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The team identified a Green noncited violaThe team identified a Green noncited violation of 10 CFR 50.65(a)(4), which states, in part, that the licensee shall assess and manage the increase in risk that may result from the proposed maintenance activities. Specifically, on October 28, 2010 the turbine driven essential feedwater pump was out of service for maintenance for approximately 12 hours. During this time the licensee unknowingly entered the Orange risk window (crossed a risk threshold) due to a faulty assumption in the probabilistic risk assessment model. This finding was entered into the licensees corrective action program as Condition Report CR-WF3-2011-06653. The team determined that the failure to perform adequate risk assessments is a performance deficiency. This finding was more than minor because it was associated with the human performance attribute of the Mitigating Systems Cornerstone, adversely affecting the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. In accordance with NRC Inspection Manual Chapter 0609, Attachment 4, Phase 1 Initial Screening and Characterization of Findings, the issue was identified as requiring a Phase 2 evaluation. A Region IV Senior Reactor Analyst performed a Phase 2 significance determination using NRC Inspection Manual Chapter 0609, Appendix K, Maintenance Risk Assessment and Risk Management Significance Determination Process. In accordance with Appendix K: Delta-CDF = (CCDPActual CCDPflawed) * duration /8760 The licensee bounded the duration of the turbine driven essential feedwater pump maintenance at 8 hours in a year. The flawed ICDP was 3.1E-5, the actual ICDP was 3.1E-5 + 1.9E-5 = 5.0E-5. The difference was 1.9E-5. Delta-CDF = 1.9E-5 * 12/8760 = 2.6E-8 Therefore, the issue was determined to have very low safety significance (Green). This finding was determined to have a cross-cutting aspect in the area of problem identification and resolution associated with the self and independent assessments component because the licensee performed a probabilistic risk assessment model update in April 2009, which failed to identify the faulty assumptionh failed to identify the faulty assumption  
23:59:59, 31 December 2011  +
05000382  +
23:59:59, 31 December 2011  +
Has query"Has query" is a predefined property that represents meta information (in form of a <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Subobject">subobject</a>) about individual queries and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
1.388889e-4 d (0.00333 hours, 1.984127e-5 weeks, 4.566e-6 months)  +  and 9.259259e-5 d (0.00222 hours, 1.322751e-5 weeks, 3.044e-6 months)  +
Modification date"Modification date" is a predefined property that corresponds to the date of the last modification of a subject and is provided by <a rel="nofollow" class="external text" href="https://www.semantic-mediawiki.org/wiki/Help:Special_properties">Semantic MediaWiki</a>.
19:06:50, 30 September 2017  +
23:59:59, 31 December 2011  +
Failure to Adequately Manage the Risk Involved with a Maintenance Window for the Turbine Driven Essential Feedwater Pump  +