ML101550570: Difference between revisions

From kanterella
Jump to navigation Jump to search
(Created page by program invented by StriderTol)
 
(Created page by program invented by StriderTol)
 
Line 16: Line 16:


=Text=
=Text=
{{#Wiki_filter:Power Reactor IEvent Number: 45299 Facility:
{{#Wiki_filter:Power Reactor                                               IEvent Number: 45299 Facility: OYSTER CREEK                                       Notification Date: 08/25/2009 Region: 1 State: NJ                                           Notification Time: 21:15 [ET]
OYSTER CREEK Notification Date: 08/25/2009 Region: 1 State: NJ Notification Time: 21:15 [ET]Unit: [1] [ ] [ ] Event Date: 08/25/2009 RX Type: [1] GE-2 Event Time: 19:35 [EDT]NRC Notified By: JOSHUA SISAK Last Update Date: 08/26/2009 HQ OPS Officer: VINCE KLCO Emergency Class: NON EMERGENCY Person (Organization):
Unit: [1] [ ] [ ]                                             Event Date: 08/25/2009 RX Type: [1] GE-2                                             Event Time: 19:35 [EDT]
10 CFR Section: JOHN WHITE (RIDO)50.72(b)(2)(xi)  
NRC Notified By: JOSHUA SISAK                                 Last Update Date: 08/26/2009 HQ OPS Officer: VINCE KLCO Emergency Class: NON EMERGENCY                               Person (Organization):
-OFFSITE NOTIFICATION SCRAM Initial Current Unit Code RX CRIT PWR Initial RX Mode PWR Current RX Mode 1 N Y 100 Power Operation 1001 Power Qperation Event Text OFFSITE NOTIFICATION DUE TO A WATER LEAK CONTAINING TRITIUM"Oyster Creek Nuclear Generating Station notified the New Jersey Department of Environmental Protection of a leak of water containing tritium from an underground condensate transfer pipe at the turbine building penetration of less than 20 gpm and concentration of approximately 10 million picocuries/milliliter.
10 CFR Section:                                               JOHN WHITE (RIDO) 50.72(b)(2)(xi) - OFFSITE NOTIFICATION SCRAM                   Initial                             Current Unit     Code     RX CRIT       PWR         Initial RX Mode         PWR       Current RX Mode 1         N         Y             100     Power Operation             1001     Power Qperation Event Text OFFSITE NOTIFICATION DUE TO A WATER LEAK CONTAINING TRITIUM "Oyster Creek Nuclear Generating Station notified the New Jersey Department of Environmental Protection of a leak of water containing tritium from an underground condensate transfer pipe at the turbine building penetration of less than 20 gpm and concentration of approximately 10 million picocuries/milliliter.                                                                       N.
N ."The leaking water is being pumped to storage drums and a plan is being developed to replace the six-inch condensate transfer piping which penetrates the turbine building inside a 42 Inch long sixteen inch diameter penetration sleeve. Previously, water was observed coming from the sleeve into the turbine building where it was draining to a sump. The leak coming out of the turbine building was uncovered during excavation to determine if the condensate was leaking to the soil." The licensee notified the NRC Resident Inspector.
"The leaking water is being pumped to storage drums and a plan is being developed to replace the six-inch condensate transfer piping which penetrates the turbine building inside a 42 Inch long sixteen inch diameter penetration sleeve. Previously, water was observed coming from the sleeve into the turbine building where it was draining to a sump. The leak coming out of the turbine building was uncovered during excavation to determine if the condensate was leaking to the soil."
The licensee notified the NRC Resident Inspector.
* *
* *
* UPDATE PROVIDED BY CALVIN TAYLOR TO JASON KOZAL AT 0907 ON 08/26/09 ***The licensee corrected the reported concentration to 10 million picocuries/liter.
* UPDATE PROVIDED BY CALVIN TAYLOR TO JASON KOZAL AT 0907 ON 08/26/09 ***
Additionally, after closer examination the leak rate was determined to be approximately 5 GPM vice the initially reported less than 20 GPM.The licensee will be issuing a press release.Notified the RIDO (White).}}
The licensee corrected the reported concentration to 10 million picocuries/liter.
Additionally, after closer examination the leak rate was determined to be approximately 5 GPM vice the initially reported less than 20 GPM.
The licensee will be issuing a press release.
Notified the RIDO (White).}}

Latest revision as of 18:28, 13 November 2019

Event Notification for Oyster Creek on Offsite Notification Due to a Water Leak Containing Tritium
ML101550570
Person / Time
Site: Oyster Creek
Issue date: 08/26/2009
From: Sisak J
AmerGen Energy Co
To:
NRC Region 1
References
Event 45299, FOIA/PA-2010-0209
Download: ML101550570 (1)


Text

Power Reactor IEvent Number: 45299 Facility: OYSTER CREEK Notification Date: 08/25/2009 Region: 1 State: NJ Notification Time: 21:15 [ET]

Unit: [1] [ ] [ ] Event Date: 08/25/2009 RX Type: [1] GE-2 Event Time: 19:35 [EDT]

NRC Notified By: JOSHUA SISAK Last Update Date: 08/26/2009 HQ OPS Officer: VINCE KLCO Emergency Class: NON EMERGENCY Person (Organization):

10 CFR Section: JOHN WHITE (RIDO) 50.72(b)(2)(xi) - OFFSITE NOTIFICATION SCRAM Initial Current Unit Code RX CRIT PWR Initial RX Mode PWR Current RX Mode 1 N Y 100 Power Operation 1001 Power Qperation Event Text OFFSITE NOTIFICATION DUE TO A WATER LEAK CONTAINING TRITIUM "Oyster Creek Nuclear Generating Station notified the New Jersey Department of Environmental Protection of a leak of water containing tritium from an underground condensate transfer pipe at the turbine building penetration of less than 20 gpm and concentration of approximately 10 million picocuries/milliliter. N.

"The leaking water is being pumped to storage drums and a plan is being developed to replace the six-inch condensate transfer piping which penetrates the turbine building inside a 42 Inch long sixteen inch diameter penetration sleeve. Previously, water was observed coming from the sleeve into the turbine building where it was draining to a sump. The leak coming out of the turbine building was uncovered during excavation to determine if the condensate was leaking to the soil."

The licensee notified the NRC Resident Inspector.

  • *
  • UPDATE PROVIDED BY CALVIN TAYLOR TO JASON KOZAL AT 0907 ON 08/26/09 ***

The licensee corrected the reported concentration to 10 million picocuries/liter.

Additionally, after closer examination the leak rate was determined to be approximately 5 GPM vice the initially reported less than 20 GPM.

The licensee will be issuing a press release.

Notified the RIDO (White).