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 Entered dateEvent description
ENS 5375728 November 2018 12:30:00At 0752 CST, on November 28, 2018, Dakota County inadvertently actuated their sirens while performing a scheduled weekly (Emergency Planning Fixed Siren Test). All seven (7) Dakota County sirens actuated for approximately 9 seconds before Dakota County Dispatch canceled the activation. This 4-hour non-emergency report is being made per 10 CFR 50.72(b)(2)(xi), Offsite Notification (which was made to Dakota County Dispatch). Capability to notify the public was never degraded during this time. All Emergency Notification sirens remain in service. No press release is planned at this time. The licensee has notified the NRC Resident Inspector.
ENS 5370028 October 2018 21:44:00

This event is being reported pursuant to 10 CFR 50.72(b)(3)(xiii) for a major loss of emergency assessment capability at the Prairie Island Nuclear Generating Plant. At 1435 CDT on October 28, 2018, troubleshooting of the Seismic Monitoring Panel resulting from the receipt of Control Room annunciator 47023-0603 (Seismic Monitor Panel) determined that the '(Operational Basis Earthquake) OBE Exceedance' alarm on the Seismic Monitoring Panel will not alarm and determined the panel is non-functional. The Seismic Monitoring Panel system functions to provide indication that the OBE threshold has been exceeded following a seismic event and is used in the Prairie Island Nuclear Generating Plant Emergency Plan to perform classification of Initiating Condition 'Seismic event greater than OBE levels' and Emergency Action Level HU2.1. Station personnel are monitoring the seismic recorders for event alarms on a 15 minute frequency due to alarm function failure. The station is developing repair plans for restoration of the alarm function. This event does not adversely affect the safe operation of the plant or health and safety of the public.

The licensee has notified the NRC Resident Inspector.

ENS 5187722 April 2016 00:03:00Missing fire barrier between Fire Area (FA) 59 and 85. During a walk down of fire barriers for the NFPA 805 project, it was determined that the fire barrier between Fire Area 59 (Unit 1) and 85 (common) is not a rated barrier due to unsealed penetrations in the barrier. Evaluation FPEE 12-006 evaluated the acceptability of the barrier being unrated based on separation of safe shutdown equipment however a review of equipment credited for Appendix R safe shutdown identified that the redundant credited Appendix R equipment is on either side of the fire barrier which is not 3 hour rated. The conclusion of the FPEE is therefore no longer valid. Fire Hazard Analysis Drawings Do Not Match Boundary Description. The plant layout in F5 Appendix F, Rev. 28, Fire Hazard Analysis (FHA), does not agree with the boundary description in the FHA for the Unit 1 and 2 Containment Annulus fire areas, Fire Area (FA) 68 and 72. The layout should but does not show the fire area boundary between the annulus and adjacent fire areas, FA 60 and 75 on 735 (foot) and 61A on 755 (foot), as an Appendix R boundary. The annulus airlock doors are 3-hour fire rated and the airlock is constructed of concrete thick enough to qualify as a 3 hour fire barrier however, there are penetrations in the barrier that are not sealed with fire rated materials or inspected as required by the Fire Protection Program. Therefore, this is an unanalyzed condition reportable under 10 CFR 50.72(b)(3)(ii)(B). This condition does not affect the health and safety of the public or station employees. The NRC Resident Inspector has been notified.
ENS 5161621 December 2015 22:12:00

As part of the License Amendment development to transition to NFPA 805, PINGP (Prairie Island Nuclear Generating Plant) Calculation ENG-ME-353, Mechanical MOV (Motor Operated Valve) Analysis to support IN-92-18 Response, revision 1, issued in 1998, was reviewed for applicability for the transition to NFPA 805. Recent consultation with an MOV engineer regarding the scope of the revision indicated ENG-ME-353 is out of date. On 12/21/2015, during technical review for a new weak link calculation, several MOVs were identified from the list of MOVs that are credited to be manually operated from outside the control room in the event of a fire in the control room or relay room per PINGP Procedure F5 Appendix B, Control Room Evacuation (Fire), that could be damaged if hot shorts were to bypass the torque and limit switches. There are also four other motor valves associated with the Gland Steam system of both Unit 1 and Unit 2 that were added to the procedure F5 Appendix B, Control Room Evacuation (Fire), that have not been analyzed for a weak link. This unanalyzed condition could impact the ability of plant operators to implement procedure F5 Appendix B, Control Room Evacuation (Fire). New hourly fire watch impairments were created for Fire Area 13 (Control Room) and Fire Area 18 (Relay and Cable Spreading Room) as compensatory measures. Therefore, this is an unanalyzed condition reportable under 10 CFR 50.72(b)(3)(ii)(B). The public health and safety is not impacted. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 0107 EST ON 01/14/16 FROM NATHAN BIBUS TO DANIEL MILLS * * *

Reviews of the list of MOVs susceptible to hot shorts bypassing the torque and limit switches credited to be manually operated from outside the control room in the event of a fire have continued. Additional valves have been noted to be affected by this failure mechanism in areas outside of the Control Room or Relay Room. The additional MOVs affected by this unanalyzed condition could impact the ability of plant operators to implement PINGP Procedure F5 Appendix D, Impact of Fire Outside Control/Relay Room. As a compensatory measure, additional hourly fire watch impairments were created for the following fire areas: Fire Area 031 ( A Train Hot Shutdown Panel & Air Compressor/Aux 695 Feedwater Room) Fire Area 032 ( B Train Hot Shutdown Panel & Air Compressor/Aux 695 Feedwater Room) Fire Area 058 (Aux Building Ground Floor Unit 1) Fire Area 073 (Auxiliary Building Ground Floor Unit 2) The public health and safety is not impacted. The (NRC) Resident Inspector has been notified. Notified R3DO (Duncan).

ENS 509503 April 2015 10:12:00On April 3, 2015 at 0652 CDT, the Unit 2 reactor was manually tripped while operating at 100 percent power due to a lockout trip of 21 Main Feedwater Pump as required by the annunciator response procedure for the lockout alarm. This also resulted in a turbine trip. The crew entered the reactor trip emergency operating procedures and stabilized the unit in Mode 3 at normal operating pressure and temperature. All control rods fully inserted into the core following the trip. The manual trip is reportable per 10 CFR 50.72(b)(2)(iv)(B). The Auxiliary Feedwater System actuated to start the auxiliary feedwater pumps as designed on low narrow range steam generator level and provided makeup flow to the steam generators. The auxiliary feedwater actuation is reportable per 10 CFR 50.72(b)(3)(iv)(A). Steam generator levels have been returned to normal. The auxiliary feedwater pumps have subsequently been secured and returned to automatic. Steam generators are being supplied by 22 Main Feedwater Pump and decay heat is being removed by the condenser steam dump system. The cause of 21 Main Feedwater Pump trip has been determined to be a failed suction pressure switch. There was no effect on Unit 1 as a result of this trip. The health and safety of the public and site personnel were not at risk at any time during this event. The NRC Senior Resident Inspector has been notified. The licensee plans to issue a press release.
ENS 4160615 April 2005 22:33:00Unit 2 Train A emergency diesel generator D5 was removed from service at 0838 CDT on 4/11/05 for surveillance testing and Technical Specification (TS) 3.8.1, 'AC Source - Operating,' Condition B, 'One DG inoperable,' was entered. TS Required Action 3.8.1.B.4 requires D5 be restored to operable status with a Completion Time of 7 days. At 1026 CDT, the test was halted due to high-indicated crankcase pressure on Engine 2 (D5 is a tandem engine generator). The test procedure specifies shutting down the DG if crankcase pressure exceeds 30 mm for more than a few minutes (the setpoint for the crankcase pressure trip is 52 mm). Investigation of the cause of the high-indicated crankcase pressure on Engine 2 (and whether Engine 1 was effected) started immediately. Unit 2 Train B emergency diesel generator was demonstrated operable by completing a surveillance test at 0423 CDT on 4/12/05. Evaluation of the scope of work to return D5 to operable status and the schedule for completing the work indicated that repairs could not be completed within the 7 days allowed outage time. Based on this assessment an orderly shutdown of Unit 2 is being performed. Shutdown of Unit 2 commenced at 21:30 CDT on 4/15/05. Unit 2 shutdown will continue until D5 is restored to operable status. The licensee intends to issue a press release. The licensee notified the NRC Resident Inspector.