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{{#Wiki_filter:Brunswick Nuclear Plant Emergency Diesel GeneratorsNRC Region II VisitOctober 22, 2009 Agenda lAC Power Reliability lEDG Historical Performance lEDG Performance Indicators lEDG #4 Governor lOrganizational Lessons and Actions from Recent Events 2
{{#Wiki_filter:Brunswick Nuclear Plant Emergency Diesel Generators NRC Region II Visit October 22, 2009  
AC Power Reliability 3Completed ActionsInstalled new 230 kV supply breakers for SATsInstalled new Unit output breakersReplaced SWYD CCVTs & Lightning ArrestorsInstalled new local 230 kV capacitor banks for voltage support on Unit 2Installed new Main Transformers -Outfitted with continuous gas monitoring instrumentationImproved material condition of spare SATReplaced sudden pressure relaysReplaced no load disconnect switches Improved PMs on Iso-Phase and Non-Seg Bus Inspected Non-Seg Bus flex linksEstablished standard preventive maintenance program for busesInstalled permanent SAMA diesel generators on Unit 2Planned ActionsInstall new local 230 kV capacitor banks for voltage Support on Unit 1Install permanent SAMA diesel generators on U1Unit Auxiliary Transformer (UAT) ReplacementReplace remaining transmission line breakers Replace Line Insulators at a rate of ~150 sets per year during each unit Completed ActionsReplaced 2 transmission line breakersReplaced 145 poles and 341 insulator sets Revised Transmission Interface Agreement to specify plant involvement/coordination of work activitiesUnder EvaluationReplace SATs w/auto load tap changing transformersUpgrade 2/3 logic for Aux Transformer Emergency Power Reliability 4Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteriesImproved CDF by 68% on Unit 1 and 66% on Unit 2 5EDG Historical Performance2007 Reliability Study wOperations wMaintenance wEngineering wTechnical Training2007 Reliability Study 6 wLicensing wProcurement wIndustry Representative wVendor RepresentativeMulti-discipline team assembled to review EDG     issues and develop short and long term action planINPO Assist lMSPI Reliability data lVendor Input/Industry OE lMaintenance Rule Functional Failures, 2000-2006 lBNP Equipment Reliability List lEDG NCRs, 2003-2006 lEDG Planned and Unplanned Out Of Service (OOS) times, 2003-2006 lEDG Corrective Work Orders, 2003-20062007 Reliability StudyInputs Used in Analysis 7 lEDG Material Costs, 2003-2006 lEDG Self Assessment & Benchmarks, 2003-2006 lEDG NRC Findings, 2003-2006 lEDG Nonconformances lEDG items on Long Range Plan lSystem Engineer brainstorming sessions EDG Actions Action 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 EDG #2 exhaust bellows Allen Bradley relays Jacket Water TCVs SAMG DGs Capacitor leakEDG PM evaluationsUltra Low Sulfur FuelLatent design issuesHuman perform issues High qual potentiometersGEMCO control switches Replace EDG #1 bearingCollector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 CompletedWorkingScheduled EDG Performance Indicators 9
 
Brunswick Unit 1Emergency AC Power System NRC Performance Indicator MSPI (36 Months) September 2009 Status: 87% Margin Remaining in Green10 Brunswick Unit 2Emergency AC Power SystemNRC Performance Indicator MSPI (36 Months)September 2009 Status: 86% Margin Remaining in Green11 MSPI EDG Failures12 5 4 3 2 1 o ...j£--2004 2005 2006 2007 2008 2009 BNP Ind (Aug) Avg/EDG Avg/EDG ft _______ 1"' _____ _
Agenda l AC Power Reliability l EDG Historical Performance l EDG Performance Indicators l EDG #4 Governor l Organizational Lessons and Actions from Recent Events 2  
Emergency Diesel GeneratorsINPO Unavailability13"'C Q) c: c: 0.025 .............................................................................................................................................................................................................................................................
 
0.005 "'C 0.02 .........................................................................................................................................................................................................................................................
AC Power Reliability 3
0.004 c: ro ro 0.015 ..........................................................................................................................................................................................................................................................
Completed Actions Installed new 230 kV supply breakers for SATs Installed new Unit output breakers Replaced SWYD CCVTs & Lightning Arrestors Installed new local 230 kV capacitor banks for voltage support on Unit 2 Installed new Main Transformers - Outfitted with continuous gas monitoring instrumentation Improved material condition of spare SAT Replaced sudden pressure relays Replaced no load disconnect switches Improved PMs on Iso-Phase and Non-Seg Bus Inspected Non-Seg Bus flex links Established standard preventive maintenance program for buses Installed permanent SAMA diesel generators on Unit 2 Planned Actions Install new local 230 kV capacitor banks for voltage Support on Unit 1 Install permanent SAMA diesel generators on U1 Unit Auxiliary Transformer (UAT) Replacement Replace remaining transmission line breakers Replace Line Insulators at a rate of ~150 sets per year during each unit Completed Actions Replaced 2 transmission line breakers Replaced 145 poles and 341 insulator sets Revised Transmission Interface Agreement to specify plant involvement/coordination of work activities Under Evaluation Replace SATs w/auto load tap changing transformers Upgrade 2/3 logic for Aux Transformer  
0.003 :5 ..c ro ro > ro c: 0.01 Q) ..c ..................................................................................................................
 
..................................................................................................................
Emergency Power Reliability 4
0.002 : > ro c: '#. ::.:R 0.005 ..................................................................................
Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteries Improved CDF by 68% on Unit 1 and 66% on Unit 2  
,. . .."",........................................................................................................................................................
 
0.001 o o o -Planned -Unplanned EDG #4 Governor 14 EDG #4 Governor lEDG #4 removed from service for 6 year preventive maintenance:
5 EDG Historical Performance 2007 Reliability Study  
w4.5 days planned unavailability wCommenced 7 day LCO on both units lDuring  Post Maintenance Testing, EDG #4 failed to start due to governor failure.
 
lGovernor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor -resulting in the expiration of the LCO prior to completing testing.15 EDG #4 Failure Analysis lFME on Pilot Plunger restricted movement lTwo possible sources for particles:
w Operations w Maintenance w Engineering w Technical Training 2007 Reliability Study 6
wInternal Wear Particles wExternal Source (FME) lFactors for wear of internal parts wOil analysis did not indicate abnormal wear of internal parts wInspection of internal parts during disassembly did not indicate wear lPotential Source(s) of FME:
w Licensing w Procurement w Industry Representative w Vendor Representative
wVendor maintenance on Pilot assembly without flush wOn-site testing/installation or oil addition/flushing activities.16 Evaluation of Governor17Pilot ValvePlungerCompensation Land(FME binding location)
*Multi-discipline team assembled to review EDG issues and develop short and long term action plan
Evaluation of Governor18Pilot Valve PlungerCentering SpringCompensation Land FME on Pilot Plunger 19 Organizational Lessons and Actions from Recent Events (2007-2009) lTechnical Rigor wTechnical Task Risk/Rigor procedure wEngineering Product Quality Procedure revision wTrending and Monitoring lPost Maintenance Testing Process Improvements wPMT specificity based upon safety related function20 Organizational Lessons and Actions from Recent Events (2007-2009) lWork Management wSensitivity to risk significant work wOutage Control Center Use wReadiness Reviews lParts Quality Interim Actions (pending permanent corrective actions) wFME requirements for vendors in Purchase Orders/Contracts wIncreased vendor surveillance wInterim EDG Spare Parts controls inspection/testing/FME inspections wReview near term EDG maintenance plans21 Organizational Lessons and Actions from Recent Events (2007-2009) lEDG Reliability Review Update wValidate Corrective actions taken from events since 2007 are bounding and comprehensive wReview problems/failures since 2007 wReview Industry Operating Experience since 2007 wBenchmark other utility EDG Reliability plans wRevise as needed near/long-term reliability improvement strategy22 Organizational Lessons and Actions from Recent Events (2007-2009) lEDG Maintenance Strategy Improvements:
*INPO Assist  
wNear Term Evaluate options to address extension of 7 day LCO:
 
uReduces overall unavailability to complete work uImproved efficiency of work planning wLonger Term -Evaluate options to address long duration LCO for EDG major overhaul/repairs uAdditional on-site emergency AC capability uAC distribution alignment wCommon Mode Failure Strategy for Maintenance implementation23 Questions?24}}
l MSPI Reliability data l
Vendor Input/Industry OE l
Maintenance Rule Functional Failures, 2000-2006 l
BNP Equipment Reliability List l
EDG NCRs, 2003-2006 l
EDG Planned and Unplanned Out Of Service (OOS) times, 2003-2006 l
EDG Corrective Work Orders, 2003-2006 2007 Reliability Study Inputs Used in Analysis 7
l EDG Material Costs, 2003-2006 l
EDG Self Assessment &
Benchmarks, 2003-2006 l
EDG NRC Findings, 2003-2006 l
EDG Nonconformances l
EDG items on Long Range Plan l
System Engineer brainstorming sessions  
 
EDG Actions Action 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 EDG #2 exhaust bellows Allen Bradley relays Jacket Water TCVs SAMG DGs Capacitor leak EDG PM evaluations Ultra Low Sulfur Fuel Latent design issues Human perform issues High qual potentiometers GEMCO control switches Replace EDG #1 bearing Collector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 Completed Working Scheduled
 
EDG Performance Indicators 9  
 
Brunswick Unit 1 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)
September 2009 Status: 87% Margin Remaining in Green 10
 
Brunswick Unit 2 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)
September 2009 Status: 86% Margin Remaining in Green 11
 
MSPI EDG Failures 12 5
4 3
2 1
o...j£--
2004 2005 2006 2007 2008 2009 BNP Ind (Aug)
Avg/EDG Avg/EDG  
~
ft _______ 1"' _____ _  
 
Emergency Diesel Generators INPO Unavailability 13
"'C Q) c:
c:
0.025  
............................................................................................................................................................................................................................................................. 0.005  
"'C 0.02  
......................................................................................................................................................................................................................................................... 0.004  
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Planned -
Unplanned
 
EDG #4 Governor 14
 
EDG #4 Governor l
EDG #4 removed from service for 6 year preventive maintenance:
w 4.5 days planned unavailability w Commenced 7 day LCO on both units l
During Post Maintenance Testing, EDG #4 failed to start due to governor failure.
l Governor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor - resulting in the expiration of the LCO prior to completing testing.
15
 
EDG #4 Failure Analysis l
FME on Pilot Plunger restricted movement l
Two possible sources for particles:
w Internal Wear Particles w External Source (FME) l Factors for wear of internal parts w Oil analysis did not indicate abnormal wear of internal parts w Inspection of internal parts during disassembly did not indicate wear l
Potential Source(s) of FME:
w Vendor maintenance on Pilot assembly without flush w On-site testing/installation or oil addition/flushing activities.
16
 
Evaluation of Governor 17 Pilot Valve Plunger Compensation Land (FME binding location)
 
Evaluation of Governor 18 Pilot Valve Plunger Centering Spring Compensation Land
 
FME on Pilot Plunger 19
 
Organizational Lessons and Actions from Recent Events (2007-2009) l Technical Rigor w Technical Task Risk/Rigor procedure w Engineering Product Quality Procedure revision w Trending and Monitoring l
Post Maintenance Testing Process Improvements w PMT specificity based upon safety related function 20
 
Organizational Lessons and Actions from Recent Events (2007-2009) l Work Management w Sensitivity to risk significant work w Outage Control Center Use w Readiness Reviews l
Parts Quality - Interim Actions (pending permanent corrective actions) w FME requirements for vendors in Purchase Orders/Contracts w Increased vendor surveillance w Interim EDG Spare Parts controls -
inspection/testing/FME inspections w Review near term EDG maintenance plans 21
 
Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Reliability Review Update w Validate Corrective actions taken from events since 2007 are bounding and comprehensive w Review problems/failures since 2007 w Review Industry Operating Experience since 2007 w Benchmark other utility EDG Reliability plans w Revise as needed near/long-term reliability improvement strategy 22
 
Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Maintenance Strategy Improvements:
w Near Term - Evaluate options to address extension of 7 day LCO:
u Reduces overall unavailability to complete work u Improved efficiency of work planning w Longer Term - Evaluate options to address long duration LCO for EDG major overhaul/repairs u Additional on-site emergency AC capability u AC distribution alignment w Common Mode Failure Strategy for Maintenance implementation 23
 
Questions?
24 }}

Latest revision as of 08:36, 14 January 2025

Emergency Diesel Generators - Progress Energy
ML093020671
Person / Time
Site: Brunswick  
Issue date: 10/22/2009
From:
Progress Energy Carolinas
To:
NRC/RGN-II
Shared Package
ML093020640 List:
References
Download: ML093020671 (24)


Text

Brunswick Nuclear Plant Emergency Diesel Generators NRC Region II Visit October 22, 2009

Agenda l AC Power Reliability l EDG Historical Performance l EDG Performance Indicators l EDG #4 Governor l Organizational Lessons and Actions from Recent Events 2

AC Power Reliability 3

Completed Actions Installed new 230 kV supply breakers for SATs Installed new Unit output breakers Replaced SWYD CCVTs & Lightning Arrestors Installed new local 230 kV capacitor banks for voltage support on Unit 2 Installed new Main Transformers - Outfitted with continuous gas monitoring instrumentation Improved material condition of spare SAT Replaced sudden pressure relays Replaced no load disconnect switches Improved PMs on Iso-Phase and Non-Seg Bus Inspected Non-Seg Bus flex links Established standard preventive maintenance program for buses Installed permanent SAMA diesel generators on Unit 2 Planned Actions Install new local 230 kV capacitor banks for voltage Support on Unit 1 Install permanent SAMA diesel generators on U1 Unit Auxiliary Transformer (UAT) Replacement Replace remaining transmission line breakers Replace Line Insulators at a rate of ~150 sets per year during each unit Completed Actions Replaced 2 transmission line breakers Replaced 145 poles and 341 insulator sets Revised Transmission Interface Agreement to specify plant involvement/coordination of work activities Under Evaluation Replace SATs w/auto load tap changing transformers Upgrade 2/3 logic for Aux Transformer

Emergency Power Reliability 4

Installed two backup diesel powered generators (SAMA diesel generators) to power the 125 VDC batteries Improved CDF by 68% on Unit 1 and 66% on Unit 2

5 EDG Historical Performance 2007 Reliability Study

w Operations w Maintenance w Engineering w Technical Training 2007 Reliability Study 6

w Licensing w Procurement w Industry Representative w Vendor Representative

  • Multi-discipline team assembled to review EDG issues and develop short and long term action plan
  • INPO Assist

l MSPI Reliability data l

Vendor Input/Industry OE l

Maintenance Rule Functional Failures, 2000-2006 l

BNP Equipment Reliability List l

EDG NCRs, 2003-2006 l

EDG Planned and Unplanned Out Of Service (OOS) times, 2003-2006 l

EDG Corrective Work Orders, 2003-2006 2007 Reliability Study Inputs Used in Analysis 7

l EDG Material Costs, 2003-2006 l

EDG Self Assessment &

Benchmarks, 2003-2006 l

EDG NRC Findings, 2003-2006 l

EDG Nonconformances l

EDG items on Long Range Plan l

System Engineer brainstorming sessions

EDG Actions Action 2007 2008 2009 2010 2011 2012 2013 2014 2015 2016 2017 2018 EDG #2 exhaust bellows Allen Bradley relays Jacket Water TCVs SAMG DGs Capacitor leak EDG PM evaluations Ultra Low Sulfur Fuel Latent design issues Human perform issues High qual potentiometers GEMCO control switches Replace EDG #1 bearing Collector ring Starting air config/quality Exciter/voltage regulator Governor upgrade Piston replacement (est) 8 Completed Working Scheduled

EDG Performance Indicators 9

Brunswick Unit 1 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)

September 2009 Status: 87% Margin Remaining in Green 10

Brunswick Unit 2 Emergency AC Power System NRC Performance Indicator - MSPI (36 Months)

September 2009 Status: 86% Margin Remaining in Green 11

MSPI EDG Failures 12 5

4 3

2 1

o...j£--

2004 2005 2006 2007 2008 2009 BNP Ind (Aug)

Avg/EDG Avg/EDG

~

ft _______ 1"' _____ _

Emergency Diesel Generators INPO Unavailability 13

"'C Q) c:

c:

0.025

............................................................................................................................................................................................................................................................. 0.005

"'C 0.02

......................................................................................................................................................................................................................................................... 0.004

~

c:

ro ro

~

~ 0.015

.......................................................................................................................................................................................................................................................... 0.003 :5

..c ro ro >

ro c:

~

0.01 Q)

..c

.................................................................................................................................................................................................................................... 0.002 :

ro c:

~

.:R 0.005

..."",........................................................................................................................................................ 0.001 o

o o

Planned -

Unplanned

EDG #4 Governor 14

EDG #4 Governor l

EDG #4 removed from service for 6 year preventive maintenance:

w 4.5 days planned unavailability w Commenced 7 day LCO on both units l

During Post Maintenance Testing, EDG #4 failed to start due to governor failure.

l Governor testing, tuning, support component replacement, and oil flushing occurred for the replaced governor - resulting in the expiration of the LCO prior to completing testing.

15

EDG #4 Failure Analysis l

FME on Pilot Plunger restricted movement l

Two possible sources for particles:

w Internal Wear Particles w External Source (FME) l Factors for wear of internal parts w Oil analysis did not indicate abnormal wear of internal parts w Inspection of internal parts during disassembly did not indicate wear l

Potential Source(s) of FME:

w Vendor maintenance on Pilot assembly without flush w On-site testing/installation or oil addition/flushing activities.

16

Evaluation of Governor 17 Pilot Valve Plunger Compensation Land (FME binding location)

Evaluation of Governor 18 Pilot Valve Plunger Centering Spring Compensation Land

FME on Pilot Plunger 19

Organizational Lessons and Actions from Recent Events (2007-2009) l Technical Rigor w Technical Task Risk/Rigor procedure w Engineering Product Quality Procedure revision w Trending and Monitoring l

Post Maintenance Testing Process Improvements w PMT specificity based upon safety related function 20

Organizational Lessons and Actions from Recent Events (2007-2009) l Work Management w Sensitivity to risk significant work w Outage Control Center Use w Readiness Reviews l

Parts Quality - Interim Actions (pending permanent corrective actions) w FME requirements for vendors in Purchase Orders/Contracts w Increased vendor surveillance w Interim EDG Spare Parts controls -

inspection/testing/FME inspections w Review near term EDG maintenance plans 21

Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Reliability Review Update w Validate Corrective actions taken from events since 2007 are bounding and comprehensive w Review problems/failures since 2007 w Review Industry Operating Experience since 2007 w Benchmark other utility EDG Reliability plans w Revise as needed near/long-term reliability improvement strategy 22

Organizational Lessons and Actions from Recent Events (2007-2009) l EDG Maintenance Strategy Improvements:

w Near Term - Evaluate options to address extension of 7 day LCO:

u Reduces overall unavailability to complete work u Improved efficiency of work planning w Longer Term - Evaluate options to address long duration LCO for EDG major overhaul/repairs u Additional on-site emergency AC capability u AC distribution alignment w Common Mode Failure Strategy for Maintenance implementation 23

Questions?

24