Semantic search

Jump to navigation Jump to search
 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 556937 January 2022 00:37:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownShutdown Initiated in Accordance with Technical SpecificationsOn January 6, 2022 at 1937 (EST), St Lucie Unit 2 commenced a reactor shutdown as required by Technical Specification 3.1.3.1 Action 'e', due to Control Element Assembly number 27 slipping from 133 inches to 120 inches withdrawn and unable to be recovered within the prescribed time limits. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 2 entered 6 hour LCO to shutdown to mode 3 at 1539 EST as required by Technical Specification 3.1.3.1 Action 'e'. There was no impact on Unit 1.
ENS 521381 August 2016 07:42:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownPlant Shutdown Due to Pressure Boundary Leakage Greater than Allowable Limit

On August 1, 2016 at 0342 EDT St. Lucie Unit 1 commenced a unit shutdown required by Technical Specifications due to Reactor Coolant System Pressure Boundary Leakage in excess of the allowable limit of zero leakage. The leak was initially identified on July 31, 2016 at 2115 EDT as not Pressure Boundary leakage. After further analysis, the leak was determined to be Reactor Coolant System Pressure Boundary leakage at 0123 on August 1, 2016. The leakage is estimated as less than one tenth of a gallon per minute and is not impacting the ability to shut down the unit. Additional impact of the leak is under evaluation. This report is submitted in accordance with 10CFR50.72(b)(2)(i) as 'The initiation of any nuclear plant shutdown required by the plant's Technical Specifications.' The location of the leak is on the Instrumentation piping welded connection at Flow Element FE-3311 attached to (the) Emergency Core Cooling System Injection header to Reactor Coolant System Loop 1A2. The leak activity is 0.167 microCuries per ml. The NRC Resident Inspector has been notified.

  • * * RETRACTION AT 1335 EDT ON 09/23/16 FROM RICHARD SCISCENTE TO JEFF HERRERA * * *

The purpose of this notification is to retract a previous report made on EN 52138. NRC notification was initially made as a result of a plant shutdown required by technical specifications (TS) for Reactor Coolant System (RCS) pressure boundary leakage. Subsequent to the initial report, St. Lucie has determined that the RCS leakage was from a seal weld on a threaded connection that was not pressure boundary leakage. However, the leak was non-isolable and required RCS depressurization to allow immediate investigation to ensure there were no faults in a RCS component body or pipe wall. The leakage was estimated to be less than one tenth of a gallon per minute and did not impact the ability to shut down the unit. No TS limits were exceeded during this event. Therefore, the plant shutdown to investigate and correct leakage past the seal weld of a threaded connection does not meet the reporting requirements of 10 CFR 50.72 or 10 CFR 50.73. The NRC Resident Inspector has been notified. Notified the R2DO (Blamey).

Reactor Coolant System
Emergency Core Cooling System
ENS 5097712 April 2015 01:00:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown Due to Safety Injection Tank Outlet Piping Leak

During investigation of a small leak on the 2B2 Safety Injection Tank inside Saint Lucie Unit 2 containment, a through wall flaw was identified on Class 2 piping associated with the 2B2 Safety Injection Tank. The 2B2 Safety Injection Tank was declared inoperable on April 11, 2015 at 1204 EDT and Unit 2 entered a 24-hour shutdown action statement for Technical Specification 3.5.1.b. On April 11, 2015 at 2100 EDT, Unit 2 initiated a plant shutdown in compliance with Technical Specifications.

This condition is being reported pursuant to 10 CFR 50.72(b)(2)(i) The electrical grid is stable and no safety-related equipment that would affect a safe shutdown was out of service at the time of the report. The licensee has notified the NRC Resident Inspector.

ENS 5031025 July 2014 15:29:0010 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
Technical Specification Required Shutdown Due to a Safety Injection Valve Defect

On July 25th, 2014 at 1129 EDT, during investigation of a small leak inside Saint Lucie Unit 2 containment, a defect was identified on a valve (V3811, Safety Injection Tank 281 Outlet Vent Valve). This valve is within the Q-Group A (ASME Class 1 equivalent) boundary of the safety injection line. The leak is currently isolated from the reactor coolant system by a Technical Specification credited isolation check valve. The affected Safety Injection Tank has been declared inoperable and the unit has entered 24 hour shutdown (Technical Specification) action statement 3.5.1.b. Unit shutdown is currently being planned for repair of the flaw. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A). The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM JOHN REXRODE TO VINCE KLCO AT 0053 EDT ON 7/26/14 * * *

On July 26, 2014 at 0002 EDT, Saint Lucie Unit 2 commenced shutdown to repair the identified leak. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(A) and 10 CFR 50.72(b)(2)(i). The NRC Resident Inspector has been notified. Unit 2 current power is 88% at 0105 EDT and expect to trip the unit at approximately 0400 EDT. Notified the R2DO (Musser).

Reactor Coolant System
ENS 4448514 September 2008 06:41:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownDropped Control Element Resulting in Entry Into Technical Specification Required Shutdown LcoAt 23:45 on 9/13/08, one control element assembly (CEA) dropped to the bottom of the core from the upper electrical limit. Technical Specification LCO 3.1.3.1 Action e. was entered. The CEA was not able to be realigned with the other CEA's in its group within the time constraints of the COLR. Technical Specification LCO 3.1.3.1 Action f. was entered and a down power to 70% was initiated. Actions to repair and retrieve the CEA could not be completed within the time constraint of LCO 3.1.3.1 Action f. and a shutdown was commenced to comply with Technical Specifications at 0241 on 9/14/08. The CEA was recovered and restored to OPERABLE at 0258 on 9/14/08 and the shutdown was halted. The plant is currently being returned to full power operation. This four hour non-emergency report is being made pursuant to 10 CFR 50.72(b)(2)(i), 'The initiation of any nuclear plant shutdown required by Technical Specifications.' The licensee notified the NRC Resident Inspector.
ENS 4387128 December 2007 09:50:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Required Shutdown - Dropped Cea

At 0347 on 12/28/07, during plant start up from a refueling outage while In Mode 2, one control element assembly (CEA) dropped to the bottom of the core from the upper electrical limit. The reactor was not critical at the time. Technical Specification LCO 3.1.3.1 action (e) was initiated to proceed to Mode 3 at 0450 while actions are taken to repair and retrieve the CEA. This four hour non-emergency report is being made pursuant to 10 CFR 50.72(b)(2)(i), the 'Initiation of any nuclear plant shutdown required by Technical Specifications'. The licensee notified the NRC Resident Inspector.

  • * * RETRACTED ON 03/26/2008 AT 1433 EDT BY JACK BREEN TO DAN LIVERMORE * * *

The licensee is retracting this report based on the following: At 03:47 on 12/28/07, during plant start up from a refueling outage while in Mode 2, one control element assembly (CEA) dropped to the bottom of the core from the upper electrical limit. The reactor was not critical at the time. Technical Specification LCO 3.1.3.1 (Action E) was initiated to proceed to Mode 3 at 0450 while actions were taken to repair and retrieve the CEA. This event was reported as a four hour non-emergency report pursuant to 10CFR 50.72(b)(2)(i), 'The initiation of any nuclear plant shutdown required by Technical Specifications.' Upon further review of the event, and since the Unit was not critical in mode 2 at the time of the event, this event is not considered reportable in accordance with the guidance provide in NUREG-1022, Rev. 2, 'Event Reporting Guidelines 10CFR50.72 and 50.73,' in which 'The initiation of any plant shutdown' does not include mode changes required by TS if initiated after the plant is already in a shutdown condition. As such this notification is being retracted. The Site Resident has been notified of this retraction.

ENS 4205212 October 2005 18:40:0010 CFR 50.72(b)(2)(i), Tech Spec Required ShutdownTechnical Specification Shutdown Based on Loss of Two Channels of Containment Isolation Radiation Monitor

On 10/12/05 at 14:40 EDT, Unit 1 experienced a loss of Channel A of the CIS (Containment Isolation Signal) Radiation Monitor which, when combined with the previous existing inoperability of Channel D of the CIS radiation monitor, required Unit 1 to enter technical specification LCO 3.0.3. If the action statement (for the CIS), LCO 3.3.2.1, cannot be met, within 1 hour, action shall be initiated to place the unit in Hot Standby with the next 6 hours, Hot Shutdown within the following 6 hours, and cold shutdown within the subsequent 24 hours. Unit shutdown is in progress. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM LICENSEE (C. MARPLE) TO NRC (HUFFMAN) AT 2145 EDT ON 10/12/05 * * *

At 2101 EDT on 10/12/05, the Unit 1 exited Technical Specification 3.0.3 when Channel D of the CIS radiation monitor was returned to service. The down-power of Unit 1 was halted at 97% power. The licensee notified the NRC Resident Inspector. R2DO(Decker) informed.