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100  +
This notification is being made pursuant tThis notification is being made pursuant to Braidwood Station Unit 1, Operating License Condition 2.G, which requires a 24 hour notification to the NRC Operations Center for reactor power operation in excess of 3586.6 megawatts thermal (100 percent rated power), i.e., a violation of Operating License Condition 2.C (1)- Braidwood Station will, following this notification, provide a written report within thirty days in accordance with the procedures described in 10 CFR 50.73(b), (c), and (e). </br>Braidwood Station, Unit 1 experienced a Feedwater temperature transient on November 18, 2004, which caused reactor power to momentarily increase and peak at approximately 101.2% as indicated on the excore nuclear instrumentation system. The duration that reactor power remained above 100% was approximately one minute. Subsequent to the event, a number of peer reviews were conducted to validate that power did not exceed 102%. The results of these reviews questioned the methodology used to determine the power level at the time of the transient. Industry was consulted regarding methodologies appropriate for power level measurement during transient conditions. At 1700 on December 2, 2005, an independent Exelon task force concluded, using a conservative methodology, that reactor power level during this transient did exceed 100% for approximately one minute and was limited to a peak of approximately 103.5% and that the appropriate reports, as specified in the Operating License, should be initiated. </br>This overpower transient, caused by the loss of a Feedwater heater string, is bounded by the Feedwater design basis transient described and analyzed in UFSAR, Section 15.1.1, "Feedwater System Malfunctions Causing a Reduction in Feedwater Temperature, therefore, the event did not place Braidwood Unit 1 in an unanalyzed condition that significantly degraded plant safety. No safety limits were exceeded and there was no impact on the health and safety of the public. The licensee has notified the Resident Inspector.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  
23:00:00, 2 December 2005  +
42,187  +
12:25:00, 3 December 2005  +
23:00:00, 2 December 2005  +
This notification is being made pursuant tThis notification is being made pursuant to Braidwood Station Unit 1, Operating License Condition 2.G, which requires a 24 hour notification to the NRC Operations Center for reactor power operation in excess of 3586.6 megawatts thermal (100 percent rated power), i.e., a violation of Operating License Condition 2.C (1)- Braidwood Station will, following this notification, provide a written report within thirty days in accordance with the procedures described in 10 CFR 50.73(b), (c), and (e). </br>Braidwood Station, Unit 1 experienced a Feedwater temperature transient on November 18, 2004, which caused reactor power to momentarily increase and peak at approximately 101.2% as indicated on the excore nuclear instrumentation system. The duration that reactor power remained above 100% was approximately one minute. Subsequent to the event, a number of peer reviews were conducted to validate that power did not exceed 102%. The results of these reviews questioned the methodology used to determine the power level at the time of the transient. Industry was consulted regarding methodologies appropriate for power level measurement during transient conditions. At 1700 on December 2, 2005, an independent Exelon task force concluded, using a conservative methodology, that reactor power level during this transient did exceed 100% for approximately one minute and was limited to a peak of approximately 103.5% and that the appropriate reports, as specified in the Operating License, should be initiated. </br>This overpower transient, caused by the loss of a Feedwater heater string, is bounded by the Feedwater design basis transient described and analyzed in UFSAR, Section 15.1.1, "Feedwater System Malfunctions Causing a Reduction in Feedwater Temperature, therefore, the event did not place Braidwood Unit 1 in an unanalyzed condition that significantly degraded plant safety. No safety limits were exceeded and there was no impact on the health and safety of the public. The licensee has notified the Resident Inspector.</br>The licensee notified the NRC Resident Inspector.ensee notified the NRC Resident Inspector.  
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2.777778e-4 d (0.00667 hours, 3.968254e-5 weeks, 9.132e-6 months)  +
100  +
00:00:00, 3 December 2005  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
02:19:45, 2 March 2018  +
12:25:00, 3 December 2005  +
false  +
0.559 d (13.42 hours, 0.0799 weeks, 0.0184 months)  +
23:00:00, 2 December 2005  +
Reactor Power Operation in Excess of Operating License Condition  +
URL"URL" is a <a href="/Special:Types/URL" title="Special:Types/URL">type</a> and predefined property provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a> to represent URI/URL values.
1  +