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{{#Wiki_filter:UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION OFFICE OF [INSERT]
{{#Wiki_filter:UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION OFFICE OF [INSERT] Eric J. Leeds, Director Proposed DD-YY-XX In the Matter of ) ) ) ) ) ) Docket No. 50-333 ENTERGY NUCLEAR OPERATIONS INC. License No. DPR-059 James A. FitzPatrick Nuclear Power Plant PROPOSED DIRECTOR'S DECISION UNDER 10 CFR 2.206 I. Introduction By electronic mail letter dated July 25, 2013, as supplemented on November 13, 2013, Mr. David Lochbaum filed a petition under Section 2.206, "Request for action under this subpart," of Title 10 of the Code of Federal Regulations on behalf of Alliance for a Green Economy, Beyond Nuclear, Citizens Awareness Network, and the Union of Concerned Scientists (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 13217 A061 ). The petitioners requested that the U.S. Nuclear Regulatory Commission (NRC) take the following action: Take enforcement action by imposing a regulatory requirement that all the condenser tubes be replaced at [the James A. FitzPatrick Nuclear Power Plant (FitzPatrick)]
Eric J. Leeds, Director Proposed DD-YY-XX In the Matter of ) ) ) ) ) ) Docket No. 50-333 ENTERGY NUCLEAR OPERATIONS INC. License No. DPR-059 James A. FitzPatrick Nuclear Power Plant PROPOSED DIRECTOR'S DECISION UNDER 10 CFR 2.206 I. Introduction By electronic mail letter dated July 25, 2013, as supplemented on November 13, 2013, Mr. David Lochbaum filed a petition under Section 2.206, "Request for action under this subpart,"
of Title 10 of the Code of Federal Regulations on behalf of Alliance for a Green Economy, Beyond Nuclear, Citizens Awareness  
: Network, and the Union of Concerned Scientists (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 13217 A061 ). The petitioners requested that the U.S. Nuclear Regulatory Commission (NRC) take the following action: Take enforcement action by imposing a regulatory requirement that all the condenser tubes be replaced at [the James A. FitzPatrick Nuclear Power Plant (FitzPatrick)]
prior to the reactor restarting from its fall 2014 refueling outage. On November 13, 2013, the petitioners met with the NRC's petition review board by teleconference to clarify the bases for the petition.
prior to the reactor restarting from its fall 2014 refueling outage. On November 13, 2013, the petitioners met with the NRC's petition review board by teleconference to clarify the bases for the petition.
The transcript of this meeting was treated as a supplement to the petition and is available under ADAMS Accession No. ML 14036A234 for inspection at the Commission's Public Document Room (PDR), located at One White Flint  North, Public File Area 01 F21, 11555 Rockville Pike (first floor), Rockville, MD. Publicly available records will be accessible from the ADAMS Public Electronic Reading Room on the NRC Web site at http://www.nrc.gov/reading-rm/adams.html.
The transcript of this meeting was treated as a supplement to the petition and is available under ADAMS Accession No. ML 14036A234 for inspection at the Commission's Public Document Room (PDR), located at One White Flint  North, Public File Area 01 F21, 11555 Rockville Pike (first floor), Rockville, MD. Publicly available records will be accessible from the ADAMS Public Electronic Reading Room on the NRC Web site at http://www.nrc.gov/reading-rm/adams.html.
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* FitzPatrick is experiencing abnormally high occurrences of condenser tube failures.
* FitzPatrick is experiencing abnormally high occurrences of condenser tube failures.
To repair these leaks, Entergy Nuclear Operations Inc. (Entergy) routinely reduces power, makes the repairs needed, and returns to full power. The petitioners state that these power excursions constitute a risk to public health and safety. The NRC's Reactor Oversight Process (ROP) also recognizes the elevated risk associated with unplanned power changes.
To repair these leaks, Entergy Nuclear Operations Inc. (Entergy) routinely reduces power, makes the repairs needed, and returns to full power. The petitioners state that these power excursions constitute a risk to public health and safety. The NRC's Reactor Oversight Process (ROP) also recognizes the elevated risk associated with unplanned power changes.
* The NRC team observed that Entergy did not properly consider FitzPatrick operating  
* The NRC team observed that Entergy did not properly consider FitzPatrick operating history, specifically the 4 years of outages, when projecting the expected condenser-tube life. Consequently, Entergy did not properly plan and design for condenser tube replacement before tube leakage, which has necessitated frequent downpowers for repair. Corrective actions include condenser-tube sleeving during the fall 2012 refueling outage and a planned complete replacement of all condenser tubes in the fall 2014 refueling outage.
: history, specifically the 4 years of outages, when projecting the expected condenser-tube life. Consequently, Entergy did not properly plan and design for condenser tube replacement before tube leakage, which has necessitated frequent downpowers for repair. Corrective actions include condenser-tube sleeving during the fall 2012 refueling outage and a planned complete replacement of all condenser tubes in the fall 2014 refueling outage.
* Operating experience indicates that condenser-tube leaks have contaminated the reactor coolant water with impurities from the condenser cooling water and have caused extensive damage to nuclear power plant components.
* Operating experience indicates that condenser-tube leaks have contaminated the reactor coolant water with impurities from the condenser cooling water and have caused extensive damage to nuclear power plant components.
* Appendix B, "Quality Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants,"
* Appendix B, "Quality Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants," to 10 CFR Part 50, "Domestic Licensing of Production and Utilization Facilities" (see collections/cfr/part050/part050-appb.html), requires that plant owners develop and maintain quality-assurance programs.
to 10 CFR Part 50, "Domestic Licensing of Production and Utilization Facilities" (see collections/cfr/part050/part050-appb.html),
This regulatory requirement explicitly states: As used in this appendix, "quality assurance" comprises all those planned and systematic actions necessary to provide adequate confidence that a structure, system, or component will perform satisfactorily in service. On February 12, 2014, the NRC staff issued an acknowledgement letter to the petitioners accepting the petition and informed the petitioners that the NRC will review the petition under the provisions of 10 CFR 2.206, as requested.
requires that plant owners develop and maintain quality-assurance programs.
The NRC staff has followed the condenser-tube leakage problems and the frequent power changes at FitzPatrick to make tube repairs. On January 21, 2013, Entergy reported to the NRC an "unplanned power change" performance indicator that crossed a threshold from green to white. Based on that report, the NRC assigned a white performance indicator action matrix input to the initiating-events cornerstone in the fourth quarter of 2012. As a followup to the action matrix input, the NRC staff performed a supplemental inspection at FitzPatrick to  determine whether (1) the root and contributing causes for the risk-significant issues were understood, (2) the extent of condition and extent of cause for identified issues were understood, and (3) corrective actions undertaken by the licensee were sufficient to address and prevent repetition of the root and contributing causes. Entergy identified the root cause of the issue to be failure to include inner-diameter condenser-tube wear in any component or system monitoring plan. The NRC staff determined that the root cause also included Entergy's failure to incorporate applicable operating experience from the 1995 condenser-tube replacement in an appropriate system or program. The NRC staff determined that the deficiency was minor because the review of the resulting extent of condition did not identify any potential safety concerns.
This regulatory requirement explicitly states: As used in this appendix, "quality assurance" comprises all those planned and systematic actions necessary to provide adequate confidence that a structure, system, or component will perform satisfactorily in service.
As a result, Entergy has now incorporated in its corrective actions a condenser-tube monitoring and trending program, retubing the main condenser and revising the Corrective Action Review Board grading sheet for cause evaluations to better identify previous corrective actions that did not prevent repetition of tube failures.
On February 12, 2014, the NRC staff issued an acknowledgement letter to the petitioners accepting the petition and informed the petitioners that the NRC will review the petition under the provisions of 10 CFR 2.206, as requested.
The NRC staff has determined that the Entergy evaluation was thorough and that the interim corrective action implemented-namely, sleeving the outlet of the condenser tubes as a temporary measure until the condenser tubes could be replaced-was a reasonable attempt to address the problem. However, this measure did not have the desired result of reducing the number of unplanned power changes. Therefore, the inspection will remain open until corrective action to significantly reduce the number of unplanned power changes is implemented.
The NRC staff has followed the condenser-tube leakage problems and the frequent power changes at FitzPatrick to make tube repairs.
On January 21, 2013, Entergy reported to the NRC an "unplanned power change" performance indicator that crossed a threshold from green to white. Based on that report, the NRC assigned a white performance indicator action matrix input to the initiating-events cornerstone in the fourth quarter of 2012. As a followup to the action matrix input, the NRC staff performed a supplemental inspection at FitzPatrick to  determine whether (1) the root and contributing causes for the risk-significant issues were understood, (2) the extent of condition and extent of cause for identified issues were understood, and (3) corrective actions undertaken by the licensee were sufficient to address and prevent repetition of the root and contributing causes. Entergy identified the root cause of the issue to be failure to include inner-diameter condenser-tube wear in any component or system monitoring plan. The NRC staff determined that the root cause also included Entergy's failure to incorporate applicable operating experience from the 1995 condenser-tube replacement in an appropriate system or program.
The NRC staff determined that the deficiency was minor because the review of the resulting extent of condition did not identify any potential safety concerns.
As a result, Entergy has now incorporated in its corrective actions a condenser-tube monitoring and trending  
: program, retubing the main condenser and revising the Corrective Action Review Board grading sheet for cause evaluations to better identify previous corrective actions that did not prevent repetition of tube failures.
The NRC staff has determined that the Entergy evaluation was thorough and that the interim corrective action implemented-namely, sleeving the outlet of the condenser tubes as a temporary measure until the condenser tubes could be replaced-was a reasonable attempt to address the problem.  
: However, this measure did not have the desired result of reducing the number of unplanned power changes.
Therefore, the inspection will remain open until corrective action to significantly reduce the number of unplanned power changes is implemented.
The petitioners stated that Appendix 8 to 10 CFR Part 50 requires that plant owners develop and maintain quality-assurance programs.
The petitioners stated that Appendix 8 to 10 CFR Part 50 requires that plant owners develop and maintain quality-assurance programs.
The main condenser is not a safety-related component and, therefore, is not directly addressed by FitzPatrick's  
The main condenser is not a safety-related component and, therefore, is not directly addressed by FitzPatrick's license, technical specifications, or Appendix 8 to 10 CFR Part Part 50. Entergy  documented that the risk consequences of condenser tube leaks are low. Condenser tube leaks are readily identified and can be isolated.
: license, technical specifications, or Appendix 8 to 10 CFR Part Part 50. Entergy  documented that the risk consequences of condenser tube leaks are low. Condenser tube leaks are readily identified and can be isolated.
Entergy also noted that severe tube leaks could result in chemistry and corrosion issues in the reactor coolant system. The water chemistry of the reactor coolant, feedwater and condensate systems is routinely monitored and procedures provide corrective actions for chemistry issues to protect the reactor and fuel. The NRC staff concluded that risk consequences and compliance concerns were appropriately documented.
Entergy also noted that severe tube leaks could result in chemistry and corrosion issues in the reactor coolant system. The water chemistry of the reactor coolant, feedwater and condensate systems is routinely monitored and procedures provide corrective actions for chemistry issues to protect the reactor and fuel. The NRC staff concluded that risk consequences and compliance concerns were appropriately documented.
Ill Conclusion The petitioners raised issues related to routine condenser tube leaks causing power reductions.
Ill Conclusion The petitioners raised issues related to routine condenser tube leaks causing power reductions.
Condenser tube leaks have caused coolant contamination which in turn has caused extensive damage to nuclear components of other plants. Entergy did not properly plan and design for condenser tube replacement which has resulted in recurring condenser tube leaks. The petitioners claim that contrary to the criteria of the NRC's Appendix B to 10 CFR Part 50, the owners of FitzPatrick have not developed and maintained adequate quality assurance for FitzPatrick condenser tubes. For these reasons the petitioners requested that the NRC take an enforcement action by issuing an Order to Entergy requiring that all the condenser tubes at FitzPatrick be replaced prior to restart from its fall 2014 refueling outage. As discussed above, based upon its Reactor Oversight  
Condenser tube leaks have caused coolant contamination which in turn has caused extensive damage to nuclear components of other plants. Entergy did not properly plan and design for condenser tube replacement which has resulted in recurring condenser tube leaks. The petitioners claim that contrary to the criteria of the NRC's Appendix B to 10 CFR Part 50, the owners of FitzPatrick have not developed and maintained adequate quality assurance for FitzPatrick condenser tubes. For these reasons the petitioners requested that the NRC take an enforcement action by issuing an Order to Entergy requiring that all the condenser tubes at FitzPatrick be replaced prior to restart from its fall 2014 refueling outage. As discussed above, based upon its Reactor Oversight Process, the NRC staff assigned a White performance indicator to Entergy because of frequent unplanned power changes to repair the leaking tubes. In response to the White performance indicator, the NRC conducted a supplemental inspection under Inspection Procedure 95001. The NRC staff concluded that the licensee's evaluation of condenser-tube failures was thorough, but the corrective actions were not effective in reducing the unplanned power outages. The NRC staff's evaluations, including consideration of tube leaks and potential primary coolant contamination,  did not find any violations that are more than minor. Consequently the petitioners request for the enforcement action is denied. The NRC staff has stated above that the FitzPatrick condenser tubes are not safety related and are not subject to the requirements of the 10 CFR Part 50, Appendix 8 quality assurance criteria.
: Process, the NRC staff assigned a White performance indicator to Entergy because of frequent unplanned power changes to repair the leaking tubes. In response to the White performance indicator, the NRC conducted a supplemental inspection under Inspection Procedure 95001. The NRC staff concluded that the licensee's evaluation of condenser-tube failures was thorough, but the corrective actions were not effective in reducing the unplanned power outages.
The NRC staff's evaluations, including consideration of tube leaks and potential primary coolant contamination,  did not find any violations that are more than minor. Consequently the petitioners request for the enforcement action is denied. The NRC staff has stated above that the FitzPatrick condenser tubes are not safety related and are not subject to the requirements of the 10 CFR Part 50, Appendix 8 quality assurance criteria.
Since the licensee's corrective actions have not been sufficient to reduce unplanned power changes, the NRC staff will keep the Supplemental Inspection 95001 open until additional licensee actions are taken. The NRC's inspection program and Reactor Oversight Process will continue to monitor performance at FitzPatrick and will ensure that the health and safety of the public is protected.
Since the licensee's corrective actions have not been sufficient to reduce unplanned power changes, the NRC staff will keep the Supplemental Inspection 95001 open until additional licensee actions are taken. The NRC's inspection program and Reactor Oversight Process will continue to monitor performance at FitzPatrick and will ensure that the health and safety of the public is protected.
As provided in 10 CFR 2.206( c), a copy of this director's decision will be filed with the Secretary of the Commission for the Commission to review. As provided by this regulation, the decision will constitute the final action of the Commission 25 days after the date of the decision unless the Commission, on its own motion, institutes a review of the decision within that time. Dated at Rockville,  
As provided in 10 CFR 2.206( c), a copy of this director's decision will be filed with the Secretary of the Commission for the Commission to review. As provided by this regulation, the decision will constitute the final action of the Commission 25 days after the date of the decision unless the Commission, on its own motion, institutes a review of the decision within that time. Dated at Rockville, Maryland, this [date] day of [Month Year]. FOR THE NUCLEAR REGULATORY COMMISSION Eric Leeds, Director Office of Nuclear Reactor Regulation}}
: Maryland, this [date] day of [Month Year]. FOR THE NUCLEAR REGULATORY COMMISSION Eric Leeds, Director Office of Nuclear Reactor Regulation}}

Revision as of 16:11, 9 July 2018

G20130561 - 2.206 Proposed Director'S Decision David Lochbaum Ltr Dtd 07/25/13 Concerning the Recurring Condenser Tube Leaks at the James a Fitzpatrick Nuclear Power Plant (TAC No. MF2521)
ML14127A338
Person / Time
Site: FitzPatrick Constellation icon.png
Issue date: 06/27/2014
From: Leeds E J
Office of Nuclear Reactor Regulation
To:
Thadani, Mohan, NRR/DORL/LPLI-1
Shared Package
ML14127A329 List:
References
2.206, G20130561, TAC MF2521
Download: ML14127A338 (6)


Text

UNITED STATES OF AMERICA NUCLEAR REGULATORY COMMISSION OFFICE OF [INSERT] Eric J. Leeds, Director Proposed DD-YY-XX In the Matter of ) ) ) ) ) ) Docket No. 50-333 ENTERGY NUCLEAR OPERATIONS INC. License No. DPR-059 James A. FitzPatrick Nuclear Power Plant PROPOSED DIRECTOR'S DECISION UNDER 10 CFR 2.206 I. Introduction By electronic mail letter dated July 25, 2013, as supplemented on November 13, 2013, Mr. David Lochbaum filed a petition under Section 2.206, "Request for action under this subpart," of Title 10 of the Code of Federal Regulations on behalf of Alliance for a Green Economy, Beyond Nuclear, Citizens Awareness Network, and the Union of Concerned Scientists (Agencywide Documents Access and Management System (ADAMS) Accession No. ML 13217 A061 ). The petitioners requested that the U.S. Nuclear Regulatory Commission (NRC) take the following action: Take enforcement action by imposing a regulatory requirement that all the condenser tubes be replaced at [the James A. FitzPatrick Nuclear Power Plant (FitzPatrick)]

prior to the reactor restarting from its fall 2014 refueling outage. On November 13, 2013, the petitioners met with the NRC's petition review board by teleconference to clarify the bases for the petition.

The transcript of this meeting was treated as a supplement to the petition and is available under ADAMS Accession No. ML 14036A234 for inspection at the Commission's Public Document Room (PDR), located at One White Flint North, Public File Area 01 F21, 11555 Rockville Pike (first floor), Rockville, MD. Publicly available records will be accessible from the ADAMS Public Electronic Reading Room on the NRC Web site at http://www.nrc.gov/reading-rm/adams.html.

Persons who do not have access to ADAMS or who encounter problems in accessing the documents stored in ADAMS should contact the NRC PDR Reference staff by telephone at 1-800-397-4209 or 301-415-4 737 or by e-mail to pdr@nrc.gov.

II. Discussion As a basis for their petition, the petitioners asserted the following:

  • FitzPatrick is experiencing abnormally high occurrences of condenser tube failures.

To repair these leaks, Entergy Nuclear Operations Inc. (Entergy) routinely reduces power, makes the repairs needed, and returns to full power. The petitioners state that these power excursions constitute a risk to public health and safety. The NRC's Reactor Oversight Process (ROP) also recognizes the elevated risk associated with unplanned power changes.

  • The NRC team observed that Entergy did not properly consider FitzPatrick operating history, specifically the 4 years of outages, when projecting the expected condenser-tube life. Consequently, Entergy did not properly plan and design for condenser tube replacement before tube leakage, which has necessitated frequent downpowers for repair. Corrective actions include condenser-tube sleeving during the fall 2012 refueling outage and a planned complete replacement of all condenser tubes in the fall 2014 refueling outage.
  • Operating experience indicates that condenser-tube leaks have contaminated the reactor coolant water with impurities from the condenser cooling water and have caused extensive damage to nuclear power plant components.
  • Appendix B, "Quality Assurance Criteria for Nuclear Power Plants and Fuel Reprocessing Plants," to 10 CFR Part 50, "Domestic Licensing of Production and Utilization Facilities" (see collections/cfr/part050/part050-appb.html), requires that plant owners develop and maintain quality-assurance programs.

This regulatory requirement explicitly states: As used in this appendix, "quality assurance" comprises all those planned and systematic actions necessary to provide adequate confidence that a structure, system, or component will perform satisfactorily in service. On February 12, 2014, the NRC staff issued an acknowledgement letter to the petitioners accepting the petition and informed the petitioners that the NRC will review the petition under the provisions of 10 CFR 2.206, as requested.

The NRC staff has followed the condenser-tube leakage problems and the frequent power changes at FitzPatrick to make tube repairs. On January 21, 2013, Entergy reported to the NRC an "unplanned power change" performance indicator that crossed a threshold from green to white. Based on that report, the NRC assigned a white performance indicator action matrix input to the initiating-events cornerstone in the fourth quarter of 2012. As a followup to the action matrix input, the NRC staff performed a supplemental inspection at FitzPatrick to determine whether (1) the root and contributing causes for the risk-significant issues were understood, (2) the extent of condition and extent of cause for identified issues were understood, and (3) corrective actions undertaken by the licensee were sufficient to address and prevent repetition of the root and contributing causes. Entergy identified the root cause of the issue to be failure to include inner-diameter condenser-tube wear in any component or system monitoring plan. The NRC staff determined that the root cause also included Entergy's failure to incorporate applicable operating experience from the 1995 condenser-tube replacement in an appropriate system or program. The NRC staff determined that the deficiency was minor because the review of the resulting extent of condition did not identify any potential safety concerns.

As a result, Entergy has now incorporated in its corrective actions a condenser-tube monitoring and trending program, retubing the main condenser and revising the Corrective Action Review Board grading sheet for cause evaluations to better identify previous corrective actions that did not prevent repetition of tube failures.

The NRC staff has determined that the Entergy evaluation was thorough and that the interim corrective action implemented-namely, sleeving the outlet of the condenser tubes as a temporary measure until the condenser tubes could be replaced-was a reasonable attempt to address the problem. However, this measure did not have the desired result of reducing the number of unplanned power changes. Therefore, the inspection will remain open until corrective action to significantly reduce the number of unplanned power changes is implemented.

The petitioners stated that Appendix 8 to 10 CFR Part 50 requires that plant owners develop and maintain quality-assurance programs.

The main condenser is not a safety-related component and, therefore, is not directly addressed by FitzPatrick's license, technical specifications, or Appendix 8 to 10 CFR Part Part 50. Entergy documented that the risk consequences of condenser tube leaks are low. Condenser tube leaks are readily identified and can be isolated.

Entergy also noted that severe tube leaks could result in chemistry and corrosion issues in the reactor coolant system. The water chemistry of the reactor coolant, feedwater and condensate systems is routinely monitored and procedures provide corrective actions for chemistry issues to protect the reactor and fuel. The NRC staff concluded that risk consequences and compliance concerns were appropriately documented.

Ill Conclusion The petitioners raised issues related to routine condenser tube leaks causing power reductions.

Condenser tube leaks have caused coolant contamination which in turn has caused extensive damage to nuclear components of other plants. Entergy did not properly plan and design for condenser tube replacement which has resulted in recurring condenser tube leaks. The petitioners claim that contrary to the criteria of the NRC's Appendix B to 10 CFR Part 50, the owners of FitzPatrick have not developed and maintained adequate quality assurance for FitzPatrick condenser tubes. For these reasons the petitioners requested that the NRC take an enforcement action by issuing an Order to Entergy requiring that all the condenser tubes at FitzPatrick be replaced prior to restart from its fall 2014 refueling outage. As discussed above, based upon its Reactor Oversight Process, the NRC staff assigned a White performance indicator to Entergy because of frequent unplanned power changes to repair the leaking tubes. In response to the White performance indicator, the NRC conducted a supplemental inspection under Inspection Procedure 95001. The NRC staff concluded that the licensee's evaluation of condenser-tube failures was thorough, but the corrective actions were not effective in reducing the unplanned power outages. The NRC staff's evaluations, including consideration of tube leaks and potential primary coolant contamination, did not find any violations that are more than minor. Consequently the petitioners request for the enforcement action is denied. The NRC staff has stated above that the FitzPatrick condenser tubes are not safety related and are not subject to the requirements of the 10 CFR Part 50, Appendix 8 quality assurance criteria.

Since the licensee's corrective actions have not been sufficient to reduce unplanned power changes, the NRC staff will keep the Supplemental Inspection 95001 open until additional licensee actions are taken. The NRC's inspection program and Reactor Oversight Process will continue to monitor performance at FitzPatrick and will ensure that the health and safety of the public is protected.

As provided in 10 CFR 2.206( c), a copy of this director's decision will be filed with the Secretary of the Commission for the Commission to review. As provided by this regulation, the decision will constitute the final action of the Commission 25 days after the date of the decision unless the Commission, on its own motion, institutes a review of the decision within that time. Dated at Rockville, Maryland, this [date] day of [Month Year]. FOR THE NUCLEAR REGULATORY COMMISSION Eric Leeds, Director Office of Nuclear Reactor Regulation