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{{#Wiki_filter:1 Final Precursor Analysis Accident Sequence Precursor Program -- Office of Nuclear Regulatory Research Millstone Power Station (Unit 2)
{{#Wiki_filter:Final Precursor Analysis Accident Sequence Precursor Program -- Office of Nuclear Regulatory Research Millstone Power                 Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Station (Unit 2)                Loss of Instrument Air LER 336/06-002; Event Date 02/23/2006           IR 05000336/2006-02;                         CCDP = 8x10-6 IR 05000336/2006-05 April 11, 2007 Event Summary On February 23, 2006, with the plant in Mode 1 and 100% power, a manual reactor trip was initiated following an instrument air (IA) leak that occurred while replacing a pipe clamp on a two-inch copper IA header in the Turbine Building. An inadequately soldered joint failed on a 1/2-inch tee connection from a two-inch IA line that resulted in rapidly lowering Instrument Air pressure that caused the excess flow check valve to shut. Numerous air operated valves shifted to their loss-of-air position. Feedwater heater high-level dump valves opened causing a reduction of heater drain flow and a loss of suction pressure to the steam generator feed pumps (SGFP). Both SGFPs tripped and a manual reactor trip was initiated. Non-Vital 120V AC Regulated AC Panels VR11' and VR21' shifted to backup power supplies as expected due to the transfer of station power from the Normal Station Service Transformer (NSST) to the Reserve Station Service Transformer (RSST) following a reactor trip. The momentary loss of power to VR11' during this transfer resulted in a loss of letdown and indication of pressurizer power operated relief valves (PORV) and main steam safety valves (MSSV) position changes.
Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air Event Date 02/23/2006 LER 336/06-002; IR 05000336/2006-02;
Operators subsequently restored letdown and confirmed no actuation of either PORVs or MSSVs had occurred during the event.
 
Following the reactor trip, control element assembly position display system (CEAPDS) indicated CEA 7' was not fully inserted and the core mimic indicated CEA 44' was not fully inserted. Upon further review, it was confirmed that both CEA 7' and 44' had fully inserted and the indication anomalies were due to reed switch indication behavior. Additionally following the trip, the auxiliary feedwater (AFW) system was automatically actuated but the plant experienced an abnormal cool down to 526 o F in part due to excessive AFW flow to Steam Generator (SG) 1'. An operator was dispatched to take manual control of the regulating valve at which point RCS temperature was restored to the normal post-trip band of 530-535o F. It was subsequently determined that AFW Regulating Valve 1' was incorrectly set. This resulted in the Auxiliary Feed Regulating Valve 1' going to its failed position (i.e., full open). All other safety systems functioned as designed, and the plant was stabilized in Mode 3 at normal operating temperature and pressure.
IR 05000336/2006-05 CCDP= 8x10
-6 April 11, 2007 Event Summary On February 23, 2006, with the plant in Mode 1 and 100% power, a manual reactor trip was initiated following an instrument air (IA) leak that occurred while replacing a pipe clamp on a
 
two-inch copper IA header in the Turbine Building. An inadequately soldered joint failed on a 1/2-
 
inch tee connection from a two-inch IA line that resulted in rapidly lowering Instrument Air
 
pressure that caused the excess flow check valve to shut. Numerous air operated valves
 
shifted to their loss-of-air position. Feedwater heater high-level dump valves opened causing a
 
reduction of heater drain flow and a loss of suction pressure to the steam generator feed pumps (SGFP). Both SGFPs tripped and a manual reactor trip was initiated. Non-Vital 120V AC
 
Regulated AC Panels 'VR11' and 'VR21' shift ed to backup power supplies as expected due to the transfer of station power from the Normal Station Service Transformer (NSST) to the
 
Reserve Station Service Transformer (RSST) following a reactor trip. The momentary loss of
 
power to 'VR11' during this transfer resulted in a loss of letdown and indication of pressurizer
 
power operated relief valves (PORV) and main steam safety valves (MSSV) position changes.
Operators subsequently restored letdown and c onfirmed no actuation of either PORVs or MSSVs had occurred during the event.
Following the reactor trip, control element assembly position display system (CEAPDS) indicated CEA '7' was not fully inserted and the core mimic indicated CEA '44' was not fully
 
inserted. Upon further review, it was confirmed that both CEA '7' and '44' had fully inserted and
 
the indication anomalies were due to reed switch indication behavior. Additionally following the
 
trip, the auxiliary feedwater (AFW) system was automatically actuated but the plant experienced an abnormal cool down to 526 o F in part due to excessive AFW flow to Steam Generator (SG)
'1'. An operator was dispatched to take manual control of the regulating valve at which point
 
RCS temperature was restored to the normal post-trip band of 530-535 o F. It was subsequently determined that AFW Regulating Valve '1' was incorrectly set. This resulted in the Auxiliary
 
Feed Regulating Valve '1' going to its failed positi on (i.e., full open). All other safety systems functioned as designed, and the plant was stabilized in Mode 3 at normal operating temperature
 
and pressure.
More details of the event can be found in the References 1, 2, and 3.
More details of the event can be found in the References 1, 2, and 3.
Cause. The cause of this event was determined to be an already weakened solder joint which was disturbed while attempting to repair an incorrectly installed clamp, not designed for IA
Cause. The cause of this event was determined to be an already weakened solder joint which was disturbed while attempting to repair an incorrectly installed clamp, not designed for IA piping. This in turn, resulted in a 1/2-inch copper line separating from a tee connection causing a partial loss of IA in the Turbine Building.
 
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piping. This in turn, resulted in a 1/2-inch copper line separating from a tee connection causing a
 
partial loss of IA in the Turbine Building.
LER 336/06-002 2 Recovery opportunities.
Following the leakage of air from a two-inch instrument air line due to failure of an inadequately soldered joint, maintenance personnel quickly reconnected the air line
 
and applied a temporary wooden wedge to support the air line (see Reference 2). However, this recovery is not credited in the event assessment because: 1) numerous air operated valves already shifted to their loss-air-failure position; and 2) recovery of air to the secondary systems
 
in the turbine building, including condensate pumps, requires quite complicated manipulations
 
outside of the control room taking quite a long time.
Other concurrent or windowed events.
No other significant operating events existed at Millstone 2 according to the LER Search Database.Analysis Results Importance The conditional core damage probability (CCDP), for this event is 8x10-6. The results of an uncertainty assessment on the CCDP are summarized below.
CCDP5%Mean95%Millstone 2 1.2x10-7 7.6x10-6 3.3x10-5 The Accident Sequence Precursor Program acceptance threshold is a CCDP of 1x10
-6 or the CCDP equivalent of an uncomplicated reactor trip with a non-recoverable loss of secondary plant systems (e.g., feedwater and condensate). This CCDP equivalent for
 
Millstone 2 is 6x10
-6.Dominant Sequences The dominant core damage sequence for this event is Loss of Main Feedwater (LOMFW) Sequence 17. The events and important component failures for LOMFW
 
Sequence 17 shown in Figure 1 (Appendix A) include:  LOMFW initiating event,successful reactor trip,failure of steam generator cooling, and failure of once through cooling.Results TablesThe conditional probabilities for the dominant sequences are shown in Table 1.The event tree sequence logic for the dominant sequences is presented in Table 2a.Table 2b defines the nomenclature used in Table 2a.The most important cut sets for the dominant sequences are listed in Table 3. Definitions and probabilities for modified or dominant basic events are provided in Table 4.
LER 336/06-002 3 Modeling Assumptions Analysis Type The Revision 3-Plus (Change 3.21) of the Millstone 2 Standardized Plant Analysis Risk (SPAR) model (Reference 4) created in October 2005 was used for this assessment.


This event was modeled as an at-power in itiating event assessment for the manual reactor trip due to a trip of both main feedwater pumps following a loss of instrument air
LER 336/06-002 Recovery opportunities. Following the leakage of air from a two-inch instrument air line due to failure of an inadequately soldered joint, maintenance personnel quickly reconnected the air line and applied a temporary wooden wedge to support the air line (see Reference 2). However, this recovery is not credited in the event assessment because: 1) numerous air operated valves already shifted to their loss-air-failure position; and 2) recovery of air to the secondary systems in the turbine building, including condensate pumps, requires quite complicated manipulations outside of the control room taking quite a long time.
 
Other concurrent or windowed events. No other significant operating events existed at Millstone 2 according to the LER Search Database.
to the turbine building. Modeling Assumptions Summary The key modeling assumptions are listed below. These assumptions are important contributors to the overall risk.
Analysis Results C      Importance The conditional core damage probability (CCDP), for this event is 8x10-6. The results of an uncertainty assessment on the CCDP are summarized below.
-Recovery of condensate injection availability.
CCDP 5%          Mean          95%
At Millstone 2, a condensate pump can be used for injection to at least one SG when both main and auxiliary
Millstone 2              1.2x10-7    7.6x10-6      3.3x10-5 The Accident Sequence Precursor Program acceptance threshold is a CCDP of 1x10-6 or the CCDP equivalent of an uncomplicated reactor trip with a non-recoverable loss of secondary plant systems (e.g., feedwater and condensate). This CCDP equivalent for Millstone 2 is 6x10-6.
 
C      Dominant Sequences The dominant core damage sequence for this event is Loss of Main Feedwater (LOMFW) Sequence 17. The events and important component failures for LOMFW Sequence 17 shown in Figure 1 (Appendix A) include:
feedwater systems are not available to remove decay heat from the steam generators. However, the condensate system flow path for injection into the steam
        !      LOMFW initiating event,
 
        !      successful reactor trip,
generators was lost during the event as a result of loss of instrument air to the
        !      failure of steam generator cooling, and
 
        !      failure of once through cooling.
turbine building. For this analysis, it was assumed that the condensate system
C      Results Tables
 
        !      The conditional probabilities for the dominant sequences are shown in Table 1.
could not be recovered within the required time frame to be used for injection into
        !      The event tree sequence logic for the dominant sequences is presented in Table 2a.
 
        !      Table 2b defines the nomenclature used in Table 2a.
the SGs because: a)Numerous air operated valves already shifted to their loss-air-failure position which would lengthen and complicate the alignment of the
        !      The most important cut sets for the dominant sequences are listed in Table 3.
 
        !      Definitions and probabilities for modified or dominant basic events are provided in Table 4.
condensate pump SG injection flow path; andb)The time to initiate condensate system injection is relatively short and would need to be recovered before the operator initiates feed and bleed
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operation (i.e., within 1 or 2 hours).
-Impact of missing PORV indication on feed and bleed operation.
At Millstone 2, feed and bleed operation using high pressure injection and PORVs is required to
 
remove decay heat when secondary cooling is needed but fails. Reference 1
 
points out that the indication of PORV position changes was lost due to a
 
momentary loss of power to 120VAC Regulated AC panel 'VR11', although the
 
operators subsequently confirmed no actuation of PORVs had occurred during the
 
event. The loss of PORV position indications in the control room could have
 
adverse impact on the manual operation of feed and bleed. The SPAR model human error probability (HEP) for feed and bleed (HPI-XHE-XM-FAB) is estimated
 
at a value of 0.1 assuming the availability of the PORV position indicators. 


LER 336/06-002 Modeling Assumptions C  Analysis Type The Revision 3-Plus (Change 3.21) of the Millstone 2 Standardized Plant Analysis Risk (SPAR) model (Reference 4) created in October 2005 was used for this assessment.
This event was modeled as an at-power initiating event assessment for the manual reactor trip due to a trip of both main feedwater pumps following a loss of instrument air to the turbine building.
C  Modeling Assumptions Summary The key modeling assumptions are listed below. These assumptions are important contributors to the overall risk.
    -    Recovery of condensate injection availability. At Millstone 2, a condensate pump can be used for injection to at least one SG when both main and auxiliary feedwater systems are not available to remove decay heat from the steam generators. However, the condensate system flow path for injection into the steam generators was lost during the event as a result of loss of instrument air to the turbine building. For this analysis, it was assumed that the condensate system could not be recovered within the required time frame to be used for injection into the SGs because:
a)    Numerous air operated valves already shifted to their loss-air-failure position which would lengthen and complicate the alignment of the condensate pump SG injection flow path; and b)    The time to initiate condensate system injection is relatively short and would need to be recovered before the operator initiates feed and bleed operation (i.e., within 1 or 2 hours).
    -    Impact of missing PORV indication on feed and bleed operation. At Millstone 2, feed and bleed operation using high pressure injection and PORVs is required to remove decay heat when secondary cooling is needed but fails. Reference 1 points out that the indication of PORV position changes was lost due to a momentary loss of power to 120VAC Regulated AC panel VR11', although the operators subsequently confirmed no actuation of PORVs had occurred during the event. The loss of PORV position indications in the control room could have adverse impact on the manual operation of feed and bleed. The SPAR model human error probability (HEP) for feed and bleed (HPI-XHE-XM-FAB) is estimated at a value of 0.1 assuming the availability of the PORV position indicators.
However, operators can infer the position of PORVs by alternative indications (e.g.,
However, operators can infer the position of PORVs by alternative indications (e.g.,
temperature gauge downstream of the PORV block valves, integrity of the rupture
temperature gauge downstream of the PORV block valves, integrity of the rupture discs, etc.) and the PORV position indication was lost only temporarily. Therefore, the best-estimate event assessment was performed without any change to the HEP of 0.1 for feed and bleed operation despite the temporary loss of the PORV position indication.
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discs, etc.) and the PORV position indication was lost only temporarily. Therefore, the best-estimate event assessment was performed without any change to the
LER 336/06-002
    -    Potential RCS Overcooling due to failure of the AFW Regulating Valve.
Reference 1 indicates that SG AFW Regulating Valve 1' went to its failed position (i.e., full open) allowing excessive flow to the SG 1', which contributed to a greater than expected, cool down of the RCS. The RCS temperature was restored to the normal post-trip band by dispatching an operator to take manual control of the regulating valve. The AFW system fault tree has been modified to include manual control of AFW flow to SG 1'.
C    Fault Tree Modifications AFW System Fault Tree. The fault tree was modified to account for operators having to take manual control of AFW flow to SG 1'. Basic event, AFW-XHE-XM-CONTROL, was added under the AND Gate AFW-2 (see Figure 2). For the base case, this event was set to IGNORE.
C    Basic Event Changes
    -    AFW-XHE-XM-CONTROL. This HEP was set to 1.1x10-2 based on evaluation using the SPAR-H Method (Reference 5). It was assumed that diagnostic activities were needed for this event, but the performance shaping factors (PSF) for the diagnosis and action portions of HEP were set to their nominal values (i.e., set to 1).
    -    CDS-XHE-XM-ERROR. The HEP was set TRUE because the condensate system was assumed to be unavailable to provide injection into the SG. This determination was made due to the insufficient time operators would have to perform this action. See the Modeling Assumptions Summary for further details.
    -     IE-LOMFW. The initiating event frequency was set 1.0. All other initiating event frequencies were set to zero.
References
: 1. LER 336/06-002, Revision 00, Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air, Event Date: February 23, 2006.
: 2. NRC Inspection Report, Millstone Power Station - NRC Integrated Inspection Report 05000336/2006002 and 05000423/2006002, May 5, 2006.
: 3. NRC Inspection Report, Millstone Power Station - NRC Integrated Inspection Report 05000336/2006005 and 05000423/2006005, January 30, 2007.
: 4. Idaho National Engineering and Environmental Laboratory, Standardized Plant Analysis Risk Model for Millstone 2, Revision 3 Plus (Change 3.21), October 2005.
: 5. Idaho National Engineering and Environmental Laboratory, The SPAR-H Human Reliability Analysis Method, INEEL/EXT-02-01307, May 2004.
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HEP of 0.1 for feed and bleed operation despite the temporary loss of the PORV
LER 336/06-002 Table 1. Conditional core damage probabilities of dominating sequences.
 
Event tree      Sequence CCDP1            Contribution name              no.
position indication.
LOMFW              17                7.0E-6                  97.2 Total (all sequences)2                7.2E-6                  100
LER 336/06-002 4 -Potential RCS Overcooling due to failure of the AFW Regulating Valve.
: 1. Values are point estimates.
Reference 1 indicates that SG AFW Regulating Valve '1' went to its failed position (i.e., full open) allowing excessive flow to the SG '1', which contributed to a greater
: 2. Total CCDP includes all sequences (including those not shown in this table).
 
Table 2a. Event tree sequence logic for dominating sequences.
than expected, cool down of the RCS. The RCS temperature was restored to the
Event tree      Sequence                                        Logic name              no.          (/ denotes success; see Table 2b for top event names)
 
LOMFW              17          /RT, SGC, OTC Table 2b. Definitions of top events listed in Table 2a.
normal post-trip band by dispatching an operator to take manual control of the
Top Event        Definition RT            REACTOR TRIP SGC            SECONDARY SIDE COOLDOWN OTC            ONCE THROUGH COOLING Table 3. Conditional cut sets for the dominant sequences.
 
Percent CCDP                                                      Minimum Cut Sets (of basic events)
regulating valve. The AFW system fault tree has been modified to include manual
Contribution Event Tree: LOMFW, Sequence 17 3.4E-006              48.21          AFW-FCV-CF-AB                  HPI-XHE-XM-FAB 9.0E-007              12.96          AFW-AOV-CC-FW43B              AFW-XHE-XM-CONTROL     HPI-XHE-XM-FAB 2.8E-007              3.97          AFW-CKV-CF-SGS                HPI-XHE-XM-FAB 2.4E-007                3.46          AFW-TNK-FC-CST                HPI-XHE-XM-FAB 1.7E-007              2.41          AFW-FCV-CF-AB                HPI-MDP-TM-1A 1.7E-007              2.41          AFW-FCV-CF-AB                HPI-MDP-TM-1C 5.8E-006              100          Total (all cutsets)1
 
: 1. Total CCDP includes all cutsets (including those not shown in this table).
control of AFW flow to SG '1'. Fault Tree Modifications AFW System Fault Tree.
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The fault tree was modified to account for operators having totake manual control of AFW flow to SG '1'. Basic event, AFW-XHE-XM-CONTROL, was
 
added under the 'AND' Gate AFW-2 (see Figure 2). For the base case, this event was
 
set to IGNORE. Basic Event Changes
-AFW-XHE-XM-CONTROL
. This HEP was set to 1.1x10
-2 based on evaluation using the SPAR-H Method (Reference 5). It was assumed that diagnostic activities
 
were needed for this event, but the performance shaping factors (PSF) for the


diagnosis and action portions of HEP were set to their nominal values (i.e., set to
LER 336/06-002 Table 4. Definitions and probabilities for modified and dominant basic events.
Probability/
Frequency Event Name                                            Description                            Modified (per year)
AFW-AOV-CC-FW43B                DISCHARGE TO SG1 AOV 2-FW-43B FAILS                      9.0E-004      No AFW-CKV-CF-SGS                  CCF OF STEAM GENERATOR CHECK VALVES                      2.8E-006      No COMMON CAUSE FAILURE OF FLOW CONTROL AFW-FCV-CF-AB                                                                            3.4E-005      No VALVES AFW-TNK-FC-CST                  AFW CONDENSATE STORAGE TANK FAILURES                      2.4E-006      No OPERATORS FAIL TO MANUALLY CONTROL LEVEL OF AFW-XHE-XM-CONTROL                                                                        1.0E-002    Yes SG 1 OPERATORS FAIL TO ALIGN CONDENSATE FOR CDS-XHE-XM-ERROR                                                                          TRUE        Yes DECAY HEAT REMOVAL HPI-MDP-TM-1A                  HPI MDP-P41A UNAVAILABLE DUE TO T & M                    5.0E-003      No HPI-MDP-TM-1C                  HPI MDP-P41C UNAVAILABLE DUE TO T & M                    5.0E-003      No OPERATOR FAILS TO INITIATE FEED AND BLEED HPI-XHE-XM-FAB                                                                            1.0E-001      No COOLING IE-LOMFW                        LOSS OF MAIN FEEDWATER INITIATING EVENT                      1.0      Yes1
: 1. Set the IE frequency to 1.0. All other initiating event frequencies were set to zero.
6


1).-CDS-XHE-XM-ERROR
LER 336/06-002 Appendix A Event Tree and Fault Tree Figures 7
. The HEP was set TRUE because the condensate system was assumed to be unavailable to provide injection into the SG. This


determination was made due to the insufficient time operators would have to
LER 336/06-002 LOSS OF  REACTOR    STEAM    PORVs  RCP SEAL    HIGH    ONCE  SECONDARY SHUTDOWN    SUMP  CONTAINMENT FEEDWATER    TRIP  GENERATOR    ARE    INTEGRITY PRESSURE  THROUGH    SIDE    COOLING  RECIRC  COOLING TRANSIENTS          COOLING  CLOSED  MAINTAINED INJECTION COOLING COOLDOWN IE-LOMFW    RT       SGC     PORV      RCPSL      HPI    OTC     SSC      SDC      HPR      CSR        #    ENDSTATE 1    OK 2     OK 3    CD 4    CD 5    CD 6     OK 7     OK 8     CD 9     CD 10    OK 11    CD 12    CD 13    CD 14    OK 15    CD 16    CD 17    CD 18 T  ATWS Figure 1. Millstone 2 Loss of Main Feedwater Event Tree (with dominant sequence highlighted).
 
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perform this action. See the Modeling Assumptions Summary for further details.
-IE-LOMFW. The initiating event frequency was set 1.0. All other initiating event frequencies were set to zero.
References 1.LER 336/06-002, Revision 00, "Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air," Event Date: February 23, 2006. 2.NRC Inspection Report, "Millstone Power Station - NRC Integrated Inspection Report 05000336/2006002 and 05000423/2006002," May 5, 2006.3.NRC Inspection Report, "Millstone Power Station - NRC Integrated Inspection Report 05000336/2006005 and 05000423/2006005," January 30, 2007.4.Idaho National Engineering and Environmental Laboratory, "Standardized Plant Analysis Risk Model for Millstone 2," Revision 3 Plus (Change 3.21), October 2005.5.Idaho National Engineering and Environmental Laboratory, "The SPAR-H HumanReliability Analysis Method," INEEL/EXT-02-01307, May 2004.
LER 336/06-002 5 Table 1.
Conditional core damage probabilities of dominating sequences.Event treenameSequence no.CCDP 1 ContributionLOMFW177.0E-697.2Total (all sequences) 27.2E-6100 1. Values are point estimates.
: 2. Total CCDP includes all sequences (including those not shown in this table).
Table 2a.
Event tree sequence logic for dominating sequences
.Event treenameSequence no.Logic ("/" denotes success; see Table 2b for top event names)LOMFW17/RT, SGC, OTC Table 2b.
Definitions of top events listed in Table 2a. Top EventDefinitionRTREACTOR TRIPSGCSECONDARY SIDE COOLDOWNOTCONCE THROUGH COOLING Table 3.
Conditional cut sets for the dominant sequences.
CCDPPercent Contribution Minimum Cut Sets (of basic events)Event Tree: LOMFW, Sequence 173.4E-006 48.21AFW-FCV-CF-ABHPI-XHE-XM-FAB9.0E-007 12.96AFW-AOV-CC-FW43BAFW-XHE-XM-CONTROLHPI-XHE-XM-FAB 2.8E-007 3.97AFW-CKV-CF-SGSHPI-XHE-XM-FAB2.4E-007      3.46     AFW-TNK-FC-CSTHPI-XHE-XM-FAB1.7E-007     2.41     AFW-FCV-CF-AB            HPI-MDP-TM-1A 1.7E-007     2.41     AFW-FCV-CF-AB            HPI-MDP-TM-1C5.8E-006100Total (all cutsets) 1 1. Total CCDP includes all cutsets (including those not shown in this table).
LER 336/06-002 6 Table 4.
Definitions and probabilities for m odified and dominant basic events.Event NameDescriptionProbability/ Frequency(per year)Modified AFW-AOV-CC-FW43BDISCHARGE TO SG1 AOV 2-FW-43B FAILS9.0E-004NoAFW-CKV-CF-SGSCCF OF STEAM GENERATOR CHECK VALVES2.8E-006No AFW-FCV-CF-ABCOMMON CAUSE FAILURE OF FLOW CONTROL VALVES3.4E-005NoAFW-TNK-FC-CSTAFW CONDENSATE STORAGE TANK FAILURES2.4E-006NoAFW-XHE-XM-CONTROLOPERATORS FAIL TO MANUALLY CONTROL LEVEL OF SG 11.0E-002Yes CDS-XHE-XM-ERROROPERATORS FAIL TO ALIGN CONDENSATE FORDECAY HEAT REMOVALTRUEYesHPI-MDP-TM-1AHPI MDP-P41A UNAVAILABLE DUE TO T & M5.0E-003NoHPI-MDP-TM-1CHPI MDP-P41C UNAVAILABLE DUE TO T & M5.0E-003NoHPI-XHE-XM-FABOPERATOR FAILS TO INITIATE FEED AND BLEED COOLING1.0E-001NoIE-LOMFWLOSS OF MAIN FEEDWATER INITIATING EVENT1.0Yes
: 11. Set the IE frequency to 1.0. All other initiating event frequencies were set to zero.
LER 336/06-002 7 Appendix A Event Tree and Fault Tree Figures


LER 336/06-002 8CSRCONTAINMENTCOOLINGHPRSUMPRECIRCSDCSHUTDOWNCOOLING SSCSECONDARYSIDECOOLDOWNOTCONCETHROUGHCOOLINGHPIHIGHPRESSUREINJECTIONRCPSLRCP SEALINTEGRITYMAINTAINEDPORVPORVsARECLOSEDSGCSTEAMGENERATORCOOLING RTREACTORTRIPIE-LOMFWLOSS OF FEEDWATER TRANSIENTS
LER 336/06-002 NO OR INSUFFICIENT AFW FLOW AFW CCF OF STEAM                        COMMON CAUSE                          AFW CONDENSATE                    AFW PUMP TRAIN GENERATOR CHECK                        FAILURE OF FLOW                          STORAGE TANK                        FAILURES VALVES                          CONTROL VALVES                            FAILURES 2.760E-6                              3.348E-5                              2.400E-6 AFW-CKV-CF-SGS                        AFW-FCV-CF-AB                          AFW-TNK-FC-CST                          AFW-1 NO AFW FLOW                                                                                                        NO AFW FLOW TO STEAM GENERATOR                                                                                                TO STEAM GENERATOR SG1                                                                                                              SG2 AFW-2                                                                                                            AFW-3 DISCHARGE TO                        DISCHARGE TO                          OPERATORS FAIL TO                    NO FLOW FROM                  DISCHARGE TO                DISCHARGE PATH SG1 AOV 2-FW-43A                    SG1 AIR ASSISTED                      MANUALLY CONTROL                    PUMP TRAINS TO                SG1 AOV 2-FW-43B            TO SG2 FAILURES CHECK VALVE 2-FW-12A                        SG 1 LEVEL                            SG1 9.000E-4                              1.000E-4                                IGNORE                                                          9.000E-4                    1.000E-4 AFW-AOV-CC-FW43A                    AFW-CKV-CC-FW12A                    AFW-XHE-XM-CONTROL                          AFW-4                    AFW-AOV-CC-FW43B            AFW-CKV-CC-FW12B Figure 2. Modified Millstone 2 AFW Fault Tree (with added basic event circled).
#  ENDSTATE1  OK2  OK3  CD4  CD5  CD6  OK7  OK8  CD9  CD10  OK11  CD 12  CD13  CD14  OK15  CD16  CD17  CD18T  ATWSFigure 1. Millstone 2 Loss of Main Feedwater Event Tree (with dominant sequence highlighted).
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LER 336/06-002 9AFW2.760E-6AFW-CKV-CF-SGS3.348E-5AFW-FCV-CF-AB2.400E-6AFW-TNK-FC-CSTAFW-1AFW-29.000E-4AFW-AOV-CC-FW43A1.000E-4AFW-CKV-CC-FW12AIGNOREAFW-XHE-XM-CONTROLAFW-4AFW-39.000E-4AFW-AOV-CC-FW43B1.000E-4AFW-CKV-CC-FW12BNO AFW FLOWTO STEAM GENERATORSG1CCF OF STEAMGENERATOR CHECKVALVESNO OR INSUFFICIENTAFW FLOWCOMMON CAUSEFAILURE OF FLOWCONTROL VALVESAFW PUMP TRAINFAILURESDISCHARGE TOSG1 AOV 2-FW-43ADISCHARGE TOSG1 AIR ASSISTEDCHECK VALVE 2-FW-12AOPERATORS FAIL TOMANUALLY CONTROLSG 1 LEVELNO FLOW FROMPUMP TRAINS TOSG1DISCHARGE TOSG1 AOV 2-FW-43BNO AFW FLOWTO STEAM GENERATORSG2DISCHARGE PATHTO SG2 FAILURESAFW CONDENSATESTORAGE TANKFAILURESFigure 2. Modified Millstone 2 AFW Fault Tree (with added basic event circled).}}

Latest revision as of 18:34, 22 March 2020

Final ASP Analysis- Millstone (LER 336/06-002)
ML071930281
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Issue date: 04/11/2007
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Sanders, Carleen, NRR/DORL 415-1603
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References
IR-06-002, IR-06-005, LER 06-002-00
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Final Precursor Analysis Accident Sequence Precursor Program -- Office of Nuclear Regulatory Research Millstone Power Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Station (Unit 2) Loss of Instrument Air LER 336/06-002; Event Date 02/23/2006 IR 05000336/2006-02; CCDP = 8x10-6 IR 05000336/2006-05 April 11, 2007 Event Summary On February 23, 2006, with the plant in Mode 1 and 100% power, a manual reactor trip was initiated following an instrument air (IA) leak that occurred while replacing a pipe clamp on a two-inch copper IA header in the Turbine Building. An inadequately soldered joint failed on a 1/2-inch tee connection from a two-inch IA line that resulted in rapidly lowering Instrument Air pressure that caused the excess flow check valve to shut. Numerous air operated valves shifted to their loss-of-air position. Feedwater heater high-level dump valves opened causing a reduction of heater drain flow and a loss of suction pressure to the steam generator feed pumps (SGFP). Both SGFPs tripped and a manual reactor trip was initiated. Non-Vital 120V AC Regulated AC Panels VR11' and VR21' shifted to backup power supplies as expected due to the transfer of station power from the Normal Station Service Transformer (NSST) to the Reserve Station Service Transformer (RSST) following a reactor trip. The momentary loss of power to VR11' during this transfer resulted in a loss of letdown and indication of pressurizer power operated relief valves (PORV) and main steam safety valves (MSSV) position changes.

Operators subsequently restored letdown and confirmed no actuation of either PORVs or MSSVs had occurred during the event.

Following the reactor trip, control element assembly position display system (CEAPDS) indicated CEA 7' was not fully inserted and the core mimic indicated CEA 44' was not fully inserted. Upon further review, it was confirmed that both CEA 7' and 44' had fully inserted and the indication anomalies were due to reed switch indication behavior. Additionally following the trip, the auxiliary feedwater (AFW) system was automatically actuated but the plant experienced an abnormal cool down to 526 o F in part due to excessive AFW flow to Steam Generator (SG) 1'. An operator was dispatched to take manual control of the regulating valve at which point RCS temperature was restored to the normal post-trip band of 530-535o F. It was subsequently determined that AFW Regulating Valve 1' was incorrectly set. This resulted in the Auxiliary Feed Regulating Valve 1' going to its failed position (i.e., full open). All other safety systems functioned as designed, and the plant was stabilized in Mode 3 at normal operating temperature and pressure.

More details of the event can be found in the References 1, 2, and 3.

Cause. The cause of this event was determined to be an already weakened solder joint which was disturbed while attempting to repair an incorrectly installed clamp, not designed for IA piping. This in turn, resulted in a 1/2-inch copper line separating from a tee connection causing a partial loss of IA in the Turbine Building.

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LER 336/06-002 Recovery opportunities. Following the leakage of air from a two-inch instrument air line due to failure of an inadequately soldered joint, maintenance personnel quickly reconnected the air line and applied a temporary wooden wedge to support the air line (see Reference 2). However, this recovery is not credited in the event assessment because: 1) numerous air operated valves already shifted to their loss-air-failure position; and 2) recovery of air to the secondary systems in the turbine building, including condensate pumps, requires quite complicated manipulations outside of the control room taking quite a long time.

Other concurrent or windowed events. No other significant operating events existed at Millstone 2 according to the LER Search Database.

Analysis Results C Importance The conditional core damage probability (CCDP), for this event is 8x10-6. The results of an uncertainty assessment on the CCDP are summarized below.

CCDP 5% Mean 95%

Millstone 2 1.2x10-7 7.6x10-6 3.3x10-5 The Accident Sequence Precursor Program acceptance threshold is a CCDP of 1x10-6 or the CCDP equivalent of an uncomplicated reactor trip with a non-recoverable loss of secondary plant systems (e.g., feedwater and condensate). This CCDP equivalent for Millstone 2 is 6x10-6.

C Dominant Sequences The dominant core damage sequence for this event is Loss of Main Feedwater (LOMFW) Sequence 17. The events and important component failures for LOMFW Sequence 17 shown in Figure 1 (Appendix A) include:

! LOMFW initiating event,

! successful reactor trip,

! failure of steam generator cooling, and

! failure of once through cooling.

C Results Tables

! The conditional probabilities for the dominant sequences are shown in Table 1.

! The event tree sequence logic for the dominant sequences is presented in Table 2a.

! Table 2b defines the nomenclature used in Table 2a.

! The most important cut sets for the dominant sequences are listed in Table 3.

! Definitions and probabilities for modified or dominant basic events are provided in Table 4.

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LER 336/06-002 Modeling Assumptions C Analysis Type The Revision 3-Plus (Change 3.21) of the Millstone 2 Standardized Plant Analysis Risk (SPAR) model (Reference 4) created in October 2005 was used for this assessment.

This event was modeled as an at-power initiating event assessment for the manual reactor trip due to a trip of both main feedwater pumps following a loss of instrument air to the turbine building.

C Modeling Assumptions Summary The key modeling assumptions are listed below. These assumptions are important contributors to the overall risk.

- Recovery of condensate injection availability. At Millstone 2, a condensate pump can be used for injection to at least one SG when both main and auxiliary feedwater systems are not available to remove decay heat from the steam generators. However, the condensate system flow path for injection into the steam generators was lost during the event as a result of loss of instrument air to the turbine building. For this analysis, it was assumed that the condensate system could not be recovered within the required time frame to be used for injection into the SGs because:

a) Numerous air operated valves already shifted to their loss-air-failure position which would lengthen and complicate the alignment of the condensate pump SG injection flow path; and b) The time to initiate condensate system injection is relatively short and would need to be recovered before the operator initiates feed and bleed operation (i.e., within 1 or 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />).

- Impact of missing PORV indication on feed and bleed operation. At Millstone 2, feed and bleed operation using high pressure injection and PORVs is required to remove decay heat when secondary cooling is needed but fails. Reference 1 points out that the indication of PORV position changes was lost due to a momentary loss of power to 120VAC Regulated AC panel VR11', although the operators subsequently confirmed no actuation of PORVs had occurred during the event. The loss of PORV position indications in the control room could have adverse impact on the manual operation of feed and bleed. The SPAR model human error probability (HEP) for feed and bleed (HPI-XHE-XM-FAB) is estimated at a value of 0.1 assuming the availability of the PORV position indicators.

However, operators can infer the position of PORVs by alternative indications (e.g.,

temperature gauge downstream of the PORV block valves, integrity of the rupture discs, etc.) and the PORV position indication was lost only temporarily. Therefore, the best-estimate event assessment was performed without any change to the HEP of 0.1 for feed and bleed operation despite the temporary loss of the PORV position indication.

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LER 336/06-002

- Potential RCS Overcooling due to failure of the AFW Regulating Valve.

Reference 1 indicates that SG AFW Regulating Valve 1' went to its failed position (i.e., full open) allowing excessive flow to the SG 1', which contributed to a greater than expected, cool down of the RCS. The RCS temperature was restored to the normal post-trip band by dispatching an operator to take manual control of the regulating valve. The AFW system fault tree has been modified to include manual control of AFW flow to SG 1'.

C Fault Tree Modifications AFW System Fault Tree. The fault tree was modified to account for operators having to take manual control of AFW flow to SG 1'. Basic event, AFW-XHE-XM-CONTROL, was added under the AND Gate AFW-2 (see Figure 2). For the base case, this event was set to IGNORE.

C Basic Event Changes

- AFW-XHE-XM-CONTROL. This HEP was set to 1.1x10-2 based on evaluation using the SPAR-H Method (Reference 5). It was assumed that diagnostic activities were needed for this event, but the performance shaping factors (PSF) for the diagnosis and action portions of HEP were set to their nominal values (i.e., set to 1).

- CDS-XHE-XM-ERROR. The HEP was set TRUE because the condensate system was assumed to be unavailable to provide injection into the SG. This determination was made due to the insufficient time operators would have to perform this action. See the Modeling Assumptions Summary for further details.

- IE-LOMFW. The initiating event frequency was set 1.0. All other initiating event frequencies were set to zero.

References

1. LER 336/06-002, Revision 00, Manual Reactor Trip Due to Trip of Both Feed Pumps Following a Loss of Instrument Air, Event Date: February 23, 2006.
2. NRC Inspection Report, Millstone Power Station - NRC Integrated Inspection Report 05000336/2006002 and 05000423/2006002, May 5, 2006.
3. NRC Inspection Report, Millstone Power Station - NRC Integrated Inspection Report 05000336/2006005 and 05000423/2006005, January 30, 2007.
4. Idaho National Engineering and Environmental Laboratory, Standardized Plant Analysis Risk Model for Millstone 2, Revision 3 Plus (Change 3.21), October 2005.
5. Idaho National Engineering and Environmental Laboratory, The SPAR-H Human Reliability Analysis Method, INEEL/EXT-02-01307, May 2004.

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LER 336/06-002 Table 1. Conditional core damage probabilities of dominating sequences.

Event tree Sequence CCDP1 Contribution name no.

LOMFW 17 7.0E-6 97.2 Total (all sequences)2 7.2E-6 100

1. Values are point estimates.
2. Total CCDP includes all sequences (including those not shown in this table).

Table 2a. Event tree sequence logic for dominating sequences.

Event tree Sequence Logic name no. (/ denotes success; see Table 2b for top event names)

LOMFW 17 /RT, SGC, OTC Table 2b. Definitions of top events listed in Table 2a.

Top Event Definition RT REACTOR TRIP SGC SECONDARY SIDE COOLDOWN OTC ONCE THROUGH COOLING Table 3. Conditional cut sets for the dominant sequences.

Percent CCDP Minimum Cut Sets (of basic events)

Contribution Event Tree: LOMFW, Sequence 17 3.4E-006 48.21 AFW-FCV-CF-AB HPI-XHE-XM-FAB 9.0E-007 12.96 AFW-AOV-CC-FW43B AFW-XHE-XM-CONTROL HPI-XHE-XM-FAB 2.8E-007 3.97 AFW-CKV-CF-SGS HPI-XHE-XM-FAB 2.4E-007 3.46 AFW-TNK-FC-CST HPI-XHE-XM-FAB 1.7E-007 2.41 AFW-FCV-CF-AB HPI-MDP-TM-1A 1.7E-007 2.41 AFW-FCV-CF-AB HPI-MDP-TM-1C 5.8E-006 100 Total (all cutsets)1

1. Total CCDP includes all cutsets (including those not shown in this table).

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LER 336/06-002 Table 4. Definitions and probabilities for modified and dominant basic events.

Probability/

Frequency Event Name Description Modified (per year)

AFW-AOV-CC-FW43B DISCHARGE TO SG1 AOV 2-FW-43B FAILS 9.0E-004 No AFW-CKV-CF-SGS CCF OF STEAM GENERATOR CHECK VALVES 2.8E-006 No COMMON CAUSE FAILURE OF FLOW CONTROL AFW-FCV-CF-AB 3.4E-005 No VALVES AFW-TNK-FC-CST AFW CONDENSATE STORAGE TANK FAILURES 2.4E-006 No OPERATORS FAIL TO MANUALLY CONTROL LEVEL OF AFW-XHE-XM-CONTROL 1.0E-002 Yes SG 1 OPERATORS FAIL TO ALIGN CONDENSATE FOR CDS-XHE-XM-ERROR TRUE Yes DECAY HEAT REMOVAL HPI-MDP-TM-1A HPI MDP-P41A UNAVAILABLE DUE TO T & M 5.0E-003 No HPI-MDP-TM-1C HPI MDP-P41C UNAVAILABLE DUE TO T & M 5.0E-003 No OPERATOR FAILS TO INITIATE FEED AND BLEED HPI-XHE-XM-FAB 1.0E-001 No COOLING IE-LOMFW LOSS OF MAIN FEEDWATER INITIATING EVENT 1.0 Yes1

1. Set the IE frequency to 1.0. All other initiating event frequencies were set to zero.

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LER 336/06-002 Appendix A Event Tree and Fault Tree Figures 7

LER 336/06-002 LOSS OF REACTOR STEAM PORVs RCP SEAL HIGH ONCE SECONDARY SHUTDOWN SUMP CONTAINMENT FEEDWATER TRIP GENERATOR ARE INTEGRITY PRESSURE THROUGH SIDE COOLING RECIRC COOLING TRANSIENTS COOLING CLOSED MAINTAINED INJECTION COOLING COOLDOWN IE-LOMFW RT SGC PORV RCPSL HPI OTC SSC SDC HPR CSR # ENDSTATE 1 OK 2 OK 3 CD 4 CD 5 CD 6 OK 7 OK 8 CD 9 CD 10 OK 11 CD 12 CD 13 CD 14 OK 15 CD 16 CD 17 CD 18 T ATWS Figure 1. Millstone 2 Loss of Main Feedwater Event Tree (with dominant sequence highlighted).

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LER 336/06-002 NO OR INSUFFICIENT AFW FLOW AFW CCF OF STEAM COMMON CAUSE AFW CONDENSATE AFW PUMP TRAIN GENERATOR CHECK FAILURE OF FLOW STORAGE TANK FAILURES VALVES CONTROL VALVES FAILURES 2.760E-6 3.348E-5 2.400E-6 AFW-CKV-CF-SGS AFW-FCV-CF-AB AFW-TNK-FC-CST AFW-1 NO AFW FLOW NO AFW FLOW TO STEAM GENERATOR TO STEAM GENERATOR SG1 SG2 AFW-2 AFW-3 DISCHARGE TO DISCHARGE TO OPERATORS FAIL TO NO FLOW FROM DISCHARGE TO DISCHARGE PATH SG1 AOV 2-FW-43A SG1 AIR ASSISTED MANUALLY CONTROL PUMP TRAINS TO SG1 AOV 2-FW-43B TO SG2 FAILURES CHECK VALVE 2-FW-12A SG 1 LEVEL SG1 9.000E-4 1.000E-4 IGNORE 9.000E-4 1.000E-4 AFW-AOV-CC-FW43A AFW-CKV-CC-FW12A AFW-XHE-XM-CONTROL AFW-4 AFW-AOV-CC-FW43B AFW-CKV-CC-FW12B Figure 2. Modified Millstone 2 AFW Fault Tree (with added basic event circled).

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