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At 1528 hours Central Time, a RPS trip occAt 1528 hours Central Time, a RPS trip occurred, all rods fully inserted. Turbine valve testing was in progress. A group 1 isolation occurred with all MSIVs closing. A partial group 2 occurred due to low reactor water level. All safety systems (valves) operated correctly. Currently reactor pressure/cooldown in progress using HPCI in pressure control, normal condensate and feedwater in service for reactor water level control. Investigation of cause is in progress.</br>Group isolations resulted from low pressure and low reactor water level. During the transient and subsequent cooldown, Operators manually opened the main steam relief valves to maintain pressure control in accordance with the plant EOPs. HPCI was manually started to maintain reactor level. The group 2 isolation has been reset. The group 1 isolation (MSIVs) will not be reset until after the main turbine control valves are shut. The plant is being cooled down to initiate RHR cooling and is in the normal shutdown electrical lineup.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
21:28:00, 10 January 2007  +
43,088  +
19:46:00, 10 January 2007  +
21:28:00, 10 January 2007  +
At 1528 hours Central Time, a RPS trip occAt 1528 hours Central Time, a RPS trip occurred, all rods fully inserted. Turbine valve testing was in progress. A group 1 isolation occurred with all MSIVs closing. A partial group 2 occurred due to low reactor water level. All safety systems (valves) operated correctly. Currently reactor pressure/cooldown in progress using HPCI in pressure control, normal condensate and feedwater in service for reactor water level control. Investigation of cause is in progress.</br>Group isolations resulted from low pressure and low reactor water level. During the transient and subsequent cooldown, Operators manually opened the main steam relief valves to maintain pressure control in accordance with the plant EOPs. HPCI was manually started to maintain reactor level. The group 2 isolation has been reset. The group 1 isolation (MSIVs) will not be reset until after the main turbine control valves are shut. The plant is being cooled down to initiate RHR cooling and is in the normal shutdown electrical lineup.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  +
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0.0177 d (0.424 hours, 0.00253 weeks, 5.81404e-4 months)  +
00:00:00, 10 January 2007  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:17:25, 2 March 2018  +
19:46:00, 10 January 2007  +
-0.0708 d (-1.7 hours, -0.0101 weeks, -0.00233 months)  +
21:28:00, 10 January 2007  +
Reactor Scram with Stuck Open Main Turbine Control Valves  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +