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 Issue dateTitleTopic
ML20207H80730 June 1999Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal OperationsAnticipated operational occurrence
Hydrostatic
ML20207H79430 June 1999Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation
ML20207H78530 June 1999Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation
ML20207H77730 June 1999Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2
ML20207H80130 November 1998Rev 0 to WCAP-15124, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal OperationAnticipated operational occurrence
Hydrostatic
ML20207H77330 November 1998Rev 0 to WCAP-15125, Evaluation of Pressurized Thermal Shock for Byron,Unit 1
ML20202F83930 November 1997Non-proprietary,Rev 2 to WCAP-14824, Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation & Surveillance Weld Metal Integration for Byron & BraidwoodAnticipated operational occurrence
Hydrostatic
ML20199E85331 October 1997Heatup & Cooldown Limit Curves for Normal OperationAnticipated operational occurrence
Hydrostatic
ML20199E82831 October 1997Heatup & Cooldown Limit Curves for Normal OperationAnticipated operational occurrence
Hydrostatic
ML20141A46830 April 1997Rev 1 to Byron Unit 1 Heatup & Cooldown Limit Curves for Normal Operation & Surveillance Weld Metal Integration for Byron & BraidwoodHydrostatic
ML20211D95430 September 1996Non-proprietary Probabilistic Analysis of Reduction in Turbine Valve in Test Frequency for Nuclear Plants W/ Westinghouse BB-296 Turbine W/Steam ChestsTurbine Missile
ML20108D24630 April 1996Nonproprietary Technical Justificaton for Eliminating Large Primary Loop Pipe Rupture as Structural Design Basis for Byron & Braidwood Units 1 & 2 Nuclear Power PlantsSafe Shutdown Earthquake
Hydrostatic
Exemption Request
Pressure Boundary Leakage
Pressure boundary leak
ML20096F29917 January 1996Non-proprietary Rev 0 to CEN-627-NP, Verification of Installation Process & Operating Performance of Abb Ceno SG Tube Sleeve for Use at Comm Ed Byron & Braidwood Units 1 & 2Hydrostatic
Finite Element Analysis
ML20093G96531 October 1995Nonproprietary Addendum 1 to Technical Support for Alternate Plugging Criteria W/Tube Expansion at TSP Intersections for Braidwood-1 & Byron-1 Model D4 SGs Addendum 1 TSP Analysis Using 'RELAP5' Loads
ML20086T35030 April 1995Nonproprietary Slide Presentation Matl NRC Meeting of 950223 Alternate Plugging Criteria W/Tube Expansion for Braidwood Unit 1 & Byron Unit 1 Model D4 Sgs
ML20087D46031 March 1995Nonproprietary Errata to Rev 3 to WCAP-14047, Braidwood Unit 1 Technical Support for Cycle 5 Steam Generator Interim Plugging Criteria, Correcting Page 4-139 Figure Title
ML20085K71031 March 1995Non-proprietary Rev 3 to Rept WCAP-14047, Braidwood Unit 1 Technical Support for Cycle 5 SG Interim Plugging Criteria
ML20092A76131 March 1995Evaluation of PTS for Braidwood Unit 1
ML20092A75431 March 1995Evaluation of PTS for Braidwood Unit 2
ML20080H35713 February 1995Technical Support for Alternate Plugging Criteria W/Tube Expansion at Tube Suppport Plate Intersections for Braidwood-1 & Byron-1 Model D4 ST for Feb 1995
ML20078Q15713 February 1995Non-proprietary Rev 2 to WCAP-14047, Braidwood Unit 1 Technical Support for Cycle 5 SG Interim Plugging CriteriaHydrostatic
Earthquake
ML20078J58330 November 1994Nonproprietary Braidwood Unit 1 & Byron Unit 1 Model D4 SG Limited Tube Support Plate Displacement Analysis in Support of Interim Plugging CriteriaHydrostatic
FLEX
ML20072Q59831 August 1994Technical Support for Cycle 5 Steam Generator Interim Plugging Criteria
ML20073B3461 June 1994Nonproprietary Topical Rept on Methodology,Verification & Applications of Computer Progra,GappipeEarthquake
ML20069P60031 May 1994Technical Support for Cycle 5 Steam Generator Interim Plugging Criteria
ML20064N32131 March 1994Commonwealth Edison Co Byron & Braidwood Unit 1 & 2 Increased Sgtp/Reduced Tdf/Pmtc Analysis Program Engineering Licensing ReptBoric Acid
Shutdown Margin
Fuel cladding
Flow Induced Vibration
ML20069B47631 March 1994Non-proprietary Rev 0 to BAW-10196, W-D4 F* Qualification ReptBoric Acid
ML20056D89531 May 1993Nonproprietary Rev 1 to WCAP-13699, Laser Welded Sleeves for 3/4 Inch Diameter Tube Feedring Type & Westinghouse Preheater SgsBoric Acid
Non-Destructive Examination
Hydrostatic
Finite Element Analysis
Liquid penetrant
Flow Induced Vibration
ML20077A31431 August 1992Nonproprietary Fracture Mechanics Evaluation Byron & Braidwood Units 1 & 2 Residual HX Tube Side Inlet & Outlet Nozzles
ML20141M45131 August 1992Nonproprietary Fracture Mechanics Evaluation,Byron Braidwood Units 1 & 2,Residual HX Tube Side Inlet & Outlet Nozzles
ML20090M83929 February 1992Nonproprietary Evaluation of Byron & Braidwood Units 1 & 2 Auxiliary Spray Lines Per NRC Bulletin 88-008Finite Element Analysis
ML20086B54830 November 1991Fracture Mechanics Evaluation,Braidwood,Unit 2 Residual Heat Exchanger Tube Side Inlet & Outlet Nozzles
ML20079P73031 October 1991Nonproprietary Byron Unit 1 & Braidwood Unit 1 Evaluation for Tube Vibration Induced FatigueFinite Element Analysis
Flow Induced Vibration
ML20070W03731 March 1991Analysis of Capsule U from Commonwealth Edison Co Braidwood Unit 2 Reactor Vessel Radiation Surveillance Program
ML20058C00231 August 1990Analysis of Capsule U from Comm Ed Braidwood Unit 1 Reactor Vessel Radiation Surveillance Program
ML20044A96431 July 1990Rev 0 to Comm Ed Topical Rept on Benchmark of PWR Nuclear Design Methods Using PHOENIX-P & Advanced Nodal Code (Anc) Computer Codes.
ML20006A82310 January 1990Errata to Rev 3 to BAW-1543, Master Integrated Reactor Vessel Surveillance Program Consisting of Revised Tables 3-20 & E-1
ML20011E24731 October 1989Analysis of Capsule U from Comm Ed Byron Unit 2 Reactor Vessel Radiation Surveillance Program.
ML20090M83430 September 1989Nonproprietary Evaluation of Thermal Stratification for Byron & Braidwood Units 1 & 2 RHR LinesPacking leak
ML19351A41930 September 1989Mark-BW Reload LOCA Analysis for Catawba & McGuire Units.Boric Acid
ML20129B54130 June 1989Reduction in Minimum Rhrs Flowrate During Mid-Loop Operation for Byron & Braidwood Power Plants Units 1 & 2Boric Acid
Shutdown Margin
ML20235M91120 February 1989Nonproprietary Catawba Unit 1 Evaluation for Tube Vibration Induced FatigueFlow Induced Vibration
ML20072H95131 December 1988Joint Westinghouse Owners Group/Westinghouse Program:Atws Rule Administration ProcessProbabilistic Risk Assessment
Failure to Scram
ML20198J57030 November 1988Non-proprietary WCAP-12046, Handbook on Flaw Evaluation for Zion,Byron & Braidwood,Units 1 & 2,Reactor Vessels
ML20207L7786 October 1988Nonproprietary WCAP 11936, McGuire Unit 2 Evaluation for Tube Vibration Induced FatigueFinite Element Analysis
Flow Induced Vibration
ML20154M24230 September 1988Simulate-3 Validation & Verification
ML20207L92630 September 1988Nonproprietary Addendum 2 to COBRA-NC,Analysis for Main Steamline Break in Catawba Unit 1 Ice Condenser Containment (Response to NRC Questions)
ML20154J98330 April 1988RCS Flow Anomaly Investigation Rept
ML20151U12730 November 1987Analysis of Capsule U from Comm Ed,Byron Unit 1 Reactor Vessel Radiation Surveillance Program
ML20237C40930 November 1987Nonproprietary Rev 2 to Byron/Braidwood T-Hot Reduction Final Licensing ReptBoric Acid
Loop seal
Turbine Missile
Fuel cladding
Flow Induced Vibration