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Declared Unusual Event due to RCS leakage … Declared Unusual Event due to RCS leakage greater than 10 gallons per minute. VCT level is lowering with constant plant temperature, pressure and pressurizer level. VCT level lowering at approximately 19 gallons per minute with associated rise in RWST level approximately 20 gallons per minute.</br>The licensee will notify the NRC Resident Inspector.</br>* * * UPDATE FROM MELIN TO W. GOTT AT 0120 ON 06/03/05 * * * </br>The licensee briefed NRC Management (McGinty, P. Hiland, R. Haag, J Munday) that the leakage was verified to be CVCS leakage and not RCS leakage. The leakage was stopped at 0055 and the licensee is evaluating termination/retraction criteria. NRC will not enter Monitoring Mode.</br>* * * UPDATE FROM G MELIN TO W. GOTT AT 0140 ON 06/03/05 * * *</br>At 0055, leakage stopped. Leakage verified to be CVCS leakage, not RCS. The leakage is stopped. Validating no other anomalies exist then will evaluate termination and retraction of UE notification.</br>* * * UPDATE FROM G MELIN TO P. SNYDER AT 0221 ON 06/03/05 * * * </br>Notification of termination of Unusual Event at 0221. Plant validation complete. RCS gross leakage is 0.07 gallon per minute and plant parameters are stable. Leakage confirmed to be from CVCS system which has been isolated.</br>The licensee will notify the NRC Resident Inspector.</br>Notified R2DO (R. Haag), NRR EO (P. Hiland), IRD (T. McGinty), R2 (J. Munday), DHS (I. Lee), FEMA (C. Ligget), and DOE (M. Smith)</br>* * * UPDATE ON 6/15/05 @ 1243 FROM JIM SPEICHER TO CHAUNCEY GOULD * * * RETRACTION</br>Event Notice 41743 reported declaration of an Unusual Event at 00:33 on 6/3/05 for RCS leakage in excess of Technical Specification Limits. The source of leakage was subsequently determined to be from the Chemical and Volume Control System (CVCS) and not from the RCS. The Unusual Event was terminated at 02:00 6/3/05 after the leak was isolated.</br>This event is retracted since the source of the leakage was not from the RCS and upon further review the event did not meet reporting requirements.</br>The NRC Resident Inspector was notified. RDO (Tom Decker), EO (M. Mayfield) and IRD (Peter Wilson) were notifiedield) and IRD (Peter Wilson) were notified
04:33:00, 3 June 2005 +
41,743 +
01:00:00, 3 June 2005 +
04:33:00, 3 June 2005 +
Declared Unusual Event due to RCS leakage … Declared Unusual Event due to RCS leakage greater than 10 gallons per minute. VCT level is lowering with constant plant temperature, pressure and pressurizer level. VCT level lowering at approximately 19 gallons per minute with associated rise in RWST level approximately 20 gallons per minute.</br>The licensee will notify the NRC Resident Inspector.</br>* * * UPDATE FROM MELIN TO W. GOTT AT 0120 ON 06/03/05 * * * </br>The licensee briefed NRC Management (McGinty, P. Hiland, R. Haag, J Munday) that the leakage was verified to be CVCS leakage and not RCS leakage. The leakage was stopped at 0055 and the licensee is evaluating termination/retraction criteria. NRC will not enter Monitoring Mode.</br>* * * UPDATE FROM G MELIN TO W. GOTT AT 0140 ON 06/03/05 * * *</br>At 0055, leakage stopped. Leakage verified to be CVCS leakage, not RCS. The leakage is stopped. Validating no other anomalies exist then will evaluate termination and retraction of UE notification.</br>* * * UPDATE FROM G MELIN TO P. SNYDER AT 0221 ON 06/03/05 * * * </br>Notification of termination of Unusual Event at 0221. Plant validation complete. RCS gross leakage is 0.07 gallon per minute and plant parameters are stable. Leakage confirmed to be from CVCS system which has been isolated.</br>The licensee will notify the NRC Resident Inspector.</br>Notified R2DO (R. Haag), NRR EO (P. Hiland), IRD (T. McGinty), R2 (J. Munday), DHS (I. Lee), FEMA (C. Ligget), and DOE (M. Smith)</br>* * * UPDATE ON 6/15/05 @ 1243 FROM JIM SPEICHER TO CHAUNCEY GOULD * * * RETRACTION</br>Event Notice 41743 reported declaration of an Unusual Event at 00:33 on 6/3/05 for RCS leakage in excess of Technical Specification Limits. The source of leakage was subsequently determined to be from the Chemical and Volume Control System (CVCS) and not from the RCS. The Unusual Event was terminated at 02:00 6/3/05 after the leak was isolated.</br>This event is retracted since the source of the leakage was not from the RCS and upon further review the event did not meet reporting requirements.</br>The NRC Resident Inspector was notified. RDO (Tom Decker), EO (M. Mayfield) and IRD (Peter Wilson) were notifiedield) and IRD (Peter Wilson) were notified
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00:00:00, 15 June 2005 +
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