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DAEC (Duane Arnold Energy Center) abnorma … DAEC (Duane Arnold Energy Center) abnormal operating procedure AOP 301.1 for Station Blackout specifies that 30 minutes are allowed to establish alternate ventilation for RCIC (Reactor Core Isolation Cooling) /HPCI (High Pressure Coolant Injection) rooms, switchgear rooms, battery rooms, and the Main control room. During validation demonstration conducted on April 5, 2006 for the NRC Components team (from NRC Region 3 Office) the 30 minutes requirement was not met with the control room alternate ventilation taking about 60 minutes and with the other areas also exceeding their time requirements. This event is reportable as an unanalyzed condition that significantly degraded plant safety pursuant to 10 CFR 50.72(b)(3)(ii) reportability notification.</br>The NRC Resident Inspector was notified of this event by the licensee.</br>* * * RETRACTION FROM MURRELL TO HUFFMAN AT 1442 EDT ON 6/01/06 * * *</br>Duane Arnold Energy Center is retracting event number 42479 which was reported to the NRC Operations Center on 4/5/06 at 1855. This event is now determined to be not reportable because further evaluation to assess the significance of the delays in establishing alternate control room ventilation determined that the delay did not result in an adverse temperature increase in the affected areas. Specifically, the control room and back panel area temperature rise was evaluated using a detailed mass and heat transfer model of the affected areas. The evaluation confirmed that delays in establishing alternate control room ventilation did not adversely impact station commitments to 10 CFR 50.63 or accident responses outlined in UFSAR Section 15.3.2. Other areas required to have alternate ventilation established within 30 minutes had previously been successfully validated. Therefore, this event is not reportable as an unanalyzed condition that significantly degraded plant safety. The analyses and the bases for this retraction can be found under the plant corrective action program.</br>The licensee notified the NRC Resident Inspector. R3DO (Kozak) notified.esident Inspector. R3DO (Kozak) notified.
23:55:00, 5 April 2006 +
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21:23:00, 5 April 2006 +
23:55:00, 5 April 2006 +
DAEC (Duane Arnold Energy Center) abnorma … DAEC (Duane Arnold Energy Center) abnormal operating procedure AOP 301.1 for Station Blackout specifies that 30 minutes are allowed to establish alternate ventilation for RCIC (Reactor Core Isolation Cooling) /HPCI (High Pressure Coolant Injection) rooms, switchgear rooms, battery rooms, and the Main control room. During validation demonstration conducted on April 5, 2006 for the NRC Components team (from NRC Region 3 Office) the 30 minutes requirement was not met with the control room alternate ventilation taking about 60 minutes and with the other areas also exceeding their time requirements. This event is reportable as an unanalyzed condition that significantly degraded plant safety pursuant to 10 CFR 50.72(b)(3)(ii) reportability notification.</br>The NRC Resident Inspector was notified of this event by the licensee.</br>* * * RETRACTION FROM MURRELL TO HUFFMAN AT 1442 EDT ON 6/01/06 * * *</br>Duane Arnold Energy Center is retracting event number 42479 which was reported to the NRC Operations Center on 4/5/06 at 1855. This event is now determined to be not reportable because further evaluation to assess the significance of the delays in establishing alternate control room ventilation determined that the delay did not result in an adverse temperature increase in the affected areas. Specifically, the control room and back panel area temperature rise was evaluated using a detailed mass and heat transfer model of the affected areas. The evaluation confirmed that delays in establishing alternate control room ventilation did not adversely impact station commitments to 10 CFR 50.63 or accident responses outlined in UFSAR Section 15.3.2. Other areas required to have alternate ventilation established within 30 minutes had previously been successfully validated. Therefore, this event is not reportable as an unanalyzed condition that significantly degraded plant safety. The analyses and the bases for this retraction can be found under the plant corrective action program.</br>The licensee notified the NRC Resident Inspector. R3DO (Kozak) notified.esident Inspector. R3DO (Kozak) notified.
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96 +
00:00:00, 1 June 2006 +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:18:39, 2 March 2018 +
21:23:00, 5 April 2006 +
true +
false +
-0.105 d (-2.53 hours, -0.0151 weeks, -0.00347 months) +
23:55:00, 5 April 2006 +
Abnormal Operating Procedure (Aop) for Station Blackout Could Not Be Performed in Specified Time Period +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.