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                                                                                  ; UNITED STATES -       _
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  (W g.                            . 'o                               ' = NUCLEAR CEGULATORY COMMISSION b , ; .
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                                        n .;                                            RE'l!!ON 11           ; 5 .,
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          *g({                       1[                       +
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                                                                              101 MARIETTA STREET,N.W.
*
                                                                                ATLANTA, GEORGIA 30323
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                              ~
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                        ***** '
RE'l!!ON 11
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                            ;?*                                                                                                       m
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            >
-
                        > Report No.':: 50-395/89-13:                                           A
'
                          Licensee:. South Carolina Electric & Gas Company ^
n .;
                                                  Columbia, SC 29218
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                          Docket No.:":50-395                                                           License No.: NPF-12.
101 MARIETTA STREET,N.W.
      .                                                                                                                       .
+
                          Facility Name':                   V. C. Summer
El1<
                                                                      .
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                          Inspection Conducted:.-July;1                             .31,<1989
-
                            Inspectors:
f
                                                ~
ATLANTA, GEORGIA 30323
                                                        b
'
                                                  R. 'L.- Prevatte
~
                                                                                              M                      Yh f 9    f
g
                                                                                                                      Date' Signed
***** '
                                                                                Yg g
y:
    l                                                    @h,idd A                                                         7A//89
.
                                                                                                                          ~
;?*
                                                  P.   C'.   Hopkins                                                 Date Signed. -
m
g                                                                                   Ug / ' '
> Report No.':: 50-395/89-13:
                          Approved by:                           Ms
A
                                                      F.1 .~ Cantrell, Secti                     ef
>
                                                                                                                      I/
Licensee:. South Carolina Electric & Gas Company ^
                                                                                                                      Da,te Signed
Columbia, SC 29218
                                                                                                                                  N
G
*            '
Docket No.:":50-395
                                                    ' Division of Reactor Pr ects
License No.: NPF-12.
              '
.
    ..
.
                                                                                          SUMMARY
Facility Name':
                          Scope:
V. C. Summer
                          This routine inspection was conducted.by the resident inspectors onsite in the
.
                          areas of' monthly surveillance, observations, monthly maintenance observation,
Inspection Conducted:.-July;1
                          operational: safety verification, action' on previous inspection findings,' and:
.31,<1989
                          other areas.' Certain tours were conducted'on backshifttor weekends. Backshift
~
                          or weekend tours were conducted on July 11, 12, 13, 18, 19. 23,'24, 25 .and 26,
b
                          1989.-
M
                          Results:
Yh f 9
                          The unit began the month at 100 percent power. A trip from 100 percent power
Inspectors:
                          occurred.on July 11, 1989, as the result.of a maintenance technician shorting.
f
      +                ' out a power supply- for the generator stator water cooling system. The unit
R. 'L.- Prevatte
                          trip and SCE&G grid heavy loading resulted in a loss of offsite power with a
Yg g
                          transfer. of the. safety related buses to the emergency diesel generators,
Date' Signed
                          paragraph 4.b.                     The unit was restarted and returned to power on July 13, 1989.=
l
l       ,                It ' operated at full ' power for the remainder of the' month.- The areas of
@h,idd A
                          maintenance and: surveillance continue to' perform satisfactorily. A violation
7A//89
                          for failure to control the temporary installation of portable demineralizers
P.
                          was identified, paragraph 4.c. The licensee's evaluation 'of this event
C'. Hopkins
                          determined that' although a seismic event could effect the operation of safety
Ug / ' '
                          equipment, the affected systems would still continue to operate satisfactorily.
Date Signed.
                              8908230003 890804
-
                              FDR       ADOCK 05000395
~
                              Q                                 FDC
g
                  -
Approved by:
                                                    _            __      -                 _                                           O
Ms
I/
N
F.1 .~ Cantrell, Secti
ef
Da,te Signed
' Division of Reactor Pr ects
*
'
'
..
SUMMARY
Scope:
This routine inspection was conducted.by the resident inspectors onsite in the
areas of' monthly surveillance, observations, monthly maintenance observation,
operational: safety verification, action' on previous inspection findings,' and:
other areas.' Certain tours were conducted'on backshifttor weekends. Backshift
or weekend tours were conducted on July 11, 12, 13, 18, 19. 23,'24, 25 .and 26,
1989.-
Results:
The unit began the month at 100 percent power.
A trip from 100 percent power
occurred.on July 11, 1989, as the result.of a maintenance technician shorting.
' out a power supply- for the generator stator water cooling system.
The unit
+
trip and SCE&G grid heavy loading resulted in a loss of offsite power with a
transfer. of the. safety related buses to the emergency diesel generators,
paragraph 4.b.
The unit was restarted and returned to power on July 13, 1989.=
l
It ' operated at full ' power for the remainder of the' month.- The areas of
,
maintenance and: surveillance continue to' perform satisfactorily.
A violation
for failure to control the temporary installation of portable demineralizers
was identified, paragraph 4.c.
The licensee's evaluation 'of this event
determined that' although a seismic event could effect the operation of safety
equipment, the affected systems would still continue to operate satisfactorily.
8908230003 890804
FDR
ADOCK 05000395
Q
FDC
-
-
_
O
_
__


-                                           _                               _
-
                                                                                          _ .-
_
  .
_
            -
_ .-
.:   .
.
              ,
-
        a
.:
                                                                                                j
.
                                            REPORT DETAILS
,
          1.-   Persons Contacted
a
                Licensee Employees
j
                W. Baehr, Manager, Chemistry and Health Physics
REPORT DETAILS
                C. Bowman, Manager, Scheduling and Modifications                               !
1.-
              *0. Bradham, Vice President, Nuclear Operations
Persons Contacted
                M. Browne, Manager, Systems Engineering & Performance
Licensee Employees
                W. Higgins, Supervisor, Regulatory Compliance
W. Baehr, Manager, Chemistry and Health Physics
                S. Hunt, Manager, Quality Systems
!
              *A. Koon, Manager, Nuclear Licensing
C. Bowman, Manager, Scheduling and Modifications
                G. Moffatt, Manager, Maintenance Servic2s
*0. Bradham, Vice President, Nuclear Operations
                D. Moore, General Manager, Engineering Services
M. Browne, Manager, Systems Engineering & Performance
              *K. Nettles, General Manager, Nuclear Safety
W. Higgins, Supervisor, Regulatory Compliance
                C. Price, Manager, Technical Oversite                                         '
S. Hunt, Manager, Quality Systems
                M. Quinton, General Manager, Station Support
*A. Koon, Manager, Nuclear Licensing
                J. Shepp, Associate Manager, Operations
G. Moffatt, Manager, Maintenance Servic2s
                J. Skolds, General Manager, Nuclear Plant Operations
D. Moore, General Manager, Engineering Services
              *G. Soult, General Manager, Operations and Maintenance
*K. Nettles, General Manager, Nuclear Safety
                      .
C. Price, Manager, Technical Oversite
                G. Taylor, Manager, Operations
'
                D. Warner, Manager, Core Engineering and Nuclear Computer Services
M. Quinton, General Manager, Station Support
              *M. Williams, General Manager, Nuclear Services
J. Shepp, Associate Manager, Operations
                K. Woodward, Manager, Nuclear Operations Education and Training
J. Skolds, General Manager, Nuclear Plant Operations
                Other licensee employees . contacted included engineers, technicians,
*G. Soult, General Manager, Operations and Maintenance
                operators, mechanics, security force members, and office personnel.
.
              * Attended exit interview
G. Taylor, Manager, Operations
                Acronyms and initialisms used throughout this report are listed in the
D. Warner, Manager, Core Engineering and Nuclear Computer Services
                last paragraph.
*M. Williams, General Manager, Nuclear Services
          2.     Monthly Surveillance Observation (61726)
K. Woodward, Manager, Nuclear Operations Education and Training
                The inspectors observed surveillance activities of safety related systems
Other licensee employees . contacted included engineers, technicians,
                and components to ascertain that these activities were conducted in
operators, mechanics, security force members, and office personnel.
                accordance with license requirements. The inspectors observed portions of
* Attended exit interview
                35 selected surveillance tests including all aspects of Reactor Building       !
Acronyms and initialisms used throughout this report are listed in the
                Closecut Inspection, STP 109.001. The inspectors verified that required
last paragraph.
                administrative approvals were obtained prior to initiating the test,
2.
                testing was accomplished by qualified personnel, required test instruments-
Monthly Surveillance Observation (61726)
                tion was properly calibrated, data met TS requirements, test discrepancies
The inspectors observed surveillance activities of safety related systems
                were rectified, and the systems were properly returned to service. The
and components to ascertain that these activities were conducted in
                licensee demonstrated good communication between test technicians and         i
accordance with license requirements. The inspectors observed portions of
                control room personnel during performance of test procedures. The
!
                materials, parts, components and test equipment used were found to be           l
35 selected surveillance tests including all aspects of Reactor Building
                correct and documented properly. Technicians had procedures available at
Closecut Inspection, STP 109.001.
                                                                                                  '
The inspectors verified that required
                all times and utilized them properly.
administrative approvals were obtained prior to initiating the test,
                No violations or deviations were identified.
testing was accomplished by qualified personnel, required test instruments-
                                                                                                  i
tion was properly calibrated, data met TS requirements, test discrepancies
      _           --   - - _                                                                   l
were rectified, and the systems were properly returned to service.
The
licensee demonstrated good communication between test technicians and
i
control room personnel during performance of test procedures.
The
materials, parts, components and test equipment used were found to be
l
'
correct and documented properly.
Technicians had procedures available at
all times and utilized them properly.
No violations or deviations were identified.
i
_
--
- - _
l


                                                                                                _ _ _
_ _ _
  r   ,
r
              -
,
    .  .
.
                ,
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          ,
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,
,
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a
a
            3. .   Menthly Maintenance Observation (62703)
3. .
                  The inspectors observed maintenance activities of safety related systems
Menthly Maintenance Observation (62703)
                  and components to ascertain that these activities were conducted in
The inspectors observed maintenance activities of safety related systems
                  accordance with approved procedures, TS, industry codes and standards.
and components to ascertain that these activities were conducted in
                  The inspectors determined that the procedures used were ' adequate to
accordance with approved procedures, TS, industry codes and standards.
                  control the activity, and that these activities were accomplished by
The inspectors determined that the procedures used were ' adequate to
                  qualified personnel.     The inspectors independently verified that the
control the activity, and that these activities were accomplished by
                  equipment was properly tested before being returned to service.
qualified personnel.
                  Additionally, the inspectors reviewed several outstanding job orders to
The inspectors independently verified that the
                  determine that the licensee was giving priority to safety related
equipment was properly tested before being returned to service.
l:                 maintenance and not developing a backlog which might affect a given
Additionally, the inspectors reviewed several outstanding job orders to
                  system's performance. The operational maintenance activities observed by
determine that the licensee was giving priority to safety related
l:
maintenance and not developing a backlog which might affect a given
'
'
                  the inspectors during this report were judged.to be satisfactory.       It
system's performance.
                  appears that with the installation of control room barriers and a new
The operational maintenance activities observed by
                  tagging desk in the control room, the traffic in the critical areas of the
the inspectors during this report were judged.to be satisfactory.
                -control room has been reduced. This has also resulted in ' smoother
It
                  processing of MWR's, STP's and other maintenance activities through. the
appears that with the installation of control room barriers and a new
                  control room.     The following specific maintenance activities were
tagging desk in the control room, the traffic in the critical areas of the
                  observed:
-control room has been reduced.
                  MWR 87C00it           Replace regulator for demineralized instrument air
This has also resulted in ' smoother
                                        supply
processing of MWR's, STP's and other maintenance activities through. the
                  MWR 8901080           Repair controller on hydrogen analyzer
control room.
                  MWR 8901211           Calibrate pressurizer control channels 444C & 444D
The following specific maintenance activities were
                  PMTS 115543           Repair air intake transmitter for SW building
observed:
                  MWR 89G0095           Repair smoke detectors
MWR 87C00it
                  PMTS 112043           Repair discharge flow transmitter on C FW booster pump
Replace regulator for demineralized instrument air
                  PMTS 116745           Calibrate heater coil temperature controller in
supply
                                        auxiliary building supply plenum
MWR 8901080
                  PMTS 118844           Calibrate temperature element on SW building pump room
Repair controller on hydrogen analyzer
                  MWR 88E0125           Repair flexible conduit to smoke analyzer
MWR 8901211
                  MWR 88E0108           Test and replace smoke analyzer
Calibrate pressurizer control channels 444C & 444D
                  PMTS 117045           Calibrate temperature alarm on SW booster pump
PMTS 115543
                  MWR 8956808           Remove necessary parts and reinstall torque motor           j
Repair air intake transmitter for SW building
                  PMTS 122056           Perform inspection on open cycle cooling water booster
MWR 89G0095
                                        pump A                                                       1
Repair smoke detectors
                                                                                                      J
PMTS 112043
Repair discharge flow transmitter on C FW booster pump
PMTS 116745
Calibrate heater coil temperature controller in
auxiliary building supply plenum
PMTS 118844
Calibrate temperature element on SW building pump room
MWR 88E0125
Repair flexible conduit to smoke analyzer
MWR 88E0108
Test and replace smoke analyzer
PMTS 117045
Calibrate temperature alarm on SW booster pump
MWR 8956808
Remove necessary parts and reinstall torque motor
j
PMTS 122056
Perform inspection on open cycle cooling water booster
pump A
1
J


                                          .   __ _   _ _-
.
                                      ..
__
  .                                     .
_
                                                  .
_ _-
                                            4
..
                                                                                              3
.
                                                    PMTS 122063               Rotate turbine on closed cycle cooling water pump A
.
                                                    PMTS 121916               Verify alignment of 480V breakers
.
                                                    PMTS 121917               Electrical adjustment on 7.2kV switchgear treaker
4
                                                    PMTS 119740               Inspection of FW pump turbine
3
                                                    MWR 8901221               Repair posit.an indication circuitry on pressurizer
PMTS 122063
                                                                              sample header isolation valve
Rotate turbine on closed cycle cooling water pump A
                                                    MWR 87G0095               Repair sample detection line
PMTS 121916
                                                    PMTS 122395               Vibration analysis check on RHR pump A
Verify alignment of 480V breakers
                                                    PMTS 121729               Vibration analysis check on EFW pump A
PMTS 121917
                                                    PMTS P122139             Audit misalignment log
Electrical adjustment on 7.2kV switchgear treaker
                                                    PMTS P122104               Inspect 7.2kV switchgear breakers
PMTS 119740
                                                    No violations or deviations were identified.
Inspection of FW pump turbine
                                              4.   Operational Safety Verification (71707)
MWR 8901221
                                                    a.       The inspectors toured the control room, reviewed plant logs and
Repair posit.an indication circuitry on pressurizer
                                                              records and held discussions with plant staff personnel to verify
sample header isolation valve
                                                              that the plant was being operated safely and in conformance with
MWR 87G0095
                                                              applicable requirements. Specific items inspected in the control
Repair sample detection line
                                                              room included: adequacy of staffing and attentiveness of control room
PMTS 122395
                                                              personnel, TS and procedural adherence, operability of equipment and
Vibration analysis check on RHR pump A
                                                              indicated control room status, control room' logs, tagout books,
PMTS 121729
                                                              operating orders, jumper / bypass controls, computer printouts and
Vibration analysis check on EFW pump A
                                                              annunciators. Tours of other plant areas were conducted to verify
PMTS P122139
                                                              equipment operability, control of ignition sources and co,mbustible
Audit misalignment log
                                                              materials, the condition of fire detection and extinguishing
PMTS P122104
                                                              equipment, the control of maintenance and surveillance cctivities in
Inspect 7.2kV switchgear breakers
                                                              progress, the implementation of radiation protective controls and the i
No violations or deviations were identified.
                                                              physical security plan.     Tours were conducted during normal and
4.
                                                              random off-hour periods.
Operational Safety Verification (71707)
                                                    b.       On July 11,1989, at 2:35     p.m., the unit tripped from 100 percent
a.
                                                              power.   The trip resulted from an I&C technician shorting a wire
The inspectors toured the control room, reviewed plant logs and
                                                              while reconnecting a thermocouple inside the stator water cooling
records and held discussions with plant staff personnel to verify
                                                              control cabinet. The short circuit blew the power supply fuses and
that the plant was being operated safely and in conformance with
                                                              resulted in a low flow signal on stator water cooling.     The normal
applicable requirements.
l                                                             protective action would have resulted in a turbine run back. This
Specific items inspected in the control
!                                                             circuit did not function correctly and resulted in a turbine trip and
room included: adequacy of staffing and attentiveness of control room
                                                              reactor trip.
personnel, TS and procedural adherence, operability of equipment and
                                                                                                                                      I
indicated control room status, control room' logs, tagout books,
                                                                                                                                      1
operating orders, jumper / bypass controls, computer printouts and
                                                                                                                                    1
annunciators.
  _ _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _                       _                                                                       a
Tours of other plant areas were conducted to verify
equipment operability, control of ignition sources and co,mbustible
materials, the condition of fire detection and extinguishing
equipment, the control of maintenance and surveillance cctivities in
progress, the implementation of radiation protective controls and the
i
physical security plan.
Tours were conducted during normal and
random off-hour periods.
b.
On July 11,1989, at 2:35
p.m.,
the unit tripped from 100 percent
power.
The trip resulted from an I&C technician shorting a wire
while reconnecting a thermocouple inside the stator water cooling
control cabinet.
The short circuit blew the power supply fuses and
resulted in a low flow signal on stator water cooling.
The normal
l
protective action would have resulted in a turbine run back.
This
!
circuit did not function correctly and resulted in a turbine trip and
reactor trip.
I
1
1
_ _ _ _ _ _ _ _ _ _ _ _ . . _ _ _ _
_
a


                -                                       ---
-
    4
---
        '
4
                  %                    vg
%
                                .
vg
                                                                                        4
'
              ,
.
                                                      At the time of.the' reactor trip the utility. grid was' experiencing.a
4
                                                      high load of approximately 3100.MW's. This loss of-the 900 MW's
,
                                                            ~
At the time of.the' reactor trip the utility. grid was' experiencing.a
                                                                                                                            .
high load of approximately 3100.MW's.
H          ,
This loss of-the 900 MW's
                                                      being generated by Summer resulted in allarge voltage oscillation
~
                                                      which actuated protective relays that 'also ' tripped 4 pumped storage
.
                                                      units at the Fairfield Pumped Storage Facility (approximately 250MW) -
being generated by Summer resulted in allarge voltage oscillation
                                                                                                ~
H
      ,
                                                      3 units'~ at the. Saluda Hydro (approximately 135MW), and both fossil
                                                      generating ' units at~ McMeekin Station (approximately 250MW). '.These
                                                      losses resulted in the 230kV offsite power source to Summer dropping
                                                      -to approximately 203kV and the 115kV source dropping to approximately-
                                                      100kV. .This . low voltage condition actuated the undervoltage' relays -
l                                                    which automatically separated the 7200 volt ESF buses from offsite
                                                      power. This started the emergency diesel' generators and placed the
,
,
which actuated protective relays that 'also ' tripped 4 pumped storage
units at the Fairfield Pumped Storage Facility (approximately 250MW) -
~
3 units'~ at the. Saluda Hydro (approximately 135MW), and both fossil
,
generating ' units at~ McMeekin Station (approximately 250MW). '.These
losses resulted in the 230kV offsite power source to Summer dropping
-to approximately 203kV and the 115kV source dropping to approximately-
100kV. .This . low voltage condition actuated the undervoltage' relays -
l
which automatically separated the 7200 volt ESF buses from offsite
power.
This started the emergency diesel' generators and placed the
safety related buses on the' diesel generator. The non-safety service
,'
buses remained connected to the degraded offsite power source and
'
'
                                                      safety related buses on the' diesel generator. The non-safety service
continued to operate throughout the event. at reduced voltages, . An
                                                      buses remained connected to the degraded offsite power source and
unusual event was declared at 3:10 p.m. due to the loss of both
                                                      continued to operate throughout the event. at reduced voltages, . An
offsite power sources. The system voltage was returned to normal and.
'
thel safety related buses were reconnected to offsite power at
                                                      unusual event was declared at 3:10 p.m. due to the loss of both
approximately 5:00 p.m.
                                                      offsite power sources. The system voltage was returned to normal and.
The DG's'were' secured and the unusual event
                                                      thel safety related buses were reconnected to offsite power at
was terminated at 5:11 p.m.
                                                      approximately 5:00 p.m. The DG's'were' secured and the unusual event
                                                      was terminated at 5:11 p.m.
,
,
                                                      Further investigation by the licensee revealed that the MVAR loading
Further investigation by the licensee revealed that the MVAR loading
                                                      of Summer, the, grid MVAR distribution at the time of the unit trip
of Summer, the, grid MVAR distribution at the time of the unit trip
                                                      and lower.than normal setpoints on some generator back-up protection.
and lower.than normal setpoints on some generator back-up protection.
                                                      relays: may have led to this event.       The licensee has developed
relays: may have led to this event.
                                                      administrative - guidelines to . provide for - improved system MVAR
The licensee has developed
                                                      distribution that should reduce the probability of future similar
administrative - guidelines to . provide for - improved system MVAR
                                                      occurrences. After completing all necessary repairs and implementing
distribution that should reduce the probability of future similar
                                                      the'above step, the unit was restarted.on July 12, 1989, and returned
occurrences. After completing all necessary repairs and implementing
                                                      to power operation on July 13,1989.         The licensee is currently
the'above step, the unit was restarted.on July 12, 1989, and returned
                                                      preparing a LER on this event.- The event will also be discussed.
to power operation on July 13,1989.
                                                      during a meeting scheduled for August 1, 1989. at NRC headquarters.
The licensee is currently
                                                  c. While. conducting a routine walkdown of the plant on July 6, 1989 -the
preparing a LER on this event.- The event will also be discussed.
                                                      inspectors discovered two temporary demineralizers on the 412
during a meeting scheduled for August 1, 1989. at NRC headquarters.
                                                      elevation of the intermediate building. These units are 24 inches in
c.
                                                      diameter and approximately six feet high and are configured to stand     'l
While. conducting a routine walkdown of the plant on July 6, 1989 -the
                                                      in an upright position.     The weight of each of the components is
inspectors discovered two temporary demineralizers on the 412
                                                      approximately 1750 lbs. The support for.these units was a 1/2-inch
elevation of the intermediate building. These units are 24 inches in
                                                      sisal' rope which attached these units to two EFW line supports and a
diameter and approximately six feet high and are configured to stand
                                                      SW line support. A concern with the effects of this installation on
'l
                                                      the operability of the SW and EFW system and nearby safety-related
in an upright position.
                                                      components during a seismic event was immediately discussed with the
The weight of each of the components is
                                                      operations shift supervisor. The shift supervisor immediately had
approximately 1750 lbs.
                                                      these units removed from the area and documented this in off-normal
The support for.these units was a 1/2-inch
                                                      occurrence 89-058 and NCN 3386.
sisal' rope which attached these units to two EFW line supports and a
SW line support.
A concern with the effects of this installation on
the operability of the SW and EFW system and nearby safety-related
components during a seismic event was immediately discussed with the
operations shift supervisor.
The shift supervisor immediately had
these units removed from the area and documented this in off-normal
occurrence 89-058 and NCN 3386.
.
.
- _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _
- _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _


                                  . _ - - _ _ - .
. _ - - _ _ - .
                                                    .
.
g                             .
.
                                                      .
g
                                                  .
.
                                                                                              5
.
                                                          Further investigation into this item revealed that these units had
5
                                                          been installed on June 1, 1989, to permit draining of the SG while the
Further investigation into this item revealed that these units had
                                                          plant was in Mode 5. This installation was accomplished without a
been installed on June 1, 1989, to permit draining of the SG while the
                                                          MWR as required by the Station Housekeeping and plant Inspection
plant was in Mode 5.
                                                          Program Procedure SAP 142, and Conduct of Maintenance Procedure
This installation was accomplished without a
                                                          SAP-300.     The unit was restarted on June 11,-1989 with the units
MWR as required by the Station Housekeeping and plant Inspection
                                                          still in place. This installation had been noted by plant management
Program Procedure SAP 142, and Conduct of Maintenance Procedure
                                                          and directions had been given to remove the units on or around June 20,
SAP-300.
                                                            1989.
The unit was restarted on June 11,-1989 with the units
                                                            In this instance personnel were deficient in not performing this work
still in place. This installation had been noted by plant management
                                                          under the licensee MWR program.       No documentation to require
and directions had been given to remove the units on or around June 20,
                                                          engineering review of this temporary installation was performed as
1989.
                                                            required by SAP 142. The above procedure was also inadequate in that
In this instance personnel were deficient in not performing this work
                                                            it did not insure that a seismic evaluation of the installation be
under the licensee MWR program.
                                                            performed and that time limits were established to insure removal of
No documentation to require
                                                            this hazard prior to plant start-up.       This is contrary to the
engineering review of this temporary installation was performed as
                                                            requirement of TS 6.8.1.a which requires that procedures be
required by SAP 142. The above procedure was also inadequate in that
                                                            established, implemented and maintained for activities referenced in
it did not insure that a seismic evaluation of the installation be
                                                          Appendix A of Regulatory Guide 1.33, Revision 2 February 1972.
performed and that time limits were established to insure removal of
                                                          This is 'a violation, " Failure to Control Temporary Installations,"
this hazard prior to plant start-up.
                                                            89-13-01.
This is contrary to the
                                                            The licensee has performed an evaluation which determined that a
requirement of TS 6.8.1.a which requires that procedures be
                                                            seismic event could have resulted in the portable demineralized
established, implemented and maintained for activities referenced in
                                                            becoming mobile and possibly damaging two FW line supports and
Appendix A of Regulatory Guide 1.33, Revision 2
                                                            shearing off a test connection on a CCW line and a drain line'in the
February 1972.
                                                            SW system. The failure of the EFW supports would not have resulted in
This is 'a violation, " Failure to Control Temporary Installations,"
                                                            the system becoming inoperable and the loss of flow in the SW and CCW
89-13-01.
                                                            system would not have degraded system flow below the worst case
The licensee has performed an evaluation which determined that a
                                                            analyzed values. The potential flooding from the lines were well
seismic event could have resulted in the portable demineralized
                                                            within the capacity of space dewatering equipment. This analysis
becoming mobile and possibly damaging two FW line supports and
                                                            determined that all systems would remain operable.
shearing off a test connection on a CCW line and a drain line'in the
                                                            This event is similar to a licensee identified violation that was
SW system. The failure of the EFW supports would not have resulted in
                                                            documented in inspection report 89-03. In that event temporary
the system becoming inoperable and the loss of flow in the SW and CCW
                                                            scaffolding had been erected for shielding of RHR piping to reduce
system would not have degraded system flow below the worst case
                                                            personnel radiation exposure while the plant was in a refueling
analyzed values.
                                                            outage. Due to procedural deficiencies and personnel errors the
The potential flooding from the lines were well
                                                            scaffolding was not removed prior to plant start-up.         That
within the capacity of space dewatering equipment.
                                                            installation had the potential to impact on system operability.
This analysis
                                                            The licensee, in their response to this violation, should address
determined that all systems would remain operable.
                                                            procedural changes made to insure that temporary installations are
This event is similar to a licensee identified violation that was
                                                            controlled and that dates or mode restraints are established to
documented in inspection report 89-03.
                                                            insure that temporary installations which are required while the
In that event temporary
                                                            plant is shutdown are removed prior to unit start-up.
scaffolding had been erected for shielding of RHR piping to reduce
                                                        Violations cr deviations were identified.
personnel radiation exposure while the plant was in a refueling
  - _ _ _ _ - - _ _ - - _ - _ _ - _ - _ _ _ _ - -                           _ _ _ _ _ _ . ._-                                     i
outage.
Due to procedural deficiencies and personnel errors the
scaffolding was not removed prior to plant start-up.
That
installation had the potential to impact on system operability.
The licensee, in their response to this violation, should address
procedural changes made to insure that temporary installations are
controlled and that dates or mode restraints are established to
insure that temporary installations which are required while the
plant is shutdown are removed prior to unit start-up.
Violations cr deviations were identified.
- _ _ _ _ - - _ _ - - _ - _ _ - _ - _ _ _ _ - -
_ _ _ _ _ _ . ._-
i


-         __                                         _
-
    .   x
__
  . '. .             +
_
                                      ,
x
        .
.
                                                                                      6
+
            5.                               Action on Prev ous Inspection Findings (92701, 92702)
.
                                                (Closed) TI2513/94, Inspection for verification of licensee changes made
'. .
                                              to comply with PWR moderator dilution requirements, multi-plant action
,
                                                item 13-03. The inspector reviewed inspection requirements specified.in
.
                                              this instruction and reviewed the V. C. Summer Safety Evaluation Report and
6
                                              supplements to determine what requirements had been established. This
5.
                                              review identified that dilution events and- preventive measures were
Action on Prev ous Inspection Findings (92701, 92702)
                                              discussed and resolved in section 15 of the SER and in supplements 1 and 3
(Closed)
                                                to the SER. However, multi-plant action item B-03 was not specifically
TI2513/94, Inspection for verification of licensee changes made
                                              discussed.     Discussion with Mr. L. Kopp, the NRR lead contact for.this
to comply with PWR moderator dilution requirements, multi-plant action
                                                item, indicates thut this item is not applicable for V. C. Summer. The
item 13-03.
                                                SIMS open item list for V. C. Summer also does not list this item. Further
The inspector reviewed inspection requirements specified.in
                                              discussion with Mr. Kopp revealed that since V.C. Summer was licensed in
this instruction and reviewed the V. C. Summer Safety Evaluation Report and
                                                1982, this issue would have been resolved in the normal licensing process
supplements to determine what requirements had been established.
                                                for V. C. Summer and all other plants licensed after 1979. Based on the
This
                                                above, this item is administratively closed.
review identified that dilution events and- preventive measures were
            6.                               Other Areas
discussed and resolved in section 15 of the SER and in supplements 1 and 3
                                              The inspectors-toured the licensee's lead dispatch center in Columbia, SC
to the SER.
                                                on July 25, 1989. Computer control and indication systems and procedures
However, multi-plant action item B-03 was not specifically
                                                that are used to operate' and control SCE&G's grid was discussed in detail.
discussed.
                                                This tour was very beneficial and provided the inspectors with a better
Discussion with Mr. L. Kopp, the NRR lead contact for.this
                                                understanding of this tystem.
item, indicates thut this item is not applicable for V. C. Summer.
            7.                                 ExitInterview(30703)
The
                                                The inspection scope and findings were summarized on July 31, 1989, with
SIMS open item list for V. C. Summer also does not list this item.
                                                those persons indicated in paragraph 1. The inspectors described the
Further
                                                areas inspected and discussed the inspection findings. The plant trip and
discussion with Mr. Kopp revealed that since V.C. Summer was licensed in
                                                the resulting offsite power loss event which occurred on July 11, 1989, was
1982, this issue would have been resolved in the normal licensing process
                                                discussed in detail. This included the short term corrective measures and
for V. C. Summer and all other plants licensed after 1979.
                                                the current investigation into root cause and long term corrective action.
Based on the
                                                The violation which resulted from the failure to control the temporary
above, this item is administratively closed.
                                                  installation of portable demineralizers in the intermediate building was
6.
                                                attributed to procedural inadequacies and a failure to follow procedures.
Other Areas
                                                  It was also noted that the violation was similar to LIV 89-03-01 when the
The inspectors-toured the licensee's lead dispatch center in Columbia, SC
                                                  plant was restarted without removing scaffolding that contained temporary
on July 25, 1989.
                                                  shielding. No dissenting comments were received from the licensee. The
Computer control and indication systems and procedures
                                                licensee did not identify as proprietary any of the materials provided to
that are used to operate' and control SCE&G's grid was discussed in detail.
                                                or reviewed by the inspectors during the inspection.
This tour was very beneficial and provided the inspectors with a better
            8.                                 Acronyms and Initialisms
understanding of this tystem.
                                                  CCW       Component Cooling Water
7.
l                                                DG         Diesel Generator                                               ,
ExitInterview(30703)
                                                  EFW       Emergency Feedwater
The inspection scope and findings were summarized on July 31, 1989, with
                                                  FW       Feedwater
those persons indicated in paragraph 1.
L-           _ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ - _ - _ _ _
The inspectors described the
                                                                                                                              \
areas inspected and discussed the inspection findings. The plant trip and
the resulting offsite power loss event which occurred on July 11, 1989, was
discussed in detail. This included the short term corrective measures and
the current investigation into root cause and long term corrective action.
The violation which resulted from the failure to control the temporary
installation of portable demineralizers in the intermediate building was
attributed to procedural inadequacies and a failure to follow procedures.
It was also noted that the violation was similar to LIV 89-03-01 when the
plant was restarted without removing scaffolding that contained temporary
shielding.
No dissenting comments were received from the licensee. The
licensee did not identify as proprietary any of the materials provided to
or reviewed by the inspectors during the inspection.
8.
Acronyms and Initialisms
CCW
Component Cooling Water
DG
Diesel Generator
,
l
EFW
Emergency Feedwater
FW
Feedwater
\\
L-
_ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ - _ - _ _ _


                              --_                   ,
--_
  L
,
                                  '*
L
        ..- -                       ,    :. ,
'*
                                      .-
..- -
                                                                                7
:. ,
,
.-
7
o
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L
L
                                                I&C   Instrumentation and Control
I&C
                                                MW   Megawatt.
Instrumentation and Control
                                              - MWR   Maintenance Work Request
MW
                                                MVAR Million Volt Amps Reactive
Megawatt.
                                                NCN   Non-Conformance Notice
- MWR
i                                               NRC   Nuclear Regulatory Commission
Maintenance Work Request
                                                NRR   Nuclear Reactor Regulation
MVAR
                                                PMTS Preventive Maintenance Task Sheet
Million Volt Amps Reactive
                                              - QC   Quality Control
NCN
                                                RHR   Residual Heat Removal
Non-Conformance Notice
                                                SAP   Station Administrative Procedure
i
                                                SCE&G South Carloina Electric & Gas Company
NRC
                                                SER   Safety Evaluation Report
Nuclear Regulatory Commission
                                                SG   Steam Generator
NRR
                                                SIMS Safety Issues Management Systems
Nuclear Reactor Regulation
                                                STP   Surveillance Test Procedures
PMTS
                                                SW   Service Water
Preventive Maintenance Task Sheet
                                                TS   Technical Specifications
- QC
Quality Control
RHR
Residual Heat Removal
SAP
Station Administrative Procedure
SCE&G
South Carloina Electric & Gas Company
SER
Safety Evaluation Report
SG
Steam Generator
SIMS
Safety Issues Management Systems
STP
Surveillance Test Procedures
SW
Service Water
TS
Technical Specifications
,
,
----________-______m_______m____
----________-______m_______m____
}}
}}

Latest revision as of 00:31, 2 December 2024

Insp Rept 50-395/89-13 on 890701-31.Violation Noted.Major Areas Inspected:Monthly Surveillance Observations,Monthly Maint Observation,Operational Safety Verification,Action on Previous Insp Findings & Other Areas
ML20246A534
Person / Time
Site: Summer 
Issue date: 08/04/1989
From: Cantrell F, Hopkins P, Prevatte R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20246A526 List:
References
50-395-89-13, NUDOCS 8908230003
Download: ML20246A534 (8)


See also: IR 05000395/1989013

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Licensee:. South Carolina Electric & Gas Company ^

Columbia, SC 29218

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Docket No.:":50-395

License No.: NPF-12.

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Facility Name':

V. C. Summer

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Inspection Conducted:.-July;1

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Inspectors:

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SUMMARY

Scope:

This routine inspection was conducted.by the resident inspectors onsite in the

areas of' monthly surveillance, observations, monthly maintenance observation,

operational: safety verification, action' on previous inspection findings,' and:

other areas.' Certain tours were conducted'on backshifttor weekends. Backshift

or weekend tours were conducted on July 11, 12, 13, 18, 19. 23,'24, 25 .and 26,

1989.-

Results:

The unit began the month at 100 percent power.

A trip from 100 percent power

occurred.on July 11, 1989, as the result.of a maintenance technician shorting.

' out a power supply- for the generator stator water cooling system.

The unit

+

trip and SCE&G grid heavy loading resulted in a loss of offsite power with a

transfer. of the. safety related buses to the emergency diesel generators,

paragraph 4.b.

The unit was restarted and returned to power on July 13, 1989.=

l

It ' operated at full ' power for the remainder of the' month.- The areas of

,

maintenance and: surveillance continue to' perform satisfactorily.

A violation

for failure to control the temporary installation of portable demineralizers

was identified, paragraph 4.c.

The licensee's evaluation 'of this event

determined that' although a seismic event could effect the operation of safety

equipment, the affected systems would still continue to operate satisfactorily.

8908230003 890804

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REPORT DETAILS

1.-

Persons Contacted

Licensee Employees

W. Baehr, Manager, Chemistry and Health Physics

!

C. Bowman, Manager, Scheduling and Modifications

  • 0. Bradham, Vice President, Nuclear Operations

M. Browne, Manager, Systems Engineering & Performance

W. Higgins, Supervisor, Regulatory Compliance

S. Hunt, Manager, Quality Systems

  • A. Koon, Manager, Nuclear Licensing

G. Moffatt, Manager, Maintenance Servic2s

D. Moore, General Manager, Engineering Services

  • K. Nettles, General Manager, Nuclear Safety

C. Price, Manager, Technical Oversite

'

M. Quinton, General Manager, Station Support

J. Shepp, Associate Manager, Operations

J. Skolds, General Manager, Nuclear Plant Operations

  • G. Soult, General Manager, Operations and Maintenance

.

G. Taylor, Manager, Operations

D. Warner, Manager, Core Engineering and Nuclear Computer Services

  • M. Williams, General Manager, Nuclear Services

K. Woodward, Manager, Nuclear Operations Education and Training

Other licensee employees . contacted included engineers, technicians,

operators, mechanics, security force members, and office personnel.

  • Attended exit interview

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Monthly Surveillance Observation (61726)

The inspectors observed surveillance activities of safety related systems

and components to ascertain that these activities were conducted in

accordance with license requirements. The inspectors observed portions of

!

35 selected surveillance tests including all aspects of Reactor Building

Closecut Inspection, STP 109.001.

The inspectors verified that required

administrative approvals were obtained prior to initiating the test,

testing was accomplished by qualified personnel, required test instruments-

tion was properly calibrated, data met TS requirements, test discrepancies

were rectified, and the systems were properly returned to service.

The

licensee demonstrated good communication between test technicians and

i

control room personnel during performance of test procedures.

The

materials, parts, components and test equipment used were found to be

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correct and documented properly.

Technicians had procedures available at

all times and utilized them properly.

No violations or deviations were identified.

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3. .

Menthly Maintenance Observation (62703)

The inspectors observed maintenance activities of safety related systems

and components to ascertain that these activities were conducted in

accordance with approved procedures, TS, industry codes and standards.

The inspectors determined that the procedures used were ' adequate to

control the activity, and that these activities were accomplished by

qualified personnel.

The inspectors independently verified that the

equipment was properly tested before being returned to service.

Additionally, the inspectors reviewed several outstanding job orders to

determine that the licensee was giving priority to safety related

l:

maintenance and not developing a backlog which might affect a given

'

system's performance.

The operational maintenance activities observed by

the inspectors during this report were judged.to be satisfactory.

It

appears that with the installation of control room barriers and a new

tagging desk in the control room, the traffic in the critical areas of the

-control room has been reduced.

This has also resulted in ' smoother

processing of MWR's, STP's and other maintenance activities through. the

control room.

The following specific maintenance activities were

observed:

MWR 87C00it

Replace regulator for demineralized instrument air

supply

MWR 8901080

Repair controller on hydrogen analyzer

MWR 8901211

Calibrate pressurizer control channels 444C & 444D

PMTS 115543

Repair air intake transmitter for SW building

MWR 89G0095

Repair smoke detectors

PMTS 112043

Repair discharge flow transmitter on C FW booster pump

PMTS 116745

Calibrate heater coil temperature controller in

auxiliary building supply plenum

PMTS 118844

Calibrate temperature element on SW building pump room

MWR 88E0125

Repair flexible conduit to smoke analyzer

MWR 88E0108

Test and replace smoke analyzer

PMTS 117045

Calibrate temperature alarm on SW booster pump

MWR 8956808

Remove necessary parts and reinstall torque motor

j

PMTS 122056

Perform inspection on open cycle cooling water booster

pump A

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PMTS 122063

Rotate turbine on closed cycle cooling water pump A

PMTS 121916

Verify alignment of 480V breakers

PMTS 121917

Electrical adjustment on 7.2kV switchgear treaker

PMTS 119740

Inspection of FW pump turbine

MWR 8901221

Repair posit.an indication circuitry on pressurizer

sample header isolation valve

MWR 87G0095

Repair sample detection line

PMTS 122395

Vibration analysis check on RHR pump A

PMTS 121729

Vibration analysis check on EFW pump A

PMTS P122139

Audit misalignment log

PMTS P122104

Inspect 7.2kV switchgear breakers

No violations or deviations were identified.

4.

Operational Safety Verification (71707)

a.

The inspectors toured the control room, reviewed plant logs and

records and held discussions with plant staff personnel to verify

that the plant was being operated safely and in conformance with

applicable requirements.

Specific items inspected in the control

room included: adequacy of staffing and attentiveness of control room

personnel, TS and procedural adherence, operability of equipment and

indicated control room status, control room' logs, tagout books,

operating orders, jumper / bypass controls, computer printouts and

annunciators.

Tours of other plant areas were conducted to verify

equipment operability, control of ignition sources and co,mbustible

materials, the condition of fire detection and extinguishing

equipment, the control of maintenance and surveillance cctivities in

progress, the implementation of radiation protective controls and the

i

physical security plan.

Tours were conducted during normal and

random off-hour periods.

b.

On July 11,1989, at 2:35

p.m.,

the unit tripped from 100 percent

power.

The trip resulted from an I&C technician shorting a wire

while reconnecting a thermocouple inside the stator water cooling

control cabinet.

The short circuit blew the power supply fuses and

resulted in a low flow signal on stator water cooling.

The normal

l

protective action would have resulted in a turbine run back.

This

!

circuit did not function correctly and resulted in a turbine trip and

reactor trip.

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At the time of.the' reactor trip the utility. grid was' experiencing.a

high load of approximately 3100.MW's.

This loss of-the 900 MW's

~

.

being generated by Summer resulted in allarge voltage oscillation

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,

which actuated protective relays that 'also ' tripped 4 pumped storage

units at the Fairfield Pumped Storage Facility (approximately 250MW) -

~

3 units'~ at the. Saluda Hydro (approximately 135MW), and both fossil

,

generating ' units at~ McMeekin Station (approximately 250MW). '.These

losses resulted in the 230kV offsite power source to Summer dropping

-to approximately 203kV and the 115kV source dropping to approximately-

100kV. .This . low voltage condition actuated the undervoltage' relays -

l

which automatically separated the 7200 volt ESF buses from offsite

power.

This started the emergency diesel' generators and placed the

safety related buses on the' diesel generator. The non-safety service

,'

buses remained connected to the degraded offsite power source and

'

continued to operate throughout the event. at reduced voltages, . An

unusual event was declared at 3:10 p.m. due to the loss of both

offsite power sources. The system voltage was returned to normal and.

thel safety related buses were reconnected to offsite power at

approximately 5:00 p.m.

The DG's'were' secured and the unusual event

was terminated at 5:11 p.m.

,

Further investigation by the licensee revealed that the MVAR loading

of Summer, the, grid MVAR distribution at the time of the unit trip

and lower.than normal setpoints on some generator back-up protection.

relays: may have led to this event.

The licensee has developed

administrative - guidelines to . provide for - improved system MVAR

distribution that should reduce the probability of future similar

occurrences. After completing all necessary repairs and implementing

the'above step, the unit was restarted.on July 12, 1989, and returned

to power operation on July 13,1989.

The licensee is currently

preparing a LER on this event.- The event will also be discussed.

during a meeting scheduled for August 1, 1989. at NRC headquarters.

c.

While. conducting a routine walkdown of the plant on July 6, 1989 -the

inspectors discovered two temporary demineralizers on the 412

elevation of the intermediate building. These units are 24 inches in

diameter and approximately six feet high and are configured to stand

'l

in an upright position.

The weight of each of the components is

approximately 1750 lbs.

The support for.these units was a 1/2-inch

sisal' rope which attached these units to two EFW line supports and a

SW line support.

A concern with the effects of this installation on

the operability of the SW and EFW system and nearby safety-related

components during a seismic event was immediately discussed with the

operations shift supervisor.

The shift supervisor immediately had

these units removed from the area and documented this in off-normal

occurrence 89-058 and NCN 3386.

.

- _ _ _ _ _ _ _ _ _ _ _ . _ _ _ _ . _ _ _ _ _ _ _ _ _

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5

Further investigation into this item revealed that these units had

been installed on June 1, 1989, to permit draining of the SG while the

plant was in Mode 5.

This installation was accomplished without a

MWR as required by the Station Housekeeping and plant Inspection

Program Procedure SAP 142, and Conduct of Maintenance Procedure

SAP-300.

The unit was restarted on June 11,-1989 with the units

still in place. This installation had been noted by plant management

and directions had been given to remove the units on or around June 20,

1989.

In this instance personnel were deficient in not performing this work

under the licensee MWR program.

No documentation to require

engineering review of this temporary installation was performed as

required by SAP 142. The above procedure was also inadequate in that

it did not insure that a seismic evaluation of the installation be

performed and that time limits were established to insure removal of

this hazard prior to plant start-up.

This is contrary to the

requirement of TS 6.8.1.a which requires that procedures be

established, implemented and maintained for activities referenced in

Appendix A of Regulatory Guide 1.33, Revision 2

February 1972.

This is 'a violation, " Failure to Control Temporary Installations,"

89-13-01.

The licensee has performed an evaluation which determined that a

seismic event could have resulted in the portable demineralized

becoming mobile and possibly damaging two FW line supports and

shearing off a test connection on a CCW line and a drain line'in the

SW system. The failure of the EFW supports would not have resulted in

the system becoming inoperable and the loss of flow in the SW and CCW

system would not have degraded system flow below the worst case

analyzed values.

The potential flooding from the lines were well

within the capacity of space dewatering equipment.

This analysis

determined that all systems would remain operable.

This event is similar to a licensee identified violation that was

documented in inspection report 89-03.

In that event temporary

scaffolding had been erected for shielding of RHR piping to reduce

personnel radiation exposure while the plant was in a refueling

outage.

Due to procedural deficiencies and personnel errors the

scaffolding was not removed prior to plant start-up.

That

installation had the potential to impact on system operability.

The licensee, in their response to this violation, should address

procedural changes made to insure that temporary installations are

controlled and that dates or mode restraints are established to

insure that temporary installations which are required while the

plant is shutdown are removed prior to unit start-up.

Violations cr deviations were identified.

- _ _ _ _ - - _ _ - - _ - _ _ - _ - _ _ _ _ - -

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6

5.

Action on Prev ous Inspection Findings (92701, 92702)

(Closed)

TI2513/94, Inspection for verification of licensee changes made

to comply with PWR moderator dilution requirements, multi-plant action

item 13-03.

The inspector reviewed inspection requirements specified.in

this instruction and reviewed the V. C. Summer Safety Evaluation Report and

supplements to determine what requirements had been established.

This

review identified that dilution events and- preventive measures were

discussed and resolved in section 15 of the SER and in supplements 1 and 3

to the SER.

However, multi-plant action item B-03 was not specifically

discussed.

Discussion with Mr. L. Kopp, the NRR lead contact for.this

item, indicates thut this item is not applicable for V. C. Summer.

The

SIMS open item list for V. C. Summer also does not list this item.

Further

discussion with Mr. Kopp revealed that since V.C. Summer was licensed in

1982, this issue would have been resolved in the normal licensing process

for V. C. Summer and all other plants licensed after 1979.

Based on the

above, this item is administratively closed.

6.

Other Areas

The inspectors-toured the licensee's lead dispatch center in Columbia, SC

on July 25, 1989.

Computer control and indication systems and procedures

that are used to operate' and control SCE&G's grid was discussed in detail.

This tour was very beneficial and provided the inspectors with a better

understanding of this tystem.

7.

ExitInterview(30703)

The inspection scope and findings were summarized on July 31, 1989, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed the inspection findings. The plant trip and

the resulting offsite power loss event which occurred on July 11, 1989, was

discussed in detail. This included the short term corrective measures and

the current investigation into root cause and long term corrective action.

The violation which resulted from the failure to control the temporary

installation of portable demineralizers in the intermediate building was

attributed to procedural inadequacies and a failure to follow procedures.

It was also noted that the violation was similar to LIV 89-03-01 when the

plant was restarted without removing scaffolding that contained temporary

shielding.

No dissenting comments were received from the licensee. The

licensee did not identify as proprietary any of the materials provided to

or reviewed by the inspectors during the inspection.

8.

Acronyms and Initialisms

CCW

Component Cooling Water

DG

Diesel Generator

,

l

EFW

Emergency Feedwater

FW

Feedwater

\\

L-

_ _ _ _ _ _ _ _ _ - _ _ _ _ - _ _ - _ - _ _ _

--_

,

L

'*

..- -

. ,

,

.-

7

o

L

I&C

Instrumentation and Control

MW

Megawatt.

- MWR

Maintenance Work Request

MVAR

Million Volt Amps Reactive

NCN

Non-Conformance Notice

i

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

PMTS

Preventive Maintenance Task Sheet

- QC

Quality Control

RHR

Residual Heat Removal

SAP

Station Administrative Procedure

SCE&G

South Carloina Electric & Gas Company

SER

Safety Evaluation Report

SG

Steam Generator

SIMS

Safety Issues Management Systems

STP

Surveillance Test Procedures

SW

Service Water

TS

Technical Specifications

,


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