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 Entered dateEvent description
ENS 4394129 January 2008 06:30:00

St Lucie Plant, Unit 2, manually tripped the reactor at 0531 hrs. EST, as part of a controlled reactor plant shutdown, in response to an RCS leak rate of 0.28 gpm, indicated to be associated with the 2B1 Reactor Coolant Pump seal package. All systems functioned as expected, satisfactorily. All CEAs fully inserted. Decay Heat removal is with Steam Generators and Main Feedwater. This report is made pursuant to 10 CFR 50.72(b)(2)(iv)(B). Unit 2 will cooldown to Mode 5 for repairs. The licensee informed the NRC Resident Inspector.

  • * * UPDATE FROM ALAN HALL TO HOWIE CROUCH @ 1218 EST ON 1/28/08 * * *

St. Lucie Plant, Unit 2, reported their manual reactor trip of 0531 hrs. EST, at 0630 hrs. EST, for an unidentified leak associated with the 2B1 RCP seal package (EN 43941). Subsequent investigation, reported to the STA (Shift Technical Advisor) at 1015 hrs. EST, determined that this leak constitutes an RCS Pressure Boundary Leak. This leak is at a pipe-to-flange weld on the outboard side of the first flanged coupling of the 2B1 RCP Upper Cavity Seal pressure sensing line. Investigation is in progress to determine the detailed configuration at the leak and root cause. There were NO ESFAS signals or actuations. Decay Heat Removal continues on Steam Generators, with MFW (Main Feedwater) and SBCS (Steam Bypass Control System); Off-Site power continues (to be) available and stable; Unit 1 at 100% power with operations and conditions normal. This report is made pursuant to 10 CFR 50.72(b)(3)(ii)(A). The licensee informed the NRC Resident Inspector of this update. Notified R2DO (Bonser).

ENS 4392923 January 2008 23:05:00St. Lucie Plant made an Unusual Event notification to the Florida State Warning Point @ 2228 EST, 01/23/08 based on a Hydrogen Tube Trailer fitting failure, and subsequent leak of hydrogen gas. The emergency classification was Emergency Action Level #20. A., per St. Lucie Plant EPIP-01, 'Classification of Emergencies'. The hydrogen leak was terminated upon discovery, with no subsequent fire and no personnel injuries. The event (and declaration) was terminated @ 2228 EST, on 01/23/08. The licensee notified the NRC Resident Inspector, and the Commonwealth of Florida Warning Point.
ENS 4387128 December 2007 06:46:00

At 0347 on 12/28/07, during plant start up from a refueling outage while In Mode 2, one control element assembly (CEA) dropped to the bottom of the core from the upper electrical limit. The reactor was not critical at the time. Technical Specification LCO 3.1.3.1 action (e) was initiated to proceed to Mode 3 at 0450 while actions are taken to repair and retrieve the CEA. This four hour non-emergency report is being made pursuant to 10 CFR 50.72(b)(2)(i), the 'Initiation of any nuclear plant shutdown required by Technical Specifications'. The licensee notified the NRC Resident Inspector.

  • * * RETRACTED ON 03/26/2008 AT 1433 EDT BY JACK BREEN TO DAN LIVERMORE * * *

The licensee is retracting this report based on the following: At 03:47 on 12/28/07, during plant start up from a refueling outage while in Mode 2, one control element assembly (CEA) dropped to the bottom of the core from the upper electrical limit. The reactor was not critical at the time. Technical Specification LCO 3.1.3.1 (Action E) was initiated to proceed to Mode 3 at 0450 while actions were taken to repair and retrieve the CEA. This event was reported as a four hour non-emergency report pursuant to 10CFR 50.72(b)(2)(i), 'The initiation of any nuclear plant shutdown required by Technical Specifications.' Upon further review of the event, and since the Unit was not critical in mode 2 at the time of the event, this event is not considered reportable in accordance with the guidance provide in NUREG-1022, Rev. 2, 'Event Reporting Guidelines 10CFR50.72 and 50.73,' in which 'The initiation of any plant shutdown' does not include mode changes required by TS if initiated after the plant is already in a shutdown condition. As such this notification is being retracted. The Site Resident has been notified of this retraction.

ENS 4205212 October 2005 16:53:00

On 10/12/05 at 14:40 EDT, Unit 1 experienced a loss of Channel A of the CIS (Containment Isolation Signal) Radiation Monitor which, when combined with the previous existing inoperability of Channel D of the CIS radiation monitor, required Unit 1 to enter technical specification LCO 3.0.3. If the action statement (for the CIS), LCO 3.3.2.1, cannot be met, within 1 hour, action shall be initiated to place the unit in Hot Standby with the next 6 hours, Hot Shutdown within the following 6 hours, and cold shutdown within the subsequent 24 hours. Unit shutdown is in progress. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM LICENSEE (C. MARPLE) TO NRC (HUFFMAN) AT 2145 EDT ON 10/12/05 * * *

At 2101 EDT on 10/12/05, the Unit 1 exited Technical Specification 3.0.3 when Channel D of the CIS radiation monitor was returned to service. The down-power of Unit 1 was halted at 97% power. The licensee notified the NRC Resident Inspector. R2DO(Decker) informed.