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On December 6, 2021, at 1125 hours EasternOn December 6, 2021, at 1125 hours Eastern Standard Time (EST), during planned maintenance activities, electrical power was lost to the 4160V emergency bus E-3. The power loss to emergency bus E-3 affected both Unit 1 and 2. Emergency Diesel Generator #3 received an automatic start signal but was under clearance for planned maintenance. Emergency bus E-3 was re-energized at 1315 EST hours via offsite power.</br>The loss of power to E3 resulted in Unit 2 Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 3 (i.e., Reactor Water Cleanup), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 10 (i.e., air isolation to the drywell) isolations. The actuations of PCIVs were completed and the affected equipment responded as designed. Per design, no Unit 1 safety system group isolations or actuations occurred. Other Unit 2 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3.</br>This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 2 and an automatic start signal to Emergency Diesel Generator #3. </br>There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.</br>Except for the Emergency Diesel Generator, which is out of service for planned maintenance, all equipment has been returned to its normal alignment.</br>* * * UPDATE FROM JJ STRNAD TO THOMAS KENDZIA AT 2028 EST ON DECEMBER 6, 2021 * * *</br>The loss of power to E3 resulted in Unit 1 Primary Containment Isolation System (PCIS) Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems). Other Unit 1 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3.</br>This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 1.</br>All Unit 1 equipment was returned to its normal alignment. The NRC Resident will be notified.</br>Notified R2DO (Miller). will be notified. Notified R2DO (Miller).  
16:25:00, 6 December 2021  +
55,627  +
18:14:00, 6 December 2021  +
16:25:00, 6 December 2021  +
On December 6, 2021, at 1125 hours EasternOn December 6, 2021, at 1125 hours Eastern Standard Time (EST), during planned maintenance activities, electrical power was lost to the 4160V emergency bus E-3. The power loss to emergency bus E-3 affected both Unit 1 and 2. Emergency Diesel Generator #3 received an automatic start signal but was under clearance for planned maintenance. Emergency bus E-3 was re-energized at 1315 EST hours via offsite power.</br>The loss of power to E3 resulted in Unit 2 Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 3 (i.e., Reactor Water Cleanup), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 10 (i.e., air isolation to the drywell) isolations. The actuations of PCIVs were completed and the affected equipment responded as designed. Per design, no Unit 1 safety system group isolations or actuations occurred. Other Unit 2 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3.</br>This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 2 and an automatic start signal to Emergency Diesel Generator #3. </br>There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.</br>Except for the Emergency Diesel Generator, which is out of service for planned maintenance, all equipment has been returned to its normal alignment.</br>* * * UPDATE FROM JJ STRNAD TO THOMAS KENDZIA AT 2028 EST ON DECEMBER 6, 2021 * * *</br>The loss of power to E3 resulted in Unit 1 Primary Containment Isolation System (PCIS) Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems). Other Unit 1 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3.</br>This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 1.</br>All Unit 1 equipment was returned to its normal alignment. The NRC Resident will be notified.</br>Notified R2DO (Miller). will be notified. Notified R2DO (Miller).  
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Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
12:30:24, 8 December 2021  +
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0.0758 d (1.82 hours, 0.0108 weeks, 0.00249 months)  +
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