ML20003A592: Difference between revisions

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| number = ML20003A592
| number = ML20003A592
| issue date = 12/18/1980
| issue date = 12/18/1980
| title = Responds to NRC 801125 Ltr Re Violations Noted in IE Insp Rept 50-302/80-33.Corrective actions:0-3000 Psig Pressure Gauges Will Be Installed & Remote Shutdown Instrumentation Calibr Will Be Revised
| title = Responds to NRC Re Violations Noted in IE Insp Rept 50-302/80-33.Corrective actions:0-3000 Psig Pressure Gauges Will Be Installed & Remote Shutdown Instrumentation Calibr Will Be Revised
| author name = Hancock J
| author name = Hancock J
| author affiliation = FLORIDA POWER CORP.
| author affiliation = FLORIDA POWER CORP.
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = CS-80-290, NUDOCS 8102040348
| document report number = CS-80-290, NUDOCS 8102040348
| title reference date = 11-25-1980
| package number = ML20003A591
| package number = ML20003A591
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
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=Text=
=Text=
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10 F C 22 N2 4 E Florida c a.o,0. u.a ~P wer December 18, 1980 3-0-3-a-2 CS-80-290 3-120-31 Mr. J, P. O'Reilly, Director Docket No. 50-302 Office of Inspection & Enforcement Licensee No DPR-72 U.S. Nuclear Regulatory Commission Ref:
80-33/RII:TFS Atlanta, GA 30303 50/302/80-33


==Dear Mr. O'Reilly:==
==Dear Mr. O'Reilly:==
We offer the following responses to the Items of Noncompliance in the referenced report.
We offer the following responses to the Items of Noncompliance in the referenced report.
NOTICE OF VIOLATION A. Based on the NRC inspection September 2 - October 3, 1980, certain of your activities were apparently not conducted in full compliance with NRC requirements as indicated below:
NOTICE OF VIOLATION A.
: a. The intent of the original procedure is not altered,
Based on the NRC inspection September 2 - October 3, 1980, certain of your activities were apparently not conducted in full compliance with NRC requirements as indicated below:
: b. The change is approved by two members of the plant staff management staff, at least one of whom holds a Senior Reactor Operator's License on the unit affected,
a.
: c. The change is documented, reviewed by the PRC and approved by the Nuclear Plant Manager within 14 days of implementation.
The intent of the original procedure is not altered, b.
The change is approved by two members of the plant staff management staff, at least one of whom holds a Senior Reactor Operator's License on the unit affected, c.
The change is documented, reviewed by the PRC and approved by the Nuclear Plant Manager within 14 days of implementation.
Contrary to the above, tn April 12, 1980, a temporary change was made to Surveillance Procedure SP-161, Remote Shutdown Instru-ment Calibration, without the approval of two members of the plant management staff and was not reviewed by the PRC and ap-proved by the Nuclear Plant Manager within 14 days of in. 'ementa-tion.
Contrary to the above, tn April 12, 1980, a temporary change was made to Surveillance Procedure SP-161, Remote Shutdown Instru-ment Calibration, without the approval of two members of the plant management staff and was not reviewed by the PRC and ap-proved by the Nuclear Plant Manager within 14 days of in. 'ementa-tion.
A. Response:          As a result of this event, appropriate plant procedures have been reviewed with the cognizant supervisers to assure their understanding of the consequences of noncompliance with procedures, A modification (80-9-76) has been initiated to install 0-3000 psig pressure gauges in place of the 0-2000 psig gauges. In addition, a revision will be submitted to Surveillance Procedure SP-161, Remote Shutdown Instrumentation Calibration to change the appropriate 810 204 0 h General Office 3201 in.rty-fourtn street soutn . P O Box 14042. st Petersburg. Fionda 33733 813 - 866-5151
A.
 
===Response===
As a result of this event, appropriate plant procedures have been reviewed with the cognizant supervisers to assure their understanding of the consequences of noncompliance with procedures, A modification (80-9-76) has been initiated to install 0-3000 psig pressure gauges in place of the 0-2000 psig gauges.
In addition, a revision will be submitted to Surveillance Procedure SP-161, Remote Shutdown Instrumentation Calibration to change the appropriate 810 204 0 h General Office 3201 in.rty-fourtn street soutn. P O Box 14042. st Petersburg. Fionda 33733 813 - 866-5151


r i,3 Notice of Violation Response-Ref: 80-33/RII:TFS Page 2 pressure indicator calibration sheets to conform to the higher range gauges.
r i,3 Notice of Violation Response-Ref: 80-33/RII:TFS Page 2 pressure indicator calibration sheets to conform to the higher range gauges.
Full compliance will be achieved upon procurement of the gauges which is anticipated prior to 1 May 1981.
Full compliance will be achieved upon procurement of the gauges which is anticipated prior to 1 May 1981.
Should you have any further questions, please contact us.
Should you have any further questions, please contact us.
Very truly yours, o                     FLORIDA POWER CORPORATION M
Very truly yours, o
O                                            7" Nuclear Plant Manager       J. A. Hancock           #
FLORIDA POWER CORPORATION O
Assistant Vice President Nuclear Operations KFL/rc w -. , p 1
M 7"
                                                                                      ,    - .}}
Nuclear Plant Manager J. A. Hancock Assistant Vice President Nuclear Operations KFL/rc w -.,
p 1
.}}

Latest revision as of 16:00, 23 December 2024

Responds to NRC Re Violations Noted in IE Insp Rept 50-302/80-33.Corrective actions:0-3000 Psig Pressure Gauges Will Be Installed & Remote Shutdown Instrumentation Calibr Will Be Revised
ML20003A592
Person / Time
Site: Crystal River 
Issue date: 12/18/1980
From: Hancock J
FLORIDA POWER CORP.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20003A591 List:
References
CS-80-290, NUDOCS 8102040348
Download: ML20003A592 (2)


Text

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10 F C 22 N2 4 E Florida c a.o,0. u.a ~P wer December 18, 1980 3-0-3-a-2 CS-80-290 3-120-31 Mr. J, P. O'Reilly, Director Docket No. 50-302 Office of Inspection & Enforcement Licensee No DPR-72 U.S. Nuclear Regulatory Commission Ref:

80-33/RII:TFS Atlanta, GA 30303 50/302/80-33

Dear Mr. O'Reilly:

We offer the following responses to the Items of Noncompliance in the referenced report.

NOTICE OF VIOLATION A.

Based on the NRC inspection September 2 - October 3, 1980, certain of your activities were apparently not conducted in full compliance with NRC requirements as indicated below:

a.

The intent of the original procedure is not altered, b.

The change is approved by two members of the plant staff management staff, at least one of whom holds a Senior Reactor Operator's License on the unit affected, c.

The change is documented, reviewed by the PRC and approved by the Nuclear Plant Manager within 14 days of implementation.

Contrary to the above, tn April 12, 1980, a temporary change was made to Surveillance Procedure SP-161, Remote Shutdown Instru-ment Calibration, without the approval of two members of the plant management staff and was not reviewed by the PRC and ap-proved by the Nuclear Plant Manager within 14 days of in. 'ementa-tion.

A.

Response

As a result of this event, appropriate plant procedures have been reviewed with the cognizant supervisers to assure their understanding of the consequences of noncompliance with procedures, A modification (80-9-76) has been initiated to install 0-3000 psig pressure gauges in place of the 0-2000 psig gauges.

In addition, a revision will be submitted to Surveillance Procedure SP-161, Remote Shutdown Instrumentation Calibration to change the appropriate 810 204 0 h General Office 3201 in.rty-fourtn street soutn. P O Box 14042. st Petersburg. Fionda 33733 813 - 866-5151

r i,3 Notice of Violation Response-Ref: 80-33/RII:TFS Page 2 pressure indicator calibration sheets to conform to the higher range gauges.

Full compliance will be achieved upon procurement of the gauges which is anticipated prior to 1 May 1981.

Should you have any further questions, please contact us.

Very truly yours, o

FLORIDA POWER CORPORATION O

M 7"

Nuclear Plant Manager J. A. Hancock Assistant Vice President Nuclear Operations KFL/rc w -.,

p 1

.