Browse wiki

Jump to navigation Jump to search
This 60-day telephone notification is beinThis 60-day telephone notification is being made under reporting requirements specified by 10CFR50.73(a)(2)(iv)(A) to describe an invalid actuation of a containment isolation signal affecting more than one system. </br>At 2043 on April 14, 2011, with the Duane Arnold Energy Center (DAEC) operating at 100% power, an invalid Group 3 isolation on the 'A' side of the Primary Containment Isolation System occurred. Group 3 isolation signals were generated for Primary Containment Isolation Valves for Drywell and Torus Ventilation, and Purge, Containment Nitrogen Compressor Suction and Discharge, Recirculation Pump Seals, and Post Accident Sample System. </br>This event was caused by a high resistance contact on connectors in the detector circuitry for the 'A' Reactor Building Vent Shaft Radiation Monitor.</br>All equipment responded in accordance with the plant design. Specifically, all actuations were complete and successful. </br>There were no safety consequences or impacts on the health and safety of the public. The event was entered into DAEC's corrective action program for resolution.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
01:43:00, 15 April 2011  +
15:19:00, 13 June 2011  +
01:43:00, 15 April 2011  +
This 60-day telephone notification is beinThis 60-day telephone notification is being made under reporting requirements specified by 10CFR50.73(a)(2)(iv)(A) to describe an invalid actuation of a containment isolation signal affecting more than one system. </br>At 2043 on April 14, 2011, with the Duane Arnold Energy Center (DAEC) operating at 100% power, an invalid Group 3 isolation on the 'A' side of the Primary Containment Isolation System occurred. Group 3 isolation signals were generated for Primary Containment Isolation Valves for Drywell and Torus Ventilation, and Purge, Containment Nitrogen Compressor Suction and Discharge, Recirculation Pump Seals, and Post Accident Sample System. </br>This event was caused by a high resistance contact on connectors in the detector circuitry for the 'A' Reactor Building Vent Shaft Radiation Monitor.</br>All equipment responded in accordance with the plant design. Specifically, all actuations were complete and successful. </br>There were no safety consequences or impacts on the health and safety of the public. The event was entered into DAEC's corrective action program for resolution.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 13 June 2011  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:06:54, 2 March 2018  +
15:19:00, 13 June 2011  +
false  +
59.567 d (1,429.6 hours, 8.51 weeks, 1.958 months)  +
01:43:00, 15 April 2011  +
Invalid Primary Containment Isolation System Actuation Due to Connector High Resistance  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +