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At 0329 CST on 11/29/2011, Unit 2 experienAt 0329 CST on 11/29/2011, Unit 2 experienced an automatic Reactor Trip while the plant was stable at 100% power in Mode 1. All systems actuated as designed. The reactor trip was caused by Generator Lockout.</br>All ESF systems actuated as designed. The following systems actuated: Auxiliary Feedwater (AFW) and Feedwater Isolation.</br>All control rods fully inserted. Steam Dump system valve FV 7485 failed open and was manually isolated. This caused a letdown isolation that was restored. No primary/secondary relief valves lifted. There were no electrical bus transfer problems. Normal operating temperature and pressure (of) 567 degrees F and 2235 psig (is being maintained). There were no significant TS LCOs entered.</br>The electrical grid is stable and is supplying power to the plant via a normal shutdown electrical line-up. Decay heat is being removed via steam dumps to the condenser with AFW supplying the steam generators. There was no effect on Unit 1.</br>The licensee has notified the NRC Resident Inspector.</br>* * * UPDATE ON 11/29/11 AT 1312 EST FROM BRINKLY TO HUFFMAN * * * </br>The licensee has issued a press release concerning this event. The NRC Resident Inspector will be notified. R4DO (Farnholtz) informed.l be notified. R4DO (Farnholtz) informed.  +
09:29:00, 29 November 2011  +
47,485  +
06:55:00, 29 November 2011  +
09:29:00, 29 November 2011  +
At 0329 CST on 11/29/2011, Unit 2 experienAt 0329 CST on 11/29/2011, Unit 2 experienced an automatic Reactor Trip while the plant was stable at 100% power in Mode 1. All systems actuated as designed. The reactor trip was caused by Generator Lockout.</br>All ESF systems actuated as designed. The following systems actuated: Auxiliary Feedwater (AFW) and Feedwater Isolation.</br>All control rods fully inserted. Steam Dump system valve FV 7485 failed open and was manually isolated. This caused a letdown isolation that was restored. No primary/secondary relief valves lifted. There were no electrical bus transfer problems. Normal operating temperature and pressure (of) 567 degrees F and 2235 psig (is being maintained). There were no significant TS LCOs entered.</br>The electrical grid is stable and is supplying power to the plant via a normal shutdown electrical line-up. Decay heat is being removed via steam dumps to the condenser with AFW supplying the steam generators. There was no effect on Unit 1.</br>The licensee has notified the NRC Resident Inspector.</br>* * * UPDATE ON 11/29/11 AT 1312 EST FROM BRINKLY TO HUFFMAN * * * </br>The licensee has issued a press release concerning this event. The NRC Resident Inspector will be notified. R4DO (Farnholtz) informed.l be notified. R4DO (Farnholtz) informed.  +
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00:00:00, 29 November 2011  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:05:21, 2 March 2018  +
06:55:00, 29 November 2011  +
-0.107 d (-2.57 hours, -0.0153 weeks, -0.00352 months)  +
09:29:00, 29 November 2011  +
Automatic Reactor Trip Due to Turbine Trip on Generator Lockout  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
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