ENS 43941: Difference between revisions

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| event date = 01/29/2008 05:31 EST
| event date = 01/29/2008 05:31 EST
| last update date = 01/29/2008
| last update date = 01/29/2008
| title = Manual Reactor Trip To Repair Rcp "2B1" Seal Package
| title = Manual Reactor Trip to Repair Rcp "2B1" Seal Package
| event text = St Lucie Plant, Unit 2, manually tripped the reactor at 0531 hrs. EST, as part of a controlled reactor plant shutdown, in response to an RCS leak rate of 0.28 gpm, indicated to be associated with the 2B1 Reactor Coolant Pump seal package. All systems functioned as expected, satisfactorily. All CEAs fully inserted. Decay Heat removal is with Steam Generators and Main Feedwater. This report is made pursuant to 10 CFR
| event text = St Lucie Plant, Unit 2, manually tripped the reactor at 0531 hrs. EST, as part of a controlled reactor plant shutdown, in response to an RCS leak rate of 0.28 gpm, indicated to be associated with the 2B1 Reactor Coolant Pump seal package. All systems functioned as expected, satisfactorily. All CEAs fully inserted. Decay Heat removal is with Steam Generators and Main Feedwater. This report is made pursuant to 10 CFR
50.72(b)(2)(iv)(B).
50.72(b)(2)(iv)(B).

Latest revision as of 22:15, 1 March 2018

ENS 43941 +/-
Where
Saint Lucie NextEra Energy icon.png
Florida (NRC Region 2)
Reporting
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation

10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Time - Person (Reporting Time:+-4.02 h-0.168 days <br />-0.0239 weeks <br />-0.00551 months <br />)
Opened: Alan Hall
06:30 Jan 29, 2008
NRC Officer: Steve Sandin
Last Updated: Jan 29, 2008
43941 - NRC Website
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