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 Issue dateTitle
ML22263A41820 September 2022Enclosure F - DBNPS, Unit 1, Technical Specification Bases, Rev. 32
ML20302A28725 September 20209 to Tech Spec Bases
L-16-256, Response to Request for Additional Information Regarding a Request to Revise the Emergency Plan6 September 2016Response to Request for Additional Information Regarding a Request to Revise the Emergency Plan
ML12258A30614 September 2012Attachment B - NRC Staff Answer to Motion for Summary Disposition of Contention 4
L-09-263, Response to NRC Request for Additional Information Regarding Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems.26 October 2009Response to NRC Request for Additional Information Regarding Generic Letter 2008-01, Managing Gas Accumulation in Emergency Core Cooling, Decay Heat Removal, and Containment Spray Systems.
ML08291011220 November 2008ITSB M - More Restrictive Changes - to Davis Besse Amendment Beyond Scope Issues
L-08-240, Improved Technical Specification Conversion License Amendment Request, Volume 14, Revision 1, ITS Section 3.9, Refueling Operations7 August 2008Improved Technical Specification Conversion License Amendment Request, Volume 14, Revision 1, ITS Section 3.9, Refueling Operations
ML0822706657 August 2008Improved Technical Specification Conversion License Amendment Request, Volume 8, Revision 1, Section 3.3 - Instrumentation
ML0722004813 August 2007Volume 14, Revision 0, Davis-Besse, Unit 1 - Improved Technical Specifications Conversion, ITS Section 3.9 Refueling Operations.
ML0722004703 August 2007Volume 8, Revision 0, Davis-Besse, Unit 1 - Improved Technical Specifications Conversion, ITS Section 3.3 Instrumentation.
IR 05000346/200600311 August 2006IR 05000346-06-003; Firstenergy Nuclear Operating Company;4/1/2006 - 6/30/2006; Davis-Besse Nuclear Power Station; Fire Protection, Surveillance Testing, Access Control to Radiologically Significant Areas, and Identification and Resolution
IR 05000346/20060024 May 2006IR 05000346-06-002; on 1/1/2006 - 3/31/2006; Davis-Besse Nuclear Power Station; Inservice Inspection
IR 05000346/200500218 March 2005IR 05000346-05-002; 1/01/2005 - 2/19/2005; Davis-Besse Nuclear Power Station; Post-Maintenance Testing
Information Notice 1999-14, Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick5 May 1999Unanticipated Reactor Water Draindown at Quad Cities Unit 2, Arkansas Nuclear One Unit 2, & FitzPatrick
ML20205G56826 March 1999Advises of Completion of Plant Performance Review on 990202 to Develop Integrated Understanding of Safety Performance. Overall Performance of Plant Acceptable.Plant Issues Matrix & Insp Plan Encl
ML20198B1512 December 1998Forwards Insp Activity Plan for Next 6 Months & Plant Issues Matrix.Infor Provided to Minimize Resource Impact on Staff & to Allow for Scheduling Conflicts & Personnel Availability to Be Resolved in Advance of Inspector Arrival Onsite
IR 05000346/199800511 June 1998Insp Rept 50-346/98-05 on 980401-0512.Violations Noted.Major Areas Inspected:Operations,Maint & Engineering
NRC Generic Letter 1998-0228 May 1998NRC Generic Letter 1998-002: Loss of Reactor Coolant Inventory and Associated Potential for Loss of Emergency Mitigation Functions While in a Shutdown Condition
Information Notice 1997-83, Recent Events Involving Reactor Coolant System Inventory Control During Shutdown5 December 1997Recent Events Involving Reactor Coolant System Inventory Control During Shutdown
Information Notice 1996-65, Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown11 December 1996Undetected Accumulation of Gas in Reactor Coolant System and Inaccurate Reactor Water Level Indication During Shutdown
Information Notice 1996-56, Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power22 October 1996Problems Associated with Testing, Tuning, or Resetting of Digital Control Systems While at Power
Information Notice 1996-42, Unexpected Opening of Multiple Safety Relief Valves5 August 1996Unexpected Opening of Multiple Safety Relief Valves
Information Notice 1996-37, Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown18 June 1996Inaccurate Reactor Water Level Indication and Inadvertent Draindown During Shutdown
Information Notice 1996-05, Partial Bypass of Shutdown Cooling Flow from Reactor Vessel18 January 1996Partial Bypass of Shutdown Cooling Flow from Reactor Vessel
Information Notice 1994-52, Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 115 July 1994Inadvertent Containment Spray and Reactor Vessel Draindown at Millstone Unit 1
Information Notice 1994-36, Undetected Accumulation of Gas in Reactor Coolant System24 May 1994Undetected Accumulation of Gas in Reactor Coolant System
ML07104001728 April 199459 FRN 12990, Biweekly Notice; Applications and Amendments to Facility Operating Licenses Involving No Significant Hazards Considerations
Information Notice 1993-89, Potential Problems with BWR Level Instrumentation Backfill Modifications26 November 1993Potential Problems with BWR Level Instrumentation Backfill Modifications
ML20056H09027 August 1993SALP Rept 50-346/93-01 for 911201-930630
Information Notice 1993-62, Thermal Stratification of Water in BWR Reactor Vessels10 August 1993Thermal Stratification of Water in BWR Reactor Vessels
Information Notice 1993-27, Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization8 April 1993Level Instrumentation Inaccuracies Observed During Normal Plant Depressurization
IR 05000346/199201812 January 1993Insp Rept 50-346/92-18 on 921207-18.No Violations Noted. Major Areas Inspected:Design Changes,Mods & Temporary Alterations Conducted Per Insp Module 37700
NRC Generic Letter 1992-0419 August 1992NRC Generic Letter 1992-004 - Resolution of Issues Related to Reactor Vessel Water Level Instrumentation in BWRs Pursuant to 10 CFR 50.54(F)
Information Notice 1992-16, Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown25 February 1992Loss of Flow from the Residual Heat Removal Pump During Refueling Cavity Draindown
Information Notice 1990-22, Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units23 March 1990Unanticipated Equipment Actuations Following Restoration of Power to Rosemount Transmitter Trip Units
ML20011F42821 February 1990Forwards Emergency Response Data Sys Data Point Library Ref Files.Util Will Contact NRC Contractor Directly in Order to Arrange Mutually Acceptable Schedule for Preliminary Testing of Sys
ML20148H60315 December 1987Summary of ACRS DHR Sys Subcommittee 871117 Meeting in Washington,Dc Re Util Decision Not to Install Dedicated Blowdown Sys at Davis Besse & Implications of Diablo Canyon Loss of Shutdown Cooling Event.Viewgraphs Encl
ML20216H60425 June 1987Advises That Based on B&W Analytical Studies for Primary Sys Blowdown Using RELAP5,use of Blowdown Valves Not Practicable for Feed & Bleed,Per 851204 Commitment.Listed Proposed Mods Will Be Implemented to Enhance Makeup Sys
ML20214T72325 November 1986Informs of Major Discrepancies Between B&W Topical Rept BAW-10075A,Rev 1, Multinode Analysis of Small Breaks for B&W 177-Fuel Assembly...Plants W/Raised Loop Arrangements & Internal Vent Valves, & as-built Configuration of Plant
ML20132A42418 September 1985Transcript of 850918 Public Meeting in Washington,Dc Re Continuation of Briefing on Plant.Pp 1-80.Supporting Documentation Encl
NRC Generic Letter 1985-0823 May 1985NRC Generic Letter 1985-008: 10 CFR 20.408 Termination Reports - Format
NRC Generic Letter 1985-072 May 1985NRC Generic Letter 1985-007: Implementation of Integrated Schedules for Plant Modifications
NRC Generic Letter 1985-0217 April 1985NRC Generic Letter 1985-002: Staff Recommended Actions Stemming from NRC Integrated Program for the Resolution of Unresolved Safety Issues Regarding Steam Generator Tube Integrity
NRC Generic Letter 1985-0531 January 1985NRC Generic Letter 1985-005: Inadvertent Boron Dilution Events
ML03115058529 January 1985Withdrawn NRC Generic Letter 1985-004: Operator Licensing Examinations
ML20087M67022 March 1984Application for Amend to License NPF-3,revising Tech Specs to Reflect Changes in post-accident Sampling Sys & post- Accident Instrumentation for in-core Thermocouple & Reactor Coolant Hot Leg Level
ML20009A51930 June 1981Abnormal Transient Operating Guideline (Atog) Program Description.
ML20207L3349 April 1980Evaluation of Licensee Compliance W/Category `A' Items of NRC Recommendations Resulting from TMI-2 Lessons Learned, Davis Besse Nuclear Power Station