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On 3/18/17 at 1107 (EDT), the Unit 3 react … On 3/18/17 at 1107 (EDT), the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. All three reactor coolant pumps (RCP) tripped and the 3B RCP was restarted for forced recirculation. The reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. In addition, Technical Specification 3.8.1.1, Action C requires a four hour report for the concurrent inoperability of the Unit 4 startup transformer to Unit 3 via the 3A 4kV bus and the Unit 3 3A diesel generator.</br>The NRC Senior Resident Inspector will be notified.</br>* * * UPDATE ON 3/18/2017 AT 1854 EDT FROM JAMES SPICHER TO BETHANY CECERE * * *</br>Update to previous report (EN 52623) to include additional reporting criteria.</br>On 3/18/17 at 1107 (EDT) the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. The 3A Emergency Diesel Generator (EDG) started on the loss of power signal but did not load, as designed, due to the bus fault. The 3A EDG was manually stopped at 1332. The Auxiliary Feedwater (AFW) System also initiated as expected. AFW was stopped at 1135. The actuations of the 3A EDG and AFW are reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A).</br>A loss of safety function affecting Units 3 and 4 occurred due to the loss of the 3A high head safety injection (HHSI) pump because it could not be powered from the faulted 3A 4kV bus with both Unit 4 HHSI pumps earlier (0624) removed from service due to planned maintenance. This caused three of the four HHSI pumps to be inoperable. The four HHSI pumps are shared by both Units 3 and 4. The safety function is achieved by two of the four HHSI pumps. Both Unit 4 HHSI pumps were restored to operable status at 1336. The loss of safety function is reportable in accordance with 10 CFR 50.72(b)(3)(v)(D).</br>The Unit 3 reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. Unit 4 remains operating at 100% power.</br>The licensee will notify the NRC Resident Inspector.</br>Notified R2DO (Ehrhardt) and NRR EO (Miller).ified R2DO (Ehrhardt) and NRR EO (Miller).
15:07:00, 18 March 2017 +
52,623 +
15:07:00, 18 March 2017 +
15:07:00, 18 March 2017 +
On 3/18/17 at 1107 (EDT), the Unit 3 react … On 3/18/17 at 1107 (EDT), the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. All three reactor coolant pumps (RCP) tripped and the 3B RCP was restarted for forced recirculation. The reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. In addition, Technical Specification 3.8.1.1, Action C requires a four hour report for the concurrent inoperability of the Unit 4 startup transformer to Unit 3 via the 3A 4kV bus and the Unit 3 3A diesel generator.</br>The NRC Senior Resident Inspector will be notified.</br>* * * UPDATE ON 3/18/2017 AT 1854 EDT FROM JAMES SPICHER TO BETHANY CECERE * * *</br>Update to previous report (EN 52623) to include additional reporting criteria.</br>On 3/18/17 at 1107 (EDT) the Unit 3 reactor tripped as a result of the loss of the 3A 4kV bus. The 3A Emergency Diesel Generator (EDG) started on the loss of power signal but did not load, as designed, due to the bus fault. The 3A EDG was manually stopped at 1332. The Auxiliary Feedwater (AFW) System also initiated as expected. AFW was stopped at 1135. The actuations of the 3A EDG and AFW are reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A).</br>A loss of safety function affecting Units 3 and 4 occurred due to the loss of the 3A high head safety injection (HHSI) pump because it could not be powered from the faulted 3A 4kV bus with both Unit 4 HHSI pumps earlier (0624) removed from service due to planned maintenance. This caused three of the four HHSI pumps to be inoperable. The four HHSI pumps are shared by both Units 3 and 4. The safety function is achieved by two of the four HHSI pumps. Both Unit 4 HHSI pumps were restored to operable status at 1336. The loss of safety function is reportable in accordance with 10 CFR 50.72(b)(3)(v)(D).</br>The Unit 3 reactor is stable in Mode 3. The 3A 4kV bus remains deenergized until troubleshooting and repairs are complete. Unit 4 remains operating at 100% power.</br>The licensee will notify the NRC Resident Inspector.</br>Notified R2DO (Ehrhardt) and NRR EO (Miller).ified R2DO (Ehrhardt) and NRR EO (Miller).
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