Browse wiki

Jump to navigation Jump to search
The following event description is based oThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.</br>On December 2, 2013, at approximately 1758 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Prior to the reactor trip, Unit 2 was operating normally at 100% power. Plant operators entered the emergency operations procedures and diagnosed an uncomplicated reactor trip but noted the 1A reactor coolant pump (RCP) was not running. All CEAs fully inserted into the core. Following the reactor trip, indications on the train A logarithmic (log) power nuclear instrument initially responded normally but then did not trend as expected. All other nuclear instruments responded normally and the train A log power channel was declared inoperable and technical specification limiting conditions for operation 3.3.10 and 3.3.11 were entered. No emergency classification was required per the PVNGS Emergency Plan.</br>The Unit 2 safety related electrical busses remained energized from normal offsite power during the event. Due to planned maintenance on one switchyard breaker, the Ruud offsite power line was disconnected from the PVNGS switchyard when the Unit 2 main generator output breakers opened. There was no impact to the required circuits between the offsite transmission network and the onsite Class 1E Electrical Power Distribution System; the offsite power grid is stable.</br>No major equipment was inoperable prior to the event that contributed to the event or complicated operator response. Unit 2 is currently stable in Mode 3 with the reactor coolant system at normal operating temperature and pressure. Preliminary information indicates the reactor trip resulted from an electrical protection trip of the power supply circuit breaker for the 1A RCP.</br>The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public.</br>The NRC Resident Inspector has been informed of the Unit 2 reactor trip.</br>There was no impact on either Unit 1 or Unit 3. was no impact on either Unit 1 or Unit 3.  
00:58:00, 3 December 2013  +
49,600  +
23:26:00, 2 December 2013  +
00:58:00, 3 December 2013  +
The following event description is based oThe following event description is based on information currently available. If through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10CFR50.73.</br>On December 2, 2013, at approximately 1758 Mountain Standard Time (MST), the Palo Verde Nuclear Generating Station (PVNGS) Unit 2 control room received reactor protection system alarms for low departure from nucleate boiling ratio and an automatic reactor trip occurred. Prior to the reactor trip, Unit 2 was operating normally at 100% power. Plant operators entered the emergency operations procedures and diagnosed an uncomplicated reactor trip but noted the 1A reactor coolant pump (RCP) was not running. All CEAs fully inserted into the core. Following the reactor trip, indications on the train A logarithmic (log) power nuclear instrument initially responded normally but then did not trend as expected. All other nuclear instruments responded normally and the train A log power channel was declared inoperable and technical specification limiting conditions for operation 3.3.10 and 3.3.11 were entered. No emergency classification was required per the PVNGS Emergency Plan.</br>The Unit 2 safety related electrical busses remained energized from normal offsite power during the event. Due to planned maintenance on one switchyard breaker, the Ruud offsite power line was disconnected from the PVNGS switchyard when the Unit 2 main generator output breakers opened. There was no impact to the required circuits between the offsite transmission network and the onsite Class 1E Electrical Power Distribution System; the offsite power grid is stable.</br>No major equipment was inoperable prior to the event that contributed to the event or complicated operator response. Unit 2 is currently stable in Mode 3 with the reactor coolant system at normal operating temperature and pressure. Preliminary information indicates the reactor trip resulted from an electrical protection trip of the power supply circuit breaker for the 1A RCP.</br>The event did not result in any challenges to fission product barriers and there were no adverse safety consequences as a result of this event. The event did not adversely affect the safe operation of the plant or the health and safety of the public.</br>The NRC Resident Inspector has been informed of the Unit 2 reactor trip.</br>There was no impact on either Unit 1 or Unit 3. was no impact on either Unit 1 or Unit 3.  
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 2 December 2013  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
01:52:28, 2 March 2018  +
23:26:00, 2 December 2013  +
-0.0638 d (-1.53 hours, -0.00911 weeks, -0.0021 months)  +
00:58:00, 3 December 2013  +
Automatic Reactor Trip Following the Loss of the 1A Reactor Coolant Pump  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
2  +