. Subsequent ultrasonic examination of the identical elbow that failed in Unit 2 revealed similar but not as severe pipe wall thinning. !

. O O e

- . _ .- . _ .- .- - . - . - - . . . 36 - The licensee gave priority to Unit 1 inspection and hardware replacement in parallel with its investigation to determine the root cause of the Unit 2 pipe rupture. This was done in order to facilitate restart of Unit 1. 15. Investigatipns and Corrective Actions Taken ~ a. Initial Activity The licensee agreed to a quarantine of all equipment and systems which could be significant to the ongoing investigation of the event. , Consequently, all activities undertaken with regard to restoration work or investigations were done with the concurrence of the NRC team on site. During the first week following the event, . concurrence was given for some turbine generator work on the turbine deck which was not relevant to the investigation and work involving cleanup and restora-- tion of the damaged area. The following equipment was inspected: (1) A main feed pump suction indication in the control room pegged at , 1000 psi. The pressure transmitter associated with this indica- tion was inspected to determine operability. Subsequently, it was determined that the transmitter housing was 1/3 full of water and it appeared that the electrical portion of the transmitter was not operable due to shorting. (2) A calibration and circuit check was performed on pressure cutoff switch for the high pressure heater drain pump. This was done to - determine if the section of line leading from the HP heater drain pump discharge to the condensate header had been pressurized to at least 600 psi. The switch was designed to cut off the pump if a 600 psi pressure was exceeded. The switch was calibrated and found to be operable indicating that a line pressure of greater ' l than 600 psi was not present. 5 On December 16, 1986, this quarantine was lifted. l b. Piping Systems , Based on the failure of Surry Unit 2 main feedwater pump suction line

and the fact that the Surry Unit 1 suction line design was similar to , Surry Unit 2, the licensee decided to shut down Surry Unit I and -

inspect the main feedwater pump suction line. The Surry Unit 1 suction line was found to have reduced wall thicknesses similar to , i Surry Unit 2. When pipe wall thinning was found in Surry Unit 1,' l the licensee decided to inspect similar piping at North Anna Unit 1. Approximately 4900 ultrasonic inspections were made on North Anna

Unit 1 piping. No measurements indicated pipe wall thickness below the required minimum. The feedwater pump suction piping and header , wall thicknesses were within original pipe manufacturing specifica- l tions, and the high pressure drain pump dischdrge piping was no more than 15 percent below the original specifications. .' l

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. . . 37 - As a result of finding thinned pipe at both units, the licensee initiated a pipe wall thickness measuring inspection program to define the extent of pipe wall thinning at Surry Units 1 and 2. The following summarizes the criteria for the program, the acceptance criteria, and the inspection results to date. (1) Corrosion / Erosion Parameters In the review to determine the parameters affecting corrosion / erosion, the licensee found limited data available from industry experience with bulk single phase corrosion / erosion. The available literature correlates single phase corrosion / erosion to two phase wet steam corrosion / erosion. The parameters that appear to affect corrosion / erosion in single phase flow are: . Material Phenomenon occurs in carbon steels. The - - resistance to corrosion / erosion ' increases with alloying. Fluid Velocities - High fluid velocities increase - corrosion / erosion. Temperature Corrosion / erosion takes place batween - - 195 and 440*F. High Water Purity- Corrosion / erosion.affected by oxygen - content. These parameters and the corrosion / erosion process relate to the rate of buildup and removal of the protective magnitite (Fe 0 ) 34 layer. Based on the above information, the licensee established the following criteria to select systems to be inspected: System handles water or steam - System piping is carbon steel - System temperature is greater than 195"F - System is deoxygenated (low ppb range) - As added verification of these criteria, the licensee also included in the program specific locations within systems outside the criteria, including safety-related systems, such as, the' auxiliary feedwater system (oxygenated and less than 195*F), charging system (stainless steel) and condensate system prior to the point heater (less than 195*F). (2) Rating Scheme Within a system, a rating scheme, based oh temperature, velocity, and geometry, was used to identify potentially high corrosion / erosion wear regions. .. . , .- 9

. .

38 . After consideration of the above criteria and rating scheme, the licensee decided to inspect components beyond those identified as priority by the rating scheme. In addition to the components picked for the auxiliary feedwater system, charging system, and condensate system to the 4th point heater, the following compo- nents were included in the wall thickness inspection program for both Surry 1 and Surry 2: Every fitting and selected locations on straight pipe from - the inlet of the 4th point heaters to the feedwater pumps and from the feedwater pumps to the feedwater regulating valves. Selected locations along sweeps and straight lengths of pipes - from the feedwater regulating valves to the containment for' loops A, B and C. There were no priority points in these sections of pipe using the rating scheme. High priority points on B feedwater loops from the contain- - ment to the steam generator. The points picked were representative of similar configurations in loops A and C and also included some unusual configurations. (3) Acceptance Criteria The licensee developed an acceptance criteria to provide guidance in determining whether a fitting or section of pipe needed to be replaced immediately, replaced at some future time in its operat- ing life, or monitored by inspection during its operating life. The acceptance criteria were based on the existing wall thickness, as measured by the inspection program, the calculated corrosion wear rate, and the Code minimum required wall thickness. The wear rate was calculated by dividing the wear to date (assumed to be the nominal specification thickness plus manufacturer's tolerance minus the existing as measured thickness) by the number of years of operating history. , The following acceptance categories were defined: (a) Immediate Replacement Existing thickness below - minimum Code or below 0.100 inches. , (b) Engineering Evaluation Existing thickness greater - than Code minimum but calculated (based on wear rate) to still be acceptable at the time to next outage plus I/2 year. .' _ -. . . . . .- . . _ , , . _ . _ _ _ _ _ . _ . , , - _ _ _ . _ . . _ , , . - , _ _ _ _ _ - _ . _ _ _ _ _ _ - . . _ . _ _ , , _ _ _ , , - . _ . . , _ _ _ . . , _ , . . . . . . , _ . _ _

.

. 39

. (c) Potential Next Outage Existing thickness greater than - Replacement acceptable thicknest at time to next outage plus 1/2 year but less than acceptable thickness at time to next two outages , , plus 1/2 year. Inspect at a _ next outage. (d) Each Outage Inspection Existing thickness greater - than acceptable thickness at time to next two outages plus 1/2 year but less than acceptable to next three outages plus one year. , (e) Place Component in Existing thickness greater - Station's Inspection than acceptable thickness at Program time to next three outages plus one year. (4) Summary of Inspection Results and Replacement as of January 8, 1987 Unit 1 Unit 2 Components to be Inspected 588 588 Inspection Requests Issued - - - - 515- 208 Inspections Complete 427 150 Components Designated for Immediate 48 7 Replacement Components Designated for Potential 8 4 Replacement at Next Refueling Outage Components Designated for Inspection 40 8 at Next Refueling Outage Components Removed 38 7 Components Installed 8 0 b. Main Steam Trip Valve Because of deficiencies found in the Unit 2 C MSTV (see paragraph 11.a.(2), the licensee inspected the internals of the remaining Unit 2 MSTV and the three Unit 1 MSTVs. No assembly deficiencies were found. In addition, each pair,of air actuating cylinders for each valve was rebuilt. .' 9 _ _ _ _ _ _ _ _ _ _ . _ _ _ _ _ . _ . . _ _ _

. . _ _ _ __. ~ . ' . 40 - c. Main Feed Pump Discharge Check Valve ' The remaining three main feed pump discharge check valves were inspected. The results were as follows: , 5 Both c' lamp assemblies had loose bolts and the Unit 2 8 Check Valve - lock wires for these bolts were missing. The lock plates exhibited some erosion but the

disc / seat assembly was not displaced. t Unit 1 B Check Valve Both clamp assemblies had loose bolts and the - lock wires for these bolts were missing. The lock plates exhibited extensive erosion but the disc / seat assembly was not displaced. The left side hinge pin was missing. Unit 1 A Check Valve - No defects found. This valve was overhauled

- in May 1986. ' The check valves will be modified as follows: (1) New hinge pins will be installed that are secured in place by a lock pin which is welded in place. The lock pin will project through a hole in the hinge pin. This modification will be completed prior to startup of the units. (2) The clamp assembly which holds the seat to the valve body will be eliminated by welding the disc / seat assembly onto the valve body. " This modification required a material change. Due to the unavail-

ability of this material, the modification will be made at the l next scheduled outage of sufficient duration when the material is available or during the next refueling outage. (3) The check valves will be periodically inspected in accordance with an inspection plan to be developed by the licensee. ' 16. Safety Considerations for Station Restart By letter dated January 14, 1987', the licensee submitted a report entitled "Surry Unit 2 Reactor Trip and Feedwater Pipe Failure." This report provides detailed information on the December 9, 1986 event and a recovery plan and corrective actions for NRC review and concurrence prior to station restart. The AIT has reviewed this report and has conducted an independent inspection effort which provides the bases for our concurrence with the licensee's restart plan. I

. ee. .. ~ . . - _ _ _ _ _ , , . _ . _,, _ _ , . - _ . .__.- , _ , . _ _ _ . . _ _ _ _ _ _ _ . - _ - . - . . . . . -. . .

_ _ _ _ _ _ _ _ _ . . > . . , 41 - ' The Itcensee's report outlines a program which has been implemented for initial inspection, hardware replacement and periodic inspection of the main feed and condensate piping systems. This program provides for development of a model which is believed to predict the erosion-corrosion mechanism and the rate of pipe wall thinning in a conservative manner. The licensee, ush g this model, developed an inspection / replacement program for various fittings in the feed / condensate systems. This program defines conservative acceptance criteria for the fitting replacement which predict the time that would elapse before minimum allowable wall thickness would occur (see Section 15.b). In addition, a periodic inspection program has been established. The periodic inspections would provide information to continually reaffirm or modify the model. Thus, the present inspection / replacement program would permit a satisfactory knowledge of the present state of the plant's condensate /feedwater systems. Future inspections together with the current information would continually provide assurance j that the loss of wall thickness is not occurring at the rate which could result-in prem.ature failure. These actions provide additional confidence in the startup and permits the carrying out of a conservative inspection program which adequately defines weak points in the feed and condensate systems. l This replacement / inspection program is an interim measure to be utilized as more information_is developed with regard to the mechanism of erosion /

corrosion. The licensee intends to develop a long range program of correc- ' tive action that includes geometry as well as material changes to the feed and condensate systems.

Inspection performed on the other single phase systems in the plant showed. - no indication of the type of failure experienced in the feed / condensate system (i.e., wall thinning due to corrosion / erosions). In addition, the licensee will continue the inspection program previously developed for two- phase flow systems. The AIT has also reviewed the licensee's corrective actions with regard to the MSTV maintenance procedures and the proposed short-term and longer term hardware improvements for the main feed pump discharge check valves, and concludes that the licensee actions are satisfactory. In addition, as a result of the AIT inspection and re. view of the licensee's program, the following conclusions and findings were developed. a. Sequence of Events . The inspectors performed an independent evaluation of the event scenario, including the sequence of events and their cause of the events. The inspectors' conclusions are that the reactor primary system and all safety-related components reacted properly to a loss of load transient initiated by the closure of one of the main steam trip valves. The pipe rupture occurred before the bain feedwater discharge l

> _ 9 - , - . - - ..-,c------- - ., - - - - . - - - - - ---,- ,- _ _ ---- .. -- - . -- - - -

. - _. . .

. 42 - check valve could malfunction. The only contribution to the event was that the malfunction of the MFW pump discharge check valve caused steam / water to be discharged from the break. We concur with the

licensee's evaluation of the sequence of events. b. WaterbammerOccurrence ' Inspection of the Surry Unit 2 condensate and feedwater piping conducted following the pipe rupture event did not indicate that feedwater system water hammer occurred during the event. Reviews of PWR operating experience regarding water hammer in feedwater systems indicate that severe water hammer loads usually result in extreme damage to pipe nanger supports and instrumentation and are usually the result of feedwater control valve instability. The Surry Unit 2 feedwater piping from the containment penetration back through the A main feedwater pump, haater drain pump and condensate pumps have been inspected by the team, and there is no indication of this type of damage anywhere but in the vicinity of the rupture. Inspection by the licensee has also indicated no such damage. In addition to this, measurements of pressure between the steam generator and feedwater control valves indicate there was no leakage from the steam generator back through the feedwater system. c. Metallurgical The pipe rupture occurred due to severe pipe wall thinning. The general thinning condition appears to have been caused by a corrosion / erosion mechanism with thinner localized areas related to high turbulent flow. The fracture appeared to have originated at one of the local severely thinned areas. The licensee's preliminary metallurgical analysis indicated that the material met all specification require- ments. Additional tests are in process by the licensee and the NRC to fully define all material properties. The licensee has outlined an inspection program for the feedwater and condensate piping systems, based on conservatively predicting the corrosion / erosion mechanism and the rate of wall thinning which should, ensure that the wall thickness is monitored adequately to preclude premature failure. The licensee's results and inspection program are outlined in their report, "Surry Unit 2 reactor trip and feedwater pipe failure" submitted by letter dated January 14, 1987. We concur that the report covers the metallur- gical aspects of the problem adequately, d. Chemistry ' The methodology used to control secondary water chemistry to prevent localized corrosion of stea:n generator components (as recommended by the Steam Generator Owners Group) may result in " aggressive" water chemistry conditions that favor general corros, ion of carbon steel. I I -

.

. _ . ,_.._,____._x _ .__.._____,__ ._. ,_,.. _ ,_________.___ ,.___ ,_. _.,___, . _____.__ __.__ - ._._____._ _.~_

._ _ .- . _ - _ _ . ._ . . . .

43 The formation and retentien of an adhesive film of magnetite on the . inner surfaces of carbon steel pipe, in regions of single phase and turbulent flow, may be affected by variables other than regeneration by oxygen. Emergen'cy Preparedness ' e. The facility's emergency organization responded to the pipe rupture event in a commendable manner. The plant staff worked together effi- ciently to minimize personnel injuries and to mitigate the consequences of the event. Offsite support requested for the injured personnel responded to the call for assistance expeditiously to transport the injured personnel to area medical facilities. Verbatim compliance with the actions specified in the Emergency Plan appears to have been .

.

exercised by the plant staff in responding to the event. <

f. Public Information Virginia Power implemented an aggressive and candid program to inform < ' news agencies - and, through them, the public - of the basic facts concerning the accident and of continually updated findings as the Company's own investigation went forward. Key ranking company execu- tive spent an unusual amount of time in briefing reporters in several

news conferences. Reporters were taken on several tours for a first- ! hand look at the accident area and at pieces of the broken pipe. I ! g. Plant Systems (1) The inspectors reviewed the' licensee's program for determining the cause of the C MSTV closure and also the failure of the MFW pump discharge check valve to fully close during the event. The licensee's technical evaluation and the corrective actions taken to restore the above components to normal operation were deter- mined to be comprehensive and acceptable. (2) An apparent violation of Maintenance Procedure MMP-C-MS-002 which initially overhauled the C MSTV wits identified. This procedure lacked detailed instructions, was not fully followed and did not provide adequate documentation to show the repair of the MSTV was accomplished in a quality manner. The licensee was informed that similar problems may exist with other system maintenance procedures and licensee review should be conducted. , (3) The inadequate maintenance performed on the C MSTV did not prevent the valve from performing its safety function or cause it to be in l noncompliance with Technical Specifications. (4) The reactor trip was a direct result of the improper overhaul of the C MSTV in conjunction with the lower than normal instrument , air pressure. However, the MFW line rupture was not caused by l the MSTV closure but occurred due to the normal pressure transient ' which followed the reactor trip.

' ,_ , , - , . - - - - - . - - , - - , - - - . - - - - - , - - . . - , - ~ , . - - - - - - - - - , - - - - . . - ~ - - - - - - - - ~ ~ - - - - - - - - - -

. . ~ 44 - . (5) The maintenance performed on the C MSTV indicated several cases where anomalies were resolved without either proper documentation, notification of supervision or engineering review. Examples are the changing of the radius levers on the rock shafts and the need to adjust the MSTV lijnit switch following maintenance. Had these problems received the proper attention and evaluation, the improper reassembly of the C MSTV could have been identified . before causing a reactor trip and a challenge to the reactor ' safety systems. (6) The post maintenance test used to check the operation of the MSTVs following maintenance only verified their safety function and compliance with Technical Specification. Additional testing should have been required to verify full are travel of the valve , disc and therefore proper reassembly of the valve would have been confirmed. h. Security The actions of security personnel during the event provided prompt personnel access to sensitive operational areas including the control room. As a result of evaluating the security aspects of the event, the licensee is considering additional training and hardware changes to further facilitate emergency access to restricted areas. 1. Fire Protection As a result of the feedwater pipe rupture event in the Surry Unit 2 4 turbine building, Units 1 and 2 cable tray room carbon dioxide fire suppression systems and emergency switchgear room Halon fire suppres- sion systems spuriously actuated causing control room habitability problems during the event. Based on our review, we conclude that the l licensee's staff has properly analyzed what caused the spurious fire ! protection system actuations and has initiated modifications to the ' subject fire suppression systems which will greatly reduce the prob- abilities that these systems will spur,iously operate due to water / steam , j intrusion. In addition, it should be noted that once carbon dioxide ! leakage into the control room was recognized, the licensee's control room operations staff initiated prompt corrective actions to maintain control room habitability. However, with respect to ensuring control room habitability and personnel safety we recommend that the licensee consider the following: The installation of a wintergreen odorizer on the Units 1 and 2 - cable tray room carbon dioxide system, The installation of a permanent carbon dioxide analyzer with a - control room audible alarm in the main co,ntrol room annex, .' 4 ,- - _ _ _. .. _ -_ _ _ __ .._,.___m...,_, , _ . _ _ _ _ , - _ _ _ , . _ , . . , _ . _ _ . _ , _ _ - _ . . _ _ _ . . _ _ _ . . . _ _

l . . '

45 . i The development of a procedure which will require the control - room operators to pressurize the control room in the event of a gaseous fire suppression system actuation in either the cable tray room or the emergency switchgear rooms, and ' , Th'e_ installation of predischarge visual and audible warning - devices near the Units 1 and 2 cable tray room doors and inside the cable tray rooms which will activate to alert personnel prior to a carbon dioxide system discharge. a . O , I . *

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. _ _ _ -_. . . _ ._. _ . _ - _ _ -. . . . ~ . t APPENDIX . CHEMISTRY-CORROSION CONSIDERATION OF THE SURRY , UNIT 2 FEEDWATER P.IPE RUPTURE EVENT 1. Fundamentals of Generalized Corrosion Although the eventual rupture of the 18-inch suction pipe may have been initiated at a point on the upper-inside region of the first elbow down- stream of the header, both visual evidence and ultrasonic measurements showed that generalized wastage of the pipe, with resulting thinning from , the nominal 0.5-inch wall thickness, had been the obvious precursor to the pipe failure. Because of the uniform nature of the thinning there was no evidence of other types of mechanical or chemical attack. Generalized thinning of iron surfaces is considered to be caused by erosion /

corrosion processes, with either process being dominant. The potential for ' mechanical and hydraulic erosion is greatest in regions of turbulence and non-single phase flow and is enhanced by increased flow and temperature. Consequently, erosion mechanisms can be expected in the regions of the tee junction of the feedwater header and suction pipe, and, to a lesser degree, in the elbow regions of the suction pipe. The role of corrosion, specifically in the Surry feedwater system, is more speculative because of the multiple chemical reactions that might have occurred during the thirteen - years of normal and abnormal chemistry control. The licensee has tenta- tively assumed that general corrosion occurred because the carbon steel ! pipes had been in contact with ' aggressive' (low dissolved oxygen) water. Removal of iron from a carbon steel pipe is thought to occur through ' oxidation processes that establish a corrosion electropotential between i metallic iron (as an anode) and an oxidant in the water layer adjacent

to the metal surface (cathode). Depending on the magnitude of the corrosion potential the oxidant in feedwater could have been hydrogen tons, cupric or i cuprous ions, or oxygen. All of these cathodic reactions are enhanced by j the presence of chloride ions. l In stagnant water systems the ferrous ions (Fe++) generated at the metal / water interface are amenable to further oxidation by dissolved oxygen to l j produce insoluble iron oxides such as Fe 02 3 (hematite) and Fe 03 4 (magnetite) l as well as other, less stable, hydrous oxides of iron. The formation of magnetite also can occur in the absence of. measurable amounts of dissolved t oxygen. One mechanism that has been prop ~osed is further electrochemical reaction of hydrogen ions (H+) and the trace concentrations of soluble ferrous hydroxide in the aqueous layer adjacent to the metal surface. The formation of magnetite rather than hematite is favored by increased [ temperature (especially between 300-350 degrees F) ,and again under stagnant conditions. Under optimum conditions, a non-porous', adhesive film of magnetite forms on iron or steel surface. The film eventually terminates '; .

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. . Appendix 2 further removal of iron by electrochemical attack by eliminating the anodic reactor (Fe*+ Fe++). The oxide is in chemical equilibrium with the adjacent water and will degrade if the equilibrium is impacted by chemical and/or hydraulic factors. 2. Role of Pass'ivity and Corrosion in the Thinning of the Feedwater Pipes a a. Observations As the result of his visual inspection the inspector could not establish the extent to which the chemistry of the feedwater abetted the thinning process or provided protection against the continuous removal of iron from regions of turbulence and single phase flow. The appearance of the pipe in Unit 1 was significantly different from Unit 2; however the extent of thinning was similar in both units, but < it was less severe in Unit 1. The presence of.a thin layer of red hematite in.the region of the rupture in Unit 2 can be attributed to removal of any previous magnetite film during the expulsion of water / steam followed by inflow of moist air while the pipes were hot. Upstream and downstream of the rupture the pipes appeared to have retained a magnetite film. The appearance of the pipe in Unit I was considered to be more repre- sentative of the true condition of the inner surface of the feedwater system during plant operation, although most the suction line had been exposed to air for 24 to 48 hours before being insps:ted. However, this unit was shut down normally and the pipes drained at ambient temperature before the pipes were cut u Such conditions.are less conducive to conversion of magnetite to hematite. The most significant nbservation was that in Unit 1 the suction pipe tee with the header and the first elbow had a black coloration although extensive thinning had occurred. Conversely, downstream sections of , l the suction lines that experienced much less thinning had a thin layer of red, non passivating, hematite. b. Effect of Chemical Variables ' The role of chemistry control, especially before the original steam generators were replaced, is also not clear. The very large amounts of iron oxide sludge that has been periodically removed from all of the steam generators throughout the thirteen years of operation is proof ! that wastage was occurring. However, this oxide sludge is thought'to have originated predominantly in the high pressure pipes of the second- ary water system which have been subjected to both dry and moisture l laden steam. l ! l - - - - - - _ - - - , , _ _ _ _ , _ _ , , _ _ _ , _ , _ _ _ _ _ _ _

. .

Appendix 3 During the last four years the deposition of sludge in the steam generators had decreased considerably, a phenomenon that has been attributed to higher purity condensate and feedwater and to AVT chemistry control following the criteria of the Steam Generators Owners Group (SGOG). . Before 1980 several relatively brief periods of inleakage of James River water upset chemistry control and allowed ppe amounts of chloride to enter the secondary water system. Consequently, stress corrosion of carbon steel and inconel components of the steam generator occurred as well as denting of the inconel steam generator tubes through formation of magnetite in the tube / tube sheet regions. The effect of these transients on the general wastage of carbon steel pipe is not obvious. The licensee's tentative scenario stresses the capability of pure, deaerated water to attack carbon steel: ! ' Fe*+ Fe*+ + 2e- 2e- +2H+ + 20H" + H + 20H'_ 2 Fe* (solid) + 2H+ + 20H + Fe++ + 20H +H (gas) ~ - 2 The trace amount of Fe (OH)2 is continuously removed from the region of formation before it can be further converted (oxidized) to adhesive and passivating magnetite. (1) Effect of pH l It is the purpose of pH control, however to minimize this 1 mechanism of attack by reducing the concentration of hydrogen ions. During the first seven years of operation the licensee controlled pH with several chemicals; i.e., sodium phosphate, cyclohexamine, morpho 11ne, and ammonia, and the pH of the feed- water and condensate varied from less than 8 (conducive to general corrosion of iron) to greater tha,n 10 (not conducive to general corrosion of iron - although conducive to loss of copper from condense and feedwater tubes.) Since startup after the steam generator replacement outages the pH has been maintained between 8.8 and 9.2, as recommended by the SGOG, as a compromise range to minimize the corrosion of copper and iron in both the low and high pressure lines in the secondary system. (2) Effect of Dissolved Oxygen The licensee, as well as various investigators of corrosion mechanisms, considers very low concentrations of oxygen to be detrimental to control of generalized thinning of carbon steel. , 1 In steady state conditions diffusion of dxygen to the metal - water interface aids in the initial formation of magnetite and its continued replacement. Under such conditions redLcing agents are ' -- -- . - , . _ , - - - . . , , - - , - - - , , . - - - - - - - , - - - - - - - - - - - - - - - - - - - - - - - - - - - , - - - - - , - - - - - - - - - - - - - - - - - -

_ _ , - _ - .__ - , .. ' Appendix 4

harmful since they tend to reverse the formation of ferrous ton through the reactions written above. However, this argument must be balanced against the cathodic attack of oxygen on iron (if the iron surface is not isolated by impervious Fe 03 4 (magnetite). 8 In' a dynamic environment, such as in the feedwater pipe, all . equilibria are changed because of the high probability that the products of electrochemical reactions will be removed immediately. 3. Conclusions On the basis of current technology and the understanding of the mechanisms of localized corrosion, the damage experienced by the or'31nal steam generator tubes during the initial seven years of plant operation is understandable. However, the inspector has not been able to correlate the - cause of steam generator tube denting to the generalized thinning of the A feedwater suct, ion pipe. Also, the inspector has not been convinced that the feedwater system was ever coated completely with magnetite, or if it were, that the magnetite protected the pipe from erosion / corrosion. It is evident that thinning occurred in regions of hydraulic turbulence, and consequently erosion appears to have been the dominant cause of thinning. The degree to which generalized corrosion mechanisms abetted the transfer of

metallic or ionic iron from the pipe surface has not been established.

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