ML093020671: Difference between revisions

From kanterella
Jump to navigation Jump to search
Created page by program invented by StriderTol
StriderTol Bot change
 
(One intermediate revision by the same user not shown)
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:Brunswick Nuclear Plant Emergency Diesel Generators NRC Region II Visit October 22, 2009 Enclosure 2
{{#Wiki_filter:Brunswick Nuclear Plant Emergency Diesel Generators NRC Region II Visit October 22, 2009  


Agenda l AC Power Reliability l EDG Historical Performance l EDG Performance Indicators l EDG #4 Governor l Organizational Lessons and Actions from Recent Events 2
Agenda l AC Power Reliability l EDG Historical Performance l EDG Performance Indicators l EDG #4 Governor l Organizational Lessons and Actions from Recent Events 2  
Enclosure 2


AC Power Reliability Completed Actions                                    Completed Actions Installed new 230 kV supply breakers for SATs   Replaced 2 transmission line breakers Installed new Unit output breakers               Replaced 145 poles and 341 insulator sets Replaced SWYD CCVTs & Lightning Arrestors       Revised Transmission Interface Agreement to specify Installed new local 230 kV capacitor banks for   plant involvement/coordination of work activities voltage support on Unit 2                                           Planned Actions Installed new Main Transformers - Outfitted with Install new local 230 kV capacitor banks for voltage continuous gas monitoring instrumentation        Support on Unit 1 Improved material condition of spare SAT        Install permanent SAMA diesel generators on U1 Replaced sudden pressure relays                  Unit Auxiliary Transformer (UAT) Replacement Replaced no load disconnect switches            Replace remaining transmission line breakers Improved PMs on Iso-Phase and Non-Seg Bus        Replace Line Insulators at a rate of ~150 sets per year Inspected Non-Seg Bus flex links                during each unit Established standard preventive maintenance                        Under Evaluation program for buses Replace SATs w/auto load tap changing transformers Installed permanent SAMA diesel generators on Unit 2                                          Upgrade 2/3 logic for Aux Transformer 3
AC Power Reliability 3
Enclosure 2
Completed Actions Installed new 230 kV supply breakers for SATs Installed new Unit output breakers Replaced SWYD CCVTs & Lightning Arrestors Installed new local 230 kV capacitor banks for voltage support on Unit 2 Installed new Main Transformers - Outfitted with continuous gas monitoring instrumentation Improved material condition of spare SAT Replaced sudden pressure relays Replaced no load disconnect switches Improved PMs on Iso-Phase and Non-Seg Bus Inspected Non-Seg Bus flex links Established standard preventive maintenance program for buses Installed permanent SAMA diesel generators on Unit 2 Planned Actions Install new local 230 kV capacitor banks for voltage Support on Unit 1 Install permanent SAMA diesel generators on U1 Unit Auxiliary Transformer (UAT) Replacement Replace remaining transmission line breakers Replace Line Insulators at a rate of ~150 sets per year during each unit Completed Actions Replaced 2 transmission line breakers Replaced 145 poles and 341 insulator sets Revised Transmission Interface Agreement to specify plant involvement/coordination of work activities Under Evaluation Replace SATs w/auto load tap changing transformers Upgrade 2/3 logic for Aux Transformer  


Emergency Power Reliability Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteries Improved CDF by 68% on Unit 1 and 66% on Unit 2 4
Emergency Power Reliability 4
Enclosure 2
Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteries Improved CDF by 68% on Unit 1 and 66% on Unit 2  


EDG Historical Performance 2007 Reliability Study 5
5 EDG Historical Performance 2007 Reliability Study  
Enclosure 2


2007 Reliability Study
w Operations w Maintenance w Engineering w Technical Training 2007 Reliability Study 6
* Multi-discipline team assembled to review EDG issues and develop short and long term action plan w Operations          w Licensing w Maintenance          w Procurement w Engineering          w Industry Representative w Technical Training  w Vendor Representative
w Licensing w Procurement w Industry Representative w Vendor Representative
* INPO Assist 6
*Multi-discipline team assembled to review EDG issues and develop short and long term action plan
Enclosure 2
*INPO Assist  


2007 Reliability Study Inputs Used in Analysis l MSPI Reliability data l EDG Material Costs, 2003-2006 l Vendor Input/Industry OE l EDG Self Assessment &
l MSPI Reliability data l
l Maintenance Rule Functional     Benchmarks, 2003-2006 Failures, 2000-2006 l EDG NRC Findings, 2003-2006 l BNP Equipment Reliability List l EDG NCRs, 2003-2006           l EDG Nonconformances l EDG Planned and Unplanned     l EDG items on Long Range Plan Out Of Service (OOS) times, 2003-2006                     l System Engineer brainstorming sessions l EDG Corrective Work Orders, 2003-2006 7
Vendor Input/Industry OE l
Enclosure 2
Maintenance Rule Functional Failures, 2000-2006 l
BNP Equipment Reliability List l
EDG NCRs, 2003-2006 l
EDG Planned and Unplanned Out Of Service (OOS) times, 2003-2006 l
EDG Corrective Work Orders, 2003-2006 2007 Reliability Study Inputs Used in Analysis 7
l EDG Material Costs, 2003-2006 l
EDG Self Assessment &
Benchmarks, 2003-2006 l
EDG NRC Findings, 2003-2006 l
EDG Nonconformances l
EDG items on Long Range Plan l
System Engineer brainstorming sessions


EDG Actions Action             2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017     2018 EDG #2 exhaust bellows Allen Bradley relays Completed Jacket Water TCVs Working SAMG DGs Scheduled Capacitor leak EDG PM evaluations Ultra Low Sulfur Fuel Latent design issues Human perform issues High qual potentiometers GEMCO control switches Replace EDG #1 bearing Collector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 Enclosure 2
EDG Actions Action 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 EDG #2 exhaust bellows Allen Bradley relays Jacket Water TCVs SAMG DGs Capacitor leak EDG PM evaluations Ultra Low Sulfur Fuel Latent design issues Human perform issues High qual potentiometers GEMCO control switches Replace EDG #1 bearing Collector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 Completed Working Scheduled


EDG Performance Indicators 9
EDG Performance Indicators 9  
Enclosure 2


Brunswick Unit 1 Emergency AC Power System NRC Performance Indicator -MSPI (36 Months)
Brunswick Unit 1 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)
September 2009 Status: 87% Margin Remaining in Green 10 Enclosure 2
September 2009 Status: 87% Margin Remaining in Green 10  


Brunswick Unit 2 Emergency AC Power System NRC Performance Indicator -MSPI (36 Months)
Brunswick Unit 2 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)
September 2009 Status: 86% Margin Remaining in Green 11 Enclosure 2
September 2009 Status: 86% Margin Remaining in Green 11  


MSPI EDG Failures 5
MSPI EDG Failures 12 5
4 3
4 3
2 1
2 1
o ...j£--
o...j£--
2004 2005 2006 2007 2008 2009   BNP       Ind (Aug) Avg/EDG Avg/EDG
2004 2005 2006 2007 2008 2009 BNP Ind (Aug)
                                        ~ ft _______ 1"' _____ _
Avg/EDG Avg/EDG  
12 Enclosure 2
~
ft _______ 1"' _____ _  


Emergency Diesel Generators INPO Unavailability 0.025 ............................................................................................................................................................................................................................................................. 0.005
Emergency Diesel Generators INPO Unavailability 13
                                                                                                                                                                                                                                                                                    "'C
"'C Q) c:
"'C Q)  0.02 ......................................................................................................................................................................................................................................................... 0.004 ~
c:
c:                                                                                                                                                                                                                                                                                c:
0.025  
c:                                                                                                                                                                                                                                                                                ro ro                                                                                                                                                                                                                                                                                 ~
............................................................................................................................................................................................................................................................. 0.005  
~     0.015 .......................................................................................................................................................................................................................................................... 0.003       :5
"'C 0.02  
..c                                                                                                                                                                                                                                                                                 Q) ro                                                                                                                                                                                                                                                                                ..c ro  0.01                      .................................................................................................................................................................................................................................... 0.002 :
......................................................................................................................................................................................................................................................... 0.004  
  >
~
ro c:                                                                                                                                                                                                                                                                                 >
c:
ro
ro ro  
~                                                                                                                                                                                                                                                                                   c:
~  
::.:R 0.005 ..................................................................................,. . .."",........................................................................................................................................................ 0.001             ~
~ 0.015  
o
.......................................................................................................................................................................................................................................................... 0.003 :5  
                                                                                                                                                                                                                                                                                    '#.
..c ro ro >
o                                                                                                                                                                                                                                                               o
ro c:
                                                                                  - Planned -                                                       Unplanned 13 Enclosure 2
~
0.01 Q)  
..c  
.................................................................................................................................................................................................................................... 0.002 :
ro c:  
~
::.:R 0.005  
..."",........................................................................................................................................................ 0.001 o
o o
Planned -
Unplanned  


EDG #4 Governor 14 Enclosure 2
EDG #4 Governor 14  


EDG #4 Governor l EDG #4 removed from service for 6 year preventive maintenance:
EDG #4 Governor l
w 4.5 days planned unavailability w Commenced 7 day LCO on both units l During Post Maintenance Testing, EDG #4 failed to start due to governor failure.
EDG #4 removed from service for 6 year preventive maintenance:
w 4.5 days planned unavailability w Commenced 7 day LCO on both units l
During Post Maintenance Testing, EDG #4 failed to start due to governor failure.
l Governor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor - resulting in the expiration of the LCO prior to completing testing.
l Governor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor - resulting in the expiration of the LCO prior to completing testing.
15 Enclosure 2
15  


EDG #4 Failure Analysis l FME on Pilot Plunger restricted movement l Two possible sources for particles:
EDG #4 Failure Analysis l
w Internal Wear Particles w External Source (FME) l Factors for wear of internal parts w Oil analysis did not indicate abnormal wear of internal parts w Inspection of internal parts during disassembly did not indicate wear l Potential Source(s) of FME:
FME on Pilot Plunger restricted movement l
Two possible sources for particles:
w Internal Wear Particles w External Source (FME) l Factors for wear of internal parts w Oil analysis did not indicate abnormal wear of internal parts w Inspection of internal parts during disassembly did not indicate wear l
Potential Source(s) of FME:
w Vendor maintenance on Pilot assembly without flush w On-site testing/installation or oil addition/flushing activities.
w Vendor maintenance on Pilot assembly without flush w On-site testing/installation or oil addition/flushing activities.
16 Enclosure 2
16  


Evaluation of Governor Compensation Land (FME binding location)
Evaluation of Governor 17 Pilot Valve Plunger Compensation Land (FME binding location)  
Pilot Valve Plunger 17 Enclosure 2


Evaluation of Governor Pilot Valve Plunger Compensation Land Centering Spring 18 Enclosure 2
Evaluation of Governor 18 Pilot Valve Plunger Centering Spring Compensation Land  


FME on Pilot Plunger 19 Enclosure 2
FME on Pilot Plunger 19  


Organizational Lessons and Actions from Recent Events (2007-2009) l Technical Rigor w Technical Task Risk/Rigor procedure w Engineering Product Quality Procedure revision w Trending and Monitoring l Post Maintenance Testing Process Improvements w PMT specificity based upon safety related function 20 Enclosure 2
Organizational Lessons and Actions from Recent Events (2007-2009) l Technical Rigor w Technical Task Risk/Rigor procedure w Engineering Product Quality Procedure revision w Trending and Monitoring l
Post Maintenance Testing Process Improvements w PMT specificity based upon safety related function 20  


Organizational Lessons and Actions from Recent Events (2007-2009) l Work Management w Sensitivity to risk significant work w Outage Control Center Use w Readiness Reviews l Parts Quality -Interim Actions (pending permanent corrective actions) w FME requirements for vendors in Purchase Orders/Contracts w Increased vendor surveillance w Interim EDG Spare Parts controls -
Organizational Lessons and Actions from Recent Events (2007-2009) l Work Management w Sensitivity to risk significant work w Outage Control Center Use w Readiness Reviews l
inspection/testing/FME inspections w Review near term EDG maintenance plans 21 Enclosure 2
Parts Quality - Interim Actions (pending permanent corrective actions) w FME requirements for vendors in Purchase Orders/Contracts w Increased vendor surveillance w Interim EDG Spare Parts controls -
inspection/testing/FME inspections w Review near term EDG maintenance plans 21  


Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Reliability Review Update w Validate Corrective actions taken from events since 2007 are bounding and comprehensive w Review problems/failures since 2007 w Review Industry Operating Experience since 2007 w Benchmark other utility EDG Reliability plans w Revise as needed near/long-term reliability improvement strategy 22 Enclosure 2
Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Reliability Review Update w Validate Corrective actions taken from events since 2007 are bounding and comprehensive w Review problems/failures since 2007 w Review Industry Operating Experience since 2007 w Benchmark other utility EDG Reliability plans w Revise as needed near/long-term reliability improvement strategy 22  


Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Maintenance Strategy Improvements:
Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Maintenance Strategy Improvements:
w Near Term -Evaluate options to address extension of 7 day LCO:
w Near Term - Evaluate options to address extension of 7 day LCO:
u Reduces overall unavailability to complete work u Improved efficiency of work planning w Longer Term - Evaluate options to address long duration LCO for EDG major overhaul/repairs u Additional on-site emergency AC capability u AC distribution alignment w Common Mode Failure Strategy for Maintenance implementation 23 Enclosure 2
u Reduces overall unavailability to complete work u Improved efficiency of work planning w Longer Term - Evaluate options to address long duration LCO for EDG major overhaul/repairs u Additional on-site emergency AC capability u AC distribution alignment w Common Mode Failure Strategy for Maintenance implementation 23  


Questions?
Questions?
24 Enclosure 2}}
24 }}

Latest revision as of 08:36, 14 January 2025

Emergency Diesel Generators - Progress Energy
ML093020671
Person / Time
Site: Brunswick  
Issue date: 10/22/2009
From:
Progress Energy Carolinas
To:
NRC/RGN-II
Shared Package
ML093020640 List:
References
Download: ML093020671 (24)


Text

Brunswick Nuclear Plant Emergency Diesel Generators NRC Region II Visit October 22, 2009

Agenda l AC Power Reliability l EDG Historical Performance l EDG Performance Indicators l EDG #4 Governor l Organizational Lessons and Actions from Recent Events 2

AC Power Reliability 3

Completed Actions Installed new 230 kV supply breakers for SATs Installed new Unit output breakers Replaced SWYD CCVTs & Lightning Arrestors Installed new local 230 kV capacitor banks for voltage support on Unit 2 Installed new Main Transformers - Outfitted with continuous gas monitoring instrumentation Improved material condition of spare SAT Replaced sudden pressure relays Replaced no load disconnect switches Improved PMs on Iso-Phase and Non-Seg Bus Inspected Non-Seg Bus flex links Established standard preventive maintenance program for buses Installed permanent SAMA diesel generators on Unit 2 Planned Actions Install new local 230 kV capacitor banks for voltage Support on Unit 1 Install permanent SAMA diesel generators on U1 Unit Auxiliary Transformer (UAT) Replacement Replace remaining transmission line breakers Replace Line Insulators at a rate of ~150 sets per year during each unit Completed Actions Replaced 2 transmission line breakers Replaced 145 poles and 341 insulator sets Revised Transmission Interface Agreement to specify plant involvement/coordination of work activities Under Evaluation Replace SATs w/auto load tap changing transformers Upgrade 2/3 logic for Aux Transformer

Emergency Power Reliability 4

Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteries Improved CDF by 68% on Unit 1 and 66% on Unit 2

5 EDG Historical Performance 2007 Reliability Study

w Operations w Maintenance w Engineering w Technical Training 2007 Reliability Study 6

w Licensing w Procurement w Industry Representative w Vendor Representative

  • Multi-discipline team assembled to review EDG issues and develop short and long term action plan
  • INPO Assist

l MSPI Reliability data l

Vendor Input/Industry OE l

Maintenance Rule Functional Failures, 2000-2006 l

BNP Equipment Reliability List l

EDG NCRs, 2003-2006 l

EDG Planned and Unplanned Out Of Service (OOS) times, 2003-2006 l

EDG Corrective Work Orders, 2003-2006 2007 Reliability Study Inputs Used in Analysis 7

l EDG Material Costs, 2003-2006 l

EDG Self Assessment &

Benchmarks, 2003-2006 l

EDG NRC Findings, 2003-2006 l

EDG Nonconformances l

EDG items on Long Range Plan l

System Engineer brainstorming sessions

EDG Actions Action 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 EDG #2 exhaust bellows Allen Bradley relays Jacket Water TCVs SAMG DGs Capacitor leak EDG PM evaluations Ultra Low Sulfur Fuel Latent design issues Human perform issues High qual potentiometers GEMCO control switches Replace EDG #1 bearing Collector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 Completed Working Scheduled

EDG Performance Indicators 9

Brunswick Unit 1 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)

September 2009 Status: 87% Margin Remaining in Green 10

Brunswick Unit 2 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)

September 2009 Status: 86% Margin Remaining in Green 11

MSPI EDG Failures 12 5

4 3

2 1

o...j£--

2004 2005 2006 2007 2008 2009 BNP Ind (Aug)

Avg/EDG Avg/EDG

~

ft _______ 1"' _____ _

Emergency Diesel Generators INPO Unavailability 13

"'C Q) c:

c:

0.025

............................................................................................................................................................................................................................................................. 0.005

"'C 0.02

......................................................................................................................................................................................................................................................... 0.004

~

c:

ro ro

~

~ 0.015

.......................................................................................................................................................................................................................................................... 0.003 :5

..c ro ro >

ro c:

~

0.01 Q)

..c

.................................................................................................................................................................................................................................... 0.002 :

ro c:

~

.:R 0.005

..."",........................................................................................................................................................ 0.001 o

o o

Planned -

Unplanned

EDG #4 Governor 14

EDG #4 Governor l

EDG #4 removed from service for 6 year preventive maintenance:

w 4.5 days planned unavailability w Commenced 7 day LCO on both units l

During Post Maintenance Testing, EDG #4 failed to start due to governor failure.

l Governor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor - resulting in the expiration of the LCO prior to completing testing.

15

EDG #4 Failure Analysis l

FME on Pilot Plunger restricted movement l

Two possible sources for particles:

w Internal Wear Particles w External Source (FME) l Factors for wear of internal parts w Oil analysis did not indicate abnormal wear of internal parts w Inspection of internal parts during disassembly did not indicate wear l

Potential Source(s) of FME:

w Vendor maintenance on Pilot assembly without flush w On-site testing/installation or oil addition/flushing activities.

16

Evaluation of Governor 17 Pilot Valve Plunger Compensation Land (FME binding location)

Evaluation of Governor 18 Pilot Valve Plunger Centering Spring Compensation Land

FME on Pilot Plunger 19

Organizational Lessons and Actions from Recent Events (2007-2009) l Technical Rigor w Technical Task Risk/Rigor procedure w Engineering Product Quality Procedure revision w Trending and Monitoring l

Post Maintenance Testing Process Improvements w PMT specificity based upon safety related function 20

Organizational Lessons and Actions from Recent Events (2007-2009) l Work Management w Sensitivity to risk significant work w Outage Control Center Use w Readiness Reviews l

Parts Quality - Interim Actions (pending permanent corrective actions) w FME requirements for vendors in Purchase Orders/Contracts w Increased vendor surveillance w Interim EDG Spare Parts controls -

inspection/testing/FME inspections w Review near term EDG maintenance plans 21

Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Reliability Review Update w Validate Corrective actions taken from events since 2007 are bounding and comprehensive w Review problems/failures since 2007 w Review Industry Operating Experience since 2007 w Benchmark other utility EDG Reliability plans w Revise as needed near/long-term reliability improvement strategy 22

Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Maintenance Strategy Improvements:

w Near Term - Evaluate options to address extension of 7 day LCO:

u Reduces overall unavailability to complete work u Improved efficiency of work planning w Longer Term - Evaluate options to address long duration LCO for EDG major overhaul/repairs u Additional on-site emergency AC capability u AC distribution alignment w Common Mode Failure Strategy for Maintenance implementation 23

Questions?

24