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On 3/31/13 at 0414 EDT, dye penetrant testOn 3/31/13 at 0414 EDT, dye penetrant testing identified a 10mm long relevant linear indication on a 3/4 inch RCS flow instrument line weld, between the RCS loop piping and the instrument isolation valve. This constitutes a weld defect in the primary coolant system that cannot be found acceptable per ASME Section XI. This section of piping is unisolable from the Reactor Coolant System. There is no evidence of active leakage currently or during the previous operating cycle, however, based on the dye penetrant testing this is considered a through wall leak. </br>This event notification is being made in accordance with 10CFR50.72(b)(3)(ii)(A), as a condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. </br>Unit 1 is currently in a scheduled refueling outage in Mode 5 making preparations to transition to Mode 6. The plant is evaluating the appropriate repair method for this condition. The condition will be corrected during the current refueling outage. Unit 2 is in Mode 1 at 100% power and is unaffected by this condition. </br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.  +
08:14:00, 31 March 2013  +
09:08:00, 31 March 2013  +
08:14:00, 31 March 2013  +
On 3/31/13 at 0414 EDT, dye penetrant testOn 3/31/13 at 0414 EDT, dye penetrant testing identified a 10mm long relevant linear indication on a 3/4 inch RCS flow instrument line weld, between the RCS loop piping and the instrument isolation valve. This constitutes a weld defect in the primary coolant system that cannot be found acceptable per ASME Section XI. This section of piping is unisolable from the Reactor Coolant System. There is no evidence of active leakage currently or during the previous operating cycle, however, based on the dye penetrant testing this is considered a through wall leak. </br>This event notification is being made in accordance with 10CFR50.72(b)(3)(ii)(A), as a condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. </br>Unit 1 is currently in a scheduled refueling outage in Mode 5 making preparations to transition to Mode 6. The plant is evaluating the appropriate repair method for this condition. The condition will be corrected during the current refueling outage. Unit 2 is in Mode 1 at 100% power and is unaffected by this condition. </br>The NRC Resident Inspector has been notified. NRC Resident Inspector has been notified.  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
00:00:00, 31 March 2013  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
22:22:53, 24 September 2017  +
09:08:00, 31 March 2013  +
false  +
0.0375 d (0.9 hours, 0.00536 weeks, 0.00123 months)  +
08:14:00, 31 March 2013  +
Rcs Flow Instrument Line Through Wall Weld Defect  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +