ML20154R821: Difference between revisions

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=Text=
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{{#Wiki_filter:r..
{{#Wiki_filter:r..
          c.L'
c.L'
        '     '
'
                      tA no
'
                3'           1                           UNITED STATES
tA no
                j'             j*          . NUCLEAR REGULATORY COMMISSION
3'
                o                                           REGION 11
1
                              #
UNITED STATES
                \'e,,,,g                               101 MARIETTA ST N.W.
j'
                                                      ATLANTA, GEORGIA 30323                           (
j
                  Report Nos.:     50-259/88-18, 50-260/88-18,-and 50-296/88-18
. NUCLEAR REGULATORY COMMISSION
                  Licensee:     Tennessee Valley Authority                                             l
o
                                  6N 38A Lookout Place                                                   '
*
                                  1101 Market Street
REGION 11
                                  Chattanooga, TN 37402 2801
#
                  Docket Nos.:     50-259, 50-260 and 50-296           License 741.: OPR-33, DPR-52,
\\'e,,,,g
                                                                                          and DPR-68
101 MARIETTA ST N.W.
                  Facility Name:     Browns Ferry 1, 2, and 3                                         ;
ATLANTA, GEORGIA 30323
    *
(
                  Inspection Conducte :       June 12-30,   988                                       -
Report Nos.:
                  Inspector-       [
50-259/88-18, 50-260/88-18,-and 50-296/88-18
                            g-- R. Brooks,~ Acting Senior Resident Inspector
Licensee:
                                                                                              f
Tennessee Valley Authority
                                                                                            Date 51gned j
l
]                 Accompanying Personnel:       E. F. Christnot, Resident Inspector                   [
6N 38A Lookout Place
                                                  W. C. Bearden, Resident Inspector                     *
'
                                                  A. H. Johnson, Project Engineer                       <
1101 Market Street
                                    //
Chattanooga, TN 37402 2801
                  Approved by:7. 5. Littler Sectioll Chief                                 / #88
Docket Nos.:
                                                                                            Date Signed i
50-259, 50-260 and 50-296
License 741.:
OPR-33, DPR-52,
and DPR-68
Facility Name:
Browns Ferry 1, 2, and 3
;
*
Inspection Conducte :
June 12-30,
988
-
Inspector-
[
f
g-- R. Brooks,~ Acting Senior Resident Inspector
Date 51gned
j
]
Accompanying Personnel:
E. F. Christnot, Resident Inspector
[
W. C. Bearden, Resident Inspector
*
A. H. Johnson, Project Engineer
<
//
Approved by:7. 5. Littler Sectioll Chief
/ #88
Date Signed
i
i
                                  Inspection Programs                                                   ,
i
l                                 TVAProjectsOfvision                                                   j
Inspection Programs
,'l                                                                                                     !
,
                                                                                                        ,
l
!                                                             SUMMARY                                   .
TVAProjectsOfvision
.                                                                                                       5
j
,'
!
l
,
!
SUMMARY
.
5
.
Scope:
This routine inspection was conducted in the areas of operational
2
2
                  Scope:      This routine inspection was conducted in the areas of operational
;
;
                              safety, maintenance observation, independent audits, and restart test     ;
safety, maintenance observation, independent audits, and restart test
;                             program,                                                                   ,
;
i                 Results: One violation (260/88-18-02) was identified for failure to document
;
,                            an inadvertent overload condition on the "0" Diesel Generator on a         :
program,
,
i
Results: One violation (260/88-18-02) was identified for failure to document
an inadvertent overload condition on the "0" Diesel Generator on a
:
,
1
1
                              Condition Adverse to Quality Report (CAQR) (see paragraph 5.c.)
Condition Adverse to Quality Report (CAQR) (see paragraph 5.c.)
,                              (Restartitem)                                                             7
(Restartitem)
:                                                                                                       i
7
,
:
i
The following inspection followup items were identified:
j
;
;
                              The following inspection followup items were identified:                  j
IFI 260/88-18-01,
,                                    IFI 260/88-18-01,     Undocumented caole conductor splice.       l
Undocumented caole conductor splice.
                                      (Restartitem)                                                     j
l
                                      IFI 260/88-18 03, Test deficiencies identified during LOP /LOCA   f
,
(Restartitem)
j
IFI 260/88-18 03, Test deficiencies identified during LOP /LOCA
f
Test "A".
(Restartitem)
l
'
'
                                      Test "A".    (Restartitem)                                        l
'
'
IFI 260/8818-04, Occumentation of offsite voltage during
                                      IFI 260/8818-04, Occumentation of offsite voltage during           [
[
                                      LOP /LOCA Test "8". (Restartitem)                                 !
LOP /LOCA Test "8".
                  GG10040366 880922                                                                     l
(Restartitem)
                    DR ADOCKCS00g}i9                                                                   l
!
                                                                                                        i
GG10040366 880922
                                                                                                        $
l
ADOCKCS00g}i9
l
DR
i
$
_ _ , . . . _ _ , _ _ _


  . - _ _ _ . __     ___ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _
. - _ _ _ . __
                                                                                      <
___ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _
                  '
<
  ..               .
'
                                                                                        2
.
                                                                                                                              i
..
                                                              IFI 259,260/88-18-05, Major discrepancies identified during     I
2
                                                              LOP /LOCA Test "C". (Restart itemi                             l
i
                                                                                                                              !
IFI 259,260/88-18-05, Major discrepancies identified during
                                                              IFI 260/88-18-06, Oeficiencies identified during LOP /LOCA Test :
LOP /LOCA Test "C".
                                                              "0". (Restart item)
(Restart itemi
                                                                                                                              i
IFI 260/88-18-06, Oeficiencies identified during LOP /LOCA Test
:
"0".
(Restart item)
i
!
!


    . _ - _ _ _ _ _     _ - - _     ___ _ _ _ _ __-_____ _ - _ _ _                 _ _ - _ _ _ _ _ _ - _       _ _ _ _ _ _ _ _ -
. _ - _ _ _ _ _
                    *
_ - - _
                      .
___ _ _ _ _ __-_____ _ - _ _ _
            ,.
_ _ - _ _ _ _ _ _ - _
                                                                                                                                        ,
_ _ _ _ _ _ _ _ -
  j                                                                            REPORT DETAILS
*
]                                1.      Persons Contacted
                                                                                                                                        L
;                                        Licensee Employees                                                                          !
                                                                                                                                        \
                                    *J. G. Walker, Plant Manager                                                                        !
                                        J. D. Martin, Assistant to the Plant Manager                                                  l
.
.
                                    *k. M. McKeon, Operations Superintendent                                                           '
,.
  l                                     T. F. Ziegler, Superintendent - Maintenance                                                   i
,
                                        D. C. Miss, Superintendent - Technical Services                                               :
j
                                        J. G. Turner, Manager - Site Quality Assurance                                                 !
REPORT DETAILS
,                                      M. J. Nay, Manager - Site Licensing                                                             i
]
                                    *J. A. Savage
1.
                                        A.W.Sorrell,ComplianceSupervisor
Persons Contacted
                                                                    Site Radiological Control Superintendent
L
                                                                                                                                        r
;
                                                                                                                                        !
Licensee Employees
4
!
                                        R. M. Tuttle, Site Security Manager                                                           !
\\
                                        L. E. Retzer, Fire Protection Supervisor                                                       ;
*J. G. Walker, Plant Manager
!
J. D. Martin, Assistant to the Plant Manager
l
.
*k. M. McKeon, Operations Superintendent
'
l
T. F. Ziegler, Superintendent - Maintenance
i
D. C. Miss, Superintendent - Technical Services
:
J. G. Turner, Manager - Site Quality Assurance
!
M. J. Nay, Manager - Site Licensing
i
,
*J. A. Savage
A.W.Sorrell,ComplianceSupervisor
r
Site Radiological Control Superintendent
!
R. M. Tuttle, Site Security Manager
!
4
L. E. Retzer, Fire Protection Supervisor
;
H. J. Kuhnert, Office of Nuclear Power, Site Representative
1
1
                                        H. J. Kuhnert, Office of Nuclear Power, Site Representative                                    -
-
                                                                                                                                        '
l
l                                        T. C. Valenzano, Director - Restart Operations Center
T. C. Valenzano, Director - Restart Operations Center
l
'
'
l
  I
Other licensee employees contacted included licensed reactor operators,
                                        Other licensee employees contacted included licensed reactor operators,                         ,
I
                                        auxiliary operators, craftsmen, technicians, public safety officers,                           :
,
                                        quality assurance personnsi, and design and engineering personnel.
'
                                                                                                                                      l
auxiliary operators, craftsmen, technicians, public safety officers,
-
:
                                      Acronyms and abbreviations used throughout the report are listed in the
quality assurance personnsi, and design and engineering personnel.
,                                        last section of this report.                                                                 ;
l
                                    * Attended exit interview
Acronyms and abbreviations used throughout the report are listed in the
-
last section of this report.
,
;
f
f
!                               2.   Operational Safety (71707, 71710)
* Attended exit interview
:                                                                                                                                       '
!
i                                       The inspectors were kept informed of the overall plant status and any                           l
2.
                                        significant safety matters related to plant operations. Daily discussions                       L
Operational Safety (71707, 71710)
:
'
i
The inspectors were kept informed of the overall plant status and any
l
significant safety matters related to plant operations.
Daily discussions
L
were held with plant management and various members of the plant operating
[
>
>
                                      were held with plant management and various members of the plant operating                      [
4
4                                      staff.                                                                                         (
staff.
)                                                                                                                                       :
(
i                                     The inspectors made routine visits to the control rooms. Ooservations                           !
)
                                        included instrument readings, setpoints and recordings; status of
:
                                      operating systems; status and alignments of emergency standby systems;
i
The inspectors made routine visits to the control rooms. Ooservations
!
included instrument readings, setpoints and recordings; status of
operating systems; status and alignments of emergency standby systems;
onsite and offsite emergency power sources available for automatic
.
operation; purpose of temporary tags on equipment controls and switches;
;
,
;
annunciator alarm status; adherence to procedures; adherence to limiting
i
.
.
                                      onsite and offsite emergency power sources available for automatic
conditions for operations * nuclear instruments operable; temporary
,                                      operation; purpose of temporary tags on equipment controls and switches;                        ;
j
;                                      annunciator alarm status; adherence to procedures; adherence to limiting                        i
i
.
alterations in effect; daily journals and logs; stack monitor recorder
                                      conditions for operations * nuclear instruments operable; temporary                             j
[
i                                     alterations in effect; daily journals and logs; stack monitor recorder                           [
traces; and control room manning.
                                      traces; and control room manning. This inspection activity also included                         s
This inspection activity also included
                                      numerous informal discussions with reactor operators and their                                   !
s
                                      supervisors.
numerous informal discussions with reactor operators and their
;                                                                                                                                       }
!
.                                                                                                                                       t
supervisors.
i                                   General plant tours were conducted on at ':.w a weekly basis.                           Portions
}
;
t
.
i
General plant tours were conducted on at ':.w a weekly basis.
Portions
4
4
                                      of the turbine building, each reactor bui; ag and outside areas were                             l
of the turbine building, each reactor bui;
:                                     visited. Observations included valve positions and system alfgnment;                             l
ag and outside areas were
                                      snubber and hanger conditions; containment isolation aligr.ments;                               ;
l
                                        instrument readings; housekeeping; proper power supply and breaker                             !
:
                                                                                                                                        !
visited.
                                                                                                                                        !
Observations included valve positions and system alfgnment;
                                                                                                            _-                   ----
l
snubber and hanger conditions; containment isolation aligr.ments;
;
instrument readings; housekeeping; proper power supply and breaker
!
!
!
-
----


      .
.
    ,.
,.
                                                2
2
            alignments: radiation area controls; tag controls on equipment; work
alignments: radiation area controls; tag controls on equipment; work
            activities in progress; and radiation protection controls.       Informal
activities in progress; and radiation protection controls.
            discussions were held with selected plant personnel in their functional
Informal
            areas during these tours.
discussions were held with selected plant personnel in their functional
            Durir.g a routine tour on June 27, 1988, the inspector observed a
areas during these tours.
            compensatory fira watch posted in the "B' Shutdown Board (SDB) room who
Durir.g a routine tour on June 27, 1988, the inspector observed a
            appearoa to be inattentive to his duties.       The inspector initiated a
compensatory fira watch posted in the
            discussion with the firewatch in order to ensure that he was alert and
"B'
            then notified a licensee representative who initiated appropriate
Shutdown Board (SDB) room who
            disciplinary action.
appearoa to be inattentive to his duties.
The inspector initiated a
discussion with the firewatch in order to ensure that he was alert and
then notified a licensee representative who initiated appropriate
disciplinary action.
;
;
            During a routine tour on June 29, 1988, the inspector observed an
During a routine tour on June 29, 1988, the inspector observed an
            unapproved flammable liquid container in a storage cage on the Refuel
unapproved flammable liquid container in a storage cage on the Refuel
            F!oor. Upon interviewing Refuel Floor personnel, the inspector learned
F!oor.
            that a glass reageat-type bottle was being used te transport acetone from
Upon interviewing Refuel Floor personnel, the inspector learned
j         the Chemistry Lab to the Refuel Fione for use in cleaning fuel channels
that a glass reageat-type bottle was being used te transport acetone from
i           and other fuel related components.     The empty bottle was stored for 7uture ,
j
the Chemistry Lab to the Refuel Fione for use in cleaning fuel channels
i
and other fuel related components.
The empty bottle was stored for 7uture
,
use.
The use of the bottle is contrary te the requirements of Staadard
'
'
            use.    The use of the bottle is contrary te the requirements of Staadard
Practice 14.36, Hazardous Chemicals / Flammable or Combustible iiquids,
            Practice 14.36, Hazardous Chemicals / Flammable or Combustible iiquids,
which cal's for VL listed cans.
            which cal's for VL listed cans.     Tne inspector contacted a site fire
Tne inspector contacted a site fire
            protection engineer who removed the bottle and instructed refuel floor
protection engineer who removed the bottle and instructed refuel floor
            and chemistry lab personnel on the use of proper containers. Since the
and chemistry lab personnel on the use of proper containers.
,
Since the
            boi.tle was not being used, it was immediately removed, and personnel were
boi.tle was not being used, it was immediately removed, and personnel were
            reinstructed, no violation or deviation will be issued.
,
reinstructed, no violation or deviation will be issued.
I
I
        3. Maintenance Observation (62703)                                               ;
3.
Maintenance Observation (62703)
;
Plant maintenance activities on selected safety-related systems and
'
'
            Plant maintenance activities on selected safety-related systems and
components were observed / reviewed to afcertain that they were conducted in
            components were observed / reviewed to afcertain that they were conducted in !
!
i         accordance with requirements. The following items were corsidered during     <
i
            this review: the Technical Specification limiting conditions for
accordance with requirements.
!         operations were met; activities were accomplisheo using approved
The following items were corsidered during
            procedures; functional testing and/or calibrations were performed prior to
<
i
this review:
            returning components or systems to service; quality control records were
the Technical Specification limiting conditions for
,          maintained; activities were accomplished by qualified personnel; parts and
!
            materials used were pro]erly certified; power tagout clearance procedures
operations were met; activities were accomplisheo using approved
  l         were adhered to; and raciological controls were implemented as required.
procedures; functional testing and/or calibrations were performed prior to
  l         Maintenance Requests (MR) were reviewed to determine the status of           ;
returning components or systems to service; quality control records were
I         outstanding jobs and to assure that priority was assigned to safety-
i
  ,
maintained; activities were accomplished by qualified personnel; parts and
            related eouipment maintenance which might affect plant safety. The
,
j           inspectors observed the below listed maintenance activities during this
materials used were pro]erly certified; power tagout clearance procedures
  l         reporting period:
l
            a.   Mechanical Maintenance Instruction (MMI) 190, Control Red Drive
were adhered to; and raciological controls were implemented as required.
                  Unlatching.                                                             ;
l
            b.   MMI 7, Control Rod Drive Changeout.
Maintenance Requests (MR) were reviewed to determine the status of
            c.   Operating Instruction (01)-85, Control Rod Insert and Withdraw
;
                  Timing, portions performed as post-maintenance testing.
I
                                                                                          .
outstanding jobs and to assure that priority was assigned to safety-
                                    *
related eouipment maintenance which might affect plant safety.
The
,
j
inspectors observed the below listed maintenance activities during this
l
reporting period:
a.
Mechanical Maintenance Instruction (MMI) 190, Control Red Drive
Unlatching.
;
b.
MMI 7, Control Rod Drive Changeout.
c.
Operating Instruction (01)-85, Control Rod Insert and Withdraw
Timing, portions performed as post-maintenance testing.
.
*


  _ _ _     __       _ _ ____                       _ _ _ _ _ _ _ _   _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _
        .       .
__
                                                                                                                                  3
_ _ ____
                                      d.         Diesel Generator (DG) "0" troubleshooting and corrective maintenance
_ _ _ _ _ _ _ _
                                                  activities related to the inadvertent overload on June 21, 1988
_ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                  (refer to paragraph 5.c, of this report for details).
.
                                      e.         MR Bf1074 dated May 10, 1988, was indicatad as being outstanding
.
                                                  durine a tour conducted on June 27, 1988. This MR documented a need
3
                                                  for c'eaning the Units 1/2 "B" DG batteries. The inspector observed                                                                           i
d.
                                                  a heavy layer of dust and white particulate material on top of the
Diesel Generator (DG) "0" troubleshooting and corrective maintenance
                                                  batteries. In addition, the inspector noted that on four of the
activities related to the inadvertent overload on June 21, 1988
                                                  battery cells, the spark arrestor vent covers were missing and the
(refer to paragraph 5.c, of this report for details).
                                                  particulate material had entered into the battery electrolyte through
e.
                                                  the openings. The inspector informed a licensee representative of
MR Bf1074 dated May 10, 1988, was indicatad as being outstanding
                                                  the deficient condition and also pointed out to the plant maintenance
durine a tour conducted on June 27, 1988.
                                                  supervisor that the more than seven week turnaround on completing a
This MR documented a need
                                                                                                                                    MR was excessive. The batteries were
for c'eaning the Units 1/2 "B" DG batteries.
The inspector observed
i
a heavy layer of dust and white particulate material on top of the
batteries.
In addition, the inspector noted that on four of the
battery cells, the spark arrestor vent covers were missing and the
particulate material had entered into the battery electrolyte through
the openings.
The inspector informed a licensee representative of
the deficient condition and also pointed out to the plant maintenance
supervisor that the more than seven week turnaround on completing a
routine "request for cleaning"ll quantity of the material in the
MR was excessive.
The batteries were
'
'
                                                  routine
immediately cleaned and a sma
                                                  immediately       "request                        cleaned       forand
electrolyte was evaluated as having no impact on battery performance.
                                                                                                                        cleaning"ll
Within this area no violations or deviations were found.
                                                                                                                          a sma     quantity of the material in the
4.
                                                  electrolyte was evaluated as having no impact on battery performance.
Independent Audits (40704)
                                      Within this area no violations or deviations were found.
a.
                  4.                   Independent Audits (40704)
Independent Safety Engineering Group (ISEG)
!
4
4
                                      a.          Independent Safety Engineering Group (ISEG)                                                                                                    !
i
                                                                                                                                                                                                  i
The licensee implemented the ISEG in early 1988 as discussed in the
                                                  The licensee implemented the ISEG in early 1988 as discussed in the
;
;                                                 BFNP Nuclear Performance Plan. Tne inspector reviewed the last three
BFNP Nuclear Performance Plan.
j                                                 monthly reports and found them to be well focussed on current
Tne inspector reviewed the last three
                                                  industry problems as well as specific site weaknesses. The reports
j
                                                  were professional and thorough. The ISEG review topics included:
monthly reports and found them to be well focussed on current
'                                                  (1l
industry problems as well as specific site weaknesses.
                                                  (3, NRCthe          Information                   Licensee Event          Report
The reports
                                                                                                                        Notices; and (LER)
were professional and thorough.
                                                                                                                                      (4) Plant          program; (2) Control
The ISEG review topics included:
                                                                                                                                                              Operations ReviewAir System;
(1l NRCthe Licensee Event Report (LER) program; (2) Control Air System;
(3,
Information Notices; and (4) Plant Operations Review
'
Committee (PORC) review of plant modifications.
With continued
,
;
diligence, the ISEG should satisfactorily fulfill its role in
;
providing appraisals of the quality and safety of operation to the
licensee s upper management.
b.
American Nuclear Insurers Nuclear Liability Insurance Inspection
j
A nuclear liability insurance inspection was conducted by the
,
;
American Nuclear Insurers during February 1988,
The inspection
report and ifcensee's response to the report were made available to
i
!
the resident inspectors.
The inspection focused on Onsite Safety
;
Review, Operations, Radwaste Management, Health Physics, and Plant
Water Chemistry.
Three recommendations were made and two suggestions
i
were offered.
The inspection findings did not point to any
,
,
                                                  Committee (PORC) review of plant modifications. With continued
programmatic weaknesses not already known to the NRC.
;                                                  diligence, the ISEG should satisfactorily fulfill its role in
The resident
;                                                  providing appraisals of the quality and safety of operation to the
had attended the exit and considered the most significant weakness
                                                  licensee s upper management.
!
                                      b.          American Nuclear Insurers Nuclear Liability Insurance Inspection
identified to be in the area of root cause analysis and recurrence
j                                                  A nuclear liability insurance inspection was conducted by the                                                                                  ,
!
;                                                  American Nuclear Insurers during February 1988, The inspection
control.
i                                                  report and ifcensee's response to the report were made available to
!                                                  the resident inspectors. The inspection focused on Onsite Safety
;                                                  Review, Operations, Radwaste Management, Health Physics, and Plant
                                                  Water Chemistry.                                                Three recommendations were made and two suggestions                            i
,                                                  were offered.                                                  The inspection findings did not point to any
                                                  programmatic weaknesses not already known to the NRC.                                                                 The resident
                                                  had attended the exit and considered the most significant weakness                                                                             !
                                                  identified to be in the area of root cause analysis and recurrence                                                                             !
,
,
                                                  control.
!
                                                                                                                                                                                                  !
'
                                                                                                                                                                                                  '
!
!
:
:
          .   -
.
                        _ _ _ _ _ _ _ _ _ _ _ _ -                   ,.                               . _ . _ _       ._     __       , _ _ _ _ _ _ . ,_ _
-
                                                                                                                                                                                ._. . - - _ _ _.
_ _ _ _ _ _ _ _ _ _ _ _ -
,.
. _ . _ _
._
__
, _ _ _ _ _ _ . ,_
._.
. - - _ _
_.
_


  _ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _
_ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _
                                    . .
.
                                                                                    4
.
                                            c.   Safety System Functional Inspecdon (SSFI)
4
                                                  The licensee's QA organization coordinated an SSFI performed pri-
c.
                                                  marily by an outside contractor during the period of June 6 - July 1,
Safety System Functional Inspecdon (SSFI)
                                                  1988.   The inspection was patterned after the NRC's SSFI as described
The licensee's QA organization coordinated an SSFI performed pri-
                                                  in NRC Inspection Manual Chapter 2515. The team identified 24
marily by an outside contractor during the period of June 6 - July 1,
                                                  concerns documented as "observations". Fourteen of the observations
1988.
                                                  were judged by the team to be safety significant or potentially
The inspection was patterned after the NRC's SSFI as described
                                                  significant depending upon the outcome of further review and analysis
in NRC Inspection Manual Chapter 2515.
                                                  to be performed by the licensee. The team reviewed the RHRSW and
The team identified 24
concerns documented as "observations".
Fourteen of the observations
were judged by the team to be safety significant or potentially
significant depending upon the outcome of further review and analysis
to be performed by the licensee.
The team reviewed the RHRSW and
EECW systems.
The majority of the observations were found to have
been previously identified by the licensee or the NRC and in some
'
'
                                                  EECW systems.      The majority of the observations were found to have
formal tracking program for closecut.
                                                  been previously identified by the licensee or the NRC and in some
,
,                                                formal tracking program for closecut.
One deficiency was found to impact system operability under the
                                                  One deficiency was found to impact system operability under the
existing plant conditions.
                                                  existing plant conditions. Due to recurring failures of valves 67-50
Due to recurring failures of valves 67-50
                                                  and 67-51, the potential for failure of these valves was judged to be
and 67-51, the potential for failure of these valves was judged to be
                                                  significant.
significant.
                                                                    These and
These are cross-connect valves between the safetyld
                                                  related EECW system     are the
related EECW system and the non-safety-related RCW system.
                                                                                cross-connect  valvesRCW
Shou
                                                                                  non-safety-related between the safetyld
these valves fsil to close as required under certain circumstances,
                                                                                                          system.   Shou
insufficient cooling water to the diesel engine coolers could result.
                                                  these valves fsil to close as required under certain circumstances,
The licensee suspended fuel handling operations on June 30, 1988,
                                                  insufficient cooling water to the diesel engine coolers could result.
until the valves were tagged closed on a clearance hold order to
                                                  The licensee suspended fuel handling operations on June 30, 1988,
eliminate this concern.
                                                  until the valves were tagged closed on a clearance hold order to
The SSFI team made several conclusions from the characterization of
                                                  eliminate this concern.
the findings.
                                                  The SSFI team made several conclusions from the characterization of
The maintenance area was judged to be the weakest of
                                                  the findings. The maintenance area was judged to be the weakest of
those evaluated.
                                                  those evaluated. Weaknesses were also noted in design calculation
Weaknesses were also noted in design calculation
                                                  verification and licensee review of calculations performed by
verification and licensee review of calculations performed by
                                                  contractors.     The team further detected a lack of sensitivity among
contractors.
;                                                 plant personnel as far as respect for the operational status of the
The team further detected a lack of sensitivity among
                                                  system.     This may be attributed to the extensive shutdown during
;
                                                which the system status was not maintained and the mind-set that
plant personnel as far as respect for the operational status of the
                                                  accompanies such a shutdown.
system.
                                                  The final SSFI report will be reviewed and TVA's response to the
This may be attributed to the extensive shutdown during
                                                  findings will be monitored.
which the system status was not maintained and the mind-set that
                                            No violations or deviations were identified.
accompanies such a shutdown.
                                        5. Costart Test Program (RTP)
The final SSFI report will be reviewed and TVA's response to the
                                            The inspector attended RTP status meetings; reviewed RTP test procedures,
findings will be monitored.
                                            test specifications, and baseline test requirement documents; observed
No violations or deviations were identified.
                                            RTP tests and associated tests performances; and reviewed RTP test results
5.
                                            including test exceptions. The inspector also attended selected Restart
Costart Test Program (RTP)
                                            Operations Center (War Room) and JTG meetings.
The inspector attended RTP status meetings; reviewed RTP test procedures,
                                            a.   Summary of RTP Activities
test specifications, and baseline test requirement documents; observed
                                                  (1) RTP-03A, Reactor Feedvater
RTP tests and associated tests performances; and reviewed RTP test results
                                                        This test was approved by the JTG for performance on June 16,
including test exceptions.
                                                        1988.   It consisted of verifying various signals, including
The inspector also attended selected Restart
                                            .                                                                             _.
Operations Center (War Room) and JTG meetings.
a.
Summary of RTP Activities
(1) RTP-03A, Reactor Feedvater
This test was approved by the JTG for performance on June 16,
1988.
It consisted of verifying various signals, including
.
_.


                                                                                          -
- - - - 7
----7
-
      .
.
  ,-
,-
                                          5
5
              reactor level and pressure signals to the reactor protective
reactor level and pressure signals to the reactor protective
              system and high reactor level trip signals to the HPCI and
system and high reactor level trip signals to the HPCI and
              RCICinjectionsystemturbines. The test was completed with the
RCICinjectionsystemturbines.
              exception of section 5.16 which, in part, requires verifying
The test was completed with the
              high reactor pressure trip of the recirculation pumps.
exception of section 5.16 which, in part, requires verifying
        (2) RTP-23, RHRSW
high reactor pressure trip of the recirculation pumps.
            Outages     continued
(2) RTP-23, RHRSW
              the majority of effortthroughout most of this the
Outages continued throughout most of this reporting) period with
                                      aimed at completing   reporting) period of
the majority of effort aimed at completing the rep acoment of
                                                                rep acoment   with
Dresser Couplings and completing "the hy"drostatic test and
            Dresser Couplings and completing "the hy"drostatic test and
restoration of the "Al",
              restoration of the "Al", "A2", "81, "B2 , "C1", "C2", "D1",
"A2", "81, "B2 , "C1", "C2", "D1",
            and "D2" pumps. Flood level switch replacement continued to be
and "D2" pumps.
            a problem, in that a dedicated switch has not been found.
Flood level switch replacement continued to be
        (3) RTP-038, RXFW
a problem, in that a dedicated switch has not been found.
            This test was released for performance by the JTG on June 30,
(3) RTP-038, RXFW
            1988.   It deals mainly with the RXFW pumas and their trips
This test was released for performance by the JTG on June 30,
              including low main condensor vacuum and ligh reactor water
1988.
              level. Monitoring of this test will be covered in future NRC
It deals mainly with the RXFW pumas and their trips
            reports.
including low main condensor vacuum and ligh reactor water
        (4) RTP-024 RCW
level.
            This test was completed during this reporting period with 47
Monitoring of this test will be covered in future NRC
            total tests exceptions identified. Of these exceptions, seven
reports.
            had hardware significance. MRs were written to correct six of
(4) RTP-024 RCW
            them however, TE-046, which deals with check valve 1-24-852,
This test was completed during this reporting period with 47
            will; require DNE resolution.
total tests exceptions identified.
        (5) RTP-030, Diesel Generator and Reactor Building Ventilation
Of these exceptions, seven
            This test continues to be delayed by parts requirements,
had hardware significance.
            especially flow switches and damper motors. Approximately 24
MRs were written to correct six of
            test exceptions have been identified with the majority involving
them however, TE-046, which deals with check valve 1-24-852,
            the failure
will; require DNE resolution.
            88-0524      of DG fans to stop or start as rewas issuedCAQR  as a result of thi
(5) RTP-030, Diesel Generator and Reactor Building Ventilation
        (6)              Control Building Heating, Ventilation, and Air
This test continues to be delayed by parts requirements,
            RTP-31A,
especially flow switches and damper motors.
            Condition ing
Approximately 24
            Section 5.1 of this test was released by the JTG for performance
test exceptions have been identified with the majority involving
            in order to support the LOP /LOCA series of tests. This section
the failure of DG fans to stop or start as rewas issued as a result of thi
            mainly involved the CREVS. Additional tests will start af ter
CAQR
            the completion of the LOP /LOCA tests. No specific test excep-
88-0524
            tions have been identified.
Control Building Heating, Ventilation, and Air
(6)
RTP-31A, ing
Condition
Section 5.1 of this test was released by the JTG for performance
in order to support the LOP /LOCA series of tests.
This section
mainly involved the CREVS.
Additional tests will start af ter
the completion of the LOP /LOCA tests.
No specific test excep-
tions have been identified.


                                                                                                                  __________ _ _____
__________ _ _____
. .
.
                                                                    6
.
    (7) RTP-318, Control Building HVAC
6
          Before this test can start, DNE must issue revision number
(7) RTP-318, Control Building HVAC
          three (Rev. 3 to BTRD-014. As of the end of June 1988, this
Before this test can start, DNE must issue revision number
          revision was ssued and the RTG group was in the final stages of
three (Rev. 3 to BTRD-014.
          writing and approving RTP-0318.
As of the end of June 1988, this
    (8) RTP-39, C02 Storage and Fire Protection
revision was ssued and the RTG group was in the final stages of
          This test was completed during this reporting period with no
writing and approving RTP-0318.
          specific test exceptions identified. The test consisted of
(8) RTP-39, C02 Storage and Fire Protection
          smoke detector activation, CO2 logic testing in DG rooms, and
This test was completed during this reporting period with no
          loss of control power tests.
specific test exceptions identified.
    (9) RTP-057-1, 120 Volt DC Battery
The test consisted of
          This test involves the 8 DGs and covers a total of 16 battery
smoke detector activation, CO2 logic testing in DG rooms, and
          chargers and battery racks. Prior to each test on the battery
loss of control power tests.
          chargers, the filter capacitors must be changed. As of the end
(9) RTP-057-1, 120 Volt DC Battery
          of June 1988, ONE was revising the BTRD and the RTP grcup was
This test involves the 8 DGs and covers a total of 16 battery
          changing the system test specification and the RTP procedure.
chargers and battery racks.
          No test exceptions were identified.
Prior to each test on the battery
    (10) RTP-57-2, 120 V AC Distribution (120V DIST)
chargers, the filter capacitors must be changed.
          This test win virtually completed during this reporting period.
As of the end
          One   outstancing
of June 1988, ONE was revising the BTRD and the RTP grcup was
          dealing    with the performance            test exception         was
changing the system test specification and the RTP procedure.
                                                                        of Test    written involving)section
No test exceptions were identified.
                                                                                  Instruction       (TI 738, which 5.2
(10) RTP-57-2, 120 V AC Distribution (120V DIST)
          could not be performed because of the fire damage in the Unit 2
This test win virtually completed during this reporting period.
          Orywell.
One outstancing test exception was written involving)section 5.2
    (11) RTP-57-4, 480 Volt Distribution (480V OIST)
dealing with the performance of Test Instruction (TI 738, which
          This test was virtually completed; however, a total of 53 test
could not be performed because of the fire damage in the Unit 2
          exceptions were identified. Of these test exceptions, ten had                                                                 l
Orywell.
          hardware related issues.                                                                                                     >
(11) RTP-57-4, 480 Volt Distribution (480V OIST)
    (12) RTP-57-5, 4160 Volt Distribution (4 KV DISTRIBUTION)
This test was virtually completed; however, a total of 53 test
          This test is ongoing and has identified approximately 20 test
exceptions were identified.
          exceptions; however, only two have hardware significance.                                             One
Of these test exceptions, ten had
          of the ma                                                                               setpoints and
l
          tolerances,jor             restraints       were todeals        with rela
hardware related issues.
                                                                                                                                        ,
>
                              which                                   be supplied   b ONE through a                                   L
(12) RTP-57-5, 4160 Volt Distribution (4 KV DISTRIBUTION)
          contractor. The six special tests involv ng the Unit 1/2 OG                                                                   ;
This test is ongoing and has identified approximately 20 test
          voltage regulators and speed governors have all been completed                                                               -
exceptions; however, only two have hardware significance.
                                                                                                                                        '
One
          and are awaiting approval by DNE.
of the ma
                                                                                                                                        ,
setpoints and
                                                                                                                                        !
tolerances,jor restraints deals with rela
                                                                                                                                        :
,
                                                                                                                                        i
which were to be supplied b
                  , ._ _ . . . , . . . . . _ . _ _ . - _ . _ _ ~ _           __     - . _ . .     -. -                           -
ONE through a
L
contractor.
The six special tests involv ng the Unit 1/2 OG
;
voltage regulators and speed governors have all been completed
-
and are awaiting approval by DNE.
'
,
:
i
_
, . _ . .
. , . . . . . _ . _ _ . - _ . _ _ ~ _
__
- . _ . .
-. -
-


  _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ - _ _
                                  '
                                    .
                    ..
                                                                          7
                                      (13) RTP-067, EECW
                                              This system, as with aystem 23 (RHRSW), was also involved with
                                              the replacement of Dresser couplings and the system hydro's.
;                                            The testing in progress involved mainly section 5.8 which deals
                                              with various chillers such as the control room emergency
                                              chillers and the SDB room chillers. One hardware test exception
                                              was identified involving temperature control valve 3-TCV-67-83.
                                      (14) RTP-069, RWCU
                                              This test was released by the JTG on June 17, 1987, and the
'
'
                                            majority of effort so far has been directed at completing
.
                                              section 2.0, Prerequisites and section 5.1, Valve Stroke Tests.
..
                                              NosignificanttestexceptIonshavebeenidentified.
7
                                      (15) RTP-070, RBCCW
(13) RTP-067, EECW
                                              This test was partially released as reported in NRC report
This system, as with aystem 23 (RHRSW), was also involved with
                                            88-10.     Since it started, approximately 27 test exceptions
the replacement of Dresser couplings and the system hydro's.
:                                             have been identified with 8 having hardware related issues.
;
                                      (16) RTP-073, HPCI
The testing in progress involved mainly section 5.8 which deals
                                              The JTG approved this test; however, it has not released the
with various chillers such as the control room emergency
chillers and the SDB room chillers.
One hardware test exception
was identified involving temperature control valve 3-TCV-67-83.
(14) RTP-069, RWCU
This test was released by the JTG on June 17, 1987, and the
majority of effort so far has been directed at completing
'
section 2.0, Prerequisites and section 5.1, Valve Stroke Tests.
NosignificanttestexceptIonshavebeenidentified.
(15) RTP-070, RBCCW
This test was partially released as reported in NRC report
88-10.
Since it started, approximately 27 test exceptions
:
have been identified with 8 having hardware related issues.
(16) RTP-073, HPCI
The JTG approved this test; however, it has not released the
l
l
                                              test for performance.
test for performance.
l                                     (17) RTP-074, RHR
l
(17) RTP-074, RHR
1
1
,                                          This test is being im) acted in Section 5.5 which requires
This test is being im) acted in Section 5.5 which requires
                                              testing of the drywell spray upper and lower header, by the
,
!                                           hydrolazing of the lower header. This activity was set to
testing of the drywell
                                              start on or about July 5, 1988. No significant hardware test
spray upper and lower header, by the
                                            exceptions have been identified.
!
                                      (18) RTP-082, Diesel Generators
hydrolazing of the lower header.
This activity was set to
start on or about July 5, 1988.
No significant hardware test
exceptions have been identified.
l
l
!                                           This system is undergoing a series of special tests involving
(18) RTP-082, Diesel Generators
;                                           all eight OGs. These are being performed by the system
!
j                                           engineers working with vendor renresentatives and onsite DNE
This system is undergoing a series of special tests involving
;
all eight OGs.
These are being performed by the system
j
engineers working with vendor renresentatives and onsite DNE
personnel.
A total of ten special tests are involved and will
,
,
                                            personnel.    A total of ten special tests are involved and will
result in the DG's speed governors (hydraulic actuators) and
.                                            result in the DG's speed governors (hydraulic actuators) and
.
                                            voltage regulators being calibrated as well as optimized for
voltage regulators being calibrated as well as optimized for
:                                           plant operations. This system test has identified over 50 test
:
!                                           exceptions; however, only three have significant hardware
plant operations.
)                                             issees.   See Section 5.c. of this report for additional
This system test has identified over 50 test
;                                             information on DG testing.
!
exceptions; however, only three have significant hardware
)
issees.
See Section 5.c. of this report for additional
;
information on DG testing.
1
1
i
i
!
!
1
1
.
-
- -
-
- -
-
.
.
. -
.
-


    .- _ _ _ _______ -____           _ _ - _ _ _ _ -         . _ _ _
.- _ _ _ _______ -____
                                                                                                                                ;
_ _ - _ _ _ _ -
  ..                     .
. _ _ _
                                                                                                                                ,
;
                                                                                                                                  '
.
                                                                                  8
..
                                                                                                                                !
,
                                                                                                                                i
'
                                                                                                                                '
8
!
i
'
(19) RTP-084, Containment Atmospheric Dilution
'
'
                            (19) RTP-084, Containment Atmospheric Dilution
This test was released by the JTG for performance on May 25,
i                                  This test was released by the JTG for performance on May 25,
i
                                    1988.               The majority of effort has been directed at completing                 ,
1988.
                                    the prerequisites. Section 5.1 deals with verifying the logic                               :
The majority of effort has been directed at completing
                                  on a series of valves and replacing Class IE splices with                                   !
,
                                  qualified Raychem splices,                                                                   t
the prerequisites.
Section 5.1 deals with verifying the logic
:
on a series of valves and replacing Class IE splices with
!
qualified Raychem splices,
t
(20) RTP-085, Control Rod Drive
f
.
.
                            (20) RTP-085, Control Rod Drive
This test was delayed by the changeout of 82 rod drive
                                                                                                                              f
i
'
'
                                  This test was delayed by the changeout of 82 rod drive                                      i
mechanisms and the repairs to several rod position indicators.
                                                                                                                                '
'
                                  mechanisms and the repairs to several rod position indicators.
Section 5.2, Rod Position Indicating System Function Test}fied.
                                                                                                                      has
[
                                  Section
has
                                  started and            5.2,no Rod     Positiontest
started and no significant test exceptions have been ident
                                                                      significant  Indicating System
(21) RTP-092, Neutron Monitoring
                                                                                      exceptions  haveFunction
                                                                                                        been identTest}fied.
                                                                                                                              [
,
,
                            (21) RTP-092, Neutron Monitoring
                                                                                                                              <
1
1
                                  This test involves the intermediate range monitors (IRMs),                                   ;
<
                                  source range monitors (SRMs), and the average power range
This test involves the intermediate range monitors (IRMs),
;                                 monitors (APRMs). The test was released for performance by the                               i
;
                                  JTG on May 23, 1988; however, a switch involved in the inop                                 1
source range monitors (SRMs), and the average power range
;                                 bypass for the SRMs                         IRMs, and APRMs were not easily obtained         -
;
i                                 and contributed to delays.                         No significant hardware test excep-
monitors (APRMs).
The test was released for performance by the
i
JTG on May 23, 1988; however, a switch involved in the inop
1
;
bypass for the SRMs
IRMs, and APRMs were not easily obtained
-
i
and contributed to delays.
No significant hardware test excep-
:
:
tions were identified.
l
,
,
                                  tions were identified.                                                                      l
;
                                                                                                                              ;
j
j                           (22) RTP-99, Reactor Protective System (RPS)                                                     j
(22) RTP-99, Reactor Protective System (RPS)
j
This test was released by the JTG for performance on June 17,
I
'
'
                                  This test was released by the JTG for performance on June 17,                                I
:
:                                  1988                 and involves all four channels of the RPS. One                         !
1988
j                                 signIficant hardware test exception was identified involving
and involves all four channels of the RPS.
                                  Section 5.27, which requires that the reactor mode switch
One
                                                                                                                                ,
!
j
signIficant hardware test exception was identified involving
,
Section 5.27, which requires that the reactor mode switch
l
3
3
                                                                                                                              l
i
i                                  contacts be verified, and concerns wires in the panel not being
contacts be verified, and concerns wires in the panel not being
1                                 mi4r ked.
f
                                                                                                                              f
1
j                            (23) RTP-8'             J C, Backup Control Test (BUC)
mi4r ked.
                                                                                                                              '
j
                                  This test procedure is over 800 pages long and includes the 4KV
(23)
                                  SD8s, 480 V SD8s, DG auxiliary boards, 480V reactor motor
RTP-8' C, Backup Control Test (BUC)
i                                 operated valve (MOV) boards, and the 250 V reactor MOV boards
J
)                                 (also any electrical system that has backup controls). The test                             ;
'
)                                 was released for performance by the JTG on June 13, 1988, and
This test procedure is over 800 pages long and includes the 4KV
                                  has been performed on a continuous basis. No significant test                               ;
SD8s, 480 V SD8s, DG auxiliary boards, 480V reactor motor
i
operated valve (MOV) boards, and the 250 V reactor MOV boards
)
(also any electrical system that has backup controls).
The test
;
)
was released for performance by the JTG on June 13, 1988, and
has been performed on a continuous basis.
No significant test
exceptions were identified.
;
.
.
                                  exceptions were identified.
The above tests were in progress and in various stages of completion
                              The above tests were in progress and in various stages of completion
at the end of this reporting period.
                              at the end of this reporting period. The inspector will continue to
The inspector will continue to
l                             observe these activities on a day-to-day basis.                                                 l
l
                                                                                                                                ?
observe these activities on a day-to-day basis.
q                                                                                                                               f
l
?
f
q
i
i
!                                                                                                                             !
!
\                                                                                                                             I
!
                                                                                                                              a
\\
I
a


,_ -_         ___ __- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
,_ -_
          -
___ __- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
        .   .
-
      .
.
                                                                                          9
.
                                                      b. RTP-075, Core Spray
.
                                                        During the performance of RTP-075, Core Spray, the RTP group was
9
                                                        using SI-4.2.8-39A(II) to meet the requirements of step 5.6.5 of the
b.
                                                        RTP test.   This was to prove that the CS system Loop II would perform
RTP-075, Core Spray
                                                        automatically when called u                     However, during the
During the performance of RTP-075, Core Spray, the RTP group was
                                                        performance of the SI, the 'pon to do so.20" CS pump automatic circuit break
using SI-4.2.8-39A(II) to meet the requirements of step 5.6.5 of the
                                                        failed to close when required. MR A-860183 was written to trouble-
RTP test.
                                                        shoot the problem and the RTP personnel wrote TE #9 to document the
This was to prove that the CS system Loop II would perform
                                                        failure. During troubleshooting, maintenace personnel discovered an
automatically when called u
                                                        undocumented splice in the white lead of cable ES-2554-II, which was
However, during the
                                                        in a cable tray surrounded by flamemastic and located in the Unit 2
performance of the SI, the 'pon to do so.20" CS pump automatic circuit break
                                                        reactor building. The maintenance personnel wrote CAQR BFP-88-0375
failed to close when required.
                                                        to document this discovery. This item is identified as inspector
MR A-860183 was written to trouble-
                                                        followup item (IFI) 260/88-18-01 Undocumented Cable Conductor Splice
shoot the problem and the RTP personnel wrote TE #9 to document the
                                                        in Core Spray Logic Wiring. Thlsitemisrequiredtobeclosedout
failure.
                                                        prior to restart.     The disposition of this CAQR will be reviewed in
During troubleshooting, maintenace personnel discovered an
                                                        a future inspection.
undocumented splice in the white lead of cable ES-2554-II, which was
                                                        One significant test exception involving the stroke time for four
in a cable tray surrounded by flamemastic and located in the Unit 2
                                                        flow control valves was identified.
reactor building.
                                                      c. RTP-082 Diesel Generators
The maintenance personnel wrote CAQR BFP-88-0375
                                                        OG "0"                     overloaded on June 21 1988, during the
to document this discovery.
                                                        conductwas    inadvertently
This item is identified as inspector
                                                                  of Special Test    (ST) 88-09, Diesel Gene,rator Governor and
followup item (IFI) 260/88-18-01 Undocumented Cable Conductor Splice
                                                        Voltage Regulator Calibration. For a period of about 30 seconds,
in Core Spray Logic Wiring.
                                                        control room indications of KW, KVAR, and AMPS were off scale high.
Thlsitemisrequiredtobeclosedout
                                                        The incident was caused by unintentional shorting of test leads by an
prior to restart.
                                                        electrician who was directed to take confirmatory measurements of a
The disposition of this CAQR will be reviewed in
                                                        parameter beint monitored on a recorder. The shorting caused fuses
a future inspection.
                                                        to blow result < ng in a loss of the voltage regulator and governor.
One significant test exception involving the stroke time for four
                                                        Since the DG was in parallel with the grid during the test, it
flow control valves was identified.
                                                        immediately accepted this additional load. An apparently pre-
c.
                                                        existing and undetected failure of an SBN switch (cell switch) in the
RTP-082 Diesel Generators
                                                        DG breaker compartment prevented an automatic clearing of the
OG "0" was inadvertently (ST) 88-09, Diesel Gene,rator Governor and
                                                        overload thus increasing the potential damage to the DG. The event
overloaded on June 21
                                                        wastermlnatedwhenthecontrolroomoperatortrippedtheDGbreaker.
1988, during the
                                                        Following the event, the electrical integrity of the DG was confirmed
conduct of Special Test
                                                        by the satisfactory performance of a high potential test at 10,000
Voltage Regulator Calibration.
                                                        VOC for one minute. Visual inspections were conducted of the
For a period of about 30 seconds,
                                                        insulation system by an experienced vendor representative. Some
control room indications of KW, KVAR, and AMPS were off scale high.
                                                        hairline cracks in the insulation were detected which were determined
The incident was caused by unintentional shorting of test leads by an
                                                        to have been recently created. These cracks were indicative of coil
electrician who was directed to take confirmatory measurements of a
                                                        movement relative to the fixed components and could have resulted
parameter beint monitored on a recorder.
                                                        from either the overload or some of the more recent stressful restart
The shorting caused fuses
                                                        testing. The vendor representative recommended followup high poten-
to blow result < ng in a loss of the voltage regulator and governor.
                                                        tial testing at 6,12 and 24 months in order to detect any further
Since the DG was in parallel with the grid during the test, it
                                                        degradation of the insulation system as a result of the overload.   No
immediately accepted this additional load.
An apparently pre-
existing and undetected failure of an SBN switch (cell switch) in the
DG breaker compartment prevented an automatic clearing of the
overload
thus increasing the potential damage to the DG.
The event
wastermlnatedwhenthecontrolroomoperatortrippedtheDGbreaker.
Following the event, the electrical integrity of the DG was confirmed
by the satisfactory performance of a high potential test at 10,000
VOC for one minute.
Visual inspections were conducted of the
insulation system by an experienced vendor representative.
Some
hairline cracks in the insulation were detected which were determined
to have been recently created.
These cracks were indicative of coil
movement relative to the fixed components and could have resulted
from either the overload or some of the more recent stressful restart
testing.
The vendor representative recommended followup high poten-
tial testing at 6,12 and 24 months in order to detect any further
degradation of the insulation system as a result of the overload.
No
L_.
L_.


                                                              _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                 .
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
    .
.
  .   .
.
.
.
,
,
        .
.
                                              10
10
              mechanical inspections were performed on the diesel engine. The
mechanical inspections were performed on the diesel engine.
              licensee relied upon the expertise of the vendor representative who
The
              waspresentattheDGduringtheoverloadtomakethisjudgment.
licensee relied upon the expertise of the vendor representative who
              The licensee prepared a critique on the event which concluded that
waspresentattheDGduringtheoverloadtomakethisjudgment.
              the capability of the DG to perform its intended function had nnt
The licensee prepared a critique on the event which concluded that
              been affected. Following a review by the PORC on June 25, 1988, the
the capability of the DG to perform its intended function had nnt
              DG was declared fully operable.
been affected.
              The inspector .eviewed the event and asked for additional information
Following a review by the PORC on June 25, 1988, the
              on:   1) the cause of failure for the SBM cell switch and whether
DG was declared fully operable.
The inspector .eviewed the event and asked for additional information
on:
1) the cause of failure for the SBM cell switch and whether
the other DG cell switches had bi:en tested 2) an approximation of
the magnitude o/ the overload; 3) a comparison of diesel operating
i
parameters such as vibration, exhaust /c
temperature, oil pressures, oil analysis, ylinder/ cooling water
and oil and fuel consump-
tion before the event with those af ter the event; and 4) other
i
i
              the other DG cell switches had bi:en tested 2) an approximation of
diagnostics and/or inspections contained in the vendor technical
              the magnitude o/ the overload; 3) a comparison of diesel operating
manuals.
              parameters such as vibration, exhaust /c
During the course of the review, the inspector learned that the
              temperature, oil pressures, oil analysis, ylinder/
incident was not documented, as required, on a CAQR.
                                                            and oil and                                                      cooling water
This may have
                                                                                                                              fuel consump-
been a contributing cause to the fragmented approach used to evaluate
              tion before the event with those af ter the event; and 4) other
and document the condition of the diesel.
i            diagnostics and/or inspections contained in the vendor technical
Part I, Section 2.16, Step
              manuals.
2.1.1.F of the Nuclear Quality Assurance Manual requires that a
              During the course of the review, the inspector learned that the
              incident was not documented, as required, on a CAQR. This may have
              been a contributing cause to the fragmented approach used to evaluate
              and document the condition of the diesel. Part I, Section 2.16, Step
,
,
              2.1.1.F of the Nuclear Quality Assurance Manual requires that a
condition adverse to quality (CAQ) be documented on a CAQR for items
              condition adverse to quality (CAQ) be documented on a CAQR for items
which have been subjected to conditions for which they have not
              which have been subjected to conditions for which they have not
been designed such as overaressure overvoltage, overheating, over-
              been designed such as overaressure overvoltage, overheating, over-
stressing, or environmenta'
i            stressing, or environmenta' conditions hazardous to their function.
conditions hazardous to their function.
i
Failure to initiate a CAQR for the overloaded DG is considered
;
;
              Failure to initiate a CAQR for the overloaded DG is considered
a violation of 10 CFR 50, Appendix B, Criterion V (259,260,296/
              a violation of 10 CFR 50, Appendix B, Criterion V (259,260,296/
88-18-02).
              88-18-02).
1
1         d. Loss of Power / Loss of Coolant Accident (LOP /LOCA) Testing
d.
Loss of Power / Loss of Coolant Accident (LOP /LOCA) Testing
I
I
              The licensee's RTP group and the system engineering group, with
The licensee's RTP group and the system engineering group, with
l'
l
              support from th viher major Browns Ferry site organizations,
support from th viher major Browns Ferry site organizations,
              performed a series of four tests referred to as LOP /LOCA testing,
'
>            which started on May 29, 1988, with LOP /LOCA Test "A" and ended at
performed a series of four tests referred to as LOP /LOCA testing,
:             approximately midnight on June 8,1988, with LOP /LOCA Test "0".
which started on May 29, 1988, with LOP /LOCA Test "A" and ended at
>
:
approximately midnight on June 8,1988, with LOP /LOCA Test "0".
)
)
              Numerous pretest meetings were bid such as LOP /LOCA thrice weekly
Numerous pretest meetings were bid such as LOP /LOCA thrice weekly
punchlist, daily RTP status, afG as needed, and a daily morning
;
;
              punchlist, daily RTP status, afG as needed, and a daily morning
J
J
              meeting with the major site organizations to update the LOP /LOCA
meeting with the major site organizations to update the LOP /LOCA
,
,
              testing status. A total of nine inspectors, five region based and
testing status.
A total of nine inspectors, five region based and
4
4
              four residents, observed the performance of the four tests, with
four residents, observed the performance of the four tests, with
LOP /LOCA Test ',C" receiving the most coverag/L A
1
1
              LOP /LOCA Test ',C"                              e.                                     The procedures used
e.
The procedures used
1
1
              for the tests were receiving
for the tests were numbered:
                                  numbered: the most  coverag/L A (RTP-L/L A),
2-BFN-RTP-L
                                                  2-BFN-RTP-L
(RTP-L/L A),
j            2-BFN-RTP-L/L B (RTP-L/L B), 2-BFN-RTP-L/L C (RTP-L/L C), and
j
2-BFN-RTP-L/L B (RTP-L/L B), 2-BFN-RTP-L/L C (RTP-L/L C), and
l
l
              2-BFN-RTP-L/L 0 (RTP-L/L 0). Revision 0 of the procedures were
2-BFN-RTP-L/L 0 (RTP-L/L 0).
Revision 0 of the procedures were
i
i
              reviewed by the JTG and approved by the Plant Manager shortly before
reviewed by the JTG and approved by the Plant Manager shortly before
              the performance of the actual tests. Last minute changes to the
the performance of the actual tests.
Last minute changes to the
4
4


      _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ ___ _           .____ ___     ___         . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _                                   _       - _ _ _ _ _ _ _ .
_ _ _ _ _ _ _ _ _ _ _ _
    .     .
_ _ _ _ _ _ _ _ ___ _
  ,
.____ ___
                                                                                                              11
___
                                            tests were reviewed and approved the day the tests were conducted and
. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                          RTP-L/L C and RTP-L/L 0 were revised approximately two days before
_
                                          the actual tests.
- _ _ _ _ _ _ _ .
                                          Each test procedure was reviewed and found to be adequate.
.
                                          (1) LOP /LOCA Test "A"
.
                                                    This test was basically a LOP test, sometimes referred to as a
,
                                                    "blackout" test, and was Jerformed on May 29, 1988.                                                       Section S.3
11
                                                    of the test called for tie simultaneous tripping of the three
tests were reviewed and approved the day the tests were conducted and
                                                    main power feeds coming into the plant from the switchyard. The
RTP-L/L C and RTP-L/L 0 were revised approximately two days before
                                                    inspectors used NRR inspection modules 703068 Loss of Offsite
the actual tests.
                                                    Power, and 704418             Emergency / Standby Power Supply System Test,
Each test procedure was reviewed and found to be adequate.
                                                    as guidance before, dur'ng and after the test. Test section
(1) LOP /LOCA Test "A"
                                                    5.4, Plant Performance, required that all eight OGs start and                                                                                   !
This test was basically a LOP test, sometimes referred to as a
                                                    tie onto their respective SD8s; that various 4-KV and 480 V load
"blackout" test, and was Jerformed on May 29, 1988.
                                                    alignments be in accordance with the applicable procedure steps;
Section S.3
                                                    that all three units receive a scram signal from loss of RPS
of the test called for tie simultaneous tripping of the three
                                                    Hotor-Generator (M/G) sets; and that reactor MOV electrical
main power feeds coming into the plant from the switchyard.
                                                    boards and ventilation boards be in the alignment specified by
The
                                                    a)plicable procedure steps. The inspectors made the following
inspectors used NRR inspection modules 703068 Loss of Offsite
                                                    osservations:                                                                                                                                 ,
Power, and 704418
                                                    (a) Unit 3 DG "30" did not appear to close onto its SDB (3EC).                                                                                 r
Emergency / Standby Power Supply System Test,
                                                          However, post test review of the visicorder traces indi-                                                                                 '
as guidance before, dur'ng and after the test.
                                                          cated that the breaker closed and stayed closed for only                                                                                 l
Test section
                                                          five cycles, approximately'one-tenth of a second, and then
5.4,
                                                          tripped off. The licensee s representatives informed the                                                                                 ;
Plant Performance, required that all eight OGs start and
                                                          inspector that an item of M&TE used to time the closure of                                                                               :
!
                                                          the breaker shorted out, )icked up the DC trip coil of the                                                                               '
tie onto their respective SD8s; that various 4-KV and 480 V load
                                                          brsaker, and caused the )reaker to trip shortly af ter
alignments be in accordance with the applicable procedure steps;
                                                          closure.
that all three units receive a scram signal from loss of RPS
                                                                                                                                                                                                  !
Hotor-Generator (M/G) sets; and that reactor MOV electrical
                                                    (b) Unit 2 RPS M/G set "2B" did not trip off upon loss of                                                                                     i
boards and ventilation boards be in the alignment specified by
                                                          aower (the breaker supalies the power to the motor).                                                                                   "
a)plicable procedure steps.
                                                          iowever, other scram signals from the RPS did initiate                                                                                 l
The inspectors made the following
                                                          a full scram for Unit 2.
osservations:
                                                    (c) Several individual items such as recirculating M/G set
,
                                                          oil pumps "2A-1", "2A-2", "28-1", and "28-2" and control                                                                               '
(a) Unit 3 DG "30" did not appear to close onto its SDB (3EC).
                                                          and service air compressor "0" were exceptions to the test
r
                                                          as far as their supply breakers tripping.                                                                                             j
However, post test review of the visicorder traces indi-
                                                                                                                                                                                                  l
'
                                                    The above items are tracked as IFI 260/88-18-03, Test Deficien-                                                                               '
cated that the breaker closed and stayed closed for only
                                                    cies Identified During LOP /LOCA Test "A". This item is                                                                                       !
l
                                                    required to be closed out prior to restart. The conduct of the
five cycles, approximately'one-tenth of a second, and then
                                                    test by the licensee's representatives was not a well run test
tripped off.
                                                    in that the control room activities appeared at times to be very                                                                             ~
The licensee s representatives informed the
                                                    hectic and a large number of personnel, more than what seemed
;
                                                    necessary, were in the control room during the test. Improve-
inspector that an item of M&TE used to time the closure of
                                                    ment in professionalism by all personnel and better crowd                                                                                   -
:
                                                    control was needed,
the breaker shorted out, )icked up the DC trip coil of the
                                                                                                                                                                                                  t
'
                                                                                                                                                                                                  I
brsaker, and caused the
L-                                                                       . _ _ . _ _ _ .                                     . _ _ _ _ - _ _ - - __ . _ _ . .                   -
)reaker to trip shortly af ter
                                                                                                                                                                                          __ -- -
closure.
!
(b) Unit 2 RPS M/G set "2B" did not trip off upon loss of
i
aower (the breaker supalies the power to the motor).
"
iowever, other scram signals from the RPS did initiate
l
a full scram for Unit 2.
(c) Several individual items such as recirculating M/G set
oil pumps "2A-1", "2A-2", "28-1", and "28-2" and control
'
and service air compressor "0" were exceptions to the test
as far as their supply breakers tripping.
j
l
The above items are tracked as IFI 260/88-18-03, Test Deficien-
'
cies Identified During LOP /LOCA Test "A".
This item is
!
required to be closed out prior to restart.
The conduct of the
test by the licensee's representatives was not a well run test
in that the control room activities appeared at times to be very
hectic and a large number of personnel, more than what seemed
~
necessary, were in the control room during the test.
Improve-
ment in professionalism by all personnel and better crowd
-
control was needed,
t
I
L-
. _ _ . _ _ _ .
. _ _ _ _ - _ _ - -
__ . _ _ . .
-
__
--
-


      _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _
    .                               .
.
  ,
.
                                                                        12
,
                                      (2) LOP /LOCA Test "B"
12
                                          This test was basically a LOCA test using offsite power (the
(2) LOP /LOCA Test "B"
                                          grid) as the power source and was performed on June 1,1988.
This test was basically a LOCA test using offsite power (the
                                          Section 5 of the test called for the application of a high
grid) as the power source and was performed on June 1,1988.
                                          drywell pressure signal Of approximately 3.0 psig using
Section 5 of the test called for the application of a high
                                            temporary test tubing and a sneumatic calibrator installed at       '
drywell pressure signal Of approximately 3.0 psig using
                                            transmitters PT 64-588 and Pr 64-580. This signal in conjunc-
temporary test tubing and a sneumatic calibrator installed at
                                            tion with the already at:nospheric pressure of t1e reactor vessel
'
                                            initiated a LOCA signal. The basic requirements of the test
transmitters PT 64-588 and Pr 64-580.
                                          were that all eight DGs start (they were not to close onto their
This signal in conjunc-
                                            respective 50Bs); all four Unit 2 CS aumps start in the proper
tion with the already at:nospheric pressure of t1e reactor vessel
                                            sequencing and at the proper times; a'l four RHR pumps start in
initiated a LOCA signal.
                                            the low pressure core injection mode in the proper sequencing
The basic requirements of the test
                                          and at the proper times; and all four RHRSW pumps used for
were that all eight DGs start (they were not to close onto their
                                          EECW start in the proper sequencing and at the proper times.
respective 50Bs); all four Unit 2 CS aumps start in the proper
                                          Additional auxiliary equipment such as reactor recirculation
sequencing and at the proper times; a'l four RHR pumps start in
                                          discharge valve closure, RHR pump cooler fans start, HPCI logic
the low pressure core injection mode in the proper sequencing
                                            trips, etc., were verified as required to meet test acceptance.
and at the proper times; and all four RHRSW pumps used for
                                          The inspectors made the following observations:
EECW start in the proper sequencing and at the proper times.
                                            (a) An inspector was stationed at the Unit 3 control room
Additional auxiliary equipment such as reactor recirculation
                                                  0G electrical panel to observe Unit 3 OG operation upon
discharge valve closure, RHR pump cooler fans start, HPCI logic
                                                  initiation of the LOCA event. Test procedure recuirements
trips, etc., were verified as required to meet test acceptance.
                                                  were that upon initiation of the LOCA event, Unit 3 DGs
The inspectors made the following observations:
                                                  ("3A", "3B", "3C", and "30") start automatically, attain
(a) An inspector was stationed at the Unit 3 control room
                                                  rated voltage and frequency, and remain unconnected to
0G electrical panel to observe Unit 3 OG operation upon
                                                  their respective 4-XV SDBs, and the SDB mode switches
initiation of the LOCA event.
                                                  transfer from "auto" to "manual". Observations of annun-
Test procedure recuirements
                                                  ciator and alarm panel indicator lights confirmed the
were that upon initiation of the LOCA event, Unit 3 DGs
                                                  aforementioned test requirements for the Unit 3 DGs.
("3A", "3B", "3C", and "30") start automatically, attain
                                            (b) An NRC inspector was stationed at the Unit 2 control room
rated voltage and frequency, and remain unconnected to
                                                  station and proceeded to the SDBs upon initiation of the
their respective 4-XV SDBs, and the SDB mode switches
                                                  LOCA events. The inspector observed TVA data takers and QA
transfer from "auto" to "manual". Observations of annun-
                                                  inspectors as well. The inspector observed no deviations
ciator and alarm panel indicator lights confirmed the
                                                  or violations of procedure and test requirements.
aforementioned test requirements for the Unit 3 DGs.
                                            (c) An NRC inspector observed the control room activities
(b) An NRC inspector was stationed at the Unit 2 control room
                                                  inside the Unit 2 main control panel "horsehoe." The
station and proceeded to the SDBs upon initiation of the
                                                  inspector used Section 5.2 of the test to verify and
LOCA events. The inspector observed TVA data takers and QA
                                                                                                          the
inspectors as well.
The inspector observed no deviations
or violations of procedure and test requirements.
(c) An NRC inspector observed the control room activities
inside the Unit 2 main control panel "horsehoe."
The
inspector used Section 5.2 of the test to verify and
document the performance of the four CS pumps, ion
the
l
l
                                                  document
four RHR pumps in the low pressure core inject
                                                  four RHR thepumpsperformance
mode, and the four RHRSW pumps used for EECW.
                                                                      in the lowofpressure
Verifi-
                                                                                    the four CS  pumps,
cation of operation involved recording motor amperage,
                                                                                              core inject ion
system flows, and system pressures.
                                                  mode, and the four RHRSW pumps used for EECW.         Verifi-
All 12 pumps
                                                  cation of operation involved recording motor amperage,
indicated electrical current flow, with the CS trains
                                                  system flows, and system pressures. All 12 pumps
indicating approximately 6200 gallons per minute (gpm)
                                                  indicated electrical current flow, with the CS trains
and approximately 250 psig each, and the RHR trains
                                                  indicating approximately 6200 gallons per minute (gpm)
indicating approximately 12000 gpm and approximately
                                                  and approximately 250 psig each, and the RHR trains
275 psig each.
                                                  indicating approximately 12000 gpm and approximately
Overall evaluation was that the major
                                                  275 psig each. Overall evaluation was that the major
items of equipment responded as required by the test.
                                                  items of equipment responded as required by the test.
L-
L-


  _ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _                     _       _   _ _ _ _ _ _ _ _ _ _ _ _   __ ____ ____ _ ___ ___- .                 _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _
    .                                       . .
_
                                                                                                                      13
_
                                                                    Upon post test review by all the inspectors involved, it was
_ _ _ _ _ _ _ _ _ _ _ _
                                                                    noted that the facilities test personnel appeared somewhat
__
                                                                    confused by what was occurring at different stages of the test.
____ ____ _ ___ ___- .
                                                                    The control room activities appeared to be more controlled thJn
_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _
                                                                    during LOP /LOCA "A".           It was noted that no direct monitoring of
.
                                                                    the incoming voltage from the grid was made by the licensee's
. .
                                                                    representatives during this test. The inspector was informed
13
                                                                    that this will be documented by calculation.                                         This item is
Upon post test review by all the inspectors involved, it was
                                                                    identified as IFI 260/88-18-04 Documentation of Offsite Voltage
noted that the facilities test personnel appeared somewhat
                                                                    During LOP /LOCA Test "B". This item is required to be closed
confused by what was occurring at different stages of the test.
                                                                    out prior to restart. The results of the test will be reviewed
The control room activities appeared to be more controlled thJn
                                                                    and commented on in a future NRC report.
during LOP /LOCA "A".
                                                              (3) LOP /LOCA Test "C"
It was noted that no direct monitoring of
                                                                    This test was a combination of a LOP signal followed six seconds
the incoming voltage from the grid was made by the licensee's
                                                                    later by a LOCA signal with the "B" DG disabled and was per-
representatives during this test.
                                                                    formed on Junt 5,1988. Section 5.3 of the test called for
The inspector was informed
                                                                    simultaneously opening the three main power feeds coming into
that this will be documented by calculation.
                                                                    the plant from the switchyard and after a3 proximately a six
This item is
                                                                    second time delay initiating the triple 1ow (Lo-Lo-Lo) or
identified as IFI 260/88-18-04 Documentation of Offsite Voltage
                                                                    Level I reactor vessel level trip; thereby setting up a LOP
During LOP /LOCA Test "B".
                                                                    followed by a LOCA.       The ins 3ectors used NRR modules 70316, Loss
This item is required to be closed
                                                                    of Offsite Power Test 70436, Engineered Safety Features Actua-
out prior to restart.
                                                                    tion System Test, and 70441, Emergency / Standby Power System
The results of the test will be reviewed
                                                                    Test     as                                                                                     Test
and commented on in a future NRC report.
                                                                    sectIon 5. 4, guidance   before, during
(3) LOP /LOCA Test "C"
                                                                                    Plant Performance,                  re and af ter the test.
This test was a combination of a LOP signal followed six seconds
                                                                    with the exception of Unit 3 DG "B"quired                   start and          that all
later by a LOCA signal with the "B" DG disabled and was per-
                                                                                                                                                          tie eight
formed on Junt 5,1988.
                                                                                                                                                              onto DGs
Section 5.3 of the test called for
                                                                                                                                                                    their
simultaneously opening the three main power feeds coming into
                                                                    respectiveSDBs;thatthe"2A"and"2C"CSpumpsstart;thatthe
the plant from the switchyard and after a3 proximately a six
                                                                    "2A', "28", and "2C" RHR pumps start; that the applicable RHRSW
second time delay initiating the triple 1ow (Lo-Lo-Lo) or
                                                                    pumps start; and that all three units receive a scram signal.
Level I reactor vessel level trip; thereby setting up a LOP
                                                                    Additional auxiliary equipment as outlined in the procedure were
followed by a LOCA.
                                                                    to activate, including Standby Gas Treatment and Control Room
The ins 3ectors used NRR modules 70316, Loss
                                                                    Emergency Ventilation as required to meet test acceptance
of Offsite Power Test 70436, Engineered Safety Features Actua-
                                                                    criteria.
tion System Test, and 70441, Emergency / Standby Power System
                                                                    The inspectors made the following observations:
Test
                                                                    (a) Unit 2 Control Room Observations
as
                                                                          After the test was initiated at 2:16 p.m., the inspector
Test
                                                                          observed that a scram sig"nal was received. RHR pumps "2A",
sectIon 5. guidance before, during and af ter the test.
                                                                          "2B", "2C" and CS pumps 2A" and "20" started as planned.
4, Plant Performance, re
                                                                          Power was lost to the "2A" reactor MOV board which did not
with the exception of Unit 3 DG "B"quired that all eight DGs
,
start and tie onto their
                                                                          transfer as expected. The transfer was manually performed
respectiveSDBs;thatthe"2A"and"2C"CSpumpsstart;thatthe
                                                                          at 2:29 p.m., and the CS inboard injection valve (2-FCV-
"2A', "28", and "2C" RHR pumps start; that the applicable RHRSW
pumps start; and that all three units receive a scram signal.
Additional auxiliary equipment as outlined in the procedure were
to activate, including Standby Gas Treatment and Control Room
Emergency Ventilation as required to meet test acceptance
criteria.
The inspectors made the following observations:
(a) Unit 2 Control Room Observations
After the test was initiated at 2:16 p.m., the inspector
observed that a scram sig"nal was received.
RHR pumps "2A",
"2B",
"2C" and CS pumps
2A" and "20" started as planned.
Power was lost to the "2A" reactor MOV board which did not
transfer as expected.
The transfer was manually performed
,
at 2:29 p.m., and the CS inboard injection valve (2-FCV-
75-25) opened (procedure step 5.4.9.1).
,
,
                                                                          75-25) opened (procedure step 5.4.9.1).
Prior to the test, RCIC was inop"erable and procedure step
                                                                          Prior to the test, RCIC was inop"erable and procedure step
5.4.12 could not be met.
                                                                          5.4.12 could not be met. The RCIC Relay "Logic Power
The
                                                                          Failure" annunciator was observed. The "2B reactor MOV
RCIC Relay "Logic Power
Failure" annunciator was observed.
The "2B
reactor MOV
l
l
L
L


                                                          _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _
_ _ _ _ _ _ _ _ _ _
    .
_ _ _ - _ _ _
  ,.
.
                                  14
,.
            board is supplied by 508 "0" and DG "0" was not tested.
14
            Accordingly, procedure steps 5.4.9.2 and 5.4.19.2 could
board is supplied by 508 "0"
            not be checked due to an absence of power.
and DG "0" was not tested.
            RHR System II flow and pressure could not be checked
Accordingly, procedure steps 5.4.9.2 and 5.4.19.2 could
            because I&C Bus "B" had no power (procedure step 5.4.24).
not be checked due to an absence of power.
            At 3:02 p.m. , 4160 V SDB "D' was restored and these were
RHR System II flow and pressure could not be checked
            checked.
because I&C Bus "B" had no power (procedure step 5.4.24).
            The alarm and annunciation table, Appendix E, had the
At 3:02 p.m. , 4160 V SDB "D' was restored and these were
            following alarms received prior to the test:
checked.
                  Unit Preferred Supply Abnormal
The alarm and annunciation table, Appendix E, had the
                  Reactor Auto Scram Channel A
following alarms received prior to the test:
                  Reactor Auto Scram Channel B
Unit Preferred Supply Abnormal
                  The "Turbine Tripped Electrical Trouble" annunciator
Reactor Auto Scram Channel A
                  was not received.
Reactor Auto Scram Channel B
      (b) During LOP /LOCA Test "C" an inspector observed Unit 3
The "Turbine Tripped Electrical Trouble" annunciator
            control room activities with regard to alarm and annuncia-
was not received.
            tor panels and noted that the Unit 3 DG started and closed
(b) During LOP /LOCA Test
            on the 4160 V SOBS. In addition, selected circuit breakers
"C" an inspector observed Unit 3
            on the Unit 3 480V SDBs "3A" and "3B" were checked to
control room activities with regard to alarm and annuncia-
            verify and obtain their LOP /LOCA positions. The following
tor
            problems were identified during the test:
panels and noted that the Unit 3 DG started and closed
            -
on the 4160 V SOBS.
                  DGs "3A", "3C" and "3D" came up to rated speed and
In addition, selected circuit breakers
                  voltage but did not tie-on to their respective 4160 V
on the Unit 3 480V SDBs "3A" and "3B" were checked to
                  SDB.     Troubleshooting and review of log'ic circuitry
verify and obtain their LOP /LOCA positions.
                  indicated that the DG "3A", "3C" and 3D" output
The following
                  breakers closed at ~6.5 seconds and at ~6.75 seconds a
problems were identified during the test:
                  LOCA signal opened the 3 DG breakers. During recharg-
DGs "3A", "3C" and "3D" came up to rated speed and
                  ing of the breakers, the anti pump relay (52Y) had
-
                  sealed in steventing the reclosure of the DG breakers
voltage but did not tie-on to their respective 4160 V
                  (i.e. , DG areaker opened -0.3 seconds and the anti-
SDB.
                  pump relay responded as designed to a fault condition
Troubleshooting and review of log'ic circuitry
                  on the 508 although the LOCA signal was the reason for
indicated that the DG "3A",
                  the DG breakers being opened).     An operator was sent
"3C" and
                  to the switchgear room where a remote panel is avail-
3D" output
                  able for local operations. The operator slowly placed
breakers closed at ~6.5 seconds and at ~6.75 seconds a
                  the normal / emergency switch (43) to the emergency
LOCA signal opened the 3 DG breakers.
                  position. The switch is a break before make design
During recharg-
                  and thus de energized the 52Y anti-pump relay setting
ing of the breakers, the anti pump relay (52Y) had
                  up the circuitry for closure of the three DG breakers.
sealed in steventing the reclosure of the DG breakers
            -
(i.e. , DG areaker opened -0.3 seconds and the anti-
                  The inspector also identified that the data recorder
pump relay responded as designed to a fault condition
                  did not have the latest data sheets for recording
on the 508 although the LOCA signal was the reason for
                  breaker positions on 480 V SDBs "3A" and "3B".
the DG breakers being opened).
An operator was sent
to the switchgear room where a remote panel is avail-
able for local operations.
The operator slowly placed
the normal / emergency switch (43) to the emergency
position.
The switch is a break before make design
and thus de energized the 52Y anti-pump relay setting
up the circuitry for closure of the three DG breakers.
The inspector also identified that the data recorder
-
did not have the latest data sheets for recording
breaker positions on 480 V SDBs "3A" and "3B".
l
l


                                                      _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ -- _
_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _
,. ..
--
                                  15
_
..
,.
15
:
:
      (c) An NRC inspector was stationed in the Unit I control room
(c) An NRC inspector was stationed in the Unit I control room
            and proceeded to the SD8s upon initiation of the LOP /LOCA
and proceeded to the SD8s upon initiation of the LOP /LOCA
            event. The inspector observed TVA data takers and QA
event. The inspector observed TVA data takers and QA
            inspectors as well.
inspectors as well.
      (d) An NRC inspector observed the initiation of the LOCA signal
(d) An NRC inspector observed the initiation of the LOCA signal
            in the Unit 2 auxiliary instrument room and noted that
in the Unit 2 auxiliary instrument room and noted that
            relay 16A-K29 in panel 9-42 did not de-energize as required
relay 16A-K29 in panel 9-42 did not de-energize as required
            for the test. This rela
for the test.
            tainment isolation logic. y is part of the primary con-
This rela
            The inspector then proceeded to SOB "0" and there observed
tainment isolation logic. y is part of the primary con-
            a Ifeensee representative performing manual manipulations
The inspector then proceeded to SOB "0" and there observed
            on 480V reactor MOV board '2A". It was later determined
a Ifeensee representative performing manual manipulations
            that this board was not initially lined up per section 5.2,
on 480V reactor MOV board
            Initial Lineup of the Test. These two items were con-
'2A".
            sideredtobemajorconcernsforthetest.
It was later determined
      (e) An NRC inspector was positioned in front of 508 "3EC" near
that this board was not initially lined up per section 5.2,
            DG breaker "3C". After the LOP initiation, the inspector
Initial Lineup of the Test.
            noted that the open/ closed flag on the breaker indicated
These two items were con-
            momentarily closed then immediately indicated open and
sideredtobemajorconcernsforthetest.
            stayed in that p"osition. The inspector then proceeded to
(e) An NRC inspector was positioned in front of 508 "3EC" near
            SDBs "3EA" "3E8
DG breaker "3C".
                                I
After the LOP initiation, the inspector
                                  and "3ED" and noted that the breakers
noted that the open/ closed flag on the breaker indicated
            for DGs "3A" and '30" were both open. Of the Unit 3 DGs,
momentarily closed then immediately indicated open and
            only the output breaker for "38" was closed on 508 "3EB".
stayed in that p"osition.
            It was later discovered that the following had occurred:
The inspector then proceeded to
                        Sequence of Events
SDBs "3EA"
        Time
"3E8
      1.5 seconds           Loss of Power - 4KV SDB De-energized; DGs
and "3ED" and noted that the breakers
                            Start
I
        5 seconds           Board undervoltage device times out and
for DGs "3A" and '30" were both open.
                            closes contacts in breaker closure circuit
Of the Unit 3 DGs,
                            (2-211-4A3)
only the output breaker for "38" was closed on 508 "3EB".
      -6.5 seconds           DGs "3A", "3C", and "30" come up to speed
It was later discovered that the following had occurred:
                            and close contacts in breaker closure
Sequence of Events
                            circuits (VSR1,VSR2)
Time
      6.55 seconds           OG breakers close ("3A", "3C", "30")
1.5 seconds
      6.55 seconds           Accidentsignalinlected,DGbreakers"3A",
Loss of Power - 4KV SDB De-energized; DGs
                            "3C", and '30" trlpped via LOCA signal,
Start
                            CASA-2 contacts closed, 52a (contact 4 4c)
5 seconds
                            closed on breaker closure. ThisenergIzed
Board undervoltage device times out and
                            52T and tripped the breaker
closes contacts in breaker closure circuit
(2-211-4A3)
-6.5 seconds
DGs "3A", "3C", and "30" come up to speed
and close contacts in breaker closure
circuits (VSR1,VSR2)
6.55 seconds
OG breakers close ("3A", "3C", "30")
6.55 seconds
Accidentsignalinlected,DGbreakers"3A",
"3C",
and '30" trlpped via LOCA signal,
CASA-2 contacts closed, 52a (contact 4 4c)
closed on breaker closure.
ThisenergIzed
52T and tripped the breaker


  _ . - _ _ _ - - _ _. __ _ - _ _ _ _ _ _ _ _ _ -                                       _ _ _ _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _                         _ _ _ _ _
_ . - _ _ _ - - _ _. __ _ - _ _ _ _ _ _ _ _ _ -
            .                     ..
_ _ _ _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _
    '
_ _ _ _ _
..
.
l
l
                                                                                  16                                                                                  ,
'
                                                                                                                                                                        t
16
                                                                                                                                                                        I
l                                                        ~6.55 seconds        When breaker closed, 452M and 52Y energized
l                                                                            to recharge breaker. Energizing 52Y                                                      ;
                                                                              isolates 52X (closure coil) from circuit,                                                r
                                                                                                                                                                        i
                                                                              Note:            It takes 2 seconds to recharge the                                      i
                                                                                                                                                                        ;
                                                                                            breaker.                                    The undervoltage device
                                                                                            did not have time to reset;                                                !
                                                                                              therefore, a closure signal is                                            '
                                                                                              sealed into the circuit. This                                          ;
                                                                                            energizes 52Y through contacts                                            ;
                                                                                                                                    This keeps the breakers
                                                                                                                                                                      '
                                                                                              7-1.                                                                    .
                                                                                              locked                                  out.  The  inspector          i
i                                                                                            considered this to be a major                                            ['
                                                                                            concern for the test.
                                                                                                                                                                      l
                                                        (f) An NRC inspector observed the control room activities                                                      t
                                                              mainly involved with the Unit 1/2 DG board. No def t-                                                    i
                                                              ciencies were identified.
                                                                                                                                                                      l
l                                                        Because of the problems that occurred a major part or all of                                                  f
                                                        Test C will be rerun.
                                                        The licensee documented the locking out of the Unit 3 DG output                                              :
,
,
                                                        breakers on CAQR BFP-88-0394, and initiated action to write a                                                ;
t
l                                                        LER.  These items are being tracked as IFI 259,260,296/88-18-05,
I
                                                        Major Olscrepancies Identified During LOP /LOCA Test "C". This
l
~6.55 seconds
When breaker closed, 452M and 52Y energized
l
to recharge breaker.
Energizing 52Y
;
isolates 52X (closure coil) from circuit,
r
i
Note:
It takes 2 seconds to recharge the
i
;
breaker.
The undervoltage device
did not have time to reset;
therefore, a closure signal is
'
'
                                                                                                                                                                      '
sealed into the circuit.
                                                        item is required to be closed out prior to restart.                                                           l
This
                                                                                                                                                                      !
;
                                                  (4) LOP /LOCA Test "0"
energizes 52Y through contacts
                                                                                                                                                                      l
;
l                                                                                                                                  nal followed at three seconds     L
7-1.
                                                  The
This keeps the breakers
                                                  by    test was
'
                                                      a LOCA      a combination
.
                                                              signal.               of a LOP sig/ hardware problem encountered!
locked
                                                                        Due to the technical
out.
The
inspector
i
considered this to be a major
[
i
concern for the test.
'
l
(f) An NRC inspector observed the control room activities
t
mainly involved with the Unit 1/2 DG board.
No def t-
i
ciencies were identified.
l
l
Because of the problems that occurred a major part or all of
f
Test C will be rerun.
The licensee documented the locking out of the Unit 3 DG output
:
,
breakers on CAQR BFP-88-0394, and initiated action to write a
;
l
LER.
These items are being tracked as IFI 259,260,296/88-18-05,
'
Major Olscrepancies Identified During LOP /LOCA Test "C".
This
'
item is required to be closed out prior to restart.
l
!
l
(4) LOP /LOCA Test "0"
l
The test was a combination of a LOP sig/ hardware problem encountered
nal followed at three seconds
L
by a LOCA signal.
Due to the technical
!
with the six second LOCA signal discovered during LOP /LOCA Test "C",
!
I
the time for initiation of the LOCA signal was changed from six
i
seconds to three seconds.
This test was performed on July 8,1988,
I
with the Unit 2 DC battery disconnected.
Section 5.3 of the test
!
called for the simultaneous opening of the three main power feeds
!
coming into the plant and after approximately a three second time
l
delay, initiating the tripIe low (Lo-Lo-Lo) or level I reactor vessel
j
,
l
trip; thereby, setting up a LOP followed by a LOCA.
Section 5.4,
,
f
Plant Performance, required that all eight DGs start (due to the
disconnection of the DC battery the Unit 3 "0" DG would not tie onto
[
508 "3E0"); that R)iR pumps "2A' , "2C" and "20" start; that trains "A"
& "B" of the SBGTS and CREYS start; and that all three units receive
I
I
                                                  with the six second LOCA signal discovered during LOP /LOCA Test "C",                                              !
a scram signal due to the loss of all six (two per unit) RPS M/G
                                                  the time for initiation of the LOCA signal was changed from six                                                    i
i
                                                  seconds to three seconds.      This test was performed on July 8,1988,                                              I
sets.
                                                  with the Unit 2 DC battery disconnected. Section 5.3 of the test                                                    !
Additional auxiliary equipment as outlined in the procedure
                                                  called for the simultaneous opening of the three main power feeds                                                  !
}
                                                  coming into the plant and after approximately a three second time                                                    l
was to activate to meet the test acceptance criteria.
,                                                delay, initiating the tripIe low (Lo-Lo-Lo) or level I reactor vessel                                              j
l
l
                                                  trip; thereby, setting up a LOP followed by a LOCA. Section 5.4,                                                    ,
The inspectors made the following observations:
                                                  Plant Performance, required that all eight DGs start (due to the                                                    f
all eight OGs
                                                  disconnection of the DC battery the Unit 3 "0" DG would not tie onto                                                [
!
                                                  508 "3E0"); that R)iR pumps "2A' , "2C" and "20" start; that trains "A"
started and tied onto their respective SOBS with the exception of
                                                  & "B" of the SBGTS and CREYS start; and that all three units receive                                                I
(
                                                  a scram signal due to the loss of all six (two per unit) RPS M/G                                                    i
OG "30"; the three units each received a scram signal due to the loss
                                                  sets. Additional auxiliary equipment as outlined in the procedure                                                  }
[
                                                  was to activate to meet the test acceptance criteria.
of RPS M/G sets; and equipment required to perform in order to meet
                                                                                                                                                                      l
[
                                                  The inspectors made the following observations: all eight OGs                                                       !
the test acceptance criteria appeared to do so.
                                                  started and tied onto their respective SOBS with the exception of                                                   (
[
                                                  OG "30"; the three units each received a scram signal due to the loss                                               [
I
                                                  of RPS M/G sets; and equipment required to perform in order to meet                                                 [
                                                  the test acceptance criteria appeared to do so.                                                                     [
l
l
                                                                                                                                                                      I
;
                                                                                                                                                                      ;
-
.
.
-


- _ - _ _ _ _ _ _ _ _ _ _ _ _   _ _ _ _ _ _
- _ - _ _ _ _ _ _ _ _ _ _ _ _
                  .
_ _ _ _ _ _
    ,.
.
                                                                            17
,.
                                                  This test appeared to be the smoothest run of all four tests.
17
                                                  However, on initial review it appears that like LOP /LOCA Test
This test appeared to be the smoothest run of all four tests.
                                                  "C", some equipment was not lined up initially as required by
However, on initial review it appears that like LOP /LOCA Test
                                                  section 5.2 of the test.     This item is identified as IFI
"C", some equipment was not lined up initially as required by
                                                  260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".
section 5.2 of the test.
                                                  This item is required to be closed out prior to restart.
This item is identified as IFI
                                            General observations made and comments about the LOP /LOCA series
260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".
                                            of tests are as follows:
This item is required to be closed out prior to restart.
                                                  The inspectors were concerned that the large number of test
General observations made and comments about the LOP /LOCA series
                                                  exceptions make it difficult to determine if in fact they have
of tests are as follows:
                                                  met the baseline program.
The inspectors were concerned that the large number of test
                                                  With the exception of the operations manager and some of the
exceptions make it difficult to determine if in fact they have
                                                  senior personnel, the operations staff did not give the
met the baseline program.
                                                  appearance of proper attitude or professionalism in conduct and
With the exception of the operations manager and some of the
                                                  attire.   Also, the inspectors could not readily tell who was in
senior personnel, the operations staff did not give the
                                                  charge of the operations shift.
appearance of proper attitude or professionalism in conduct and
                                                  Operator logs did not contain enough detail to recreate opera-
attire.
                                                  tional events.
Also, the inspectors could not readily tell who was in
                                                  Proper professionalism was not displayed when the pre-o) LOP /
charge of the operations shift.
                                                  LOCA briefings were delayed in starting: cat calls and fokes by
Operator logs did not contain enough detail to recreate opera-
                                                  attendees were noted. Also there appeared to be a lack of
tional events.
                                                  seriousness and interest shown by some individuals involved in
Proper professionalism was not displayed when the pre-o) LOP /
                                                  this series of RTP testing.
LOCA briefings were delayed in starting:
                                                  On positive side, the RTP technical staff appeared to be very
cat calls and fokes by
                                                  professional and concerned. The compliance staff and site
attendees were noted.
                                                  licensing staff appea:ed to be very professional and had been
Also there appeared to be a lack of
                                                  responsive to all of the NRC concerns and requests.
seriousness and interest shown by some individuals involved in
                                            These observations have been discussed with various department
this series of RTP testing.
                                            managers at the site. It is the conclusion of the inspectors that
On positive side, the RTP technical staff appeared to be very
                                            the series of tests were not as successful as they could have been,
professional and concerned.
                                            especially LOP /LOCA Test "C". In the area of pre-test preparations,
The compliance staff and site
                                            a vast improvement is called for; in the area of operator activities,
licensing staff appea:ed to be very professional and had been
                                            improvement is needed; and in the area of test exceptions, clari-
responsive to all of the NRC concerns and requests.
                                            fication is needed. The licensee subsequently decided to rerun much
These observations have been discussed with various department
                                            of LOP /LOCA "C".
managers at the site.
                              6.             Review of Quality Assurance Monitoring (QAM) Surveillances
It is the conclusion of the inspectors that
                                            During the reporting period, the inspector observed QAM personnel in
the series of tests were not as successful as they could have been,
                                            the field actively monitoring RTP testing.       The following QAM
especially LOP /LOCA Test "C".
                                            surveillances were reviewed by the inspector:
In the area of pre-test preparations,
                                                Number                           Description
a vast improvement is called for; in the area of operator activities,
                                            QBF-88-0352           This surveillance documented the activities
improvement is needed; and in the area of test exceptions, clari-
                                                                  involving the RTP daily status meetings.
fication is needed.
The licensee subsequently decided to rerun much
of LOP /LOCA "C".
6.
Review of Quality Assurance Monitoring (QAM) Surveillances
During the reporting period, the inspector observed QAM personnel in
the field actively monitoring RTP testing.
The following QAM
surveillances were reviewed by the inspector:
Number
Description
QBF-88-0352
This surveillance documented the activities
involving the RTP daily status meetings.


                                                                                        _ _ _ _ _ _ _ _ _ _ _ _ __
_ _ _ _ _ _ _ _ _
    ..
_ _ _ __
  ..
..
                                18
..
18
L
L
l         Number                       Description
l
Number
Description
I
i
i
QBF-88-00436
This item documented the activities involving the
I
I
        QBF-88-00436 This item documented the activities involving the                                            I
ST 88-17 on DG "B" and indicated that the DG was
                    ST 88-17 on DG "B" and indicated that the DG was                                             !
!
                      started with the cylinder vents open.
                                                                                                                  '
l
l
                                                                                                                  ;
started with the cylinder vents open.
        QBF-88-00455 This item documented the activities involving ST                                             !
'
                    88 17 and RTP-082 on DG "B" and indicated that
;
                    the DG was started with the load limiter on zero.                                             l
QBF-88-00455
        QBF-88-0465 This item documented activities               involving
This item documented the activities involving ST
                    ST 88-07 on DG "A".                                                                           .
!
        QBF-88-0475 This itcm documented activities involving
88 17 and RTP-082 on DG "B" and indicated that
the DG was started with the load limiter on zero.
l
QBF-88-0465
This
item documented activities
involving
ST 88-07 on DG "A".
.
QBF-88-0475
This
itcm documented activities
involving
i
i
ST 88-07 on OG "A" and indicated that MR 860262
'
'
                    ST 88-07 on OG "A" and indicated that MR 860262
was performed to troubleshoot the DGs droop
                    was performed to troubleshoot the DGs droop
circuit.
                    circuit.                                                                                     '
'
'
        QBF-88-0610 This item documented activities involving                                                     l
'
                    LOP /LOCA Test "C" and indicated that the "3A",                                               !
QBF-88-0610
                    "3C", and "30" DGs failed to perform as expected                                             1
This
                    and that relay 16A-K29 did not de-energize.                                                   ,
item documented activities
1                   Additional test exceptions were also documented.
involving
        QBF-88-0637 This item documented activities involving                                                     l
l
                    LOP /LOCA Test "0" and did not indicate any major
LOP /LOCA Test "C" and indicated that the "3A",
                    equipment failure; however, several test
!
                    exceptions were documented.                                                                   ;
"3C", and "30" DGs failed to perform as expected
        QBF-88-0643 This item documented activities           involving
1
                    ST 88-08 on DG "C".
and that relay 16A-K29 did not de-energize.
        QBF-88-0653 This item documented the followup activities of
,
                    QBF-88-0455 and indicated that CAQR-BFP-88-0403
1
                    was initiated by RTP personnel. O
Additional test exceptions were also documented.
                    personnel initiated Critique 88-027. perations
QBF-88-0637
        QBF-88-0666 This item documented the activities involving
This item documented activities
                    RTP-075, Core Spray, and indicated that Loop II
involving
                    failed an SI due to an undocumented cable splice.
l
        QBF-88-0667 This     item documented activities       involving
LOP /LOCA Test "0" and did not indicate any major
                    ST 88-08 on OG "0"   and indicated that                 RHR pump
equipment
                    "28"   tripped during the test and that                   an
failure;
                    imediate temporary change (ITC) was initiated to
however,
                    lift a lead to prevent t11s from happening again.
several
        QBF-88-0669 This item documented activities         involving
test
                    ST 88-09 on DG "0".
exceptions were documented.
;
QBF-88-0643
This
item documented activities
involving
ST 88-08 on DG "C".
QBF-88-0653
This item documented the followup activities of
QBF-88-0455 and indicated that CAQR-BFP-88-0403
was initiated by RTP personnel. O
personnel initiated Critique 88-027. perations
QBF-88-0666
This item documented the activities involving
RTP-075, Core Spray, and indicated that Loop II
failed an SI due to an undocumented cable splice.
QBF-88-0667
This
item documented activities
involving
ST 88-08 on OG "0" and indicated that RHR pump
"28"
tripped during the test and that an
imediate temporary change (ITC) was initiated to
lift a lead to prevent t11s from happening again.
QBF-88-0669
This
item documented activities
involving
ST 88-09 on DG "0".
I
I
i                                                           - - - _ - - - _ _ . _ _                     ____
i
- - - _ - - - _ _ . _ _
____


                                                                                  _ _ _ _
_ _ _ _
                                                                                                _ _ _ _ _ _ _ _ _ _ _ - _ _ -
_ _ _ _ _ _ _ _ _ _ _ - _ _ -
    . . .
. .
  ,
.
                                                  19
,
19
Number
Description
<
<
                      Number                              Description
QBF-88-0674
                    QBF-88-0674                                                                         LOP /
This item documented activities involving"3C"
                                        This
LOP /
                                        LOCAitem
LOCA Test
                                              Test documented    activities
"A" and indicated that the DG
                                                    "A" and indicated     thatinvolving"3C"
output breakers did not perform as required due
                                                                                the DG
to measuring and test equipment (M&TE) problems.
                                        output breakers did not perform as required due
QBF-88-0680
                                        to measuring and test equipment (M&TE) problems.
This
                    QBF-88-0680         This   item documented activities               involving
item documented activities
                                        ST 88-09 on DG   "0".
involving
                    QBF-88-0687         These items documented activities involving the
ST 88-09 on DG "0".
                    QBF-88-0691         daily RTP testing status meetings.
QBF-88-0687
                    QBF-88-0695         This   item documented activities involving
These items documented activities involving the
                                        RTP-057-4, 4 KV Ofstribution.
QBF-88-0691
!                   The above reviews indicated that QAM personnel were adequately
daily RTP testing status meetings.
                    performing surveillances and identifying and documenting problems.
QBF-88-0695
          7. Exit Interview
This
l           The inspection scope and findings were summarized on July 8,1988, with
item documented activities involving
:            the Plant Manager, Superintendents, and other members of his staff. New
RTP-057-4, 4 KV Ofstribution.
              items identified were:
!
              a.    Inspector Followu
The above reviews indicated that QAM personnel were adequately
                    Conductor SpItce. p Item (IFI) 260/88-18 01, Undocumented Cable
performing surveillances and identifying and documenting problems.
i            b.   Violation 259,260 2                 Failure to Document Overload
7.
'
Exit Interview
                    Conditiononthe"d"96/88-18-02,
l
                                          DieselGeneratoronaCAQR.
The inspection scope and findings were summarized on July 8,1988, with
;             c.         260/88-18-03, Test Deficiencies Identified During LOP /LOCA Test
the Plant Manager, Superintendents, and other members of his staff.
              d.   IFI 260/88-18-04, Documentation of Offsite Voltage During LOP /LOCA
New
l                 Test "B".
:
              e.   IFI 259,260,296/88-18-05, Major Discrepancies Identified During
items identified were:
                    LOP /LOCA Test "C".
Inspector Followu
.            f.   IFI 260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".
Conductor SpItce. p Item (IFI) 260/88-18 01, Undocumented Cable
              The above items are all identified as restart items.
a.
l
Violation 259,260 2
Failure to Document Overload
i
b.
Conditiononthe"d"96/88-18-02,
'
DieselGeneratoronaCAQR.
;
c.
260/88-18-03, Test Deficiencies Identified During LOP /LOCA Test
d.
IFI 260/88-18-04, Documentation of Offsite Voltage During LOP /LOCA
l
Test "B".
e.
IFI 259,260,296/88-18-05, Major Discrepancies Identified During
LOP /LOCA Test "C".
f.
IFI 260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".
.
The above items are all identified as restart items.
l
l
l
.
.


-       .
-
    ..
.
  ,.
..
                                                20
,.
          8. Acronyms and Abbreviations
20
            8FN       -
8.
                          Browns Ferry Nuclear
Acronyms and Abbreviations
            BTRD       -
8FN
                          Baseline Test Requirements Occument
Browns Ferry Nuclear
            CAD       -
-
                          Containment Atmospheric Dilution
BTRD
            CAQR
Baseline Test Requirements Occument
                        -
-
                          Conditions Adverse to Quality Report
CAD
            CREVS     -
Containment Atmospheric Dilution
                          Control Room Emergency Ventilation System
-
            CS         -
CAQR
                          Core Spray
Conditions Adverse to Quality Report
            DG       -
-
                          Ofesel Generator
CREVS
            DNE       -
Control Room Emergency Ventilation System
                          Department of Nuclear Engineering
-
            ECCS       -
CS
                          Essential Core Cooling Systems
Core Spray
            EECW     -
-
                          Emergency Equipment Cooling Water
DG
            FI       -
Ofesel Generator
                          Flow Indicator
-
            HPCI     -
DNE
                          HighPressureCoolantInjection
Department of Nuclear Engineering
            HVAC     -
-
                          Heating Ventilation and Air Conditioning
ECCS
            ISEG     -
Essential Core Cooling Systems
                          Independent Safety Engineering Group
-
            JTG       -
EECW
                          Joint Test Group
Emergency Equipment Cooling Water
            LER       -
-
                          Licensee Event Report
FI
            LOP /LOCA -
Flow Indicator
                          Loss of Power / Loss of Coolant Accident
-
            M/G       -
HPCI
                          Motor Generator
HighPressureCoolantInjection
            MR       -
-
                          Maintenance Request
HVAC
            M&TE     -
Heating Ventilation and Air Conditioning
                          Measuring & Test Equipment
-
            PORC     -
ISEG
                          Plant Operations Review Committee
Independent Safety Engineering Group
            QA
-
                      -
JTG
                          Quality Assurance
Joint Test Group
            QAM
-
                      -
LER
                          Quality Assurance Monitoring
Licensee Event Report
            RBCCW     -
-
                          Reactor Building Closed Cooling Water
LOP /LOCA
            RCW       -
Loss of Power / Loss of Coolant Accident
                          Raw Cooling Water
-
            RCIC     -
M/G
                          Reactor Core Isolation Cooling
Motor Generator
            RHR       -
-
                          Residual Heat Removal
MR
            RHRSW     -
Maintenance Request
                          Residual Heat Removal Service Water
-
            RPS       -
M&TE
                          Reactor Protection System
Measuring & Test Equipment
            RTP       -
-
                          Restart Test Program
PORC
            RWCU     -
Plant Operations Review Committee
                          Reactor Water Cleanup
-
            RXFW     -
QA
                          Reactor feedwater
Quality Assurance
            508       -
-
                          Shutdown Board
Quality Assurance Monitoring
            SGTS     -
QAM
                          Standby Gas Treatment System
-
            SI        -
RBCCW
                          Surveillance Instruction
Reactor Building Closed Cooling Water
            SSFI     -
-
                          Safety System functional Inspection
RCW
            ST       -
Raw Cooling Water
                          Special Test
-
                                                                    _________________ -__________ -
RCIC
Reactor Core Isolation Cooling
-
RHR
Residual Heat Removal
-
RHRSW
Residual Heat Removal Service Water
-
RPS
Reactor Protection System
-
RTP
Restart Test Program
-
RWCU
Reactor Water Cleanup
-
RXFW
Reactor feedwater
-
508
Shutdown Board
-
SGTS
Standby Gas Treatment System
-
Surveillance Instruction
SI
-
SSFI
Safety System functional Inspection
-
ST
Special Test
-
_________________ -__________ -
}}
}}

Latest revision as of 22:53, 10 December 2024

Insp Repts 50-259/88-18,50-260/88-18 & 50-296/88-18 on 880612-30.Violations Noted.Major Areas Inspected:Operational Safety,Maint Observation,Independent Audits & Restart Test Program
ML20154R821
Person / Time
Site: Browns Ferry  
Issue date: 09/15/1988
From: Brooks C, Little W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20154R808 List:
References
50-259-88-18, 50-260-88-18, 50-296-88-18, NUDOCS 8810040366
Download: ML20154R821 (22)


See also: IR 05000259/1988018

Text

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1

UNITED STATES

j'

j

. NUCLEAR REGULATORY COMMISSION

o

REGION 11

\\'e,,,,g

101 MARIETTA ST N.W.

ATLANTA, GEORGIA 30323

(

Report Nos.:

50-259/88-18, 50-260/88-18,-and 50-296/88-18

Licensee:

Tennessee Valley Authority

l

6N 38A Lookout Place

'

1101 Market Street

Chattanooga, TN 37402 2801

Docket Nos.:

50-259, 50-260 and 50-296

License 741.:

OPR-33, DPR-52,

and DPR-68

Facility Name:

Browns Ferry 1, 2, and 3

Inspection Conducte :

June 12-30,

988

-

Inspector-

[

f

g-- R. Brooks,~ Acting Senior Resident Inspector

Date 51gned

j

]

Accompanying Personnel:

E. F. Christnot, Resident Inspector

[

W. C. Bearden, Resident Inspector

A. H. Johnson, Project Engineer

<

//

Approved by:7. 5. Littler Sectioll Chief

/ #88

Date Signed

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i

Inspection Programs

,

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TVAProjectsOfvision

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,

!

SUMMARY

.

5

.

Scope:

This routine inspection was conducted in the areas of operational

2

safety, maintenance observation, independent audits, and restart test

program,

,

i

Results: One violation (260/88-18-02) was identified for failure to document

an inadvertent overload condition on the "0" Diesel Generator on a

,

1

Condition Adverse to Quality Report (CAQR) (see paragraph 5.c.)

(Restartitem)

7

,

i

The following inspection followup items were identified:

j

IFI 260/88-18-01,

Undocumented caole conductor splice.

l

,

(Restartitem)

j

IFI 260/88-18 03, Test deficiencies identified during LOP /LOCA

f

Test "A".

(Restartitem)

l

'

'

IFI 260/8818-04, Occumentation of offsite voltage during

[

LOP /LOCA Test "8".

(Restartitem)

!

GG10040366 880922

l

ADOCKCS00g}i9

l

DR

i

$

_ _ , . . . _ _ , _ _ _

. - _ _ _ . __

___ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _

<

'

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..

2

i

IFI 259,260/88-18-05, Major discrepancies identified during

LOP /LOCA Test "C".

(Restart itemi

IFI 260/88-18-06, Oeficiencies identified during LOP /LOCA Test

"0".

(Restart item)

i

!

. _ - _ _ _ _ _

_ - - _

___ _ _ _ _ __-_____ _ - _ _ _

_ _ - _ _ _ _ _ _ - _

_ _ _ _ _ _ _ _ -

.

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REPORT DETAILS

]

1.

Persons Contacted

L

Licensee Employees

!

\\

  • J. G. Walker, Plant Manager

!

J. D. Martin, Assistant to the Plant Manager

l

.

  • k. M. McKeon, Operations Superintendent

'

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T. F. Ziegler, Superintendent - Maintenance

i

D. C. Miss, Superintendent - Technical Services

J. G. Turner, Manager - Site Quality Assurance

!

M. J. Nay, Manager - Site Licensing

i

,

  • J. A. Savage

A.W.Sorrell,ComplianceSupervisor

r

Site Radiological Control Superintendent

!

R. M. Tuttle, Site Security Manager

!

4

L. E. Retzer, Fire Protection Supervisor

H. J. Kuhnert, Office of Nuclear Power, Site Representative

1

-

l

T. C. Valenzano, Director - Restart Operations Center

'

l

Other licensee employees contacted included licensed reactor operators,

I

,

'

auxiliary operators, craftsmen, technicians, public safety officers,

quality assurance personnsi, and design and engineering personnel.

l

Acronyms and abbreviations used throughout the report are listed in the

-

last section of this report.

,

f

  • Attended exit interview

!

2.

Operational Safety (71707, 71710)

'

i

The inspectors were kept informed of the overall plant status and any

l

significant safety matters related to plant operations.

Daily discussions

L

were held with plant management and various members of the plant operating

[

>

4

staff.

(

)

i

The inspectors made routine visits to the control rooms. Ooservations

!

included instrument readings, setpoints and recordings; status of

operating systems; status and alignments of emergency standby systems;

onsite and offsite emergency power sources available for automatic

.

operation; purpose of temporary tags on equipment controls and switches;

,

annunciator alarm status; adherence to procedures; adherence to limiting

i

.

conditions for operations * nuclear instruments operable; temporary

j

i

alterations in effect; daily journals and logs; stack monitor recorder

[

traces; and control room manning.

This inspection activity also included

s

numerous informal discussions with reactor operators and their

!

supervisors.

}

t

.

i

General plant tours were conducted on at ':.w a weekly basis.

Portions

4

of the turbine building, each reactor bui;

ag and outside areas were

l

visited.

Observations included valve positions and system alfgnment;

l

snubber and hanger conditions; containment isolation aligr.ments;

instrument readings; housekeeping; proper power supply and breaker

!

!

!

-


.

,.

2

alignments: radiation area controls; tag controls on equipment; work

activities in progress; and radiation protection controls.

Informal

discussions were held with selected plant personnel in their functional

areas during these tours.

Durir.g a routine tour on June 27, 1988, the inspector observed a

compensatory fira watch posted in the

"B'

Shutdown Board (SDB) room who

appearoa to be inattentive to his duties.

The inspector initiated a

discussion with the firewatch in order to ensure that he was alert and

then notified a licensee representative who initiated appropriate

disciplinary action.

During a routine tour on June 29, 1988, the inspector observed an

unapproved flammable liquid container in a storage cage on the Refuel

F!oor.

Upon interviewing Refuel Floor personnel, the inspector learned

that a glass reageat-type bottle was being used te transport acetone from

j

the Chemistry Lab to the Refuel Fione for use in cleaning fuel channels

i

and other fuel related components.

The empty bottle was stored for 7uture

,

use.

The use of the bottle is contrary te the requirements of Staadard

'

Practice 14.36, Hazardous Chemicals / Flammable or Combustible iiquids,

which cal's for VL listed cans.

Tne inspector contacted a site fire

protection engineer who removed the bottle and instructed refuel floor

and chemistry lab personnel on the use of proper containers.

Since the

boi.tle was not being used, it was immediately removed, and personnel were

,

reinstructed, no violation or deviation will be issued.

I

3.

Maintenance Observation (62703)

Plant maintenance activities on selected safety-related systems and

'

components were observed / reviewed to afcertain that they were conducted in

!

i

accordance with requirements.

The following items were corsidered during

<

this review:

the Technical Specification limiting conditions for

!

operations were met; activities were accomplisheo using approved

procedures; functional testing and/or calibrations were performed prior to

returning components or systems to service; quality control records were

i

maintained; activities were accomplished by qualified personnel; parts and

,

materials used were pro]erly certified; power tagout clearance procedures

l

were adhered to; and raciological controls were implemented as required.

l

Maintenance Requests (MR) were reviewed to determine the status of

I

outstanding jobs and to assure that priority was assigned to safety-

related eouipment maintenance which might affect plant safety.

The

,

j

inspectors observed the below listed maintenance activities during this

l

reporting period:

a.

Mechanical Maintenance Instruction (MMI) 190, Control Red Drive

Unlatching.

b.

MMI 7, Control Rod Drive Changeout.

c.

Operating Instruction (01)-85, Control Rod Insert and Withdraw

Timing, portions performed as post-maintenance testing.

.

_ _ _

__

_ _ ____

_ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

3

d.

Diesel Generator (DG) "0" troubleshooting and corrective maintenance

activities related to the inadvertent overload on June 21, 1988

(refer to paragraph 5.c, of this report for details).

e.

MR Bf1074 dated May 10, 1988, was indicatad as being outstanding

durine a tour conducted on June 27, 1988.

This MR documented a need

for c'eaning the Units 1/2 "B" DG batteries.

The inspector observed

i

a heavy layer of dust and white particulate material on top of the

batteries.

In addition, the inspector noted that on four of the

battery cells, the spark arrestor vent covers were missing and the

particulate material had entered into the battery electrolyte through

the openings.

The inspector informed a licensee representative of

the deficient condition and also pointed out to the plant maintenance

supervisor that the more than seven week turnaround on completing a

routine "request for cleaning"ll quantity of the material in the

MR was excessive.

The batteries were

'

immediately cleaned and a sma

electrolyte was evaluated as having no impact on battery performance.

Within this area no violations or deviations were found.

4.

Independent Audits (40704)

a.

Independent Safety Engineering Group (ISEG)

!

4

i

The licensee implemented the ISEG in early 1988 as discussed in the

BFNP Nuclear Performance Plan.

Tne inspector reviewed the last three

j

monthly reports and found them to be well focussed on current

industry problems as well as specific site weaknesses.

The reports

were professional and thorough.

The ISEG review topics included:

(1l NRCthe Licensee Event Report (LER) program; (2) Control Air System;

(3,

Information Notices; and (4) Plant Operations Review

'

Committee (PORC) review of plant modifications.

With continued

,

diligence, the ISEG should satisfactorily fulfill its role in

providing appraisals of the quality and safety of operation to the

licensee s upper management.

b.

American Nuclear Insurers Nuclear Liability Insurance Inspection

j

A nuclear liability insurance inspection was conducted by the

,

American Nuclear Insurers during February 1988,

The inspection

report and ifcensee's response to the report were made available to

i

!

the resident inspectors.

The inspection focused on Onsite Safety

Review, Operations, Radwaste Management, Health Physics, and Plant

Water Chemistry.

Three recommendations were made and two suggestions

i

were offered.

The inspection findings did not point to any

,

programmatic weaknesses not already known to the NRC.

The resident

had attended the exit and considered the most significant weakness

!

identified to be in the area of root cause analysis and recurrence

!

control.

,

!

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-

_ _ _ _ _ _ _ _ _ _ _ _ -

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. _ . _ _

._

__

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._.

. - - _ _

_.

_

_ _ _ _ _ _ _ - _ _ - _ _ _ _ _ _ _

.

.

4

c.

Safety System Functional Inspecdon (SSFI)

The licensee's QA organization coordinated an SSFI performed pri-

marily by an outside contractor during the period of June 6 - July 1,

1988.

The inspection was patterned after the NRC's SSFI as described

in NRC Inspection Manual Chapter 2515.

The team identified 24

concerns documented as "observations".

Fourteen of the observations

were judged by the team to be safety significant or potentially

significant depending upon the outcome of further review and analysis

to be performed by the licensee.

The team reviewed the RHRSW and

EECW systems.

The majority of the observations were found to have

been previously identified by the licensee or the NRC and in some

'

formal tracking program for closecut.

,

One deficiency was found to impact system operability under the

existing plant conditions.

Due to recurring failures of valves 67-50

and 67-51, the potential for failure of these valves was judged to be

significant.

These are cross-connect valves between the safetyld

related EECW system and the non-safety-related RCW system.

Shou

these valves fsil to close as required under certain circumstances,

insufficient cooling water to the diesel engine coolers could result.

The licensee suspended fuel handling operations on June 30, 1988,

until the valves were tagged closed on a clearance hold order to

eliminate this concern.

The SSFI team made several conclusions from the characterization of

the findings.

The maintenance area was judged to be the weakest of

those evaluated.

Weaknesses were also noted in design calculation

verification and licensee review of calculations performed by

contractors.

The team further detected a lack of sensitivity among

plant personnel as far as respect for the operational status of the

system.

This may be attributed to the extensive shutdown during

which the system status was not maintained and the mind-set that

accompanies such a shutdown.

The final SSFI report will be reviewed and TVA's response to the

findings will be monitored.

No violations or deviations were identified.

5.

Costart Test Program (RTP)

The inspector attended RTP status meetings; reviewed RTP test procedures,

test specifications, and baseline test requirement documents; observed

RTP tests and associated tests performances; and reviewed RTP test results

including test exceptions.

The inspector also attended selected Restart

Operations Center (War Room) and JTG meetings.

a.

Summary of RTP Activities

(1) RTP-03A, Reactor Feedvater

This test was approved by the JTG for performance on June 16,

1988.

It consisted of verifying various signals, including

.

_.

- - - - 7

-

.

,-

5

reactor level and pressure signals to the reactor protective

system and high reactor level trip signals to the HPCI and

RCICinjectionsystemturbines.

The test was completed with the

exception of section 5.16 which, in part, requires verifying

high reactor pressure trip of the recirculation pumps.

(2) RTP-23, RHRSW

Outages continued throughout most of this reporting) period with

the majority of effort aimed at completing the rep acoment of

Dresser Couplings and completing "the hy"drostatic test and

restoration of the "Al",

"A2", "81, "B2 , "C1", "C2", "D1",

and "D2" pumps.

Flood level switch replacement continued to be

a problem, in that a dedicated switch has not been found.

(3) RTP-038, RXFW

This test was released for performance by the JTG on June 30,

1988.

It deals mainly with the RXFW pumas and their trips

including low main condensor vacuum and ligh reactor water

level.

Monitoring of this test will be covered in future NRC

reports.

(4) RTP-024 RCW

This test was completed during this reporting period with 47

total tests exceptions identified.

Of these exceptions, seven

had hardware significance.

MRs were written to correct six of

them however, TE-046, which deals with check valve 1-24-852,

will; require DNE resolution.

(5) RTP-030, Diesel Generator and Reactor Building Ventilation

This test continues to be delayed by parts requirements,

especially flow switches and damper motors.

Approximately 24

test exceptions have been identified with the majority involving

the failure of DG fans to stop or start as rewas issued as a result of thi

CAQR

88-0524

Control Building Heating, Ventilation, and Air

(6)

RTP-31A, ing

Condition

Section 5.1 of this test was released by the JTG for performance

in order to support the LOP /LOCA series of tests.

This section

mainly involved the CREVS.

Additional tests will start af ter

the completion of the LOP /LOCA tests.

No specific test excep-

tions have been identified.

__________ _ _____

.

.

6

(7) RTP-318, Control Building HVAC

Before this test can start, DNE must issue revision number

three (Rev. 3 to BTRD-014.

As of the end of June 1988, this

revision was ssued and the RTG group was in the final stages of

writing and approving RTP-0318.

(8) RTP-39, C02 Storage and Fire Protection

This test was completed during this reporting period with no

specific test exceptions identified.

The test consisted of

smoke detector activation, CO2 logic testing in DG rooms, and

loss of control power tests.

(9) RTP-057-1, 120 Volt DC Battery

This test involves the 8 DGs and covers a total of 16 battery

chargers and battery racks.

Prior to each test on the battery

chargers, the filter capacitors must be changed.

As of the end

of June 1988, ONE was revising the BTRD and the RTP grcup was

changing the system test specification and the RTP procedure.

No test exceptions were identified.

(10) RTP-57-2, 120 V AC Distribution (120V DIST)

This test win virtually completed during this reporting period.

One outstancing test exception was written involving)section 5.2

dealing with the performance of Test Instruction (TI 738, which

could not be performed because of the fire damage in the Unit 2

Orywell.

(11) RTP-57-4, 480 Volt Distribution (480V OIST)

This test was virtually completed; however, a total of 53 test

exceptions were identified.

Of these test exceptions, ten had

l

hardware related issues.

>

(12) RTP-57-5, 4160 Volt Distribution (4 KV DISTRIBUTION)

This test is ongoing and has identified approximately 20 test

exceptions; however, only two have hardware significance.

One

of the ma

setpoints and

tolerances,jor restraints deals with rela

,

which were to be supplied b

ONE through a

L

contractor.

The six special tests involv ng the Unit 1/2 OG

voltage regulators and speed governors have all been completed

-

and are awaiting approval by DNE.

'

,

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_

, . _ . .

. , . . . . . _ . _ _ . - _ . _ _ ~ _

__

- . _ . .

-. -

-

_ _ _ _ _ _ _ _ _ _ _ _ _ - _ _

'

.

..

7

(13) RTP-067, EECW

This system, as with aystem 23 (RHRSW), was also involved with

the replacement of Dresser couplings and the system hydro's.

The testing in progress involved mainly section 5.8 which deals

with various chillers such as the control room emergency

chillers and the SDB room chillers.

One hardware test exception

was identified involving temperature control valve 3-TCV-67-83.

(14) RTP-069, RWCU

This test was released by the JTG on June 17, 1987, and the

majority of effort so far has been directed at completing

'

section 2.0, Prerequisites and section 5.1, Valve Stroke Tests.

NosignificanttestexceptIonshavebeenidentified.

(15) RTP-070, RBCCW

This test was partially released as reported in NRC report

88-10.

Since it started, approximately 27 test exceptions

have been identified with 8 having hardware related issues.

(16) RTP-073, HPCI

The JTG approved this test; however, it has not released the

l

test for performance.

l

(17) RTP-074, RHR

1

This test is being im) acted in Section 5.5 which requires

,

testing of the drywell

spray upper and lower header, by the

!

hydrolazing of the lower header.

This activity was set to

start on or about July 5, 1988.

No significant hardware test

exceptions have been identified.

l

(18) RTP-082, Diesel Generators

!

This system is undergoing a series of special tests involving

all eight OGs.

These are being performed by the system

j

engineers working with vendor renresentatives and onsite DNE

personnel.

A total of ten special tests are involved and will

,

result in the DG's speed governors (hydraulic actuators) and

.

voltage regulators being calibrated as well as optimized for

plant operations.

This system test has identified over 50 test

!

exceptions; however, only three have significant hardware

)

issees.

See Section 5.c. of this report for additional

information on DG testing.

1

i

!

1

.

-

- -

-

- -

-

.

.

. -

.

-

.- _ _ _ _______ -____

_ _ - _ _ _ _ -

. _ _ _

.

..

,

'

8

!

i

'

(19) RTP-084, Containment Atmospheric Dilution

'

This test was released by the JTG for performance on May 25,

i

1988.

The majority of effort has been directed at completing

,

the prerequisites.

Section 5.1 deals with verifying the logic

on a series of valves and replacing Class IE splices with

!

qualified Raychem splices,

t

(20) RTP-085, Control Rod Drive

f

.

This test was delayed by the changeout of 82 rod drive

i

'

mechanisms and the repairs to several rod position indicators.

'

Section 5.2, Rod Position Indicating System Function Test}fied.

[

has

started and no significant test exceptions have been ident

(21) RTP-092, Neutron Monitoring

,

1

<

This test involves the intermediate range monitors (IRMs),

source range monitors (SRMs), and the average power range

monitors (APRMs).

The test was released for performance by the

i

JTG on May 23, 1988; however, a switch involved in the inop

1

bypass for the SRMs

IRMs, and APRMs were not easily obtained

-

i

and contributed to delays.

No significant hardware test excep-

tions were identified.

l

,

j

(22) RTP-99, Reactor Protective System (RPS)

j

This test was released by the JTG for performance on June 17,

I

'

1988

and involves all four channels of the RPS.

One

!

j

signIficant hardware test exception was identified involving

,

Section 5.27, which requires that the reactor mode switch

l

3

i

contacts be verified, and concerns wires in the panel not being

f

1

mi4r ked.

j

(23)

RTP-8' C, Backup Control Test (BUC)

J

'

This test procedure is over 800 pages long and includes the 4KV

SD8s, 480 V SD8s, DG auxiliary boards, 480V reactor motor

i

operated valve (MOV) boards, and the 250 V reactor MOV boards

)

(also any electrical system that has backup controls).

The test

)

was released for performance by the JTG on June 13, 1988, and

has been performed on a continuous basis.

No significant test

exceptions were identified.

.

The above tests were in progress and in various stages of completion

at the end of this reporting period.

The inspector will continue to

l

observe these activities on a day-to-day basis.

l

?

f

q

i

!

!

\\

I

a

,_ -_

___ __- _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-

.

.

.

9

b.

RTP-075, Core Spray

During the performance of RTP-075, Core Spray, the RTP group was

using SI-4.2.8-39A(II) to meet the requirements of step 5.6.5 of the

RTP test.

This was to prove that the CS system Loop II would perform

automatically when called u

However, during the

performance of the SI, the 'pon to do so.20" CS pump automatic circuit break

failed to close when required.

MR A-860183 was written to trouble-

shoot the problem and the RTP personnel wrote TE #9 to document the

failure.

During troubleshooting, maintenace personnel discovered an

undocumented splice in the white lead of cable ES-2554-II, which was

in a cable tray surrounded by flamemastic and located in the Unit 2

reactor building.

The maintenance personnel wrote CAQR BFP-88-0375

to document this discovery.

This item is identified as inspector

followup item (IFI) 260/88-18-01 Undocumented Cable Conductor Splice

in Core Spray Logic Wiring.

Thlsitemisrequiredtobeclosedout

prior to restart.

The disposition of this CAQR will be reviewed in

a future inspection.

One significant test exception involving the stroke time for four

flow control valves was identified.

c.

RTP-082 Diesel Generators

OG "0" was inadvertently (ST) 88-09, Diesel Gene,rator Governor and

overloaded on June 21

1988, during the

conduct of Special Test

Voltage Regulator Calibration.

For a period of about 30 seconds,

control room indications of KW, KVAR, and AMPS were off scale high.

The incident was caused by unintentional shorting of test leads by an

electrician who was directed to take confirmatory measurements of a

parameter beint monitored on a recorder.

The shorting caused fuses

to blow result < ng in a loss of the voltage regulator and governor.

Since the DG was in parallel with the grid during the test, it

immediately accepted this additional load.

An apparently pre-

existing and undetected failure of an SBN switch (cell switch) in the

DG breaker compartment prevented an automatic clearing of the

overload

thus increasing the potential damage to the DG.

The event

wastermlnatedwhenthecontrolroomoperatortrippedtheDGbreaker.

Following the event, the electrical integrity of the DG was confirmed

by the satisfactory performance of a high potential test at 10,000

VOC for one minute.

Visual inspections were conducted of the

insulation system by an experienced vendor representative.

Some

hairline cracks in the insulation were detected which were determined

to have been recently created.

These cracks were indicative of coil

movement relative to the fixed components and could have resulted

from either the overload or some of the more recent stressful restart

testing.

The vendor representative recommended followup high poten-

tial testing at 6,12 and 24 months in order to detect any further

degradation of the insulation system as a result of the overload.

No

L_.

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

.

.

,

.

10

mechanical inspections were performed on the diesel engine.

The

licensee relied upon the expertise of the vendor representative who

waspresentattheDGduringtheoverloadtomakethisjudgment.

The licensee prepared a critique on the event which concluded that

the capability of the DG to perform its intended function had nnt

been affected.

Following a review by the PORC on June 25, 1988, the

DG was declared fully operable.

The inspector .eviewed the event and asked for additional information

on:

1) the cause of failure for the SBM cell switch and whether

the other DG cell switches had bi:en tested 2) an approximation of

the magnitude o/ the overload; 3) a comparison of diesel operating

i

parameters such as vibration, exhaust /c

temperature, oil pressures, oil analysis, ylinder/ cooling water

and oil and fuel consump-

tion before the event with those af ter the event; and 4) other

i

diagnostics and/or inspections contained in the vendor technical

manuals.

During the course of the review, the inspector learned that the

incident was not documented, as required, on a CAQR.

This may have

been a contributing cause to the fragmented approach used to evaluate

and document the condition of the diesel.

Part I, Section 2.16, Step

2.1.1.F of the Nuclear Quality Assurance Manual requires that a

,

condition adverse to quality (CAQ) be documented on a CAQR for items

which have been subjected to conditions for which they have not

been designed such as overaressure overvoltage, overheating, over-

stressing, or environmenta'

conditions hazardous to their function.

i

Failure to initiate a CAQR for the overloaded DG is considered

a violation of 10 CFR 50, Appendix B, Criterion V (259,260,296/

88-18-02).

1

d.

Loss of Power / Loss of Coolant Accident (LOP /LOCA) Testing

I

The licensee's RTP group and the system engineering group, with

l

support from th viher major Browns Ferry site organizations,

'

performed a series of four tests referred to as LOP /LOCA testing,

which started on May 29, 1988, with LOP /LOCA Test "A" and ended at

>

approximately midnight on June 8,1988, with LOP /LOCA Test "0".

)

Numerous pretest meetings were bid such as LOP /LOCA thrice weekly

punchlist, daily RTP status, afG as needed, and a daily morning

J

meeting with the major site organizations to update the LOP /LOCA

,

testing status.

A total of nine inspectors, five region based and

4

four residents, observed the performance of the four tests, with

LOP /LOCA Test ',C" receiving the most coverag/L A

1

e.

The procedures used

1

for the tests were numbered:

2-BFN-RTP-L

(RTP-L/L A),

j

2-BFN-RTP-L/L B (RTP-L/L B), 2-BFN-RTP-L/L C (RTP-L/L C), and

l

2-BFN-RTP-L/L 0 (RTP-L/L 0).

Revision 0 of the procedures were

i

reviewed by the JTG and approved by the Plant Manager shortly before

the performance of the actual tests.

Last minute changes to the

4

_ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _ _ _ ___ _

.____ ___

___

. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

_

- _ _ _ _ _ _ _ .

.

.

,

11

tests were reviewed and approved the day the tests were conducted and

RTP-L/L C and RTP-L/L 0 were revised approximately two days before

the actual tests.

Each test procedure was reviewed and found to be adequate.

(1) LOP /LOCA Test "A"

This test was basically a LOP test, sometimes referred to as a

"blackout" test, and was Jerformed on May 29, 1988.

Section S.3

of the test called for tie simultaneous tripping of the three

main power feeds coming into the plant from the switchyard.

The

inspectors used NRR inspection modules 703068 Loss of Offsite

Power, and 704418

Emergency / Standby Power Supply System Test,

as guidance before, dur'ng and after the test.

Test section

5.4,

Plant Performance, required that all eight OGs start and

!

tie onto their respective SD8s; that various 4-KV and 480 V load

alignments be in accordance with the applicable procedure steps;

that all three units receive a scram signal from loss of RPS

Hotor-Generator (M/G) sets; and that reactor MOV electrical

boards and ventilation boards be in the alignment specified by

a)plicable procedure steps.

The inspectors made the following

osservations:

,

(a) Unit 3 DG "30" did not appear to close onto its SDB (3EC).

r

However, post test review of the visicorder traces indi-

'

cated that the breaker closed and stayed closed for only

l

five cycles, approximately'one-tenth of a second, and then

tripped off.

The licensee s representatives informed the

inspector that an item of M&TE used to time the closure of

the breaker shorted out, )icked up the DC trip coil of the

'

brsaker, and caused the

)reaker to trip shortly af ter

closure.

!

(b) Unit 2 RPS M/G set "2B" did not trip off upon loss of

i

aower (the breaker supalies the power to the motor).

"

iowever, other scram signals from the RPS did initiate

l

a full scram for Unit 2.

(c) Several individual items such as recirculating M/G set

oil pumps "2A-1", "2A-2", "28-1", and "28-2" and control

'

and service air compressor "0" were exceptions to the test

as far as their supply breakers tripping.

j

l

The above items are tracked as IFI 260/88-18-03, Test Deficien-

'

cies Identified During LOP /LOCA Test "A".

This item is

!

required to be closed out prior to restart.

The conduct of the

test by the licensee's representatives was not a well run test

in that the control room activities appeared at times to be very

hectic and a large number of personnel, more than what seemed

~

necessary, were in the control room during the test.

Improve-

ment in professionalism by all personnel and better crowd

-

control was needed,

t

I

L-

. _ _ . _ _ _ .

. _ _ _ _ - _ _ - -

__ . _ _ . .

-

__

--

-

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

.

,

12

(2) LOP /LOCA Test "B"

This test was basically a LOCA test using offsite power (the

grid) as the power source and was performed on June 1,1988.

Section 5 of the test called for the application of a high

drywell pressure signal Of approximately 3.0 psig using

temporary test tubing and a sneumatic calibrator installed at

'

transmitters PT 64-588 and Pr 64-580.

This signal in conjunc-

tion with the already at:nospheric pressure of t1e reactor vessel

initiated a LOCA signal.

The basic requirements of the test

were that all eight DGs start (they were not to close onto their

respective 50Bs); all four Unit 2 CS aumps start in the proper

sequencing and at the proper times; a'l four RHR pumps start in

the low pressure core injection mode in the proper sequencing

and at the proper times; and all four RHRSW pumps used for

EECW start in the proper sequencing and at the proper times.

Additional auxiliary equipment such as reactor recirculation

discharge valve closure, RHR pump cooler fans start, HPCI logic

trips, etc., were verified as required to meet test acceptance.

The inspectors made the following observations:

(a) An inspector was stationed at the Unit 3 control room

0G electrical panel to observe Unit 3 OG operation upon

initiation of the LOCA event.

Test procedure recuirements

were that upon initiation of the LOCA event, Unit 3 DGs

("3A", "3B", "3C", and "30") start automatically, attain

rated voltage and frequency, and remain unconnected to

their respective 4-XV SDBs, and the SDB mode switches

transfer from "auto" to "manual". Observations of annun-

ciator and alarm panel indicator lights confirmed the

aforementioned test requirements for the Unit 3 DGs.

(b) An NRC inspector was stationed at the Unit 2 control room

station and proceeded to the SDBs upon initiation of the

LOCA events. The inspector observed TVA data takers and QA

inspectors as well.

The inspector observed no deviations

or violations of procedure and test requirements.

(c) An NRC inspector observed the control room activities

inside the Unit 2 main control panel "horsehoe."

The

inspector used Section 5.2 of the test to verify and

document the performance of the four CS pumps, ion

the

l

four RHR pumps in the low pressure core inject

mode, and the four RHRSW pumps used for EECW.

Verifi-

cation of operation involved recording motor amperage,

system flows, and system pressures.

All 12 pumps

indicated electrical current flow, with the CS trains

indicating approximately 6200 gallons per minute (gpm)

and approximately 250 psig each, and the RHR trains

indicating approximately 12000 gpm and approximately

275 psig each.

Overall evaluation was that the major

items of equipment responded as required by the test.

L-

_ _ _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _ _ _ _

_

_

_ _ _ _ _ _ _ _ _ _ _ _

__

____ ____ _ ___ ___- .

_ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

.

. .

13

Upon post test review by all the inspectors involved, it was

noted that the facilities test personnel appeared somewhat

confused by what was occurring at different stages of the test.

The control room activities appeared to be more controlled thJn

during LOP /LOCA "A".

It was noted that no direct monitoring of

the incoming voltage from the grid was made by the licensee's

representatives during this test.

The inspector was informed

that this will be documented by calculation.

This item is

identified as IFI 260/88-18-04 Documentation of Offsite Voltage

During LOP /LOCA Test "B".

This item is required to be closed

out prior to restart.

The results of the test will be reviewed

and commented on in a future NRC report.

(3) LOP /LOCA Test "C"

This test was a combination of a LOP signal followed six seconds

later by a LOCA signal with the "B" DG disabled and was per-

formed on Junt 5,1988.

Section 5.3 of the test called for

simultaneously opening the three main power feeds coming into

the plant from the switchyard and after a3 proximately a six

second time delay initiating the triple 1ow (Lo-Lo-Lo) or

Level I reactor vessel level trip; thereby setting up a LOP

followed by a LOCA.

The ins 3ectors used NRR modules 70316, Loss

of Offsite Power Test 70436, Engineered Safety Features Actua-

tion System Test, and 70441, Emergency / Standby Power System

Test

as

Test

sectIon 5. guidance before, during and af ter the test.

4, Plant Performance, re

with the exception of Unit 3 DG "B"quired that all eight DGs

start and tie onto their

respectiveSDBs;thatthe"2A"and"2C"CSpumpsstart;thatthe

"2A', "28", and "2C" RHR pumps start; that the applicable RHRSW

pumps start; and that all three units receive a scram signal.

Additional auxiliary equipment as outlined in the procedure were

to activate, including Standby Gas Treatment and Control Room

Emergency Ventilation as required to meet test acceptance

criteria.

The inspectors made the following observations:

(a) Unit 2 Control Room Observations

After the test was initiated at 2:16 p.m., the inspector

observed that a scram sig"nal was received.

RHR pumps "2A",

"2B",

"2C" and CS pumps

2A" and "20" started as planned.

Power was lost to the "2A" reactor MOV board which did not

transfer as expected.

The transfer was manually performed

,

at 2:29 p.m., and the CS inboard injection valve (2-FCV-

75-25) opened (procedure step 5.4.9.1).

,

Prior to the test, RCIC was inop"erable and procedure step

5.4.12 could not be met.

The

RCIC Relay "Logic Power

Failure" annunciator was observed.

The "2B

reactor MOV

l

L

_ _ _ _ _ _ _ _ _ _

_ _ _ - _ _ _

.

,.

14

board is supplied by 508 "0"

and DG "0" was not tested.

Accordingly, procedure steps 5.4.9.2 and 5.4.19.2 could

not be checked due to an absence of power.

RHR System II flow and pressure could not be checked

because I&C Bus "B" had no power (procedure step 5.4.24).

At 3:02 p.m. , 4160 V SDB "D' was restored and these were

checked.

The alarm and annunciation table, Appendix E, had the

following alarms received prior to the test:

Unit Preferred Supply Abnormal

Reactor Auto Scram Channel A

Reactor Auto Scram Channel B

The "Turbine Tripped Electrical Trouble" annunciator

was not received.

(b) During LOP /LOCA Test

"C" an inspector observed Unit 3

control room activities with regard to alarm and annuncia-

tor

panels and noted that the Unit 3 DG started and closed

on the 4160 V SOBS.

In addition, selected circuit breakers

on the Unit 3 480V SDBs "3A" and "3B" were checked to

verify and obtain their LOP /LOCA positions.

The following

problems were identified during the test:

DGs "3A", "3C" and "3D" came up to rated speed and

-

voltage but did not tie-on to their respective 4160 V

SDB.

Troubleshooting and review of log'ic circuitry

indicated that the DG "3A",

"3C" and

3D" output

breakers closed at ~6.5 seconds and at ~6.75 seconds a

LOCA signal opened the 3 DG breakers.

During recharg-

ing of the breakers, the anti pump relay (52Y) had

sealed in steventing the reclosure of the DG breakers

(i.e. , DG areaker opened -0.3 seconds and the anti-

pump relay responded as designed to a fault condition

on the 508 although the LOCA signal was the reason for

the DG breakers being opened).

An operator was sent

to the switchgear room where a remote panel is avail-

able for local operations.

The operator slowly placed

the normal / emergency switch (43) to the emergency

position.

The switch is a break before make design

and thus de energized the 52Y anti-pump relay setting

up the circuitry for closure of the three DG breakers.

The inspector also identified that the data recorder

-

did not have the latest data sheets for recording

breaker positions on 480 V SDBs "3A" and "3B".

l

_ _ - _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ - _

--

_

..

,.

15

(c) An NRC inspector was stationed in the Unit I control room

and proceeded to the SD8s upon initiation of the LOP /LOCA

event. The inspector observed TVA data takers and QA

inspectors as well.

(d) An NRC inspector observed the initiation of the LOCA signal

in the Unit 2 auxiliary instrument room and noted that

relay 16A-K29 in panel 9-42 did not de-energize as required

for the test.

This rela

tainment isolation logic. y is part of the primary con-

The inspector then proceeded to SOB "0" and there observed

a Ifeensee representative performing manual manipulations

on 480V reactor MOV board

'2A".

It was later determined

that this board was not initially lined up per section 5.2,

Initial Lineup of the Test.

These two items were con-

sideredtobemajorconcernsforthetest.

(e) An NRC inspector was positioned in front of 508 "3EC" near

DG breaker "3C".

After the LOP initiation, the inspector

noted that the open/ closed flag on the breaker indicated

momentarily closed then immediately indicated open and

stayed in that p"osition.

The inspector then proceeded to

SDBs "3EA"

"3E8

and "3ED" and noted that the breakers

I

for DGs "3A" and '30" were both open.

Of the Unit 3 DGs,

only the output breaker for "38" was closed on 508 "3EB".

It was later discovered that the following had occurred:

Sequence of Events

Time

1.5 seconds

Loss of Power - 4KV SDB De-energized; DGs

Start

5 seconds

Board undervoltage device times out and

closes contacts in breaker closure circuit

(2-211-4A3)

-6.5 seconds

DGs "3A", "3C", and "30" come up to speed

and close contacts in breaker closure

circuits (VSR1,VSR2)

6.55 seconds

OG breakers close ("3A", "3C", "30")

6.55 seconds

Accidentsignalinlected,DGbreakers"3A",

"3C",

and '30" trlpped via LOCA signal,

CASA-2 contacts closed, 52a (contact 4 4c)

closed on breaker closure.

ThisenergIzed

52T and tripped the breaker

_ . - _ _ _ - - _ _. __ _ - _ _ _ _ _ _ _ _ _ -

_ _ _ _ - _ - _ _ _ _ _ _ - _ _ _ _ _ _ _

_ _ _ _ _

..

.

l

'

16

,

t

I

l

~6.55 seconds

When breaker closed, 452M and 52Y energized

l

to recharge breaker.

Energizing 52Y

isolates 52X (closure coil) from circuit,

r

i

Note:

It takes 2 seconds to recharge the

i

breaker.

The undervoltage device

did not have time to reset;

therefore, a closure signal is

'

sealed into the circuit.

This

energizes 52Y through contacts

7-1.

This keeps the breakers

'

.

locked

out.

The

inspector

i

considered this to be a major

[

i

concern for the test.

'

l

(f) An NRC inspector observed the control room activities

t

mainly involved with the Unit 1/2 DG board.

No def t-

i

ciencies were identified.

l

l

Because of the problems that occurred a major part or all of

f

Test C will be rerun.

The licensee documented the locking out of the Unit 3 DG output

,

breakers on CAQR BFP-88-0394, and initiated action to write a

l

LER.

These items are being tracked as IFI 259,260,296/88-18-05,

'

Major Olscrepancies Identified During LOP /LOCA Test "C".

This

'

item is required to be closed out prior to restart.

l

!

l

(4) LOP /LOCA Test "0"

l

The test was a combination of a LOP sig/ hardware problem encountered

nal followed at three seconds

L

by a LOCA signal.

Due to the technical

!

with the six second LOCA signal discovered during LOP /LOCA Test "C",

!

I

the time for initiation of the LOCA signal was changed from six

i

seconds to three seconds.

This test was performed on July 8,1988,

I

with the Unit 2 DC battery disconnected.

Section 5.3 of the test

!

called for the simultaneous opening of the three main power feeds

!

coming into the plant and after approximately a three second time

l

delay, initiating the tripIe low (Lo-Lo-Lo) or level I reactor vessel

j

,

l

trip; thereby, setting up a LOP followed by a LOCA.

Section 5.4,

,

f

Plant Performance, required that all eight DGs start (due to the

disconnection of the DC battery the Unit 3 "0" DG would not tie onto

[

508 "3E0"); that R)iR pumps "2A' , "2C" and "20" start; that trains "A"

& "B" of the SBGTS and CREYS start; and that all three units receive

I

a scram signal due to the loss of all six (two per unit) RPS M/G

i

sets.

Additional auxiliary equipment as outlined in the procedure

}

was to activate to meet the test acceptance criteria.

l

The inspectors made the following observations:

all eight OGs

!

started and tied onto their respective SOBS with the exception of

(

OG "30"; the three units each received a scram signal due to the loss

[

of RPS M/G sets; and equipment required to perform in order to meet

[

the test acceptance criteria appeared to do so.

[

I

l

-

.

.

-

- _ - _ _ _ _ _ _ _ _ _ _ _ _

_ _ _ _ _ _

.

,.

17

This test appeared to be the smoothest run of all four tests.

However, on initial review it appears that like LOP /LOCA Test

"C", some equipment was not lined up initially as required by

section 5.2 of the test.

This item is identified as IFI

260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".

This item is required to be closed out prior to restart.

General observations made and comments about the LOP /LOCA series

of tests are as follows:

The inspectors were concerned that the large number of test

exceptions make it difficult to determine if in fact they have

met the baseline program.

With the exception of the operations manager and some of the

senior personnel, the operations staff did not give the

appearance of proper attitude or professionalism in conduct and

attire.

Also, the inspectors could not readily tell who was in

charge of the operations shift.

Operator logs did not contain enough detail to recreate opera-

tional events.

Proper professionalism was not displayed when the pre-o) LOP /

LOCA briefings were delayed in starting:

cat calls and fokes by

attendees were noted.

Also there appeared to be a lack of

seriousness and interest shown by some individuals involved in

this series of RTP testing.

On positive side, the RTP technical staff appeared to be very

professional and concerned.

The compliance staff and site

licensing staff appea:ed to be very professional and had been

responsive to all of the NRC concerns and requests.

These observations have been discussed with various department

managers at the site.

It is the conclusion of the inspectors that

the series of tests were not as successful as they could have been,

especially LOP /LOCA Test "C".

In the area of pre-test preparations,

a vast improvement is called for; in the area of operator activities,

improvement is needed; and in the area of test exceptions, clari-

fication is needed.

The licensee subsequently decided to rerun much

of LOP /LOCA "C".

6.

Review of Quality Assurance Monitoring (QAM) Surveillances

During the reporting period, the inspector observed QAM personnel in

the field actively monitoring RTP testing.

The following QAM

surveillances were reviewed by the inspector:

Number

Description

QBF-88-0352

This surveillance documented the activities

involving the RTP daily status meetings.

_ _ _ _ _ _ _ _ _

_ _ _ __

..

..

18

L

l

Number

Description

I

i

QBF-88-00436

This item documented the activities involving the

I

ST 88-17 on DG "B" and indicated that the DG was

!

l

started with the cylinder vents open.

'

QBF-88-00455

This item documented the activities involving ST

!

88 17 and RTP-082 on DG "B" and indicated that

the DG was started with the load limiter on zero.

l

QBF-88-0465

This

item documented activities

involving

ST 88-07 on DG "A".

.

QBF-88-0475

This

itcm documented activities

involving

i

ST 88-07 on OG "A" and indicated that MR 860262

'

was performed to troubleshoot the DGs droop

circuit.

'

'

QBF-88-0610

This

item documented activities

involving

l

LOP /LOCA Test "C" and indicated that the "3A",

!

"3C", and "30" DGs failed to perform as expected

1

and that relay 16A-K29 did not de-energize.

,

1

Additional test exceptions were also documented.

QBF-88-0637

This item documented activities

involving

l

LOP /LOCA Test "0" and did not indicate any major

equipment

failure;

however,

several

test

exceptions were documented.

QBF-88-0643

This

item documented activities

involving

ST 88-08 on DG "C".

QBF-88-0653

This item documented the followup activities of

QBF-88-0455 and indicated that CAQR-BFP-88-0403

was initiated by RTP personnel. O

personnel initiated Critique 88-027. perations

QBF-88-0666

This item documented the activities involving

RTP-075, Core Spray, and indicated that Loop II

failed an SI due to an undocumented cable splice.

QBF-88-0667

This

item documented activities

involving

ST 88-08 on OG "0" and indicated that RHR pump

"28"

tripped during the test and that an

imediate temporary change (ITC) was initiated to

lift a lead to prevent t11s from happening again.

QBF-88-0669

This

item documented activities

involving

ST 88-09 on DG "0".

I

i

- - - _ - - - _ _ . _ _

____

_ _ _ _

_ _ _ _ _ _ _ _ _ _ _ - _ _ -

. .

.

,

19

Number

Description

<

QBF-88-0674

This item documented activities involving"3C"

LOP /

LOCA Test

"A" and indicated that the DG

output breakers did not perform as required due

to measuring and test equipment (M&TE) problems.

QBF-88-0680

This

item documented activities

involving

ST 88-09 on DG "0".

QBF-88-0687

These items documented activities involving the

QBF-88-0691

daily RTP testing status meetings.

QBF-88-0695

This

item documented activities involving

RTP-057-4, 4 KV Ofstribution.

!

The above reviews indicated that QAM personnel were adequately

performing surveillances and identifying and documenting problems.

7.

Exit Interview

l

The inspection scope and findings were summarized on July 8,1988, with

the Plant Manager, Superintendents, and other members of his staff.

New

items identified were:

Inspector Followu

Conductor SpItce. p Item (IFI) 260/88-18 01, Undocumented Cable

a.

Violation 259,260 2

Failure to Document Overload

i

b.

Conditiononthe"d"96/88-18-02,

'

DieselGeneratoronaCAQR.

c.

260/88-18-03, Test Deficiencies Identified During LOP /LOCA Test

d.

IFI 260/88-18-04, Documentation of Offsite Voltage During LOP /LOCA

l

Test "B".

e.

IFI 259,260,296/88-18-05, Major Discrepancies Identified During

LOP /LOCA Test "C".

f.

IFI 260/88-18-06, Deficiencies Identified During LOP /LOCA Test "0".

.

The above items are all identified as restart items.

l

l

.

-

.

..

,.

20

8.

Acronyms and Abbreviations

8FN

Browns Ferry Nuclear

-

BTRD

Baseline Test Requirements Occument

-

CAD

Containment Atmospheric Dilution

-

CAQR

Conditions Adverse to Quality Report

-

CREVS

Control Room Emergency Ventilation System

-

CS

Core Spray

-

DG

Ofesel Generator

-

DNE

Department of Nuclear Engineering

-

ECCS

Essential Core Cooling Systems

-

EECW

Emergency Equipment Cooling Water

-

FI

Flow Indicator

-

HPCI

HighPressureCoolantInjection

-

HVAC

Heating Ventilation and Air Conditioning

-

ISEG

Independent Safety Engineering Group

-

JTG

Joint Test Group

-

LER

Licensee Event Report

-

LOP /LOCA

Loss of Power / Loss of Coolant Accident

-

M/G

Motor Generator

-

MR

Maintenance Request

-

M&TE

Measuring & Test Equipment

-

PORC

Plant Operations Review Committee

-

QA

Quality Assurance

-

Quality Assurance Monitoring

QAM

-

RBCCW

Reactor Building Closed Cooling Water

-

RCW

Raw Cooling Water

-

RCIC

Reactor Core Isolation Cooling

-

RHR

Residual Heat Removal

-

RHRSW

Residual Heat Removal Service Water

-

RPS

Reactor Protection System

-

RTP

Restart Test Program

-

RWCU

Reactor Water Cleanup

-

RXFW

Reactor feedwater

-

508

Shutdown Board

-

SGTS

Standby Gas Treatment System

-

Surveillance Instruction

SI

-

SSFI

Safety System functional Inspection

-

ST

Special Test

-

_________________ -__________ -