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At 1039 Kewaunee Power Station experienced … At 1039 Kewaunee Power Station experienced a loss of auto stop oil pressure on the main turbine while performing the monthly Turbine Trip Mechanism Test resulting in a reactor trip. No safeguards equipment was out of service at time of trip. Following the trip one of the moisture separators associated with the main turbine had its associated steam inlet valve fail open, which resulted in RCS temperature decreasing to 536 degrees F. This valve was manually isolated and RCS temperature returned to normal 547 degrees F. Normal heat sink via the condenser was available during the event. Investigation is continuing into the cause of the turbine trip.</br>This event is being reported under 10CFR50.72(b)(2)(iv)(B) for actuation of the Reactor Protection System and 10CFR50.72(b)(3)(iv)(A) for actuation of the Auxiliary Feedwater System." </br>All rods fully inserted and no primary or secondary PORV's lifted. There was no injection from any safety systems, other than AFW. Decay heat is being dumped to the condenser via steam dumps. The reactor coolant pressure and temperature are stable.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector. +
16:39:00, 12 January 2007 +
43,096 +
12:39:00, 12 January 2007 +
16:39:00, 12 January 2007 +
At 1039 Kewaunee Power Station experienced … At 1039 Kewaunee Power Station experienced a loss of auto stop oil pressure on the main turbine while performing the monthly Turbine Trip Mechanism Test resulting in a reactor trip. No safeguards equipment was out of service at time of trip. Following the trip one of the moisture separators associated with the main turbine had its associated steam inlet valve fail open, which resulted in RCS temperature decreasing to 536 degrees F. This valve was manually isolated and RCS temperature returned to normal 547 degrees F. Normal heat sink via the condenser was available during the event. Investigation is continuing into the cause of the turbine trip.</br>This event is being reported under 10CFR50.72(b)(2)(iv)(B) for actuation of the Reactor Protection System and 10CFR50.72(b)(3)(iv)(A) for actuation of the Auxiliary Feedwater System." </br>All rods fully inserted and no primary or secondary PORV's lifted. There was no injection from any safety systems, other than AFW. Decay heat is being dumped to the condenser via steam dumps. The reactor coolant pressure and temperature are stable.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector. +
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Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
22:37:27, 24 September 2017 +
12:39:00, 12 January 2007 +
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16:39:00, 12 January 2007 +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.