ML19308D130: Difference between revisions
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| document report number = NUDOCS 8002270611 | | document report number = NUDOCS 8002270611 | ||
| package number = ML19308D119 | | package number = ML19308D119 | ||
| document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO | | document type = REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER), TEXT-SAFETY REPORT | ||
| page count = 2 | | page count = 2 | ||
}} | }} | ||
=Text= | =Text= | ||
{{#Wiki_filter:m.-.._- | {{#Wiki_filter:m.-.._- | ||
CONTAOL ULOCK. | |||
l | l l | ||
l l | |||
( jj [ F l L l C l R l P l 3 l | l (PLEASE P AINT ALL REQUIAEC INFC A.*.1?.T.Cl. | ||
IB9 | l 1 | ||
M l N dundancy was maintained with the low pressure injection system. | 6 N | ||
- LCENSEE LCENSE EVENT f' | |||
7 09 | i NAME LCENSE NUMBEA TYPE Type | ||
7 89 | ( jj [ F l L l C l R l P l 3 l l0l0l-l0l0l0l0l0l-l0l0l l 4l 1 l1-l1 l1 l l0 l 3l IB9 14 15 25 26 30 31 32 77PU NN coCxf7 NuM0ta EVEM TE AEPORT CATE CAftCCav O 1 CON'T ! -l -l lL l lL l l 0 l 5 l 0 l-l 0 l 3 l 0 l 2 l l0 l5 Il lo !7 l7 l l O! 6l ?! 0l 7l 7' 7 | ||
8' 57 LO 59 60 61 68 69 74 75 GL EVENT DESCniPTION a | |||
l In mode 3 (hot standby) preparing for plant startup, both chemical addition pumps | |||
.p 7 89 h | |||
[Nl 48 CAUSE DESCA:PTJON | C3 l CAP-3A & 3B were found to be inoperable contrary to Technical Specification 3.1.2.2. | ||
J 7 09 S. | |||
M l N dundancy was maintained with the low pressure injection system. | |||
Event was not i | |||
7 83 Eu | |||
@l repetitive. Both pumos were flushed with demin watar and restored operable within 7 09 go Q] two (2) hours. | |||
7 89 ge | |||
%g (LER 77-53; E | |||
CCCE COMPCNENT COCE S | |||
R M | |||
C W TCN O | |||
l Rl Bl { | |||
l Pl Ul Ml Pl Xl.] | |||
lN l lC l 3l 0l 0l | |||
[Nl 7 89 10 11 12 17 43 44 47 48 CAUSE DESCA:PTJON 9 | |||
grj l The cause of this event has not been determined. | grj l The cause of this event has not been determined. | ||
It has not reo ccurred. Corrective | |||
]" | |||
gl Action will be taken pending the results of an engineering evaluation now in progress. | 7 89 GO gl Action will be taken pending the results of an engineering evaluation now in progress. | ||
7 85 | 7 85 BC | ||
#1 I | |||
Facufy METHCO OF STATUS | |||
% POWER oTHER STATUS 0.SCavERY QSCOVEAY DESCA'"TCN lCl l 4 4 0l l NA l | |||
PERSONNEL INJUDICS NUMBER | lAl l. | ||
NA J | |||
16 7 89 | 1 7 0 9 | ||
PUBLICITY | 10 12 13 44 45 46 60 FCAM CF AMOUNT OF ACTMTV LOCATCN CF AELEASE RELE SEO OF ASE l l | ||
l | l | ||
7 89 | .NA l | ||
l | 12 NA 7 8 9 | ||
[ | 10 11 44 45 60 PEnnN'JEL EXPOSURES NUMBEA TYPE CESCM' TION Ql0l0l Wl NA j | ||
( | 13 7 89 11 12 13 GC PERSONNEL INJUDICS NUMBER CESCAipflGN l 0l 0 l 0 l l | ||
NA l | |||
7 89 | 14 7 89 11 12 et OFFSITE CONSEQUENCES M l NA l | ||
7 89 OU LOSS OR CAMAGE TO FACILITY TYPE CESCA:PficN l | |||
dl 16 NA l | |||
7 89 10 1,L PUBLICITY NA l | |||
1 7 89 6. | |||
l ACOITIONAL FACTCAS | |||
[ | |||
]l See attached Suonlemene m In fore en | |||
( | |||
,09 | |||
$l 8002270 (// | |||
7 89 | |||
,, f in. | |||
N. P. Stewart | |||
(,,,th (813) 866-4159 NAME: | |||
PHONE: | |||
w;/ | |||
un m.sei | |||
SUPPLEMENTARY INFORMATION (V') | SUPPLEMENTARY INFORMATION (V' - | ||
) | |||
l. | |||
Report Nc. | |||
50-302/77-53 2. | |||
Facility: | |||
Crystal River Unit #3 3: Report Date: | |||
20, June 1977 4. | |||
Occurrence Date: 29 May 1977 5. | |||
Identification of occurrence: | |||
Chemica1' addition pumps CAP-3A & 3B inoparable contrary to Technical Specification 3.1.2.2. | Chemica1' addition pumps CAP-3A & 3B inoparable contrary to Technical Specification 3.1.2.2. | ||
6. | |||
Conditions Prior to Occurrence: | |||
The plant was preparing to achieve' criticality by adjusting boron for the accept-able critical rod position.. | The plant was preparing to achieve' criticality by adjusting boron for the accept-able critical rod position.. | ||
7. | |||
Description of Occurrence: | |||
l At 0700 in preparation for criticality, an attempt to adjust Reactor Coolant boron f-concentration for acceptable critical rod position revealed that r.either chemical addition pump CAP-3A or CAP-3B would deliver boric acid to the makeup tank. -Both chemical addition pumps were flushed with demineralized water and the pumps restored operable within two (2) hours. Startup resumed without incident. | |||
8. | |||
Designatio'n of Apparent Cause: | |||
The cause of P.his event has not been determined as of this' date, as the event has not reoccurred. | The cause of P.his event has not been determined as of this' date, as the event has not reoccurred. | ||
9. | |||
Analysis of occurrence: | |||
This event had no safety implications as the high pressure injection pumps and the bor9ted water storage tank were available and operable. | |||
10. | |||
Corrective Action: | |||
An evaluation of this occurrence has been requested and corrective action will be taken pending results of the evaluation. | An evaluation of this occurrence has been requested and corrective action will be taken pending results of the evaluation. | ||
11. | |||
Failure Data: | |||
This was not a repetitive occurrence. | This was not a repetitive occurrence. | ||
V | V i | ||
i | .}} | ||
Latest revision as of 04:22, 2 January 2025
| ML19308D130 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 06/20/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19308D119 | List: |
| References | |
| NUDOCS 8002270611 | |
| Download: ML19308D130 (2) | |
Text
m.-.._-
CONTAOL ULOCK.
l l
l l
l (PLEASE P AINT ALL REQUIAEC INFC A.*.1?.T.Cl.
l 1
6 N
- LCENSEE LCENSE EVENT f'
i NAME LCENSE NUMBEA TYPE Type
( jj [ F l L l C l R l P l 3 l l0l0l-l0l0l0l0l0l-l0l0l l 4l 1 l1-l1 l1 l l0 l 3l IB9 14 15 25 26 30 31 32 77PU NN coCxf7 NuM0ta EVEM TE AEPORT CATE CAftCCav O 1 CON'T ! -l -l lL l lL l l 0 l 5 l 0 l-l 0 l 3 l 0 l 2 l l0 l5 Il lo !7 l7 l l O! 6l ?! 0l 7l 7' 7
8' 57 LO 59 60 61 68 69 74 75 GL EVENT DESCniPTION a
l In mode 3 (hot standby) preparing for plant startup, both chemical addition pumps
.p 7 89 h
C3 l CAP-3A & 3B were found to be inoperable contrary to Technical Specification 3.1.2.2.
J 7 09 S.
M l N dundancy was maintained with the low pressure injection system.
Event was not i
7 83 Eu
@l repetitive. Both pumos were flushed with demin watar and restored operable within 7 09 go Q] two (2) hours.
7 89 ge
%g (LER 77-53; E
CCCE COMPCNENT COCE S
R M
C W TCN O
l Rl Bl {
l Pl Ul Ml Pl Xl.]
lN l lC l 3l 0l 0l
[Nl 7 89 10 11 12 17 43 44 47 48 CAUSE DESCA:PTJON 9
grj l The cause of this event has not been determined.
It has not reo ccurred. Corrective
]"
7 89 GO gl Action will be taken pending the results of an engineering evaluation now in progress.
7 85 BC
- 1 I
Facufy METHCO OF STATUS
% POWER oTHER STATUS 0.SCavERY QSCOVEAY DESCA'"TCN lCl l 4 4 0l l NA l
lAl l.
NA J
1 7 0 9
10 12 13 44 45 46 60 FCAM CF AMOUNT OF ACTMTV LOCATCN CF AELEASE RELE SEO OF ASE l l
l
.NA l
12 NA 7 8 9
10 11 44 45 60 PEnnN'JEL EXPOSURES NUMBEA TYPE CESCM' TION Ql0l0l Wl NA j
13 7 89 11 12 13 GC PERSONNEL INJUDICS NUMBER CESCAipflGN l 0l 0 l 0 l l
NA l
14 7 89 11 12 et OFFSITE CONSEQUENCES M l NA l
7 89 OU LOSS OR CAMAGE TO FACILITY TYPE CESCA:PficN l
dl 16 NA l
7 89 10 1,L PUBLICITY NA l
1 7 89 6.
l ACOITIONAL FACTCAS
[
]l See attached Suonlemene m In fore en
(
,09
$l 8002270 (//
7 89
,, f in.
N. P. Stewart
(,,,th (813) 866-4159 NAME:
PHONE:
w;/
un m.sei
SUPPLEMENTARY INFORMATION (V' -
)
l.
Report Nc.
50-302/77-53 2.
Facility:
Crystal River Unit #3 3: Report Date:
20, June 1977 4.
Occurrence Date: 29 May 1977 5.
Identification of occurrence:
Chemica1' addition pumps CAP-3A & 3B inoparable contrary to Technical Specification 3.1.2.2.
6.
Conditions Prior to Occurrence:
The plant was preparing to achieve' criticality by adjusting boron for the accept-able critical rod position..
7.
Description of Occurrence:
l At 0700 in preparation for criticality, an attempt to adjust Reactor Coolant boron f-concentration for acceptable critical rod position revealed that r.either chemical addition pump CAP-3A or CAP-3B would deliver boric acid to the makeup tank. -Both chemical addition pumps were flushed with demineralized water and the pumps restored operable within two (2) hours. Startup resumed without incident.
8.
Designatio'n of Apparent Cause:
The cause of P.his event has not been determined as of this' date, as the event has not reoccurred.
9.
Analysis of occurrence:
This event had no safety implications as the high pressure injection pumps and the bor9ted water storage tank were available and operable.
10.
Corrective Action:
An evaluation of this occurrence has been requested and corrective action will be taken pending results of the evaluation.
11.
Failure Data:
This was not a repetitive occurrence.
V i
.