ML17334B364: Difference between revisions

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| number = ML17334B364
| number = ML17334B364
| issue date = 04/11/1990
| issue date = 04/11/1990
| title = Responds to NRC 900301 Ltr Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated
| title = Responds to NRC Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated
| author name = ALEXICH M P
| author name = Alexich M
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| author affiliation = INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
| addressee name = DAVIS A B
| addressee name = Davis A
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| addressee affiliation = NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
| docket = 05000315, 05000316
| docket = 05000315, 05000316
Line 11: Line 11:
| contact person =  
| contact person =  
| document report number = AEP:NRC:1125A, NUDOCS 9004200632
| document report number = AEP:NRC:1125A, NUDOCS 9004200632
| title reference date = 03-01-1990
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| document type = CORRESPONDENCE-LETTERS, INCOMING CORRESPONDENCE, UTILITY TO NRC
| page count = 38
| page count = 38
}}
}}
See also: [[followed by::IR 05000315/1989031]]


=Text=
=Text=
{{#Wiki_filter:\r Indiana'Achrga~Power Company~~0 80 c'.663'Nl7lAMA
{{#Wiki_filter:\\
NTCHIGAN POWER AEP:NRC:1125A
r Indiana 'Achrga~
Donald C.Cook Nuclear Plant Units 1 and 2 Docket Nos.50-315 and 50-316 License Nos.DPR-58 and DPR-74 NRC INSPECTION
Power Company~
NOS.50-315/89031
~ 0 80 c'.663'Nl7lAMA NTCHIGAN POWER AEP:NRC:1125A Donald C.
AND 50-316/89031:
Cook Nuclear Plant Units 1 and 2
RESPONSE TO VIOLATION U.S.Nuclear Regulatory
Docket Nos.
Commission
50-315 and 50-316 License Nos.
Attn: Document Control Desk Washington, D.C.20555 Attn: A.B.Davi.s April ll, 1990 Dear Mr.Davis: This letter is in response to Mr.H.J.Miller's letter dated March 1, 1990, which forwarded the report on the special maintenance
DPR-58 and DPR-74 NRC INSPECTION NOS.
team inspection
50-315/89031 AND 50-316/89031:
conducted by Mr.Z.Falevits and others of your staff.This inspection
 
was conducted from December 4 through 8, and December 18 through 22, 1989, on activities
===RESPONSE===
at the Cook Nuclear Plant associated
TO VIOLATION U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.
with the support and implementation
20555 Attn: A. B. Davi.s April ll, 1990
of maintenance
 
to ensure that plant structures, systems and components
==Dear Mr. Davis:==
reliably perform on demand.The Notice of Violation attached to Mr.Miller's letter identified
This letter is in response to Mr. H. J. Miller's {{letter dated|date=March 1, 1990|text=letter dated March 1, 1990}}, which forwarded the report on the special maintenance team inspection conducted by Mr. Z. Falevits and others of your staff.
six weaknesses
This inspection was conducted from December 4 through 8, and December 18 through 22,
and four Severity Level IV violations
: 1989, on activities at the Cook Nuclear Plant associated with the support and implementation of maintenance to ensure that plant structures, systems and components reliably perform on demand.
relating to our maintenance
The Notice of Violation attached to Mr. Miller's letter identified six weaknesses and four Severity Level IV violations relating to our maintenance program.
program.The weaknesses
The weaknesses are addressed in Attachment 1 to this letter.
are addressed in Attachment
The violations are addressed in Attachment 2 to this letter.
1 to this letter.The violations
A 14-day extension for our response was granted on March 15, 1990
are addressed in Attachment
'his document has been prepared following Corporate procedures that incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.
2 to this letter.A 14-day extension for our response was granted on March 15, 1990'his document has been prepared following Corporate procedures
Sincerely, M. P. Al ich Vice President ldp Attachments
that incorporate
~)g4QOCk&2 90041 1 pgg ADQcK o>oog+~~
a reasonable
~
set of controls to ensure its accuracy and completeness
I pp 1/00
prior to signature by the undersigned.
 
Sincerely, M.P.Al ich Vice President ldp Attachments
Mr. A. B. Davis AEP:NRC:1125A cc:
~)g4QOCk&2
D.
90041 1 pgg ADQcK o>oog+~~~I pp 1/00  
H. Williams, Jr.
Mr.A.B.Davis AEP:NRC:1125A
A. A. Blind - Bridgman R.
cc: D.H.Williams, Jr.A.A.Blind-Bridgman R.C.Callen G.Charnoff NRC Resident Inspector-Bridgman NFEM Section Chief  
C. Callen G. Charnoff NRC Resident Inspector
ATTACHMENT
- Bridgman NFEM Section Chief
1 TO AEP:NRC:1125A
 
RESPONSE TO NRC-IDENTIFIED
ATTACHMENT 1 TO AEP:NRC:1125A
WEAKNESSES
 
Attachment
===RESPONSE===
1 to AEP:NRC:1125A
TO NRC-IDENTIFIED WEAKNESSES
Page 1 NRC-Identified
 
Weakness (1)"Lack of or ineffective
Attachment 1 to AEP:NRC:1125A Page 1
action to correct numerous self identified
NRC-Identified Weakness (1)
maintenance
"Lack of or ineffective action to correct numerous self identified maintenance problems identified in February
problems identified
: 1988, many of which were identified by the team during this inspection."
in February 1988, many of which were identified
 
by the team during this inspection." Response to Weakness (1)Corrective
===Response===
Actions Taken As a result of the 1988 Maintenance
to Weakness (1) Corrective Actions Taken As a result of the 1988 Maintenance Self-Assessment
Self-Assessment
: Report, AEPSC contracted IMPELL to assist in identifying and formulating appropriate corrective actions to address the self-identified deficiencies.
Report, AEPSC contracted
The results of thi,s effort are in a document
IMPELL to assist in identifying
: entitled, D.
and formulating
C.
appropriate
Cook Plant PM Pro ram U
corrective
rade Strate
actions to address the self-identified
: Document, dated November 1988.
deficiencies.
This study contained a strategy for AEP to accomplish a planned upgrade of the Preventive Maintenance (PM)
The results of thi,s effort are in a document entitled, D.C.Cook Plant PM Pro ram U rade Strate Document, dated November 1988.This study contained a strategy for AEP to accomplish
Program at the Cook Nuclear Plant.
a planned upgrade of the Preventive
It identified reasonable goals and achievable objectives for the PM Upgrade Program based on AEPSC/Cook Nuclear Plant philosophy, resources and capabilities.
Maintenance (PM)Program at the Cook Nuclear Plant.It identified
The specific implementation tasks and strategic considerations were presented for obtaining the desired upgrade results.
reasonable
This effort'ot only addressed improvements in the PM Program itself, but also examined related organization and automation requirements to support the improved PM Program.
goals and achievable
Based on the results of this study, numerous corrective actions were initiated in January 1989.
objectives
The first was the initiation of a reliability-centered maintenance (RCM) program.
for the PM Upgrade Program based on AEPSC/Cook
This major task has two phases:
Nuclear Plant philosophy, resources and capabilities.
analysis and implementation.
The specific implementation
AEPSC has been working closely with General Physics on the analysis portion that will form the foundation of the RCM program.
tasks and strategic considerations
This work includes:
were presented for obtaining the desired upgrade results.This effort'ot only addressed improvements
defining system boundaries and functions identifying dominant failure modes determining criti.cal failure modes and criti.cal components identifying applicable and effective preventive maintenance tasks to prevent failures completing analysis of selected plant systems
in the PM Program itself, but also examined related organization
 
and automation
Attachment 1 to AEP:NRC:1125A Page 2
requirements
Implementation of the RCM Program began in August 1989 with the development of plant procedures, identification of system boundaries, and establishment of an RCM database.
to support the improved PM Program.Based on the results of this study, numerous corrective
The first syst: em analysis was completed in February 1990 on the feedwater system.
actions were initiated in January 1989.The first was the initiation
Analysis of 22 additional plant systems/functional areas will take place over the next three years.
of a reliability-centered
Another outgrowth of the Maintenance Self-Assessment Report and the AEPSC/IMPELL study was the development of the System Engineer Program.
maintenance (RCM)program.This major task has two phases: analysis and implementation.
The goal of the System Engineer Program is to provide training to enable individuals to provide the engineering expertise required for safe, efficient and reliable operation of systems for which they are responsible.
AEPSC has been working closely with General Physics on the analysis portion that will form the foundation
The System Engineer discharges this responsibility by performing assigned
of the RCM program.This work includes: defining system boundaries
: tasks, and maintaining cognizance of all work associated with the assigned system(s).
and functions identifying
In addition, AEPSC contracted TENERA Systems and Software to provide a computerized maintenance management information system.
dominant failure modes determining
This system, referred to as the Nuclear Plant Maintenance Module (NPM) System, discussed in more detail in our response to weakness (3), will allow plant staff to initiate, issue, prioritize and track all maintenance work at the plant.
criti.cal failure modes and criti.cal components
This same software is currently being used at Pacific Gas and Electric's Diablo Canyon, and Public Service Electric and Gas's Salem and Hope Creek Generating Stations.
identifying
In addition, it was recently chosen by Electricite de France for use in all fifty of its nuclear plants.
applicable
These three programs, RCM, System Engineer and NPM, are just part of the actions that are being taken to respond to the Self-Assessment.
and effective preventive
The November 1989 reorganization of Cook Nuclear Plant's management is another important element in the upgrade of our maintenance program.
maintenance
The intent of the new organization is to place emphasis on maintenance,
tasks to prevent failures completing
: outages, and human'resources, Other actions, which have or are being taken are as follows:
analysis of selected plant systems  
o An AEP and Cook Nuclear Plant policy on maintenance was developed and approved in December 1989 by AEP senior management.
Attachment
An additional plant-specific maintenance policy established in accordance with INPO guidelines is being developed to clarify maintenance philosophies and responsibilities for all maintenance groups
1 to AEP:NRC:1125A
 
Page 2 Implementation
Attachment 1 to AEP:NRC:1125A Page 3
of the RCM Program began in August 1989 with the development
o Corporate reviews have been conducted, which have resulted in improvements being made to shop areas used by the maintenance groups o
of plant procedures, identification
Staffing studies are being performed, which have already resulted in an increase in the number of engineers and radiation protection technicians on site.
of system boundaries, and establishment
o Other programs of note that address maintenance self-assessment findings include the maintenance procedure rewrite (See Weakness (6)), the long-range plan and the outage guideline development plan.
of an RCM database.The first syst: em analysis was completed in February 1990 on the feedwater system.Analysis of 22 additional
(2) Benefits To Be Derived From Corrective Actions RCM, the System Engineer Program and NPM were initiated to address many of the Maintenance Self-Assessment's identified deficiencies.
plant systems/functional
When all of our efforts have been completely implemented, each of the major findings of the self assessment will have been addressed.
areas will take place over the next three years.Another outgrowth of the Maintenance
,As a result of these corrective actions. we anticipate having a
Self-Assessment
state of the art maintenance program which will result in improved plant safety, reliability and accountability.
Report and the AEPSC/IMPELL
(3) Date When Benefits Vill Be Realized As previously stated, we started the RCM Program in August 1989.
study was the development
: However, we anticipate that the program will not be completely implemented for all the critical plant systems until the end of 1992.
of the System Engineer Program.The goal of the System Engineer Program is to provide training to enable individuals
As each system is analyzed, benefits will be realized so that when this program is completed we will have a fully integrated preventive maintenance program.
to provide the engineering
The System Engineer Program, like RCM, is still in the early stages of implementation.
expertise required for safe, efficient and reliable operation of systems for which they are responsible.
A document which clearly delineates the responsibilities of the engineers is currently in the final stages of review and approval.
The System Engineer discharges
AEPSC's acquisition of TENERA's NPM system was approved in December 1989.
this responsibility
However, it will not be in place and operational until August 1990, when data will be entered.
by performing
Ve will be conducting QA audits or surveillances to access the status and effectiveness of some of our corrective actions as they develop.
assigned tasks, and maintaining
In addition, the Maintenance Improvement Plan will review and resolve, as appropriate, the Maintenance Self-Assessment items'he Improvement Plan includes milestones and a built-in mechanism that requires regular re-evaluation.
cognizance
 
of all work associated
Attachment 1 to AEP:NRC:1125A Page 4
with the assigned system(s).
While we are already realizing benefits from our efforts, we do not anticipate the full benefit for several years.
In addition, AEPSC contracted
In order to effectively implement programs as encompassing and comprehensive as these, significant analysis, planning and coordination are needed.
TENERA Systems and Software to provide a computerized
As a result, their benefits will not be fully realized until mid 1993.
maintenance
 
management
Attachment 1 to AEP:NRC:1125A Page 5
information
NRC-Identified Weakness (2)
system.This system, referred to as the Nuclear Plant Maintenance
"An ineffective preventive maintenance program that resulted, for example, in failures of 4KV circuit breakers"
Module (NPM)System, discussed in more detail in our response to weakness (3), will allow plant staff to initiate, issue, prioritize
 
and track all maintenance
===Response===
work at the plant.This same software is currently being used at Pacific Gas and Electric's
to Weakness We concur that the Preventive Maintenance Program can be improved and, as previously discussed, we are taking steps to do so.
Diablo Canyon, and Public Service Electric and Gas's Salem and Hope Creek Generating
: However, Cook Nuclear Plant's availability in 1989 is evidence that the present preventive maintenance program is effective.
Stations.In addition, it was recently chosen by Electricite
During 1989, Cook Nuclear Plant generated 12 million net MWHRS, the most since 1984.
de France for use in all fifty of its nuclear plants.These three programs, RCM, System Engineer and NPM, are just part of the actions that are being taken to respond to the Self-Assessment.
The 69.3% availability for Unit 1 in 1989 contributed to an average availability of 79.4%
The November 1989 reorganization
since 1985 'lthough Unit 2 overall availability has not been as high due to steam generator tube degradatidn, its 74.4%
of Cook Nuclear Plant's management
availability in 1989 was the highest since 1983.
is another important element in the upgrade of our maintenance
On December 8, the 111-day record for the longest run with both units operating was broken.
program.The intent of the new organization
This record was extended to 140 days when Unit 2 was brought off-line for a surveillance outage on January 6,
is to place emphasis on maintenance, outages, and human'resources, Other actions, which have or are being taken are as follows: o An AEP and Cook Nuclear Plant policy on maintenance
1990.
was developed and approved in December 1989 by AEP senior management.
Unit 1 ended 1989 with its longest run of 175 days and continued operating until March 17, 1990 (a Cook Nuclear Plant record run of 251 days) when the unit was brought off line for a planned surveillance outage.
An additional
As discussed in our response to NRC violation (2) of the inspection report, the 4KV circuit breakers failure was detected during preventive maintenance testing.
plant-specific
As a result, appropriate corrective action was.subsequently taken which resulted in improvements to our 4KV breakers.
maintenance
: Also, we notified the industry of the problem via a Part 21 report.
policy established
 
in accordance
Attachment 1 to AEP:NRC:1125A Page 6
with INPO guidelines
NRC-Identified Veakness (3)
is being developed to clarify maintenance
"An extensive backlog of non-outage corrective maintenance job orders partly caused by lack of integrated planning and scheduling methodology."
philosophies
 
and responsibilities
===Response===
for all maintenance
to Weakness "Maintaining the Cook Nuclear Plant involves the completion of approximately 20,000 Job Orders annually.
groups
The relative priorities of jobs change frequently due to a number of factors, the primary reason being plant conditions.
Attachment
Managing the information contained within the backlog of yet-to-be completed Job Orders can be critical to plant availability and reliability.
1 to AEP:NRC:1125A
These efforts are presently hampered by the logistics of paper filing systems and computer tracking systems that lack needed flexibilityin hardware and software.
Page 3 o Corporate reviews have been conducted, which have resulted in improvements
(1) Corrective Actions Taken The Cook Nuclear Plant Information Management System (IMS) plan, approved for development in February of 1989 identified nine computer system modules that, when completed, will form a single, integrated information management system.
being made to shop areas used by the maintenance
This automated information system will be used by both plant site and corporate personnel to support plant operation and maintenance.
groups o Staffing studies are being performed, which have already resulted in an increase in the number of engineers and radiation protection
It will provide for the scheduling and initiation of maintenance tasks and support the assignment of responsibilities and accountabilities for these tasks.
technicians
Specifically, for maintenance, the Nuclear Plant Maintenance Module (NPM) of the Cook Nuclear Plant's IMS plan will allow plant staff to initiate, issue, prioritize, and track all maintenance work at the plant.
on site.o Other programs of note that address maintenance
The NPM module of the IMS plan will also maintain a history of maintenance work.
self-assessment
The primary objectives of the NPM module are to improve plant availability and to optimize the use of plant resources with the overall goal of reducing plant maintenance.
findings include the maintenance
The NPM system is designed to allow any NPM user to initiate a structured request that the user believes should be reviewed and, if warranted, acted upon.
procedure rewrite (See Weakness (6)), the long-range
This action request feature provides a process for screening those actions requiring work, and will serve as a focal point for initiating and tracking Job Orders.
plan and the outage guideline development
Plant personnel will enter data into the NPM system defining the component that needs work and briefly describing that work.
plan.(2)Benefits To Be Derived From Corrective
The system is designed to eliminate all paper in this process except the actual Job Order itself.
Actions RCM, the System Engineer Program and NPM were initiated to address many of the Maintenance
 
Self-Assessment's
Attachment 1 to AEP:NRC:1125A Page 7
identified
The reviews that take place in the Job Order system are performed on-line.
deficiencies.
This on-line capability allows for pending Job Orders to be sorted in various ways and the reviewing individuals have'mmediate access to this information.
When all of our efforts have been completely
implemented, each of the major findings of the self assessment
will have been addressed.,As a result of these corrective
actions.we anticipate
having a state of the art maintenance
program which will result in improved plant safety, reliability
and accountability.
(3)Date When Benefits Vill Be Realized As previously
stated, we started the RCM Program in August 1989.However, we anticipate
that the program will not be completely
implemented
for all the critical plant systems until the end of 1992.As each system is analyzed, benefits will be realized so that when this program is completed we will have a fully integrated
preventive
maintenance
program.The System Engineer Program, like RCM, is still in the early stages of implementation.
A document which clearly delineates
the responsibilities
of the engineers is currently in the final stages of review and approval.AEPSC's acquisition
of TENERA's NPM system was approved in December 1989.However, it will not be in place and operational
until August 1990, when data will be entered.Ve will be conducting
QA audits or surveillances
to access the status and effectiveness
of some of our corrective
actions as they develop.In addition, the Maintenance
Improvement
Plan will review and resolve, as appropriate, the Maintenance
Self-Assessment
items'he Improvement
Plan includes milestones
and a built-in mechanism that requires regular re-evaluation.  
Attachment
1 to AEP:NRC:1125A
Page 4 While we are already realizing benefits from our efforts, we do not anticipate
the full benefit for several years.In order to effectively
implement programs as encompassing
and comprehensive
as these, significant
analysis, planning and coordination
are needed.As a result, their benefits will not be fully realized until mid 1993.  
Attachment
1 to AEP:NRC:1125A
Page 5 NRC-Identified
Weakness (2)"An ineffective
preventive
maintenance
program that resulted, for example, in failures of 4KV circuit breakers" Response to Weakness We concur that the Preventive
Maintenance
Program can be improved and, as previously
discussed, we are taking steps to do so.However, Cook Nuclear Plant's availability
in 1989 is evidence that the present preventive
maintenance
program is effective.
During 1989, Cook Nuclear Plant generated 12 million net MWHRS, the most since 1984.The 69.3%availability
for Unit 1 in 1989 contributed
to an average availability
of 79.4%since 1985'lthough Unit 2 overall availability
has not been as high due to steam generator tube degradatidn, its 74.4%availability
in 1989 was the highest since 1983.On December 8, the 111-day record for the longest run with both units operating was broken.This record was extended to 140 days when Unit 2 was brought off-line for a surveillance
outage on January 6, 1990.Unit 1 ended 1989 with its longest run of 175 days and continued operating until March 17, 1990 (a Cook Nuclear Plant record run of 251 days)when the unit was brought off line for a planned surveillance
outage.As discussed in our response to NRC violation (2)of the inspection
report, the 4KV circuit breakers failure was detected during preventive
maintenance
testing.As a result, appropriate
corrective
action was.subsequently
taken which resulted in improvements
to our 4KV breakers.Also, we notified the industry of the problem via a Part 21 report.  
Attachment
1 to AEP:NRC:1125A
Page 6 NRC-Identified
Veakness (3)"An extensive backlog of non-outage
corrective
maintenance
job orders partly caused by lack of integrated
planning and scheduling
methodology." Response to Weakness"Maintaining
the Cook Nuclear Plant involves the completion
of approximately
20,000 Job Orders annually.The relative priorities
of jobs change frequently
due to a number of factors, the primary reason being plant conditions.
Managing the information
contained within the backlog of yet-to-be completed Job Orders can be critical to plant availability
and reliability.
These efforts are presently hampered by the logistics of paper filing systems and computer tracking systems that lack needed flexibility
in hardware and software.(1)Corrective
Actions Taken The Cook Nuclear Plant Information
Management
System (IMS)plan, approved for development
in February of 1989 identified
nine computer system modules that, when completed, will form a single, integrated
information
management
system.This automated information
system will be used by both plant site and corporate personnel to support plant operation and maintenance.
It will provide for the scheduling
and initiation
of maintenance
tasks and support the assignment
of responsibilities
and accountabilities
for these tasks.Specifically, for maintenance, the Nuclear Plant Maintenance
Module (NPM)of the Cook Nuclear Plant's IMS plan will allow plant staff to initiate, issue, prioritize, and track all maintenance
work at the plant.The NPM module of the IMS plan will also maintain a history of maintenance
work.The primary objectives
of the NPM module are to improve plant availability
and to optimize the use of plant resources with the overall goal of reducing plant maintenance.
The NPM system is designed to allow any NPM user to initiate a structured
request that the user believes should be reviewed and, if warranted, acted upon.This action request feature provides a process for screening those actions requiring work, and will serve as a focal point for initiating
and tracking Job Orders.Plant personnel will enter data into the NPM system defining the component that needs work and briefly describing
that work.The system is designed to eliminate all paper in this process except the actual Job Order itself.  
Attachment
1 to AEP:NRC:1125A
Page 7 The reviews that take place in the Job Order system are performed on-line.This on-line capability
allows for pending Job Orders to be sorted in various ways and the reviewing individuals
have'mmediate
access to this information.
Once reviews are performed the actual Job Orders can be printed for the work to be performed.
Once reviews are performed the actual Job Orders can be printed for the work to be performed.
Once a Job Order has been initiated, starting from the very first entry into the system and not just from the time it gets printed, the Job Order processing
Once a Job Order has been initiated, starting from the very first entry into the system and not just from the time it gets
system can track the status of the Job Order.This is accomplished
: printed, the Job Order processing system can track the status of the Job Order.
through the use of status code fields.Some of the codes represent situations
This is accomplished through the use of status code fields.
such as waiting for materials, or waiting for approval of the reviews, or other types of conditions.
Some of the codes represent situations such as waiting for materials, or waiting for approval of the reviews, or other types of conditions.
This feature is very helpful for planning and scheduling
This feature is very helpful for planning and scheduling the many Job Orders in the system.
the many Job Orders in the system.The NPM system will permit the plant staff to assign specific Job Orders, at the activity level, to a scheduled date, crew and supervisor.
The NPM system will permit the plant staff to assign specific Job Orders, at the activity level, to a scheduled
Upon completion'f
: date, crew and supervisor.
the crew assignments
Upon completion'f the crew assignments and confirmation of permit requirements, the system produces a
and confirmation
supervisory assignment report and prints the Job Order.
of permit requirements, the system produces a supervisory
The completed work package includes the Job Order, equipment descriptions, parts list, and testing forms along with other needed documents.
assignment
Once the work related to a Job Order has been completed and
report and prints the Job Order.The completed work package includes the Job Order, equipment descriptions, parts list, and testing forms along with other needed documents.
: tested, the Job Order is reviewed and closed out, on-line.
Once the work related to a Job Order has been completed and tested, the Job Order is reviewed and closed out, on-line.The NPM system maintains a complete history of all completed and closed-out
The NPM system maintains a complete history of all completed and closed-out Job Orders.
Job Orders.This feature allows for rapid access to all history on Job Orders.The NPM system prevents a Job Order from being closed-out
This feature allows for rapid access to all history on Job Orders.
until all reviews and tests have been completed.
The NPM system prevents a Job Order from being closed-out until all reviews and tests have been completed.
Zn addition, the NPM system will be a repository
Zn addition, the NPM system will be a repository for previous repetitive tasks.
for previous repetitive
This function eliminates the need for individuals to recreate Job Orders that are repetitive in
tasks.This function eliminates
: nature, The NPM system will automatically generate the Job Orders,, according to the appropriate due dates, or as directed by a planner.
the need for individuals
The NPM system will also provide for continuous monitoring of surveillance tests and preventive maintenance work to meet regulatory or plant requirements.
to recreate Job Orders that are repetitive
Once the repetitive or preventive maintenance Job Orders are
in nature, The NPM system will automatically
: created, they are available for reviews and executions in the same manner as any of the other Job Orders.
generate the Job Orders,, according to the appropriate
This system will also be used to develop Job Orders for planned outages such as refueling outages.
due dates, or as directed by a planner.The NPM system will also provide for continuous
 
monitoring
Attachment 1 to AEP:NRC:1125A Page 8
of surveillance
(2) Benefits To Be Derived From Corrective Actions The data entered into the NPM system, and the processing that the system does with this data, will eliminate the multiple manual data entry steps of our present process.
tests and preventive
Eliminating redundant manual systems is of significance itself.
maintenance
: However, more importantly are the anticipated improvements in plant availability and labor productivity.
work to meet regulatory
Along with improved ability to plan and schedule work comes an increased amount of time available for more careful consideration of other aspects of the work to be performed, for
or plant requirements.
: example, personnel safety.
Once the repetitive
Improvements can be expected and will certainly be strived for.
or preventive
The NPM system will also identify and coordinate maintenance on related equipment and systems, thus decreasing down time on components removed from service.
maintenance
Quick access to the information in the NPM data bases makes the supervisors in both the operations and maintenance areas more aware of Job Order progress.
Job Orders are created, they are available for reviews and executions
It is anticipated that the NPM system w'ill help us realize our goal of a non-outage corrective maintenance job order backlog not in excess of 90 days.
in the same manner as any of the other Job Orders.This system will also be used to develop Job Orders for planned outages such as refueling outages.  
(3) Date When Benefits Will Be Achieved We currently anticipate having the computerized automated maintenance system in place and operational by August 1990.
Attachment
At that time, data validation and loading, procedure changes and training of personnel will begin.
1 to AEP:NRC:1125A
 
Page 8 (2)Benefits To Be Derived From Corrective
Attachment 1 to AEP:NRC:1125A Page 9
Actions The data entered into the NPM system, and the processing
NRC-Identified Weakness (4)
that the system does with this data, will eliminate the multiple manual data entry steps of our present process.Eliminating
"Poor material condition especially as evidenced by the high number of oil, steam and water leaks."
redundant manual systems is of significance
 
itself.However, more importantly
===Response===
are the anticipated
to Weakness (1) Corrective Actions Taken While it is AEPSC's policy to keep all of its facilities, in good material condition, we recognize the need for improvement in this area.
improvements
As a result, the management of the Cook Nuclear Plant has launched a concerted effort to improve plant material condition.
in plant availability
This is evidenced by the allocation of funds to support the following physical improvements that are currently taking place:
and labor productivity.
o Auxiliary building painting o
Along with improved ability to plan and schedule work comes an increased amount of time available for more careful consideration
Contaminated equipment storage area expansion I
of other aspects of the work to be performed, for example, personnel safety.Improvements
o Decontamination area redesign o
can be expected and will certainly be strived for.The NPM system will also identify and coordinate
Improved lighting o
maintenance
Installation of 18 personnel whole body contamination monitors It is Cook Nuclear Plant policy that no leak is considered acceptable.
on related equipment and systems, thus decreasing
Consequently, during the 1988/1989 refueling outages we refurbished about 1,780 valves and packed them with Chesterton packing.
down time on components
A breakdown of this effort is as follows:
removed from service.Quick access to the information
Unit 1 Unit 2 Total Auxiliary Building Containment Turbine Hall Miscellaneous 254 130 225 21 150 280 700 925 50 71 250 504 Nevertheless, a substantial number of leaks still exist in the auxiliary building, ranging from small traces of dried boric acid to dripping.
in the NPM data bases makes the supervisors
These leaks have been entered into a computer data base, have been chalked
in both the operations
: down, and job orders have been written.
and maintenance
The leaks are currently being prioritized and efforts will be made to repair them during the next refueling outage, if not before.
areas more aware of Job Order progress.It is anticipated
 
that the NPM system w'ill help us realize our goal of a non-outage
Attachment 1 to AEP:NRC:1125A Page 10 The plant manager has reaffirmed his commitment to good plant material condition and personal accountability by sending a
corrective
memorandum to each employee.
maintenance
This commitment has been supported by continued radiation worker awareness
job order backlog not in excess of 90 days.(3)Date When Benefits Will Be Achieved We currently anticipate
: training, and operator training on venting and draining.
having the computerized
In addition, decontamination efforts continue, which have already reduced the contaminated area from approximately 45,000 feet in 1986 to the current 25,000 feet (excluding laydown areas).
automated maintenance
Our goal is to reduce these contaminated areas to 20,000 square feet in 1990 and 10,000 square feet prior to the outage in 1991.
system in place and operational
(2) Benefits To Be Derived from Corrective Actions There are numerous benefits gained from having the plant in good physical condition, the most important of these being increased plant safety and reliability.
by August 1990.At that time, data validation
A related benefit is improved radiation protection and worker safety.
and loading, procedure changes and training of personnel will begin.  
However, another important, but less quantifiable benefit is the improvement to worker morale.
(3) Date When Benefits Will Be Realized While maintaining the plant in good physical condition is an ongoing process, we anticipate major improvements within the next year.
Attachment
The refueling outage will facilitate the refurbishment of valises, as well as other repairs and modifications.
1 to AEP:NRC:1125A
 
Page 9 NRC-Identified
Attachment 1 to AEP:NRC:1125A Page 11 NRC-Identified Weakness (5)
Weakness (4)"Poor material condition especially
"Inadequate trending, root cause analysis and action to correct, for example, numerous leaking safety relief valves."
as evidenced by the high number of oil, steam and water leaks." Response to Weakness (1)Corrective
 
Actions Taken While it is AEPSC's policy to keep all of its facilities, in good material condition, we recognize the need for improvement
===Response===
in this area.As a result, the management
to Weakness (1) Corrective Actions Taken This weakness is being addressed by three programs:
of the Cook Nuclear Plant has launched a concerted effort to improve plant material condition.
the NPM system which is discussed in detail in our response to weaknesses (1) and (3), the System Engineer
This is evidenced by the allocation
: Program, discussed in our response to weakness (1), and the RCM Program discussed in our response to weakness (1).
of funds to support the following physical improvements
(2) Benefits To Be Derived from Corrective Actions The NPM system will provide for a complete component history.
that are currently taking place: o Auxiliary building painting o Contaminated
The component history will provide a chronological listing of work, modifications or inspections that have been performed on a particular component.
equipment storage area expansion I o Decontamination
This process creates an indexed historical record for components or functional equipment groups and catalogs completion dates, failure codes, as-found and as-left conditions, parts replaced, test results, etc.
area redesign o Improved lighting o Installation
The System Engineers are expected to identify and trend appropriate system parameters, with the goal of obtaining pertinent data for system performance and reliability monitoring.
of 18 personnel whole body contamination
The parameters trended shall be periodically reviewed and approved to allow timely preventive or corrective actions to be implemented.
monitors It is Cook Nuclear Plant policy that no leak is considered
Based on the trended data, the System Engineer is expected to recognize significant system/component degradation or abnormal operating conditions from both a historical basis, as well as current status.
acceptable.
The System Engineer may require the support of technical experts to analyze specific areas of concern and will work closely with our Corporate Nuclear Engineering Division engineers in this regard.
Consequently, during the 1988/1989 refueling outages we refurbished
The System Engineers are expected to perform root cause analyses on the systems assigned.
about 1,780 valves and packed them with Chesterton
Consequently, the System Engineers will be trained in root cause analysis.
packing.A breakdown of this effort is as follows: Unit 1 Unit 2 Total Auxiliary Building Containment
In addition, the System Engineer is expected to:
Turbine Hall Miscellaneous
Evaluate system/component failure impact on plant safety and unit power operations Prepare and perform special system/component performance tests.
254 130 225 21 150 280 700 925 50 71 250 504 Nevertheless, a substantial
 
number of leaks still exist in the auxiliary building, ranging from small traces of dried boric acid to dripping.These leaks have been entered into a computer data base, have been chalked down, and job orders have been written.The leaks are currently being prioritized
Attachment 1 to AEP:NRC:1125A Page 12 The RCM Program wt.ll contribute to resolving this issue by identifying dominant failure modes and critical components.
and efforts will be made to repair them during the next refueling outage, if not before.  
(3) Date When Benefits Will Be Realized As previously stated, we expect the NPM system to be in place and operational in August 1990.
At that time, personnel training and data loading will begin.
Attachment
Several system engineers have been assigned at Cook Nuclear Plant and benefits have already been realized from this program.
1 to AEP:NRC:1125A
An effort is currently being made to recruit System Engineers.
Page 10 The plant manager has reaffirmed
: However, we anticipate it will take at least a year before the program is fully staffed.
his commitment
 
to good plant material condition and personal accountability
Attachment 1 to AEP:NRC:1125A Page 13 NRC-Identified Weakness (6)
by sending a memorandum
"In several instances procedures were not followed, were poor or did not exist especially in the balance of plant area."
to each employee.This commitment
 
has been supported by continued radiation worker awareness training, and operator training on venting and draining.In addition, decontamination
===Response===
efforts continue, which have already reduced the contaminated
to Weakness (1) Corrective Actions Taken Key to the safe and efficient operation of any nuclear power plant is strict adherence to procedures.
area from approximately
As such, employees are shown during the Nuclear General Employee Training (NGET)
45,000 feet in 1986 to the current 25,000 feet (excluding
: classes, a videotape of David Williams, Jr.,
laydown areas).Our goal is to reduce these contaminated
Senior Executive V.P., Engineering and Construction, mandating the adherence to procedures.
areas to 20,000 square feet in 1990 and 10,000 square feet prior to the outage in 1991.(2)Benefits To Be Derived from Corrective
It is AEPSC's long-standing policy that failure to follow procedures will result in disciplinary action.
Actions There are numerous benefits gained from having the plant in good physical condition, the most important of these being increased plant safety and reliability.
In order for this policy to have any benefit, well-written and accurate procedures must be in place.
A related benefit is improved radiation protection
Consequently, AEPSC is purchasing PRONET and the services of consultant procedure writers to upgrade or write 690 maintenance procedures (268 maintenance, 422 I&C).
and worker safety.However, another important, but less quantifiable
Critical balance of plant components will be addressed as they arise in the RCM program.
benefit is the improvement
The Maintenance Improvement Plan provides guidance that clearly defines what procedure compliance is.
to worker morale.(3)Date When Benefits Will Be Realized While maintaining
In addition, a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.
the plant in good physical condition is an ongoing process, we anticipate
(2) Benefits To Be Derived from Corrective Actions PRONET is a state of the art computer system that integrates writer's guidelines, word processing, graphics and data base functions into a centralized procedure management system.
major improvements
Development, commitment, scheduling and reporting functions will be controlled by this menu-driven network.
within the next year.The refueling outage will facilitate
This integrated approach will result in a program that reduces development time and provides efficient long-term procedure maintenance and commitment/reference tracking.
the refurbishment
(3) Date When Benefits Will Be Realized Although a consultant will train plant staff on the use of
of valises, as well as other repairs and modifications.  
: PRONET, the bulk of the procedure upgrade work will be performed by consultant personnel.
Attachment
By using contract workers we will not impact the plant staff. If the existing staff were used, it is anticipated that the effort would take four to five years.
1 to AEP:NRC:1125A
This is considered to be an unacceptable time frame for this work.
Page 11 NRC-Identified
By using contract workers, we will obtain professionally prepared procedures in a reasonable time frame.
Weakness (5)"Inadequate
The effort is scheduled to be completed by December 1991.
trending, root cause analysis and action to correct, for example, numerous leaking safety relief valves." Response to Weakness (1)Corrective
 
Actions Taken This weakness is being addressed by three programs: the NPM system which is discussed in detail in our response to weaknesses
ATTACHMENT 2 TO AEP:NRC:1125A
(1)and (3), the System Engineer Program, discussed in our response to weakness (1), and the RCM Program discussed in our response to weakness (1).(2)Benefits To Be Derived from Corrective
 
Actions The NPM system will provide for a complete component history.The component history will provide a chronological
===RESPONSE===
listing of work, modifications
TO NRC-IDENTIFIED VIOLATIONS
or inspections
 
that have been performed on a particular
Attachment 2 to AEP:NRC:1125A Page 1
component.
NRC Violation 1 "10 CFR 50, Appendix B, Criterion V, as implemented by Section 1.7.5 of the Donald C.
This process creates an indexed historical
Cook Nuclear Plant Operational Quality Assurance Program requires that activities related to quality be prescribed by documented instructions, procedures, and drawings, that those activities be accomplished in accordance with those instructions, procedures and drawings, and that instructions, procedures or drawings include appropriate quantitative or qualitative acceptance criteria for determining that important activt,ties have been satisfactorily accomplished.
record for components
a
or functional
~
equipment groups and catalogs completion
Procedure PMI-2290, "Job Orders," Revision 8, required in Sections 4.4.8 and 4.4.8.3 that upon completion of the physical work, the job order tags be removed and discarded.
dates, failure codes, as-found and as-left conditions, parts replaced, test results, etc.The System Engineers are expected to identify and trend appropriate
Contrary to the abo~e, tags
system parameters, with the goal of obtaining pertinent data for system performance
: 15119, 029643,
and reliability
: B012209, B016950,
monitoring.
: B016832, and B017240 were not removed although the job orders were cancelled or completed.
The parameters
As a result, status of equipment condi.tion remained indeterminate (315/89031-01A; 316/89031-01A)
trended shall be periodically
~
reviewed and approved to allow timely preventive
b.
or corrective
Request For Change 12-2180 required installation of 200%
actions to be implemented.
overload motor protection and that the thermal overload be set at the low trip current rating.
Based on the trended data, the System Engineer is expected to recognize significant
Contrary to the above, on December 19,
system/component
: 1989, the inspectors observed that the thermal overload heater associated with residual heat removal loop isolation motor-operated valve ICM-111 was set at the high trip current rating.
degradation
Numerous additional thermal overloads in the diesel generator motor control center were also observed to be the wrong size or set at the wrong current rating, which will result in premature removal of operating voltage from the motors (315/89031-01B; 316/89031-01B)
or abnormal operating conditions
~
from both a historical
c
basis, as well as current status.The System Engineer may require the support of technical experts to analyze specific areas of concern and will work closely with our Corporate Nuclear Engineering
~
Division engineers in this regard.The System Engineers are expected to perform root cause analyses on the systems assigned.Consequently, the System Engineers will be trained in root cause analysis.In addition, the System Engineer is expected to: Evaluate system/component
Procedure PMI-2030, "Document Control," Revision 10, failed to include requirements for the Master Drawing Indexes to be reviewed by intended users for the latest as built drawings located in the plant master file.
failure impact on plant safety and unit power operations
Consequently, drawings issued by the document control center for field verifications were not the latest as built drawings or revisions (315/89031-01C; 316/89031/01C).
Prepare and perform special system/component
The "Pump Operator's Data" manual and the vendor manual for'he Auxiliary Feedwater (AFV) pump required that the pump packing be adjusted while the pump is operating.
performance
Contrary to the above, this requirement was not incorporated into the AFV maintenance procdures
tests.  
[sic).
Attachment
Although no problems were noted, inadequate attention to this requirement could result in rotor seizure, scored shaft sleeves, or burned packing (315/89031-01D; 316/89031-01D).
1 to AEP:NRC:1125A
 
Page 12 The RCM Program wt.ll contribute
Attachment 2 to AEP:NRC:1125A Page 2
to resolving this issue by identifying
Procedure 12 THP 6030 IMP.014 "Protective Relay Calibration", Revision 8, Step 8.1.2-2 specified that black electrical tape be used when cleaning the disk and drag magnet mechanism on Time Overcurrent (IAC) relays.
dominant failure modes and critical components.
Contrary to the above, on December 5,
(3)Date When Benefits Will Be Realized As previously
: 1989, a technician was observed using an unused calibration sticker to clean the 2AB EDG Time Overcurrent test relay.
stated, we expect the NPM system to be in place and operational
As a result, cleanliness of the contacts was questionable (315/89031-01E; 316/89031-01E).
in August 1990.At that time, personnel training and data loading will begin.Several system engineers have been assigned at Cook Nuclear Plant and benefits have already been realized from this program.An effort is currently being made to recruit System Engineers.
f.
However, we anticipate
Procedure PMI-2010 "Plant Manager and Department Head Instructions, Procedures and Index," Revision 17, Policy Statement 3.1, Section 3 required that "double asterisked" procedures for plant activities be "in-hand" when implementing the procedure.
it will take at least a year before the program is fully staffed.  
Contrary to the above, on December 6,
Attachment
: 1989, the inspector observed an operator rack in "2A" Train Reactor Trip Bypass Breaker without having "in hand" double asterisked procedure
1 to AEP:NRC:1125A
~12-OHP 4021.082.018 "Racking In and Out Reactor Trip, Reactor Trip Bypass and MG Set Output Breakers,"
Page 13 NRC-Identified
Revision 2.
Weakness (6)"In several instances procedures
Even though no adverse affects were noted, in the past under similar circumstances, a reactor trip occurred (315/89031-01F; 316/89031-01F).
were not followed, were poor or did not exist especially
Procedure PMI-2010, "Plant Manager and Department Head Instructions, Procedures and Index," Revision 17, requires in Section 3.14.1 that all effective instructions and procedures be reviewed no less frequent than once every two years.
in the balance of plant area." Response to Weakness (1)Corrective
Contrary to the above, maintenance procedure MHI 2070, MHI 7090, PMI 4050, 12 THP 6030 IMP ~ 071, and 12 THP IMP.062 were not reviewed in the last two years.
Actions Taken Key to the safe and efficient operation of any nuclear power plant is strict adherence to procedures.
As a result, the procedures were not updated to reflect feedback and changes to preventive maintenance activities (315/89031-01G; 316/89031-1G)."
As such, employees are shown during the Nuclear General Employee Training (NGET)classes, a videotape of David Williams, Jr., Senior Executive V.P., Engineering
 
and Construction, mandating the adherence to procedures.
===Response===
It is AEPSC's long-standing
to Violation la Plant procedure PMI-2290 requires that tags placed at or near equipment needing repair be removed when the item is repaired or if the Job Order is cancelled.
policy that failure to follow procedures
As noted in the text, six Job Order tags were found in the plant for work that had been cancelled or completed which constitutes failure to follow procedure.
will result in disciplinary
The conclusion made in Inspection Report 89031 was that equipment status was "indeterminate."
action.In order for this policy to have any benefit, well-written
While the presence of Job Order tags was contrary to the requirements of PMI-2290, the status of equipment/components involved would not be affected.
and accurate procedures
The information placed on a tag identifies to personnel
must be in place.Consequently, AEPSC is purchasing
: 1) that a Job Order has been written for repair with number noted,
PRONET and the services of consultant
: 2) the nature of repairs/adjustments required as determined by the person initiating the Job Order and 3) helps locate the specific component.
procedure writers to upgrade or write 690 maintenance
By itself, a Job Order tag has no impact on system or equipment operability, does
procedures
 
(268 maintenance, 422 I&C).Critical balance of plant components
Attachment 2 to AEP:NRC.:1125A Page 3
will be addressed as they arise in the RCM program.The Maintenance
not indicate that equipment has been tagged out, and does not direct any other activity involving the equipment.
Improvement
Other systems such as the clearance permit system logs and the deficiency logs indicate the equipment status.
Plan provides guidance that clearly defines what procedure compliance
(1) Corrective Action Taken and Results Achieved Job Order tags identified during the inspection were subsequently removed to achieve compliance with applicable sections of PMI-2290.
is.In addition, a procedure writer'/user's
(2) Corrective Action Taken To Avoid Further Violation The Plant Manager will i.ssue a
guide will address the circumstances
memo on procedural compliance to ensure that all personnel are fully aware of the meaning of compliance, consequences of failure and what actions to take
for changing a procedure to ensure procedural
~ when a procedure cannot be followed as written.
compliance.
The Maintenance Improvement Plan includes issuance of a department policy on procedure compliance.
(2)Benefits To Be Derived from Corrective
Included will be guidance on the monitoring of the effectiveness of procedure compliance.
Actions PRONET is a state of the art computer system that integrates
Also a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.
writer's guidelines, word processing, graphics and data base functions into a centralized
(3) Date When Full Com liance Will Be Achieved The final draft of the policy will be issued on July 15, 1990.
procedure management
Guidance on the effectiveness monitoring will be issued on August 15, 1990.
system.Development, commitment, scheduling
The Plant Manager's memo will be issued on May 1, 1990.
and reporting functions will be controlled
 
by this menu-driven
===Response===
network.This integrated
to Violation lb The Notice of Violation identified that thermal overloads in the plant had been installed at an incorrect trip current rating.
approach will result in a program that reduces development
As a result of the inspection, plant personnel investigated the problem and addressed it in Problem Report 90-81.
time and provides efficient long-term procedure maintenance
(1) Corrective Action Taken and Results Achieved The improper positioning and/or mis-sizing of the overload heaters resulted from errors made during initial installations.
and commitment/reference
tracking.(3)Date When Benefits Will Be Realized Although a consultant
will train plant staff on the use of PRONET, the bulk of the procedure upgrade work will be performed by consultant
personnel.
By using contract workers we will not impact the plant staff.If the existing staff were used, it is anticipated
that the effort would take four to five years.This is considered
to be an unacceptable
time frame for this work.By using contract workers, we will obtain professionally
prepared procedures
in a reasonable
time frame.The effort is scheduled to be completed by December 1991.  
ATTACHMENT
2 TO AEP:NRC:1125A
RESPONSE TO NRC-IDENTIFIED
VIOLATIONS
Attachment
2 to AEP:NRC:1125A
Page 1 NRC Violation 1"10 CFR 50, Appendix B, Criterion V, as implemented
by Section 1.7.5 of the Donald C.Cook Nuclear Plant Operational
Quality Assurance Program requires that activities
related to quality be prescribed
by documented
instructions, procedures, and drawings, that those activities
be accomplished
in accordance
with those instructions, procedures
and drawings, and that instructions, procedures
or drawings include appropriate
quantitative
or qualitative
acceptance
criteria for determining
that important activt,ties
have been satisfactorily
accomplished.
a~Procedure PMI-2290,"Job Orders," Revision 8, required in Sections 4.4.8 and 4.4.8.3 that upon completion
of the physical work, the job order tags be removed and discarded.
Contrary to the abo~e, tags 15119, 029643, B012209, B016950, B016832, and B017240 were not removed although the job orders were cancelled or completed.
As a result, status of equipment condi.tion
remained indeterminate
(315/89031-01A;
316/89031-01A)
~b.Request For Change 12-2180 required installation
of 200%overload motor protection
and that the thermal overload be set at the low trip current rating.Contrary to the above, on December 19, 1989, the inspectors
observed that the thermal overload heater associated
with residual heat removal loop isolation motor-operated
valve ICM-111 was set at the high trip current rating.Numerous additional
thermal overloads in the diesel generator motor control center were also observed to be the wrong size or set at the wrong current rating, which will result in premature removal of operating voltage from the motors (315/89031-01B;
316/89031-01B)
~c~Procedure PMI-2030,"Document Control," Revision 10, failed to include requirements
for the Master Drawing Indexes to be reviewed by intended users for the latest as built drawings located in the plant master file.Consequently, drawings issued by the document control center for field verifications
were not the latest as built drawings or revisions (315/89031-01C;
316/89031/01C).
The"Pump Operator's
Data" manual and the vendor manual for'he Auxiliary Feedwater (AFV)pump required that the pump packing be adjusted while the pump is operating.
Contrary to the above, this requirement
was not incorporated
into the AFV maintenance
procdures[sic).Although no problems were noted, inadequate
attention to this requirement
could result in rotor seizure, scored shaft sleeves, or burned packing (315/89031-01D;
316/89031-01D).  
Attachment
2 to AEP:NRC:1125A
Page 2 Procedure 12 THP 6030 IMP.014"Protective
Relay Calibration", Revision 8, Step 8.1.2-2 specified that black electrical
tape be used when cleaning the disk and drag magnet mechanism on Time Overcurrent (IAC)relays.Contrary to the above, on December 5, 1989, a technician
was observed using an unused calibration
sticker to clean the 2AB EDG Time Overcurrent
test relay.As a result, cleanliness
of the contacts was questionable
(315/89031-01E;
316/89031-01E).
f.Procedure PMI-2010"Plant Manager and Department
Head Instructions, Procedures
and Index," Revision 17, Policy Statement 3.1, Section 3 required that"double asterisked" procedures
for plant activities
be"in-hand" when implementing
the procedure.
Contrary to the above, on December 6, 1989, the inspector observed an operator rack in"2A" Train Reactor Trip Bypass Breaker without having"in hand" double asterisked
procedure~12-OHP 4021.082.018"Racking In and Out Reactor Trip, Reactor Trip Bypass and MG Set Output Breakers," Revision 2.Even though no adverse affects were noted, in the past under similar circumstances, a reactor trip occurred (315/89031-01F;
316/89031-01F).
Procedure PMI-2010,"Plant Manager and Department
Head Instructions, Procedures
and Index," Revision 17, requires in Section 3.14.1 that all effective instructions
and procedures
be reviewed no less frequent than once every two years.Contrary to the above, maintenance
procedure MHI 2070, MHI 7090, PMI 4050, 12 THP 6030 IMP~071, and 12 THP IMP.062 were not reviewed in the last two years.As a result, the procedures
were not updated to reflect feedback and changes to preventive
maintenance
activities
(315/89031-01G;
316/89031-1G)." Response to Violation la Plant procedure PMI-2290 requires that tags placed at or near equipment needing repair be removed when the item is repaired or if the Job Order is cancelled.
As noted in the text, six Job Order tags were found in the plant for work that had been cancelled or completed which constitutes
failure to follow procedure.
The conclusion
made in Inspection
Report 89031 was that equipment status was"indeterminate." While the presence of Job Order tags was contrary to the requirements
of PMI-2290, the status of equipment/components
involved would not be affected.The information
placed on a tag identifies
to personnel 1)that a Job Order has been written for repair with number noted, 2)the nature of repairs/adjustments
required as determined
by the person initiating
the Job Order and 3)helps locate the specific component.
By itself, a Job Order tag has no impact on system or equipment operability, does  
Attachment
2 to AEP:NRC.:1125A
Page 3 not indicate that equipment has been tagged out, and does not direct any other activity involving the equipment.
Other systems such as the clearance permit system logs and the deficiency
logs indicate the equipment status.(1)Corrective
Action Taken and Results Achieved Job Order tags identified
during the inspection
were subsequently
removed to achieve compliance
with applicable
sections of PMI-2290.(2)Corrective
Action Taken To Avoid Further Violation The Plant Manager will i.ssue a memo on procedural
compliance
to ensure that all personnel are fully aware of the meaning of compliance, consequences
of failure and what actions to take~when a procedure cannot be followed as written.The Maintenance
Improvement
Plan includes issuance of a department
policy on procedure compliance.
Included will be guidance on the monitoring
of the effectiveness
of procedure compliance.
Also a procedure writer'/user's
guide will address the circumstances
for changing a procedure to ensure procedural
compliance.
(3)Date When Full Com liance Will Be Achieved The final draft of the policy will be issued on July 15, 1990.Guidance on the effectiveness
monitoring
will be issued on August 15, 1990.The Plant Manager's memo will be issued on May 1, 1990.Response to Violation lb The Notice of Violation identified
that thermal overloads in the plant had been installed at an incorrect trip current rating.As a result of the inspection, plant personnel investigated
the problem and addressed it in Problem Report 90-81.(1)Corrective
Action Taken and Results Achieved The improper positioning
and/or mis-sizing
of the overload heaters resulted from errors made during initial installations.
Twenty overloads were inspected and evaluated by plant and AEPSC engineers.
Twenty overloads were inspected and evaluated by plant and AEPSC engineers.
Eleven were found to b'e correct.One was found on a breaker for a resistive heater where overload protection
Eleven were found to b'e correct.
was not considered
One was found on a breaker for a resistive heater where overload protection was not considered critical as molded case circuit breakers protection was provided.
critical as molded case circuit breakers protection
On four breakers (including ICM-111) the as-found heater size agreed with the calculated, but arrow position did not agree.
was provided.On four breakers (including
Full load amps was at the dividing point for selecting up or down posi.tion.
ICM-111)the as-found heater size agreed with the calculated, but arrow position did not agree.Full load amps was at the dividing point for selecting up or down posi.tion.
Slight changes in motor protection resulted but did not affect the operability of load.
Slight changes in motor protection
Four feeders on BOP were found to be mis-sized.
resulted but did not affect the operability
Of those four
of load.Four feeders on BOP were found to be mis-sized.
 
Of those four  
Attachment 2 to AEP:NRC:1125A
Attachment
-Page 4
2 to AEP:NRC:1125A-Page 4 one was mis-sized to a degree that replacement
one was mis-sized to a degree that replacement was needed to ensure adequate protection.
was needed to ensure adequate protection.
Of the three other overload
Of the three other overload heaters, though improperly
: heaters, though improperly set, would have provided thermal overload protection for equipment.
set, would have provided thermal overload protection
Job Orders to correct these settings by October 30,
for equipment.
: 1990, have been written.
Job Orders to correct these settings by October 30, 1990, have been written.(2)Corrective
(2) Corrective Action Taken To Avoid Further Violation In the course of the plant's investigation it was determined that the mis-sizing and/or mispositioning of the thermal overloads had occurred during initial installation in 1977 and 1978.
Action Taken To Avoid Further Violation In the course of the plant's investigation
Lacking vendor information, calculations were most likely developed by plant personnel for positions/sizes which in some of the cases, proved incorrect.
it was determined
The design change process has evolved since that time to a level that reasonably ensures that repetition of a similar condition will not occur.
that the mis-sizing
Specifically, general procedures now require that design calculations be verified and documented by qualified personnel.
and/or mispositioning
(3) Date When Full Com liance Will Be Achieved Based on the engineering evaluation completed January 15,'990, the deficiencies in the thermal overload heater settings would not have affected the operability of the ICM-111 breaker.
of the thermal overloads had occurred during initial installation
Other deficiencies did not degrade the thermal overload protection of the equipment breakers.
in 1977 and 1978.Lacking vendor information, calculations
Current procedures/practices should prevent recurrence of this problem.
were most likely developed by plant personnel for positions/sizes
 
which in some of the cases, proved incorrect.
===Response===
The design change process has evolved since that time to a level that reasonably
to Violation lc In the course of the inspection it was found that a plant instruction utilized for document control (drawings) contained no provision mandating that the user of the index verify that it was the most recent update.
ensures that repetition
We concur with the inspector's conclusion that an instruction to users of the Master Drawing Index to ensure that it references up-to-date as-built drawings should be included in procedures.
of a similar condition will not occur.Specifically, general procedures
(1) Corrective Action Taken and Results Achieved As a result of the inspection, PMI-2030, "Document Control," was revised to instruct a Master Data Index user to ensure that it reflects the latest as-built drawings located in the plant's master file.
now require that design calculations
(2) Corrective Action Taken To Avoid Further Violation Revision 11 to PMI-2030 is being routed for approval from plant management.
be verified and documented
The revision addresses the inspector's concern noted in the Notice of Violation.
by qualified personnel.
 
(3)Date When Full Com liance Will Be Achieved Based on the engineering
I Attachment 2 to AEP:NRC:1125A Page 5
evaluation
(3) Date When Full Com lienee Will Be Achieved The revised version of PMI-2030 will be effective by May 1, 1990.
completed January 15,'990, the deficiencies
 
in the thermal overload heater settings would not have affected the operability
===Response===
of the ICM-111 breaker.Other deficiencies
to Violation ld Procedural revision to incorporate a direction to run a pump in order to properly adjust packing is not viewed as necessary.
did not degrade the thermal overload protection
Personnel performing packing adjustments meet the requirements of ANSI Standard N18-1 (4.5.3).
of the equipment breakers.Current procedures/practices
Consistent with that standard, maintenance personnel receive formal training in subjects associated with their position.
should prevent recurrence
Included in the plant's training is a course on pumps that directly references the correct methodology for adjusting the packing on pumps.
of this problem.Response to Violation lc In the course of the inspection
This teaches maintenance personnel that adjustments will only be made to packing when the pump is operating.
it was found that a plant instruction
As required by ANSI Standard N18-7, Section 4.1 (2), plant procedures are developed with the objective of providing adequate information to personnel involved in a given task considering the skill they are provided through the training program.
utilized for document control (drawings)
(1) Corrective Action Taken and Results Achieved Those persons who would be involved in pump packing work are hired and trained consistent with ANSI N18-1.
contained no provision mandating that the user of the index verify that it was the most recent update.We concur with the inspector's
(2) Corrective Action Taken to Avoid Further Violation The hiring practices and training programs have proven adequate to prevent problems due to pump packing (3) Date When Full Com liance Will Be Achieved No violation occurred as practices are in accordance with N18-1 and personnel are fully qualified.
conclusion
 
that an instruction
===Response===
to users of the Master Drawing Index to ensure that it references
to Violation le While the intent of Step 8.1.2-2 of maintenance procedure 12 THP 6030.IMP.014 was to ensure that technicians performing cleaning would utilize tape or similar adhesive-backed material.
up-to-date
Black electrical tape, was specified because it is a commonly available item.
as-built drawings should be included in procedures.
: However, use of a calibration sticker did
(1)Corrective
- constitute a violation of the procedure as written.
Action Taken and Results Achieved As a result of the inspection, PMI-2030,"Document Control," was revised to instruct a Master Data Index user to ensure that it reflects the latest as-built drawings located in the plant's master file.(2)Corrective
(1) Corrective Action Taken and Results Achieved Maintenance supervision reviewed the net effect of utilizing the sticker in the course of cleaning and determined that satisfactory results were obtained.
Action Taken To Avoid Further Violation Revision 11 to PMI-2030 is being routed for approval from plant management.
No re-cleaning was deemed
The revision addresses the inspector's
 
concern noted in the Notice of Violation.  
Attachment 2 to AEP:NRC:1125A Page 6
I Attachment
necessary.
2 to AEP:NRC:1125A
12 THP 6030.IMP.014 had been revised via a change sheet initiated April 2, 1990, to remove reference to black electrical tape.
Page 5 (3)Date When Full Com lienee Will Be Achieved The revised version of PMI-2030 will be effective by May 1, 1990.Response to Violation ld Procedural
(2) Corrective Action Taken To Avoid Further Violation The Plant Manager will issue a
revision to incorporate
memo on procedural compliance to ensure that all personnel are fully aware of the meaning of compliance, consequences of failure and what actions to take when a procedure cannot be followed as written.
a direction to run a pump in order to properly adjust packing is not viewed as necessary.
The Maintenance Improvement Plan includes issuance of a department policy on procedure compliance.
Personnel performing
Included will be guidance on the monitoring of the effectiveness of procedure compliance.
packing adjustments
Also a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.
meet the requirements
(3) Date When Full Com lienee Will Be Achieved The final draft of the policy will be issued on July 15, 1990.
of ANSI Standard N18-1 (4.5.3).Consistent
Guidance on the effectiveness monitoring will be issued on August 15, 1990.
with that standard, maintenance
The Plant Manager's memo will be issued on May 1, 1990.
personnel receive formal training in subjects associated
 
with their position.Included in the plant's training is a course on pumps that directly references
===Response===
the correct methodology
to Violation lf (1) Corrective Action Taken and Results Achieved The Auxiliary Equipment Operator (AEO) involved in this event had received training on the operation of reactor trip breakers and the existence of the procedure prior to this event.
for adjusting the packing on pumps.This teaches maintenance
The AEO, however, overlooked the reactor trip breaker procedure was required to be "in hand" whenever performing racking operations.
personnel that adjustments
Although the racking evolution was done in accordance with the.
will only be made to packing when the pump is operating.
procedure requirements, this event was a violation because the requirement to have the procedure "in hand" was not satisfied.
As required by ANSI Standard N18-7, Section 4.1 (2), plant procedures
A memorandum was issued to Operations personnel on January 19, 1990, to remind them of the "in hand" requirement for the reactor trip breaker procedure.
are developed with the objective of providing adequate information
(2) Corrective Action To Be Taken To Avoid Further Violation The routine surveillance procedures for reactor trip breaker testing were revised on December 13, 1989, to reference the requirement for having the reactor trip breaker racking procedure "in hand" for the racking evolutions.
to personnel involved in a given task considering
The startup surveillance procedures, which require racking of the reactor trip breakers, will be revised by June 4,
the skill they are provided through the training program.(1)Corrective
1990, to reference the requirement for having the reactor trip breaker procedure "in hand."
Action Taken and Results Achieved Those persons who would be involved in pump packing work are hired and trained consistent
 
with ANSI N18-1.(2)Corrective
Attachment 2 to AEP:NRC:1125A Page 7
Action Taken to Avoid Further Violation The hiring practices and training programs have proven adequate to prevent problems due to pump packing (3)Date When Full Com liance Will Be Achieved No violation occurred as practices are in accordance
During the concluded, procedures Therefore, past two years, QA audits/surveillances have except for a "few isolated cases,"
with N18-1 and personnel are fully qualified.
double asterisked have in fact been "in hand" when required.
Response to Violation le While the intent of Step 8.1.2-2 of maintenance
no generic programmatic problem exists.
procedure 12 THP 6030.IMP.014
(3) Date When Full Com liance Will Be Achieved Full compliance was achieved on December 6,
was to ensure that technicians
: 1989, when the
performing
'involved AEO was reinstructed of the "in hand" procedural requirement.
cleaning would utilize tape or similar adhesive-backed
 
material.Black electrical
===Response===
tape, was specified because it is a commonly available item.However, use of a calibration
to Violation lg Five procedures/instructions were cited in the Notice of Violation as not having been reviewed within the two-year limit established in plant procedure PMI-2010.
sticker did-constitute
However, in each case the documents had been reviewed and documentation to that effect was on file.
a violation of the procedure as written.(1)Corrective
Upon request one of the inspectors was provided with biannual review documents for IMP.071 and IMP.062.
Action Taken and Results Achieved Maintenance
The instruction does not require an approved revision within two
supervision
: years, only a review prior to such revision.
reviewed the net effect of utilizing the sticker in the course of cleaning and determined
This information may not have been adequately communicated.
that satisfactory
(1) Corrective Action Taken and Results Achieved Further review of the Notice of Violation by the plant identified that procedures/instructions noted had received review as required by PMI-2010, Rev.
results were obtained.No re-cleaning
17.
was deemed  
(2) Corrective Action Taken to Avoid Further Violation Tracking and review of procedures is presently adequate.
Attachment
(3) Date When Full Com liance Will Be Achieved No violation occurred.
2 to AEP:NRC:1125A
 
Page 6 necessary.
Attachment 2 to AEP:NRC:1125A Page 8
12 THP 6030.IMP.014
NRC Violation 2 "10 CFR 50, Appendix B, Criterion VIII, as implemented by Section 1.7.8 of the Donald CD Cook Operational Quality Assurance Program required that measures be established for the identification of materials, parts and components such as by part number, serial number, or other appropriate means on the item or records traceable to the item throughout fabrication, installation and use of the item."
had been revised via a change sheet initiated April 2, 1990, to remove reference to black electrical
"Contrary to the above, identification of materials and components for traceability was not accomplished for cable extension portions and aluminum splicing sleeves for connections to several safety-related motor control centers installed under the Request For Change 1482 modification (315/89031-02; 316/89031-02)."
tape.(2)Corrective
 
Action Taken To Avoid Further Violation The Plant Manager will issue a memo on procedural
===Response===
compliance
to Violation 2 RFC-1482 installed transition pieces (sleeves) to splice copper to aluminum cables in various motor control centers.
to ensure that all personnel are fully aware of the meaning of compliance, consequences
Per RFC instructions, the transition pieces were to be installed in accordance with Engineering Design Specification (EDS) 607 and EDS 608'he installation took place between June of 1979 and September of 1981 when the final summary was issued.
of failure and what actions to take when a procedure cannot be followed as written.The Maintenance
A search of the completed RFC package (including installation job orders) and of the microfilm of the completed job order packages revealed no documentation of the parts (sleeves) used for the installation.
Improvement
Individuals who were involved with the Maintenance Department at that time stated that personnel would have installed the transition pieces per the EDS as stated in the RFC.
Plan includes issuance of a department
Inadequate documentation of material installed by a Job Order during the design change process was the root cause of this violation.
policy on procedure compliance.
Additionally, there were inadequate review of the completed job orders and the design change package upon completion.
Included will be guidance on the monitoring
(1) Corrective Action Taken and Results Achieved The installation took place approximately 10 years ago and was performed in accordance with EDS 608, which was referenced in the RFC package.
of the effectiveness
Actual application for the past ten years has functionally demonstrated the adequacy of subject materials'
of procedure compliance.
 
Also a procedure writer'/user's
Attachment 2 to AEP:NRC:1125A Page 9
guide will address the circumstances
(2) Corrective Action Taken To Avoid Further Violation Current procurement/dedication practices ensure proper documentation is developed to demonstrate control over the suitability of material, parts and components.
for changing a procedure to ensure procedural
(3) Date When Full Com liance Will Be Achieved Current procedures/practice's should prevent recurrence of this problem and ensure future compliance.
compliance.
 
(3)Date When Full Com lienee Will Be Achieved The final draft of the policy will be issued on July 15, 1990.Guidance on the effectiveness
Attachment 2 to AEP:NRC:1125A Page 10 NRC Violation 3 "10 CFR 50, Appendix B, Criterion XI, as implemented by Section 1.7.11 of the Donald C.
monitoring
Cook Operational Quality Assurance Program required that a test program be established to assure testing to demonstrate that systems and components will perform satisfactorily in service in accordance with test procedures which incorporate requirements and acceptance limits contained in applicable design documents, and that adequate test instrumentation was available and used."
will be issued on August 15, 1990.The Plant Manager's memo will be issued on May 1, 1990.Response to Violation lf (1)Corrective
"Contrary to the above, test instruments were not sensitive or accurate enough to verify the calibration of the undervoltage relays that actuate the Emergency Diesel Generators.
Action Taken and Results Achieved The Auxiliary Equipment Operator (AEO)involved in this event had received training on the operation of reactor trip breakers and the existence of the procedure prior to this event.The AEO, however, overlooked
Procedure 2
the reactor trip breaker procedure was required to be"in hand" whenever performing
THP 6030 IMP.250, "4kV Diesel Start, 4kV ESS Bus Undervoltage Relay Calibration," Revision 7, Section 3.0, required the use of a Westinghouse type PA-161 AC anolog [sic]
racking operations.
voltmeter or its equivalent with equal or better accuracy and adequate range to measure the desired parameters.
Although the racking evolution was done in accordance
: However, the voltmeter had a tolerance of +1.5 volts that was not sufficiently accurate to measure the desired parameter of 90.3 to 91.8 volts specified in Technical Specification 3.3.2.
with the.procedure requirements, this event was a violation because the requirement
In
to have the procedure"in hand" was not satisfied.
: addition, the voltmeter indicated to the nearest whole volt and did not have division markings between the numbers.
A memorandum
Technicians had to interpolate results and record values to the nearest tenth of a volt while the voltmeter's dial indicator was moving in the increasing or decreasing direction.
was issued to Operations
Furthermore, the technicians used hand signals to communicate the moment the under voltage relay operated.
personnel on January 19, 1990, to remind them of the"in hand" requirement
Based on the inaccuracy and insensitivity of the voltmeter, and poor testing technique, results of the undervoltage test were not conclusive (315/89031-03; 316/89031-03)."
for the reactor trip breaker procedure.
 
(2)Corrective
===Response===
Action To Be Taken To Avoid Further Violation The routine surveillance
to Violation 3 The meter used was first specified in the original procedure developed before initial plant start-up.
procedures
The specific reasons for using this meter could not be determined.
for reactor trip breaker testing were revised on December 13, 1989, to reference the requirement
However, it is believed that this was the limit of the available technology at that time.
for having the reactor trip breaker racking procedure"in hand" for the racking evolutions.
The only other meter available was a basic digital type, which could not be used due to the inherently slow response and update time, causing a greater uncertainty of specific setpoint value than the analog meter.
The startup surveillance
 
procedures, which require racking of the reactor trip breakers, will be revised by June 4, 1990, to reference the requirement
Attachment 2 to AEP:NRC:1125A Page 11 (1) Corrective Actions and Results Achieved Z&C now uses the Fluke Model 45 digital meter during testing of the 4KV diesel start and 4KV ESS bus undervoltage relays.
for having the reactor trip breaker procedure"in hand."  
Recent developments in digital meters which include faster response times and update times and minimum/maximum modifier features has made their use acceptable.
The digital meter currently being used has an accuracy of + 0.3 percent.
Attachment
The previous test method provided acceptable
2 to AEP:NRC:1125A
: results, based on the as-found values on the first use of the digital meters being in specification by comparable percentages.'2)
Page 7 During the concluded, procedures
Corrective Actions Taken To Avoid Further Violation The calibration procedures which currently allow use of either analog or digital meters will be changed to specify the use of the Fluke Model 45 digital meter, or its equivalent, to ensure consistent use of a digital meter.
Therefore, past two years, QA audits/surveillances
(3) Date When Full Com lienee Will Be Achieved The procedure changes will be completed before April 30, 1990.
have except for a"few isolated cases," double asterisked
 
have in fact been"in hand" when required.no generic programmatic
~
problem exists.(3)Date When Full Com liance Will Be Achieved Full compliance
~
was achieved on December 6, 1989, when the'involved AEO was reinstructed
 
of the"in hand" procedural
Attachment 2 to AEP:NRC:1125A Page 12 NRC. Violation 4 "10 CFR 50, Appendix B, Criterion XVI, as implemented in Section 1.7.16 of the Donald C.
requirement.
Cook Operational Quality Assurance Program required that measures be established to assure that conditions adverse to quality were promptly identified and corrected.
Response to Violation lg Five procedures/instructions
In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition was determined and corrective action taken to preclude repetition.
were cited in the Notice of Violation as not having been reviewed within the two-year limit established
"Contrary to the above:
in plant procedure PMI-2010.However, in each case the documents had been reviewed and documentation
The Plant Assessment Group Committee's review in March 1989 for Problem Report 89-245, concerned with the February 1989 failure of two safety-related 4kV breakers T-11D6 and T-1104 to close on demand during tests due to lubrication hardening, failed to specify corrective action to prevent recurrence.
to that effect was on file.Upon request one of the inspectors
Furthermore, no action was taken to inspect other 4kV breakers for common mode failure.
was provided with biannual review documents for IMP.071 and IMP.062.The instruction
Consequently, in March and April of 1989 seven additional safety related and balance of plant breakers failed to close during
does not require an approved revision within two.years, only a review prior to such revision.This information
: testing, which was also caused by hardening of the lubricant on the breaker linkage (315/89031-04A; 316/89031-04A).
may not have been adequately
b.
communicated.
Corrective action was neither prompt nor adequate to correct maintenance related'roblems identified by the licensee in February 1988.
(1)Corrective
In December
Action Taken and Results Achieved Further review of the Notice of Violation by the plant identified
: 1989, 36 of these 71 self identified findings and recommendations were reopened.
that procedures/instructions
During this inspection many of the same problems were identified that reflect a significant weakness in the corrective action system (315/89031-04B; 316/89031-04B)."
noted had received review as required by PMI-2010, Rev.17.(2)Corrective
 
Action Taken to Avoid Further Violation Tracking and review of procedures
===Response===
is presently adequate.(3)Date When Full Com liance Will Be Achieved No violation occurred.  
to Violation 4a Based on review of Problem Report 89-245, which was addressed in the Notice of Violation it is our position that no actual violation occurred.
Attachment
The February 27, 1989, condition was identified during scheduled 'preventive maintenance work and resulted in the problem report.
2 to AEP:NRC:1125A
That discovery, coupled with a similar condition also found during preventive maintenance, resulted in a Part 21 report.
Page 8 NRC Violation 2"10 CFR 50, Appendix B, Criterion VIII, as implemented
The Part 21 investigation revealed that vendor-specified information contained no instruction for periodic lubrication of the breakers.
by Section 1.7.8 of the Donald CD Cook Operational
Similar breakers used in the plant had, until that time, passed test requirements'he plant's actions which were taken promptly, included revision of the procedure based on new input from the manufacturer, initiation of Job Orders to inspect all other similar breakers installed in both units, and establishment of scheduled inspections to identify possible repetition of the
Quality Assurance Program required that measures be established
 
for the identification
C. I 1
of materials, parts and components
 
such as by part number, serial number, or other appropriate
Attachment 2 to AEP:NRC:1125A Page 13 condition in the future.
means on the item or records traceable to the item throughout
The Notice of Violation incorrectly concluded that no action was taken to inspect additional breakers or develop corrective action.
fabrication, installation
Two subsequent problem reports were initiated as a result of deficiencies found in the inspections and tests covered by our expanded action for Problem Report 89-245 and the associated Part 21 review.
and use of the item.""Contrary to the above, identification
Those reports were initiated to document the similar conditions on the noted breakers.
of materials and components
Within two months of the March 1,
for traceability
: 1989, Part 21 report to the NRC, the plant had completed the inspections, cleaned and relubricated the breakers in both units as recommended by the revised vendor information, and documented each case when a similar condition was found.
was not accomplished
(1) Corrective Action Taken and Results Achieved The result of Problem Report 89-245, which was reviewed by the Plant Assessment Group on March 17,
for cable extension portions and aluminum splicing sleeves for connections
: 1989, was to inspect, clean and lubricate similar breakers in both units and document the results.
to several safety-related
(2) Corrective Action Taken to Avoid Further Violation Procedure changes and inspections were scheduled as a result of addressing the problem reported in Problem Report 89-245 on similar breakers.
motor control centers installed under the Request For Change 1482 modification
These actions generated additional Job Orders and condition reports which were referenced in the inspection report.
(315/89031-02;
(3) Date When Full Com liance Will Be Achieved No violation occurred.
316/89031-02)." Response to Violation 2 RFC-1482 installed transition
 
pieces (sleeves)to splice copper to aluminum cables in various motor control centers.Per RFC instructions, the transition
===Response===
pieces were to be installed in accordance
to Violation 4b As discussed in our response to Weakness (1),
with Engineering
AEP has taken numerous corrective actions to address the problems identified by the Maintenance Self-Assessment.
Design Specification (EDS)607 and EDS 608'he installation
These actions include:
took place between June of 1979 and September of 1981 when the final summary was issued.A search of the completed RFC package (including
o the development of a RCM Program o
installation
the acquisition of the Nuclear Plant Maintenance (NPM)
job orders)and of the microfilm of the completed job order packages revealed no documentation
Module o
of the parts (sleeves)used for the installation.
the development of a System Engineer Program o
Individuals
the acquisition of NUS's PRONET and the servt.ces of NUS's procedure writers.
who were involved with the Maintenance
 
Department
Attachment 2 to AEP:NRC:1125A Page 14 In order to effectively implement programs as encompassing and comprehensive as these, significant analysis, planning and coordination are needed.
at that time stated that personnel would have installed the transition
As such, it will take several years to completely implement some of the corrective actions we have initiated.
pieces per the EDS as stated in the RFC.Inadequate
(1) Corrective Actions and Results Achieved Maintenance-related problems identified in the Maintenance Self-Assessment will be reviewed and resolved as appropriate, with implementation of the Maintenance Improvement Plan.
documentation
(2) Corrective Actions Taken to Avoid Further Violation The Improvement Plan includes milestones and a built-in mechanism that requires regular re-evaluation of the plan and monitoring of its effectiveness to ensure that it is providing the desired results and that there is continuing improvement in all maintenance-related areas'3)
of material installed by a Job Order during the design change process was the root cause of this violation.
Date When Full Com liance Will Be Achieved Resolution and documentation of the identified items will be completed by June 1,
Additionally, there were inadequate
1991.}}
review of the completed job orders and the design change package upon completion.
(1)Corrective
Action Taken and Results Achieved The installation
took place approximately
10 years ago and was performed in accordance
with EDS 608, which was referenced
in the RFC package.Actual application
for the past ten years has functionally
demonstrated
the adequacy of subject materials'  
Attachment
2 to AEP:NRC:1125A
Page 9 (2)Corrective
Action Taken To Avoid Further Violation Current procurement/dedication
practices ensure proper documentation
is developed to demonstrate
control over the suitability
of material, parts and components.
(3)Date When Full Com liance Will Be Achieved Current procedures/practice's
should prevent recurrence
of this problem and ensure future compliance.  
Attachment
2 to AEP:NRC:1125A
Page 10 NRC Violation 3"10 CFR 50, Appendix B, Criterion XI, as implemented
by Section 1.7.11 of the Donald C.Cook Operational
Quality Assurance Program required that a test program be established
to assure testing to demonstrate
that systems and components
will perform satisfactorily
in service in accordance
with test procedures
which incorporate
requirements
and acceptance
limits contained in applicable
design documents, and that adequate test instrumentation
was available and used.""Contrary to the above, test instruments
were not sensitive or accurate enough to verify the calibration
of the undervoltage
relays that actuate the Emergency Diesel Generators.
Procedure 2 THP 6030 IMP.250,"4kV Diesel Start, 4kV ESS Bus Undervoltage
Relay Calibration," Revision 7, Section 3.0, required the use of a Westinghouse
type PA-161 AC anolog[sic]voltmeter or its equivalent
with equal or better accuracy and adequate range to measure the desired parameters.
However, the voltmeter had a tolerance of+1.5 volts that was not sufficiently
accurate to measure the desired parameter of 90.3 to 91.8 volts specified in Technical Specification
3.3.2.In addition, the voltmeter indicated to the nearest whole volt and did not have division markings between the numbers.Technicians
had to interpolate
results and record values to the nearest tenth of a volt while the voltmeter's
dial indicator was moving in the increasing
or decreasing
direction.
Furthermore, the technicians
used hand signals to communicate
the moment the under voltage relay operated.Based on the inaccuracy
and insensitivity
of the voltmeter, and poor testing technique, results of the undervoltage
test were not conclusive
(315/89031-03;
316/89031-03)." Response to Violation 3 The meter used was first specified in the original procedure developed before initial plant start-up.The specific reasons for using this meter could not be determined.
However, it is believed that this was the limit of the available technology
at that time.The only other meter available was a basic digital type, which could not be used due to the inherently
slow response and update time, causing a greater uncertainty
of specific setpoint value than the analog meter.  
Attachment
2 to AEP:NRC:1125A
Page 11 (1)Corrective
Actions and Results Achieved Z&C now uses the Fluke Model 45 digital meter during testing of the 4KV diesel start and 4KV ESS bus undervoltage
relays.Recent developments
in digital meters which include faster response times and update times and minimum/maximum
modifier features has made their use acceptable.
The digital meter currently being used has an accuracy of+0.3 percent.The previous test method provided acceptable
results, based on the as-found values on the first use of the digital meters being in specification
by comparable
percentages.'2)
Corrective
Actions Taken To Avoid Further Violation The calibration
procedures
which currently allow use of either analog or digital meters will be changed to specify the use of the Fluke Model 45 digital meter, or its equivalent, to ensure consistent
use of a digital meter.(3)Date When Full Com lienee Will Be Achieved The procedure changes will be completed before April 30, 1990.  
~~  
Attachment
2 to AEP:NRC:1125A
Page 12 NRC.Violation 4"10 CFR 50, Appendix B, Criterion XVI, as implemented
in Section 1.7.16 of the Donald C.Cook Operational
Quality Assurance Program required that measures be established
to assure that conditions
adverse to quality were promptly identified
and corrected.
In the case of significant
conditions
adverse to quality, the measures shall assure that the cause of the condition was determined
and corrective
action taken to preclude repetition."Contrary to the above: The Plant Assessment
Group Committee's
review in March 1989 for Problem Report 89-245, concerned with the February 1989 failure of two safety-related
4kV breakers T-11D6 and T-1104 to close on demand during tests due to lubrication
hardening, failed to specify corrective
action to prevent recurrence.
Furthermore, no action was taken to inspect other 4kV breakers for common mode failure.Consequently, in March and April of 1989 seven additional
safety related and balance of plant breakers failed to close during testing, which was also caused by hardening of the lubricant on the breaker linkage (315/89031-04A;
316/89031-04A).
b.Corrective
action was neither prompt nor adequate to correct maintenance
related'roblems
identified
by the licensee in February 1988.In December 1989, 36 of these 71 self identified
findings and recommendations
were reopened.During this inspection
many of the same problems were identified
that reflect a significant
weakness in the corrective
action system (315/89031-04B;
316/89031-04B)." Response to Violation 4a Based on review of Problem Report 89-245, which was addressed in the Notice of Violation it is our position that no actual violation occurred.The February 27, 1989, condition was identified
during scheduled'preventive
maintenance
work and resulted in the problem report.That discovery, coupled with a similar condition also found during preventive
maintenance, resulted in a Part 21 report.The Part 21 investigation
revealed that vendor-specified
information
contained no instruction
for periodic lubrication
of the breakers.Similar breakers used in the plant had, until that time, passed test requirements'he
plant's actions which were taken promptly, included revision of the procedure based on new input from the manufacturer, initiation
of Job Orders to inspect all other similar breakers installed in both units, and establishment
of scheduled inspections
to identify possible repetition
of the  
C.I 1  
Attachment
2 to AEP:NRC:1125A
Page 13 condition in the future.The Notice of Violation incorrectly
concluded that no action was taken to inspect additional
breakers or develop corrective
action.Two subsequent
problem reports were initiated as a result of deficiencies
found in the inspections
and tests covered by our expanded action for Problem Report 89-245 and the associated
Part 21 review.Those reports were initiated to document the similar conditions
on the noted breakers.Within two months of the March 1, 1989, Part 21 report to the NRC, the plant had completed the inspections, cleaned and relubricated
the breakers in both units as recommended
by the revised vendor information, and documented
each case when a similar condition was found.(1)Corrective
Action Taken and Results Achieved The result of Problem Report 89-245, which was reviewed by the Plant Assessment
Group on March 17, 1989, was to inspect, clean and lubricate similar breakers in both units and document the results.(2)Corrective
Action Taken to Avoid Further Violation Procedure changes and inspections
were scheduled as a result of addressing
the problem reported in Problem Report 89-245 on similar breakers.These actions generated additional
Job Orders and condition reports which were referenced
in the inspection
report.(3)Date When Full Com liance Will Be Achieved No violation occurred.Response to Violation 4b As discussed in our response to Weakness (1), AEP has taken numerous corrective
actions to address the problems identified
by the Maintenance
Self-Assessment.
These actions include: o the development
of a RCM Program o the acquisition
of the Nuclear Plant Maintenance (NPM)Module o the development
of a System Engineer Program o the acquisition
of NUS's PRONET and the servt.ces of NUS's procedure writers.  
Attachment
2 to AEP:NRC:1125A
Page 14 In order to effectively
implement programs as encompassing
and comprehensive
as these, significant
analysis, planning and coordination
are needed.As such, it will take several years to completely
implement some of the corrective
actions we have initiated.
(1)Corrective
Actions and Results Achieved Maintenance-related
problems identified
in the Maintenance
Self-Assessment
will be reviewed and resolved as appropriate, with implementation
of the Maintenance
Improvement
Plan.(2)Corrective
Actions Taken to Avoid Further Violation The Improvement
Plan includes milestones
and a built-in mechanism that requires regular re-evaluation
of the plan and monitoring
of its effectiveness
to ensure that it is providing the desired results and that there is continuing
improvement
in all maintenance-related
areas'3)Date When Full Com liance Will Be Achieved Resolution
and documentation
of the identified
items will be completed by June 1, 1991.
}}

Latest revision as of 13:33, 7 January 2025

Responds to NRC Re Violations Noted in Insp Repts 50-315/89-31 & 50-316/89-31.Corrective Actions:Reliability Centered Maint Program Initiated
ML17334B364
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 04/11/1990
From: Alexich M
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To: Davis A
NRC OFFICE OF INFORMATION RESOURCES MANAGEMENT (IRM)
References
AEP:NRC:1125A, NUDOCS 9004200632
Download: ML17334B364 (38)


Text

\\

r Indiana 'Achrga~

Power Company~

~ 0 80 c'.663'Nl7lAMA NTCHIGAN POWER AEP:NRC:1125A Donald C.

Cook Nuclear Plant Units 1 and 2

Docket Nos.

50-315 and 50-316 License Nos.

DPR-58 and DPR-74 NRC INSPECTION NOS.

50-315/89031 AND 50-316/89031:

RESPONSE

TO VIOLATION U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D.C.

20555 Attn: A. B. Davi.s April ll, 1990

Dear Mr. Davis:

This letter is in response to Mr. H. J. Miller's letter dated March 1, 1990, which forwarded the report on the special maintenance team inspection conducted by Mr. Z. Falevits and others of your staff.

This inspection was conducted from December 4 through 8, and December 18 through 22,

1989, on activities at the Cook Nuclear Plant associated with the support and implementation of maintenance to ensure that plant structures, systems and components reliably perform on demand.

The Notice of Violation attached to Mr. Miller's letter identified six weaknesses and four Severity Level IV violations relating to our maintenance program.

The weaknesses are addressed in Attachment 1 to this letter.

The violations are addressed in Attachment 2 to this letter.

A 14-day extension for our response was granted on March 15, 1990

'his document has been prepared following Corporate procedures that incorporate a reasonable set of controls to ensure its accuracy and completeness prior to signature by the undersigned.

Sincerely, M. P. Al ich Vice President ldp Attachments

~)g4QOCk&2 90041 1 pgg ADQcK o>oog+~~

~

I pp 1/00

Mr. A. B. Davis AEP:NRC:1125A cc:

D.

H. Williams, Jr.

A. A. Blind - Bridgman R.

C. Callen G. Charnoff NRC Resident Inspector

- Bridgman NFEM Section Chief

ATTACHMENT 1 TO AEP:NRC:1125A

RESPONSE

TO NRC-IDENTIFIED WEAKNESSES

Attachment 1 to AEP:NRC:1125A Page 1

NRC-Identified Weakness (1)

"Lack of or ineffective action to correct numerous self identified maintenance problems identified in February

1988, many of which were identified by the team during this inspection."

Response

to Weakness (1) Corrective Actions Taken As a result of the 1988 Maintenance Self-Assessment

Report, AEPSC contracted IMPELL to assist in identifying and formulating appropriate corrective actions to address the self-identified deficiencies.

The results of thi,s effort are in a document

entitled, D.

C.

Cook Plant PM Pro ram U

rade Strate

Document, dated November 1988.

This study contained a strategy for AEP to accomplish a planned upgrade of the Preventive Maintenance (PM)

Program at the Cook Nuclear Plant.

It identified reasonable goals and achievable objectives for the PM Upgrade Program based on AEPSC/Cook Nuclear Plant philosophy, resources and capabilities.

The specific implementation tasks and strategic considerations were presented for obtaining the desired upgrade results.

This effort'ot only addressed improvements in the PM Program itself, but also examined related organization and automation requirements to support the improved PM Program.

Based on the results of this study, numerous corrective actions were initiated in January 1989.

The first was the initiation of a reliability-centered maintenance (RCM) program.

This major task has two phases:

analysis and implementation.

AEPSC has been working closely with General Physics on the analysis portion that will form the foundation of the RCM program.

This work includes:

defining system boundaries and functions identifying dominant failure modes determining criti.cal failure modes and criti.cal components identifying applicable and effective preventive maintenance tasks to prevent failures completing analysis of selected plant systems

Attachment 1 to AEP:NRC:1125A Page 2

Implementation of the RCM Program began in August 1989 with the development of plant procedures, identification of system boundaries, and establishment of an RCM database.

The first syst: em analysis was completed in February 1990 on the feedwater system.

Analysis of 22 additional plant systems/functional areas will take place over the next three years.

Another outgrowth of the Maintenance Self-Assessment Report and the AEPSC/IMPELL study was the development of the System Engineer Program.

The goal of the System Engineer Program is to provide training to enable individuals to provide the engineering expertise required for safe, efficient and reliable operation of systems for which they are responsible.

The System Engineer discharges this responsibility by performing assigned

tasks, and maintaining cognizance of all work associated with the assigned system(s).

In addition, AEPSC contracted TENERA Systems and Software to provide a computerized maintenance management information system.

This system, referred to as the Nuclear Plant Maintenance Module (NPM) System, discussed in more detail in our response to weakness (3), will allow plant staff to initiate, issue, prioritize and track all maintenance work at the plant.

This same software is currently being used at Pacific Gas and Electric's Diablo Canyon, and Public Service Electric and Gas's Salem and Hope Creek Generating Stations.

In addition, it was recently chosen by Electricite de France for use in all fifty of its nuclear plants.

These three programs, RCM, System Engineer and NPM, are just part of the actions that are being taken to respond to the Self-Assessment.

The November 1989 reorganization of Cook Nuclear Plant's management is another important element in the upgrade of our maintenance program.

The intent of the new organization is to place emphasis on maintenance,

outages, and human'resources, Other actions, which have or are being taken are as follows:

o An AEP and Cook Nuclear Plant policy on maintenance was developed and approved in December 1989 by AEP senior management.

An additional plant-specific maintenance policy established in accordance with INPO guidelines is being developed to clarify maintenance philosophies and responsibilities for all maintenance groups

Attachment 1 to AEP:NRC:1125A Page 3

o Corporate reviews have been conducted, which have resulted in improvements being made to shop areas used by the maintenance groups o

Staffing studies are being performed, which have already resulted in an increase in the number of engineers and radiation protection technicians on site.

o Other programs of note that address maintenance self-assessment findings include the maintenance procedure rewrite (See Weakness (6)), the long-range plan and the outage guideline development plan.

(2) Benefits To Be Derived From Corrective Actions RCM, the System Engineer Program and NPM were initiated to address many of the Maintenance Self-Assessment's identified deficiencies.

When all of our efforts have been completely implemented, each of the major findings of the self assessment will have been addressed.

,As a result of these corrective actions. we anticipate having a

state of the art maintenance program which will result in improved plant safety, reliability and accountability.

(3) Date When Benefits Vill Be Realized As previously stated, we started the RCM Program in August 1989.

However, we anticipate that the program will not be completely implemented for all the critical plant systems until the end of 1992.

As each system is analyzed, benefits will be realized so that when this program is completed we will have a fully integrated preventive maintenance program.

The System Engineer Program, like RCM, is still in the early stages of implementation.

A document which clearly delineates the responsibilities of the engineers is currently in the final stages of review and approval.

AEPSC's acquisition of TENERA's NPM system was approved in December 1989.

However, it will not be in place and operational until August 1990, when data will be entered.

Ve will be conducting QA audits or surveillances to access the status and effectiveness of some of our corrective actions as they develop.

In addition, the Maintenance Improvement Plan will review and resolve, as appropriate, the Maintenance Self-Assessment items'he Improvement Plan includes milestones and a built-in mechanism that requires regular re-evaluation.

Attachment 1 to AEP:NRC:1125A Page 4

While we are already realizing benefits from our efforts, we do not anticipate the full benefit for several years.

In order to effectively implement programs as encompassing and comprehensive as these, significant analysis, planning and coordination are needed.

As a result, their benefits will not be fully realized until mid 1993.

Attachment 1 to AEP:NRC:1125A Page 5

NRC-Identified Weakness (2)

"An ineffective preventive maintenance program that resulted, for example, in failures of 4KV circuit breakers"

Response

to Weakness We concur that the Preventive Maintenance Program can be improved and, as previously discussed, we are taking steps to do so.

However, Cook Nuclear Plant's availability in 1989 is evidence that the present preventive maintenance program is effective.

During 1989, Cook Nuclear Plant generated 12 million net MWHRS, the most since 1984.

The 69.3% availability for Unit 1 in 1989 contributed to an average availability of 79.4%

since 1985 'lthough Unit 2 overall availability has not been as high due to steam generator tube degradatidn, its 74.4%

availability in 1989 was the highest since 1983.

On December 8, the 111-day record for the longest run with both units operating was broken.

This record was extended to 140 days when Unit 2 was brought off-line for a surveillance outage on January 6,

1990.

Unit 1 ended 1989 with its longest run of 175 days and continued operating until March 17, 1990 (a Cook Nuclear Plant record run of 251 days) when the unit was brought off line for a planned surveillance outage.

As discussed in our response to NRC violation (2) of the inspection report, the 4KV circuit breakers failure was detected during preventive maintenance testing.

As a result, appropriate corrective action was.subsequently taken which resulted in improvements to our 4KV breakers.

Also, we notified the industry of the problem via a Part 21 report.

Attachment 1 to AEP:NRC:1125A Page 6

NRC-Identified Veakness (3)

"An extensive backlog of non-outage corrective maintenance job orders partly caused by lack of integrated planning and scheduling methodology."

Response

to Weakness "Maintaining the Cook Nuclear Plant involves the completion of approximately 20,000 Job Orders annually.

The relative priorities of jobs change frequently due to a number of factors, the primary reason being plant conditions.

Managing the information contained within the backlog of yet-to-be completed Job Orders can be critical to plant availability and reliability.

These efforts are presently hampered by the logistics of paper filing systems and computer tracking systems that lack needed flexibilityin hardware and software.

(1) Corrective Actions Taken The Cook Nuclear Plant Information Management System (IMS) plan, approved for development in February of 1989 identified nine computer system modules that, when completed, will form a single, integrated information management system.

This automated information system will be used by both plant site and corporate personnel to support plant operation and maintenance.

It will provide for the scheduling and initiation of maintenance tasks and support the assignment of responsibilities and accountabilities for these tasks.

Specifically, for maintenance, the Nuclear Plant Maintenance Module (NPM) of the Cook Nuclear Plant's IMS plan will allow plant staff to initiate, issue, prioritize, and track all maintenance work at the plant.

The NPM module of the IMS plan will also maintain a history of maintenance work.

The primary objectives of the NPM module are to improve plant availability and to optimize the use of plant resources with the overall goal of reducing plant maintenance.

The NPM system is designed to allow any NPM user to initiate a structured request that the user believes should be reviewed and, if warranted, acted upon.

This action request feature provides a process for screening those actions requiring work, and will serve as a focal point for initiating and tracking Job Orders.

Plant personnel will enter data into the NPM system defining the component that needs work and briefly describing that work.

The system is designed to eliminate all paper in this process except the actual Job Order itself.

Attachment 1 to AEP:NRC:1125A Page 7

The reviews that take place in the Job Order system are performed on-line.

This on-line capability allows for pending Job Orders to be sorted in various ways and the reviewing individuals have'mmediate access to this information.

Once reviews are performed the actual Job Orders can be printed for the work to be performed.

Once a Job Order has been initiated, starting from the very first entry into the system and not just from the time it gets

printed, the Job Order processing system can track the status of the Job Order.

This is accomplished through the use of status code fields.

Some of the codes represent situations such as waiting for materials, or waiting for approval of the reviews, or other types of conditions.

This feature is very helpful for planning and scheduling the many Job Orders in the system.

The NPM system will permit the plant staff to assign specific Job Orders, at the activity level, to a scheduled

date, crew and supervisor.

Upon completion'f the crew assignments and confirmation of permit requirements, the system produces a

supervisory assignment report and prints the Job Order.

The completed work package includes the Job Order, equipment descriptions, parts list, and testing forms along with other needed documents.

Once the work related to a Job Order has been completed and

tested, the Job Order is reviewed and closed out, on-line.

The NPM system maintains a complete history of all completed and closed-out Job Orders.

This feature allows for rapid access to all history on Job Orders.

The NPM system prevents a Job Order from being closed-out until all reviews and tests have been completed.

Zn addition, the NPM system will be a repository for previous repetitive tasks.

This function eliminates the need for individuals to recreate Job Orders that are repetitive in

nature, The NPM system will automatically generate the Job Orders,, according to the appropriate due dates, or as directed by a planner.

The NPM system will also provide for continuous monitoring of surveillance tests and preventive maintenance work to meet regulatory or plant requirements.

Once the repetitive or preventive maintenance Job Orders are

created, they are available for reviews and executions in the same manner as any of the other Job Orders.

This system will also be used to develop Job Orders for planned outages such as refueling outages.

Attachment 1 to AEP:NRC:1125A Page 8

(2) Benefits To Be Derived From Corrective Actions The data entered into the NPM system, and the processing that the system does with this data, will eliminate the multiple manual data entry steps of our present process.

Eliminating redundant manual systems is of significance itself.

However, more importantly are the anticipated improvements in plant availability and labor productivity.

Along with improved ability to plan and schedule work comes an increased amount of time available for more careful consideration of other aspects of the work to be performed, for

example, personnel safety.

Improvements can be expected and will certainly be strived for.

The NPM system will also identify and coordinate maintenance on related equipment and systems, thus decreasing down time on components removed from service.

Quick access to the information in the NPM data bases makes the supervisors in both the operations and maintenance areas more aware of Job Order progress.

It is anticipated that the NPM system w'ill help us realize our goal of a non-outage corrective maintenance job order backlog not in excess of 90 days.

(3) Date When Benefits Will Be Achieved We currently anticipate having the computerized automated maintenance system in place and operational by August 1990.

At that time, data validation and loading, procedure changes and training of personnel will begin.

Attachment 1 to AEP:NRC:1125A Page 9

NRC-Identified Weakness (4)

"Poor material condition especially as evidenced by the high number of oil, steam and water leaks."

Response

to Weakness (1) Corrective Actions Taken While it is AEPSC's policy to keep all of its facilities, in good material condition, we recognize the need for improvement in this area.

As a result, the management of the Cook Nuclear Plant has launched a concerted effort to improve plant material condition.

This is evidenced by the allocation of funds to support the following physical improvements that are currently taking place:

o Auxiliary building painting o

Contaminated equipment storage area expansion I

o Decontamination area redesign o

Improved lighting o

Installation of 18 personnel whole body contamination monitors It is Cook Nuclear Plant policy that no leak is considered acceptable.

Consequently, during the 1988/1989 refueling outages we refurbished about 1,780 valves and packed them with Chesterton packing.

A breakdown of this effort is as follows:

Unit 1 Unit 2 Total Auxiliary Building Containment Turbine Hall Miscellaneous 254 130 225 21 150 280 700 925 50 71 250 504 Nevertheless, a substantial number of leaks still exist in the auxiliary building, ranging from small traces of dried boric acid to dripping.

These leaks have been entered into a computer data base, have been chalked

down, and job orders have been written.

The leaks are currently being prioritized and efforts will be made to repair them during the next refueling outage, if not before.

Attachment 1 to AEP:NRC:1125A Page 10 The plant manager has reaffirmed his commitment to good plant material condition and personal accountability by sending a

memorandum to each employee.

This commitment has been supported by continued radiation worker awareness

training, and operator training on venting and draining.

In addition, decontamination efforts continue, which have already reduced the contaminated area from approximately 45,000 feet in 1986 to the current 25,000 feet (excluding laydown areas).

Our goal is to reduce these contaminated areas to 20,000 square feet in 1990 and 10,000 square feet prior to the outage in 1991.

(2) Benefits To Be Derived from Corrective Actions There are numerous benefits gained from having the plant in good physical condition, the most important of these being increased plant safety and reliability.

A related benefit is improved radiation protection and worker safety.

However, another important, but less quantifiable benefit is the improvement to worker morale.

(3) Date When Benefits Will Be Realized While maintaining the plant in good physical condition is an ongoing process, we anticipate major improvements within the next year.

The refueling outage will facilitate the refurbishment of valises, as well as other repairs and modifications.

Attachment 1 to AEP:NRC:1125A Page 11 NRC-Identified Weakness (5)

"Inadequate trending, root cause analysis and action to correct, for example, numerous leaking safety relief valves."

Response

to Weakness (1) Corrective Actions Taken This weakness is being addressed by three programs:

the NPM system which is discussed in detail in our response to weaknesses (1) and (3), the System Engineer

Program, discussed in our response to weakness (1), and the RCM Program discussed in our response to weakness (1).

(2) Benefits To Be Derived from Corrective Actions The NPM system will provide for a complete component history.

The component history will provide a chronological listing of work, modifications or inspections that have been performed on a particular component.

This process creates an indexed historical record for components or functional equipment groups and catalogs completion dates, failure codes, as-found and as-left conditions, parts replaced, test results, etc.

The System Engineers are expected to identify and trend appropriate system parameters, with the goal of obtaining pertinent data for system performance and reliability monitoring.

The parameters trended shall be periodically reviewed and approved to allow timely preventive or corrective actions to be implemented.

Based on the trended data, the System Engineer is expected to recognize significant system/component degradation or abnormal operating conditions from both a historical basis, as well as current status.

The System Engineer may require the support of technical experts to analyze specific areas of concern and will work closely with our Corporate Nuclear Engineering Division engineers in this regard.

The System Engineers are expected to perform root cause analyses on the systems assigned.

Consequently, the System Engineers will be trained in root cause analysis.

In addition, the System Engineer is expected to:

Evaluate system/component failure impact on plant safety and unit power operations Prepare and perform special system/component performance tests.

Attachment 1 to AEP:NRC:1125A Page 12 The RCM Program wt.ll contribute to resolving this issue by identifying dominant failure modes and critical components.

(3) Date When Benefits Will Be Realized As previously stated, we expect the NPM system to be in place and operational in August 1990.

At that time, personnel training and data loading will begin.

Several system engineers have been assigned at Cook Nuclear Plant and benefits have already been realized from this program.

An effort is currently being made to recruit System Engineers.

However, we anticipate it will take at least a year before the program is fully staffed.

Attachment 1 to AEP:NRC:1125A Page 13 NRC-Identified Weakness (6)

"In several instances procedures were not followed, were poor or did not exist especially in the balance of plant area."

Response

to Weakness (1) Corrective Actions Taken Key to the safe and efficient operation of any nuclear power plant is strict adherence to procedures.

As such, employees are shown during the Nuclear General Employee Training (NGET)

classes, a videotape of David Williams, Jr.,

Senior Executive V.P., Engineering and Construction, mandating the adherence to procedures.

It is AEPSC's long-standing policy that failure to follow procedures will result in disciplinary action.

In order for this policy to have any benefit, well-written and accurate procedures must be in place.

Consequently, AEPSC is purchasing PRONET and the services of consultant procedure writers to upgrade or write 690 maintenance procedures (268 maintenance, 422 I&C).

Critical balance of plant components will be addressed as they arise in the RCM program.

The Maintenance Improvement Plan provides guidance that clearly defines what procedure compliance is.

In addition, a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.

(2) Benefits To Be Derived from Corrective Actions PRONET is a state of the art computer system that integrates writer's guidelines, word processing, graphics and data base functions into a centralized procedure management system.

Development, commitment, scheduling and reporting functions will be controlled by this menu-driven network.

This integrated approach will result in a program that reduces development time and provides efficient long-term procedure maintenance and commitment/reference tracking.

(3) Date When Benefits Will Be Realized Although a consultant will train plant staff on the use of

PRONET, the bulk of the procedure upgrade work will be performed by consultant personnel.

By using contract workers we will not impact the plant staff. If the existing staff were used, it is anticipated that the effort would take four to five years.

This is considered to be an unacceptable time frame for this work.

By using contract workers, we will obtain professionally prepared procedures in a reasonable time frame.

The effort is scheduled to be completed by December 1991.

ATTACHMENT 2 TO AEP:NRC:1125A

RESPONSE

TO NRC-IDENTIFIED VIOLATIONS

Attachment 2 to AEP:NRC:1125A Page 1

NRC Violation 1 "10 CFR 50, Appendix B, Criterion V, as implemented by Section 1.7.5 of the Donald C.

Cook Nuclear Plant Operational Quality Assurance Program requires that activities related to quality be prescribed by documented instructions, procedures, and drawings, that those activities be accomplished in accordance with those instructions, procedures and drawings, and that instructions, procedures or drawings include appropriate quantitative or qualitative acceptance criteria for determining that important activt,ties have been satisfactorily accomplished.

a

~

Procedure PMI-2290, "Job Orders," Revision 8, required in Sections 4.4.8 and 4.4.8.3 that upon completion of the physical work, the job order tags be removed and discarded.

Contrary to the abo~e, tags

15119, 029643,
B012209, B016950,
B016832, and B017240 were not removed although the job orders were cancelled or completed.

As a result, status of equipment condi.tion remained indeterminate (315/89031-01A; 316/89031-01A)

~

b.

Request For Change 12-2180 required installation of 200%

overload motor protection and that the thermal overload be set at the low trip current rating.

Contrary to the above, on December 19,

1989, the inspectors observed that the thermal overload heater associated with residual heat removal loop isolation motor-operated valve ICM-111 was set at the high trip current rating.

Numerous additional thermal overloads in the diesel generator motor control center were also observed to be the wrong size or set at the wrong current rating, which will result in premature removal of operating voltage from the motors (315/89031-01B; 316/89031-01B)

~

c

~

Procedure PMI-2030, "Document Control," Revision 10, failed to include requirements for the Master Drawing Indexes to be reviewed by intended users for the latest as built drawings located in the plant master file.

Consequently, drawings issued by the document control center for field verifications were not the latest as built drawings or revisions (315/89031-01C; 316/89031/01C).

The "Pump Operator's Data" manual and the vendor manual for'he Auxiliary Feedwater (AFV) pump required that the pump packing be adjusted while the pump is operating.

Contrary to the above, this requirement was not incorporated into the AFV maintenance procdures

[sic).

Although no problems were noted, inadequate attention to this requirement could result in rotor seizure, scored shaft sleeves, or burned packing (315/89031-01D; 316/89031-01D).

Attachment 2 to AEP:NRC:1125A Page 2

Procedure 12 THP 6030 IMP.014 "Protective Relay Calibration", Revision 8, Step 8.1.2-2 specified that black electrical tape be used when cleaning the disk and drag magnet mechanism on Time Overcurrent (IAC) relays.

Contrary to the above, on December 5,

1989, a technician was observed using an unused calibration sticker to clean the 2AB EDG Time Overcurrent test relay.

As a result, cleanliness of the contacts was questionable (315/89031-01E; 316/89031-01E).

f.

Procedure PMI-2010 "Plant Manager and Department Head Instructions, Procedures and Index," Revision 17, Policy Statement 3.1, Section 3 required that "double asterisked" procedures for plant activities be "in-hand" when implementing the procedure.

Contrary to the above, on December 6,

1989, the inspector observed an operator rack in "2A" Train Reactor Trip Bypass Breaker without having "in hand" double asterisked procedure

~12-OHP 4021.082.018 "Racking In and Out Reactor Trip, Reactor Trip Bypass and MG Set Output Breakers,"

Revision 2.

Even though no adverse affects were noted, in the past under similar circumstances, a reactor trip occurred (315/89031-01F; 316/89031-01F).

Procedure PMI-2010, "Plant Manager and Department Head Instructions, Procedures and Index," Revision 17, requires in Section 3.14.1 that all effective instructions and procedures be reviewed no less frequent than once every two years.

Contrary to the above, maintenance procedure MHI 2070, MHI 7090, PMI 4050, 12 THP 6030 IMP ~ 071, and 12 THP IMP.062 were not reviewed in the last two years.

As a result, the procedures were not updated to reflect feedback and changes to preventive maintenance activities (315/89031-01G; 316/89031-1G)."

Response

to Violation la Plant procedure PMI-2290 requires that tags placed at or near equipment needing repair be removed when the item is repaired or if the Job Order is cancelled.

As noted in the text, six Job Order tags were found in the plant for work that had been cancelled or completed which constitutes failure to follow procedure.

The conclusion made in Inspection Report 89031 was that equipment status was "indeterminate."

While the presence of Job Order tags was contrary to the requirements of PMI-2290, the status of equipment/components involved would not be affected.

The information placed on a tag identifies to personnel

1) that a Job Order has been written for repair with number noted,
2) the nature of repairs/adjustments required as determined by the person initiating the Job Order and 3) helps locate the specific component.

By itself, a Job Order tag has no impact on system or equipment operability, does

Attachment 2 to AEP:NRC.:1125A Page 3

not indicate that equipment has been tagged out, and does not direct any other activity involving the equipment.

Other systems such as the clearance permit system logs and the deficiency logs indicate the equipment status.

(1) Corrective Action Taken and Results Achieved Job Order tags identified during the inspection were subsequently removed to achieve compliance with applicable sections of PMI-2290.

(2) Corrective Action Taken To Avoid Further Violation The Plant Manager will i.ssue a

memo on procedural compliance to ensure that all personnel are fully aware of the meaning of compliance, consequences of failure and what actions to take

~ when a procedure cannot be followed as written.

The Maintenance Improvement Plan includes issuance of a department policy on procedure compliance.

Included will be guidance on the monitoring of the effectiveness of procedure compliance.

Also a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.

(3) Date When Full Com liance Will Be Achieved The final draft of the policy will be issued on July 15, 1990.

Guidance on the effectiveness monitoring will be issued on August 15, 1990.

The Plant Manager's memo will be issued on May 1, 1990.

Response

to Violation lb The Notice of Violation identified that thermal overloads in the plant had been installed at an incorrect trip current rating.

As a result of the inspection, plant personnel investigated the problem and addressed it in Problem Report 90-81.

(1) Corrective Action Taken and Results Achieved The improper positioning and/or mis-sizing of the overload heaters resulted from errors made during initial installations.

Twenty overloads were inspected and evaluated by plant and AEPSC engineers.

Eleven were found to b'e correct.

One was found on a breaker for a resistive heater where overload protection was not considered critical as molded case circuit breakers protection was provided.

On four breakers (including ICM-111) the as-found heater size agreed with the calculated, but arrow position did not agree.

Full load amps was at the dividing point for selecting up or down posi.tion.

Slight changes in motor protection resulted but did not affect the operability of load.

Four feeders on BOP were found to be mis-sized.

Of those four

Attachment 2 to AEP:NRC:1125A

-Page 4

one was mis-sized to a degree that replacement was needed to ensure adequate protection.

Of the three other overload

heaters, though improperly set, would have provided thermal overload protection for equipment.

Job Orders to correct these settings by October 30,

1990, have been written.

(2) Corrective Action Taken To Avoid Further Violation In the course of the plant's investigation it was determined that the mis-sizing and/or mispositioning of the thermal overloads had occurred during initial installation in 1977 and 1978.

Lacking vendor information, calculations were most likely developed by plant personnel for positions/sizes which in some of the cases, proved incorrect.

The design change process has evolved since that time to a level that reasonably ensures that repetition of a similar condition will not occur.

Specifically, general procedures now require that design calculations be verified and documented by qualified personnel.

(3) Date When Full Com liance Will Be Achieved Based on the engineering evaluation completed January 15,'990, the deficiencies in the thermal overload heater settings would not have affected the operability of the ICM-111 breaker.

Other deficiencies did not degrade the thermal overload protection of the equipment breakers.

Current procedures/practices should prevent recurrence of this problem.

Response

to Violation lc In the course of the inspection it was found that a plant instruction utilized for document control (drawings) contained no provision mandating that the user of the index verify that it was the most recent update.

We concur with the inspector's conclusion that an instruction to users of the Master Drawing Index to ensure that it references up-to-date as-built drawings should be included in procedures.

(1) Corrective Action Taken and Results Achieved As a result of the inspection, PMI-2030, "Document Control," was revised to instruct a Master Data Index user to ensure that it reflects the latest as-built drawings located in the plant's master file.

(2) Corrective Action Taken To Avoid Further Violation Revision 11 to PMI-2030 is being routed for approval from plant management.

The revision addresses the inspector's concern noted in the Notice of Violation.

I Attachment 2 to AEP:NRC:1125A Page 5

(3) Date When Full Com lienee Will Be Achieved The revised version of PMI-2030 will be effective by May 1, 1990.

Response

to Violation ld Procedural revision to incorporate a direction to run a pump in order to properly adjust packing is not viewed as necessary.

Personnel performing packing adjustments meet the requirements of ANSI Standard N18-1 (4.5.3).

Consistent with that standard, maintenance personnel receive formal training in subjects associated with their position.

Included in the plant's training is a course on pumps that directly references the correct methodology for adjusting the packing on pumps.

This teaches maintenance personnel that adjustments will only be made to packing when the pump is operating.

As required by ANSI Standard N18-7, Section 4.1 (2), plant procedures are developed with the objective of providing adequate information to personnel involved in a given task considering the skill they are provided through the training program.

(1) Corrective Action Taken and Results Achieved Those persons who would be involved in pump packing work are hired and trained consistent with ANSI N18-1.

(2) Corrective Action Taken to Avoid Further Violation The hiring practices and training programs have proven adequate to prevent problems due to pump packing (3) Date When Full Com liance Will Be Achieved No violation occurred as practices are in accordance with N18-1 and personnel are fully qualified.

Response

to Violation le While the intent of Step 8.1.2-2 of maintenance procedure 12 THP 6030.IMP.014 was to ensure that technicians performing cleaning would utilize tape or similar adhesive-backed material.

Black electrical tape, was specified because it is a commonly available item.

However, use of a calibration sticker did

- constitute a violation of the procedure as written.

(1) Corrective Action Taken and Results Achieved Maintenance supervision reviewed the net effect of utilizing the sticker in the course of cleaning and determined that satisfactory results were obtained.

No re-cleaning was deemed

Attachment 2 to AEP:NRC:1125A Page 6

necessary.

12 THP 6030.IMP.014 had been revised via a change sheet initiated April 2, 1990, to remove reference to black electrical tape.

(2) Corrective Action Taken To Avoid Further Violation The Plant Manager will issue a

memo on procedural compliance to ensure that all personnel are fully aware of the meaning of compliance, consequences of failure and what actions to take when a procedure cannot be followed as written.

The Maintenance Improvement Plan includes issuance of a department policy on procedure compliance.

Included will be guidance on the monitoring of the effectiveness of procedure compliance.

Also a procedure writer'/user's guide will address the circumstances for changing a procedure to ensure procedural compliance.

(3) Date When Full Com lienee Will Be Achieved The final draft of the policy will be issued on July 15, 1990.

Guidance on the effectiveness monitoring will be issued on August 15, 1990.

The Plant Manager's memo will be issued on May 1, 1990.

Response

to Violation lf (1) Corrective Action Taken and Results Achieved The Auxiliary Equipment Operator (AEO) involved in this event had received training on the operation of reactor trip breakers and the existence of the procedure prior to this event.

The AEO, however, overlooked the reactor trip breaker procedure was required to be "in hand" whenever performing racking operations.

Although the racking evolution was done in accordance with the.

procedure requirements, this event was a violation because the requirement to have the procedure "in hand" was not satisfied.

A memorandum was issued to Operations personnel on January 19, 1990, to remind them of the "in hand" requirement for the reactor trip breaker procedure.

(2) Corrective Action To Be Taken To Avoid Further Violation The routine surveillance procedures for reactor trip breaker testing were revised on December 13, 1989, to reference the requirement for having the reactor trip breaker racking procedure "in hand" for the racking evolutions.

The startup surveillance procedures, which require racking of the reactor trip breakers, will be revised by June 4,

1990, to reference the requirement for having the reactor trip breaker procedure "in hand."

Attachment 2 to AEP:NRC:1125A Page 7

During the concluded, procedures Therefore, past two years, QA audits/surveillances have except for a "few isolated cases,"

double asterisked have in fact been "in hand" when required.

no generic programmatic problem exists.

(3) Date When Full Com liance Will Be Achieved Full compliance was achieved on December 6,

1989, when the

'involved AEO was reinstructed of the "in hand" procedural requirement.

Response

to Violation lg Five procedures/instructions were cited in the Notice of Violation as not having been reviewed within the two-year limit established in plant procedure PMI-2010.

However, in each case the documents had been reviewed and documentation to that effect was on file.

Upon request one of the inspectors was provided with biannual review documents for IMP.071 and IMP.062.

The instruction does not require an approved revision within two

years, only a review prior to such revision.

This information may not have been adequately communicated.

(1) Corrective Action Taken and Results Achieved Further review of the Notice of Violation by the plant identified that procedures/instructions noted had received review as required by PMI-2010, Rev.

17.

(2) Corrective Action Taken to Avoid Further Violation Tracking and review of procedures is presently adequate.

(3) Date When Full Com liance Will Be Achieved No violation occurred.

Attachment 2 to AEP:NRC:1125A Page 8

NRC Violation 2 "10 CFR 50, Appendix B, Criterion VIII, as implemented by Section 1.7.8 of the Donald CD Cook Operational Quality Assurance Program required that measures be established for the identification of materials, parts and components such as by part number, serial number, or other appropriate means on the item or records traceable to the item throughout fabrication, installation and use of the item."

"Contrary to the above, identification of materials and components for traceability was not accomplished for cable extension portions and aluminum splicing sleeves for connections to several safety-related motor control centers installed under the Request For Change 1482 modification (315/89031-02; 316/89031-02)."

Response

to Violation 2 RFC-1482 installed transition pieces (sleeves) to splice copper to aluminum cables in various motor control centers.

Per RFC instructions, the transition pieces were to be installed in accordance with Engineering Design Specification (EDS) 607 and EDS 608'he installation took place between June of 1979 and September of 1981 when the final summary was issued.

A search of the completed RFC package (including installation job orders) and of the microfilm of the completed job order packages revealed no documentation of the parts (sleeves) used for the installation.

Individuals who were involved with the Maintenance Department at that time stated that personnel would have installed the transition pieces per the EDS as stated in the RFC.

Inadequate documentation of material installed by a Job Order during the design change process was the root cause of this violation.

Additionally, there were inadequate review of the completed job orders and the design change package upon completion.

(1) Corrective Action Taken and Results Achieved The installation took place approximately 10 years ago and was performed in accordance with EDS 608, which was referenced in the RFC package.

Actual application for the past ten years has functionally demonstrated the adequacy of subject materials'

Attachment 2 to AEP:NRC:1125A Page 9

(2) Corrective Action Taken To Avoid Further Violation Current procurement/dedication practices ensure proper documentation is developed to demonstrate control over the suitability of material, parts and components.

(3) Date When Full Com liance Will Be Achieved Current procedures/practice's should prevent recurrence of this problem and ensure future compliance.

Attachment 2 to AEP:NRC:1125A Page 10 NRC Violation 3 "10 CFR 50, Appendix B, Criterion XI, as implemented by Section 1.7.11 of the Donald C.

Cook Operational Quality Assurance Program required that a test program be established to assure testing to demonstrate that systems and components will perform satisfactorily in service in accordance with test procedures which incorporate requirements and acceptance limits contained in applicable design documents, and that adequate test instrumentation was available and used."

"Contrary to the above, test instruments were not sensitive or accurate enough to verify the calibration of the undervoltage relays that actuate the Emergency Diesel Generators.

Procedure 2

THP 6030 IMP.250, "4kV Diesel Start, 4kV ESS Bus Undervoltage Relay Calibration," Revision 7, Section 3.0, required the use of a Westinghouse type PA-161 AC anolog [sic]

voltmeter or its equivalent with equal or better accuracy and adequate range to measure the desired parameters.

However, the voltmeter had a tolerance of +1.5 volts that was not sufficiently accurate to measure the desired parameter of 90.3 to 91.8 volts specified in Technical Specification 3.3.2.

In

addition, the voltmeter indicated to the nearest whole volt and did not have division markings between the numbers.

Technicians had to interpolate results and record values to the nearest tenth of a volt while the voltmeter's dial indicator was moving in the increasing or decreasing direction.

Furthermore, the technicians used hand signals to communicate the moment the under voltage relay operated.

Based on the inaccuracy and insensitivity of the voltmeter, and poor testing technique, results of the undervoltage test were not conclusive (315/89031-03; 316/89031-03)."

Response

to Violation 3 The meter used was first specified in the original procedure developed before initial plant start-up.

The specific reasons for using this meter could not be determined.

However, it is believed that this was the limit of the available technology at that time.

The only other meter available was a basic digital type, which could not be used due to the inherently slow response and update time, causing a greater uncertainty of specific setpoint value than the analog meter.

Attachment 2 to AEP:NRC:1125A Page 11 (1) Corrective Actions and Results Achieved Z&C now uses the Fluke Model 45 digital meter during testing of the 4KV diesel start and 4KV ESS bus undervoltage relays.

Recent developments in digital meters which include faster response times and update times and minimum/maximum modifier features has made their use acceptable.

The digital meter currently being used has an accuracy of + 0.3 percent.

The previous test method provided acceptable

results, based on the as-found values on the first use of the digital meters being in specification by comparable percentages.'2)

Corrective Actions Taken To Avoid Further Violation The calibration procedures which currently allow use of either analog or digital meters will be changed to specify the use of the Fluke Model 45 digital meter, or its equivalent, to ensure consistent use of a digital meter.

(3) Date When Full Com lienee Will Be Achieved The procedure changes will be completed before April 30, 1990.

~

~

Attachment 2 to AEP:NRC:1125A Page 12 NRC. Violation 4 "10 CFR 50, Appendix B, Criterion XVI, as implemented in Section 1.7.16 of the Donald C.

Cook Operational Quality Assurance Program required that measures be established to assure that conditions adverse to quality were promptly identified and corrected.

In the case of significant conditions adverse to quality, the measures shall assure that the cause of the condition was determined and corrective action taken to preclude repetition.

"Contrary to the above:

The Plant Assessment Group Committee's review in March 1989 for Problem Report 89-245, concerned with the February 1989 failure of two safety-related 4kV breakers T-11D6 and T-1104 to close on demand during tests due to lubrication hardening, failed to specify corrective action to prevent recurrence.

Furthermore, no action was taken to inspect other 4kV breakers for common mode failure.

Consequently, in March and April of 1989 seven additional safety related and balance of plant breakers failed to close during

testing, which was also caused by hardening of the lubricant on the breaker linkage (315/89031-04A; 316/89031-04A).

b.

Corrective action was neither prompt nor adequate to correct maintenance related'roblems identified by the licensee in February 1988.

In December

1989, 36 of these 71 self identified findings and recommendations were reopened.

During this inspection many of the same problems were identified that reflect a significant weakness in the corrective action system (315/89031-04B; 316/89031-04B)."

Response

to Violation 4a Based on review of Problem Report 89-245, which was addressed in the Notice of Violation it is our position that no actual violation occurred.

The February 27, 1989, condition was identified during scheduled 'preventive maintenance work and resulted in the problem report.

That discovery, coupled with a similar condition also found during preventive maintenance, resulted in a Part 21 report.

The Part 21 investigation revealed that vendor-specified information contained no instruction for periodic lubrication of the breakers.

Similar breakers used in the plant had, until that time, passed test requirements'he plant's actions which were taken promptly, included revision of the procedure based on new input from the manufacturer, initiation of Job Orders to inspect all other similar breakers installed in both units, and establishment of scheduled inspections to identify possible repetition of the

C. I 1

Attachment 2 to AEP:NRC:1125A Page 13 condition in the future.

The Notice of Violation incorrectly concluded that no action was taken to inspect additional breakers or develop corrective action.

Two subsequent problem reports were initiated as a result of deficiencies found in the inspections and tests covered by our expanded action for Problem Report 89-245 and the associated Part 21 review.

Those reports were initiated to document the similar conditions on the noted breakers.

Within two months of the March 1,

1989, Part 21 report to the NRC, the plant had completed the inspections, cleaned and relubricated the breakers in both units as recommended by the revised vendor information, and documented each case when a similar condition was found.

(1) Corrective Action Taken and Results Achieved The result of Problem Report 89-245, which was reviewed by the Plant Assessment Group on March 17,

1989, was to inspect, clean and lubricate similar breakers in both units and document the results.

(2) Corrective Action Taken to Avoid Further Violation Procedure changes and inspections were scheduled as a result of addressing the problem reported in Problem Report 89-245 on similar breakers.

These actions generated additional Job Orders and condition reports which were referenced in the inspection report.

(3) Date When Full Com liance Will Be Achieved No violation occurred.

Response

to Violation 4b As discussed in our response to Weakness (1),

AEP has taken numerous corrective actions to address the problems identified by the Maintenance Self-Assessment.

These actions include:

o the development of a RCM Program o

the acquisition of the Nuclear Plant Maintenance (NPM)

Module o

the development of a System Engineer Program o

the acquisition of NUS's PRONET and the servt.ces of NUS's procedure writers.

Attachment 2 to AEP:NRC:1125A Page 14 In order to effectively implement programs as encompassing and comprehensive as these, significant analysis, planning and coordination are needed.

As such, it will take several years to completely implement some of the corrective actions we have initiated.

(1) Corrective Actions and Results Achieved Maintenance-related problems identified in the Maintenance Self-Assessment will be reviewed and resolved as appropriate, with implementation of the Maintenance Improvement Plan.

(2) Corrective Actions Taken to Avoid Further Violation The Improvement Plan includes milestones and a built-in mechanism that requires regular re-evaluation of the plan and monitoring of its effectiveness to ensure that it is providing the desired results and that there is continuing improvement in all maintenance-related areas'3)

Date When Full Com liance Will Be Achieved Resolution and documentation of the identified items will be completed by June 1,

1991.