ML19308D130
| ML19308D130 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 06/20/1977 |
| From: | Stewart W FLORIDA POWER CORP. |
| To: | |
| Shared Package | |
| ML19308D119 | List: |
| References | |
| NUDOCS 8002270611 | |
| Download: ML19308D130 (2) | |
Text
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CONTAOL ULOCK.
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l (PLEASE P AINT ALL REQUIAEC INFC A.*.1?.T.Cl.
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- LCENSEE LCENSE EVENT f'
i NAME LCENSE NUMBEA TYPE Type
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8' 57 LO 59 60 61 68 69 74 75 GL EVENT DESCniPTION a
l In mode 3 (hot standby) preparing for plant startup, both chemical addition pumps
.p 7 89 h
C3 l CAP-3A & 3B were found to be inoperable contrary to Technical Specification 3.1.2.2.
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M l N dundancy was maintained with the low pressure injection system.
Event was not i
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@l repetitive. Both pumos were flushed with demin watar and restored operable within 7 09 go Q] two (2) hours.
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CCCE COMPCNENT COCE S
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[Nl 7 89 10 11 12 17 43 44 47 48 CAUSE DESCA:PTJON 9
grj l The cause of this event has not been determined.
It has not reo ccurred. Corrective
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7 89 GO gl Action will be taken pending the results of an engineering evaluation now in progress.
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Facufy METHCO OF STATUS
% POWER oTHER STATUS 0.SCavERY QSCOVEAY DESCA'"TCN lCl l 4 4 0l l NA l
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1 7 0 9
10 12 13 44 45 46 60 FCAM CF AMOUNT OF ACTMTV LOCATCN CF AELEASE RELE SEO OF ASE l l
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10 11 44 45 60 PEnnN'JEL EXPOSURES NUMBEA TYPE CESCM' TION Ql0l0l Wl NA j
13 7 89 11 12 13 GC PERSONNEL INJUDICS NUMBER CESCAipflGN l 0l 0 l 0 l l
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14 7 89 11 12 et OFFSITE CONSEQUENCES M l NA l
7 89 OU LOSS OR CAMAGE TO FACILITY TYPE CESCA:PficN l
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7 89 10 1,L PUBLICITY NA l
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l ACOITIONAL FACTCAS
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N. P. Stewart
(,,,th (813) 866-4159 NAME:
PHONE:
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SUPPLEMENTARY INFORMATION (V' -
)
l.
Report Nc.
50-302/77-53 2.
Facility:
Crystal River Unit #3 3: Report Date:
20, June 1977 4.
Occurrence Date: 29 May 1977 5.
Identification of occurrence:
Chemica1' addition pumps CAP-3A & 3B inoparable contrary to Technical Specification 3.1.2.2.
6.
Conditions Prior to Occurrence:
The plant was preparing to achieve' criticality by adjusting boron for the accept-able critical rod position..
7.
Description of Occurrence:
l At 0700 in preparation for criticality, an attempt to adjust Reactor Coolant boron f-concentration for acceptable critical rod position revealed that r.either chemical addition pump CAP-3A or CAP-3B would deliver boric acid to the makeup tank. -Both chemical addition pumps were flushed with demineralized water and the pumps restored operable within two (2) hours. Startup resumed without incident.
8.
Designatio'n of Apparent Cause:
The cause of P.his event has not been determined as of this' date, as the event has not reoccurred.
9.
Analysis of occurrence:
This event had no safety implications as the high pressure injection pumps and the bor9ted water storage tank were available and operable.
10.
Corrective Action:
An evaluation of this occurrence has been requested and corrective action will be taken pending results of the evaluation.
11.
Failure Data:
This was not a repetitive occurrence.
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