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ENS 562648 December 2022 19:02:00Unusual Event Due to Excessive Reactor Coolant System Leakage

At 1402 EST Turkey Point Unit 3, while operating at 100 percent, declared an Unusual Event due to unidentified leakage greater than 10 gallons per minute for more than 15 minutes. The abnormal procedure for Reactor Coolant System leakage was entered. The plant remains at 100 percent power. The cause of the leakage is under investigation. At 1446 EST it was verified that the leak had been isolated. The plant remains at 100 percent power. Unit 4 was unaffected. State and local authorities were notified by the licensee. The NRC Resident Inspector has been notified. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS NRCC THD Dest (email), and DHS Nuclear SSA (email).

  • * * UPDATE ON 12/08/22 AT 1621 (EST) FROM SZEMEI CHOI TO THOMAS HERRITY * * *

Turkey Point Unit 3 has isolated the leak. The Unusual Event was terminated at 1558 EST. The NRC Resident Inspector has been notified. Notified R2DO (Miller), NRR EO (Miller), and IR MOC (Crouch). Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS NRCC THD Dest (email), and DHS Nuclear SSA (email).

  • * * RETRACTION FROM BRANDEN NATHE TO DONALD NORWOOD AT 1446 EST ON 1/9/2023 * * *

Turkey Point Nuclear Unit 3 is retracting this notification based on the following additional information not available at the time of the notification, Following the event for unidentified RCS leakage on 12/8/22 at 1403 EST, additional information demonstrated that an RCS leak did not exist. A review of indications showed that the in-service seal water return filter D/P (Differential Pressure) rose from 1 psid to 6 psid with a corresponding rise in VCT (Volume Control Tank) level as would be seen with an increase in excess letdown flowrate. Additionally, the on-contact radiation dose rate from the excess letdown piping in the U3 Pipe and Valve Room was measured by RP (Radiation Personnel) to be significantly higher than normal with no other sources of elevated radiation levels noted. Following the closure of CV-3-387, RCS To Excess Letdown HX (Heat Exchanger) Control Valve, a nominal input/output flow balance was able to be restored. Containment parameters including pressure, temperature, sump level and radiation level did not change during the event. Due to the shared nature of piping between excess letdown and seal water return, a challenge to system integrity would not allow RCP (Reactor Coolant Pump) controlled bleed-off to remain in service with a normal flow balance which it has at all times subsequent to the event. Turkey Point Nuclear reported initially based on the available information at the time and to ensure timeliness with emergency declaration and reporting notification requirements. The NRC Resident Inspector has been notified. Notified R2DO (Miller).

Unidentified leakage
ENS 558317 April 2022 23:00:00Both Trains of Residual Heat Removal Inoperable

The following information was provided by the licensee via fax or email: At 1900 EDT on 04/07/22, while Unit 4 was in Mode 4 following a refueling outage, it was discovered that both trains of residual heat removal (RHR) were simultaneously inoperable due to gas voiding. At 2032 EDT corrective actions were completed and both trains of RHR were declared operable. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(B). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 04/11/22 AT 1022 EST FROM DAVID STOIA TO BRIAN SMITH * * *

The following information was provided by the licensee via email: On 4/8/2022 at 0110 EDT Turkey Point Unit 4 notified the (NRC Operations Center (NRCOC)) pursuant to 10 CFR 50.72(b)(3)(v)(B) that both trains of Residual Heat Removal (RHR) were simultaneously inoperable due to the presence of gas voids that were identified during scheduled system gas accumulation testing. Subsequent evaluation by (Florida Power & Light (FPL)) Engineering has concluded that both trains of RHR remained operable and capable of performing their specified safety function. This NRCOC notification is a retraction of EN# 55831. The licensee notified the NRC Resident Inspector. Notified R2DO (Miller)

ENS 5578512 March 2022 05:50:00Main Steam Isolation Valve Failed to Shut

The following information was provided by the licensee via email: At 0050 EST on 3/12/22, while shutting down for entry into a scheduled refueling outage, the station discovered that a single Main Steam Isolation Valve (4A MSIV) did not fully close on demand. All other equipment operated as expected. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 04/26/22 AT 1422 EDT FROM DAVID STOIA TO BRIAN PARKS * * *

The following information was provided by the licensee via email: On 3/12/2022 at 0656 EDT Turkey Point Unit 4 notified the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) that a single Main Steam Isolation Valve (MSIV) did not fully close when manually demanded from the control room during shutdown of Unit 4 for a refueling outage. Following disassembly and inspection of the MSIV, Florida Power & Light Engineering identified the cause of the deficiency and determined that the valve would have fully seated under its design accident conditions. This notification is a retraction of EN# 55785. The NRC Resident Inspector has been notified of this retraction. Notified R2DO (Miller).

ENS 5557412 November 2021 21:05:00Reactor Coolant System Pressure Boundary Degraded

At 1605 EST on 11/12/21, it was determined that the RCS Pressure Boundary does not meet ASME Section XI, Table IWB-341 0-1, 'Acceptable Standards' due to a through wall leak of the Core Exit Thermocouple Nozzle Assembly. Measures have been taken to establish Mode 5 for corrective actions. This event is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 3/28/2022 AT 0849 EDT FROM DAVID STOIA TO MIKE STAFFORD * * *

The following information was provided by the licensee via email: On 11/12/2021 EN 55574 reported possible evidence of pressure boundary through-wall leakage observed on a Core Exit Thermocouple (CET) tube. On 3/10/2022, based on laboratory analysis of the affected CET tube section, FPL Engineering determined that there was no pressure boundary through-wall leakage associated with this event. Analysis identified that the leakage likely originated from an adjacent threaded compression fitting on a tubing joint. This condition complies with ASME Section XI requirements and is therefore not reportable. This follow-up NRCOC notification is a retraction of EN 55574. The NRC Resident Inspector has been notified. Notified R2DO (Miller).

Through Wall Leak
Through-Wall Leakage
ENS 5503614 December 2020 17:40:00Charging Pump and Boration Flowpaths Simultaneously Inoperable

At 1240 EST on 12/14/20, it was determined that all Unit 4 Charging Pumps and Boration Flowpaths were simultaneously inoperable. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 2/10/2021 AT 1210 EST FROM DAVID STOIA TO BETHANY CECERE * * *

On 1/21/21 a past operability review was completed that assessed the event reported on 12/14/20. The evaluation concluded that the condition did not render any Unit 4 Charging Pump or all boration flowpaths inoperable, and that the 8-hour notification submitted on 12/14/20 was not required. This notification is a retraction of EN #55036. The NRC Site Resident has been notified of the EN #55036 retraction. Notified R2DO (Miller).

Past operability
ENS 5114711 June 2015 12:22:00Offsite Notification Due to Inadvertent Emergency Plan Siren Actuation

This is a non-emergency notification to the NRC in accordance with 10 CFR 50.72(b)(2)(xi). On 6/11/15, at 0822 (EDT), Miami-Dade Fire Department notified the site of an alarming single Emergency Plan siren. Investigation is ongoing for alarming siren. At no time was there an emergency requiring the siren activation. FPL (Florida Power and Light) has not issued a news release. This notification is made in accordance with 10 CFR 50.72 (b)(2)(xi). The Senior NRC Resident (Inspector) has been notified.

  • * * RETRACTION FROM ALEX CHOMAT TO DANIEL MILLS AT 1552 EDT ON 6/11/15 * * *

The investigation of the reported alarming EP siren did not confirm that it had been activated or had malfunctioned. The notification received from the Miami-Dade Fire Department apparently resulted from an erroneous call from a member of the public. This event notification is retracted based on the fact that no EP siren activation occurred necessitating notifications. The Senior NRC Resident (Inspector) has been updated. Notified R2DO (Guthrie)

Siren
ENS 507142 January 2015 14:25:00High Head Safety Injection Inoperable Due to Voids Identified in Piping

At 0925 (EST) on 1/2/2015, Engineering personnel identified a gas void in each of two Unit 4 cold leg High Head Safety Injection (HHSI) discharge lines which exceeded procedural gas accumulation acceptance criteria. This condition rendered the cold leg HHSI flow path inoperable and required entry into Technical Specification 3.0.3. The voids were vented and Technical Specification (TS) 3.0.3 was exited at 1032. The testing for gas voids conducted on 1/2/2015 was a follow-up to a gas void found in one Unit 4 HHSI line on 12/26/2014. On 12/26/14, TS 3.0.3 was entered at 1020 and exited at 1048 after the gas void was vented. After further review, the 12/26/2014 event was also reportable in accordance with 10 CFR 50.72(b)(3)(v)(D). Engineering evaluation will be performed for both events to determine the specific impact of the gas voids on HHSI system function. Cause evaluation is being conducted to determine the source of the gas and any needed corrective actions. Unit 3 was verified to not have this voiding issue. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM SEAN BLOOM TO VINCE KLCO AT 1120 EDT ON 3/11/15 * * *

On 1/2/2015 at 1645 (EST), Event Notification 50714 reported to the NRCOC (Nuclear Regulatory Commission Operations Center) gas voids detected on 12/26/2014 and 1/2/2015 in Unit 4 cold leg High Head Safety Injection (HHSI) piping which exceeded procedural gas accumulation acceptance criteria. Subsequent analysis has determined that if a HHSI pump started with the measured gas voids present, the resulting system conditions would not have impacted the integrity of the Unit 4 HHSI discharge flow path to the reactor coolant system (RCS) and therefore its safety related function would not be impaired. The Unit 4 HHSI system discharge flow path to the RCS had been operable with the voids present, Technical Specification (TS) requirements were met, and entry into TS 3.0.3 was not required. The HHSI system remained capable of fulfilling the safety function to mitigate the consequences of an accident on Unit 4. Therefore, the immediate notification to the NRCOC on 1/2/2015 at 1645 in accordance with 10 CFR 50.72(b)(3)(v)(D) is hereby retracted. The NRC Resident Inspector has been informed. Notified R2DO (Shaeffer).

ENS 4738728 October 2011 18:30:00Tsc Unavailable for Emergency Conditions

At 1430 (EDT) on 10/28/11, it was discovered that due to an Equipment Clearance Order (ECO), the HVAC recirculation capability of the Technical Support Center (TSC) was lost. The TSC dampers were deenergized in the non-emergency position while the ECO was in effect. The ECO was put into effect on 10/10/11. The ECO was released at 1630 (EDT) on 10/28/2011 and functionally tested restoring TSC HVAC recirculation capability. While the ECO was in effect and under certain accident conditions, the TSC may have been unavailable due to the inability of the charcoal filtration system to maintain a habitable atmosphere. The alternate TSC remained available, during the time the ECO was in effect, as defined in the Emergency Plan Implementing Procedures. This 8 hour notification is required per 10 CFR 50.72(b)(3)(xiii). The alternate TSC remained available during this period. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JOSE VASQUEZ TO VINCE KLCO ON 12/14/2011 AT 1852 EST * * *

A Functionality Assessment (FA) has concluded that the Turkey Point TSC was able to perform it's intended function of ensuring habitability to TSC responders during the period 10/10/11 through 10/28/11 with the TSC ventilation system in the degraded condition. A dose analysis was performed, modeled after the design basis LOCA analysis for the TSC, using alternate source term, no filtration, containment leakage based on the most recent ILRTs, current data on ECCS leakage, and meteorological conditions existent during the period. Dose to TSC responders would have been less than the general design criterion limit of 5 REM. The licensee notified the NRC Resident Inspector.

Functionality Assessment