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At 0052 on 10/28/04 the Unit 2 reactor wasAt 0052 on 10/28/04 the Unit 2 reactor was manually tripped after an electrical fault caused Shutdown Bank D control rods to drop into the core. An automatic start of the Auxiliary Feedwater system occurred when water levels in all four Steam Generators reduced to the Lo-Lo level setpoint. A letdown isolation occurred on Lo Pressurizer level resulting from the cooldown of the primary system after the Auxiliary Feedwater system start. Reactor Coolant system temperature has been recovered and the plant has been stabilized at Hot Shutdown conditions.</br>The licensee stated that there were no complications during the trip. All systems functioned as required. No significant safety systems were out of service when the trip occurred. No primary or secondary relief valves lifted during the transient. Decay heat is currently being removed using aux feedwater to the steam generators steaming to the main condenser. Tave dropped to a low point of 540 degrees F during the transient. The reactor was manually tripped in approximately 18 seconds after the shutdown bank dropped. The licensee plans to remain in mode 3.</br>The licensee will notify the NRC Resident Inspector. The licensee will also notify state and local authorities in North and South Carolina.l authorities in North and South Carolina.  +
04:52:00, 28 October 2004  +
03:29:00, 28 October 2004  +
04:52:00, 28 October 2004  +
At 0052 on 10/28/04 the Unit 2 reactor wasAt 0052 on 10/28/04 the Unit 2 reactor was manually tripped after an electrical fault caused Shutdown Bank D control rods to drop into the core. An automatic start of the Auxiliary Feedwater system occurred when water levels in all four Steam Generators reduced to the Lo-Lo level setpoint. A letdown isolation occurred on Lo Pressurizer level resulting from the cooldown of the primary system after the Auxiliary Feedwater system start. Reactor Coolant system temperature has been recovered and the plant has been stabilized at Hot Shutdown conditions.</br>The licensee stated that there were no complications during the trip. All systems functioned as required. No significant safety systems were out of service when the trip occurred. No primary or secondary relief valves lifted during the transient. Decay heat is currently being removed using aux feedwater to the steam generators steaming to the main condenser. Tave dropped to a low point of 540 degrees F during the transient. The reactor was manually tripped in approximately 18 seconds after the shutdown bank dropped. The licensee plans to remain in mode 3.</br>The licensee will notify the NRC Resident Inspector. The licensee will also notify state and local authorities in North and South Carolina.l authorities in North and South Carolina.  +
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00:00:00, 28 October 2004  +
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22:42:15, 24 September 2017  +
03:29:00, 28 October 2004  +
-0.0575 d (-1.38 hours, -0.00821 weeks, -0.00189 months)  +
04:52:00, 28 October 2004  +
Manual Reactor Trip After Shutdown Bank Dropped Into Core  +
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2  +