Semantic search

Jump to navigation Jump to search
 Start dateTitleDescriptionTopic
ENS 532351 March 2018 18:10:00En Revision Imported Date 11/8/2019

EN Revision Text: UNANALYZED CONDITION FOR TORNADO GENERATED MISSILES On March 1, 2018, during evaluation of protection for Technical Specifications (TS) equipment from the damaging effects of tornado generated missiles, Quad Cities Station identified a non-conforming condition in the plant design such that specific TS equipment is considered to not be adequately protected from tornado generated missiles. Tornado generated missiles could strike the Unit l, Unit 1/2, and Unit 2 Emergency Diesel Generator intake and exhaust stacks, day tank vents, and main fuel oil tank vents. This could result in crimping of the intake/exhaust stacks and vents, which would affect the ability of the Emergency Diesel Generators to perform their function if a tornado would occur. This condition is reportable in accordance with 10 CFR 50.72(b)(3)(ii)(B) as a condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and 10 CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. This condition is being addressed in accordance with NRC enforcement guidance provided in Enforcement Guidance Memorandum (EGM) 15-002, 'Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1, and DSS-ISG-2016-01, 'Clarification of Licensee Actions in Receipt of Enforcement Discretion per Enforcement Guidance Memorandum EGM 15-002, Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1. Compensatory measures have been implemented in accordance with these documents. The NRC Resident Inspector has been informed of this notification.

  • * * RETRACTION FROM NICK JOHNSON TO HOWIE CROUCH AT 1900 EST ON 11/7/19 * * *

The purpose of this notification today (11/07/19) is to retract event notification #53235 made on March 1, 2018, for Quad Cities Station. Additional review determined that the current design of all three Emergency Diesel Generators and associated Day Tanks and Main Fuel Oil Storage Tanks Vents is consistent with the licensing basis for Quad Cities Station. There was no non-conformance of Quad Cities' tornado missile protection design, and the EDGs were operable at the time the event notification was made. Therefore, this event does not meet the criteria of 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D) and ENS report #53235 is being retracted. The NRC Resident Inspector has been informed of this notification. Notified R3DO (Peterson).

Unanalyzed Condition
Time of Discovery
Enforcement Discretion
Tornado Generated Missile
Tornado Missile Protection
ENS 5308923 November 2017 02:43:00Lpci Inoperability Due to Overvoltage Relay Actuation

On November 22, 2017, at 2043 (CST), Unit I MCC (Motor Control Center) 18/19-5 overvoltage relay target was found actuated and would not reset. MCC 18/19-5 was powered from the normal feed, Bus 19. Bus 19 voltages were verified to be normal. The overvoltage relay actuation would result in MCC 18/19-5 being de-energized in the event of a DBA LOCA (Design Basis Accident Loss of Coolant Accident) in which the 1/2 Emergency Diesel Generator fails to energize Bus 18, therefore rendering both divisions of the Low Pressure Cooling Injection (LPCI) mode of Residual Heat Removal (RHR) system inoperable. Technical Specification 3.5.1 Condition E was entered, requiring restoration of LPCI in 72 hours. The overvoltage target was subsequently able to be reset at 2114 (CST), restoring the LPCI function of RHR. Technical Specification 3.5.1 Condition E was exited at that time. This event is reportable under 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM RONALD SNOOK TO STEVEN VITTO ON 01/11/18 AT 1913 EST * * *

The purpose of this notification today (01/11/18) is to retract the ENS Report made on November 23, 2017 at 0248 hours EST (ENS Report #53089). Upon further review, it was determined that the Unit 1 MCC 18/19-5 overvoltage relay target that was found actuated and would initially not reset was caused only by intermittent degraded DC control power. During this event, MCC 18/19-5 remained powered from the normal feed Bus 19, and Bus 19 voltages were verified to be normal. It was further determined from plant drawings that under this condition the degraded DC control power to the Unit 1 MCC 18/19-5 overvoltage relay has no impact to the Technical Specification 3.5.1 required capability to auto transfer power from the normal Bus 19 to the alternate Bus 18 should Bus 19 lose power such as during a DBA LOCA. This overvoltage relay was installed in the early 1990's only to support enhanced reliability of the power supply to the LPCI injection valves, and its actuation due to degraded DC control power would not impact the ability to auto transfer to alternate Bus 18. Therefore, both divisions of the Low Pressure Cooling Injection (LPCI) mode of Residual Heat Removal (RHR) system would have remained fully operable under the as-found relay condition, and Technical Specification 3.5.1 Condition E was not required to be entered. On December 6, 2017, it was determined that a loose fuse clip terminal had caused the DC control power to the overvoltage relay to become degraded which in turn caused the relay target and its reset to become erratic. This fuse clip terminal was repaired on December 6, 2017. Based on the subsequent reviews of this event, the LPCI system was not required to be declared inoperable in accordance with Technical Specifications 3.5.1 during the period of the MCC 18/19-5 overvoltage relay actuation (i.e., 31 minutes on 11/22/17), and hence was not required to be reported under 10CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented fulfillment of a safety function. Therefore, based on this information, ENS Report #53089 is being retracted. The NRC Resident Inspector has been notified. R3DO(Jeffers) has been notified.

ENS 529558 September 2017 16:30:00Hpci System Inoperable

On September 8, 2017 at 1130 hours CDT, Unit Two High Pressure Coolant Injection (HPCI) Minimum Flow Valve MO 2-2301-14 flow indicating switch (FIS 2-2354) failed to meet the Technical Specification Allowable Value during calibration testing. Technical Specification Table 3.3.5.1-1 Allowable Value (3.f) requires greater than or equal to 634 gpm (3.14 inches water column as required by procedure). HPCI was subsequently declared inoperable. This event is being reported as a condition that could have prevented fulfillment of a safety function in accordance with 10CFR50.72(b)(3)(v)(D). The HPCI system is a single train system and the loss of HPCI could impact the plant's ability to mitigate the consequences of an accident. The Reactor Core Isolation Cooling (RCIC) system was confirmed operable. Note: On September 8, 2017 at 1140 hours CDT, the HPCI Minimum Flow Valve MO 2-2301-14 flow indicating switch (FIS 2- 2354) was successfully recalibrated and HPCI was returned to Operable status. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION AT 1216 EDT ON 10/19/17 FROM RYAN DECKER TO DONG PARK * * *

The purpose of this notification today (10/19/17) is to retract the ENS Report made on September 8, 2017 at 1545 hours CDT (ENS Report #52955). Upon further investigation, it was determined that a surveillance procedure contained an overly restrictive statement that directed operators to immediately declare the High Pressure Coolant Injection (HPCI) system inoperable when the HPCI Minimum Flow Valve MO 2-2301-14 flow indicating switch (FIS 2-2354) fails. This statement was in conflict with existing Technical Specification (TS) 3.3.5.1, Condition E, that allows seven days to restore the HPCI FIS (instrument channel only) to an operable status prior to entry into TS 3.3.5.1, Condition H, which requires declaring HPCI inoperable immediately. Hence, during the period of FIS inoperability (i.e., 10 minutes), the HPCI system was not required to be declared inoperable in accordance with Technical Specifications. Therefore, based on this information, ENS Report # 52955 is being retracted. Note: On September 8, 2017 at 1140 hours CDT, the HPCI Minimum Flow Valve MO 2-2301-14 flow indicating switch (FIS 2-2354) was successfully recalibrated and HPCI was returned to Operable status. The NRC Resident Inspector has been notified. Notified R3DO (Daley).

ENS 5233431 October 2016 07:39:00High Pressure Coolant Injection (Hpci) Inoperable

On October 31, 2016, at 0239 hours (CDT), a defect (minor audible through-wall leak) was identified on the steam line drain valve 1-2301-55, HPCI Steam Line Drain Line Steam Trap Outlet Valve. The defect was identified by Operations personnel traversing through the HPCI room as part of normal rounds. HPCI was declared inoperable under Tech Specs 3.5.1, Condition G. The Reactor Core Isolation Cooling (RCIC) system was verified operable. HPCI remains available (but not operable). The leak has been isolated. The 1-2301-55 is a manual valve downstream of the HPCI steam line drain trap. In a standby line-up, this line drains condensation from the HPCI steam supply line to the main condenser. During operation in an accident scenario, this line drains condensation from the HPCI steam supply line to the Torus via a drain pot. The location of the defect is in class 2 safety related piping. HPCI is a single train safety system and this notification is being made in accordance with 10CFR50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified. Technical Specification 3.5.1, condition G requires that HPCI be Operable within 14 days.

  • * * RETRACTION ON 12/05/2016 AT 1505 EST FROM MARK BRIDGES TO STEVEN VITTO * * *

The purpose of this notification is to retract the ENS Report made on October 31, 2016, at 0239 hours CDT (ENS Report #52334). Upon further investigation, a pinhole through-wall leak was discovered in the body of the 1-2301-55 valve (HPCI Steam Line Drain Line Steam Trap Outlet Valve). The defect was characterized as a 1/32-inch rounded hole due to a manufacturing defect in the casting located on the downstream side of the valve near the piping connection. A subsequent evaluation performed by Quad Cities Station considering the defect size, location, and characterization, confirmed the Unit 1 High Pressure Coolant Injection (HPCI) system would have performed its safety function when required. Based on this subsequent evaluation, ENS Report 52334 is being retracted. Note: On November 1, 2016, at 1624 hours CDT, the 1-2301-55 valve (HPCI Steam Line Drain Line Steam Trap Outlet Valve) was successfully repaired and HPCI was returned to Operable status. The NRC Resident Inspector has been notified. Notified R3DO (Stone).

Through-Wall Leak
ENS 505976 November 2014 01:38:00Six Unit 2 Control Rod Drive Hydraulic Control Units Inoperable

Six (6) U2 CRD (Control Rod Drive) HCU (Hydraulic Control Unit) accumulators were identified with riser brackets that were installed incorrectly. This issue impacts U2 CRD HCU accumulators only. The incorrect riser bracket installation could challenge the ability of the CRD hydraulic control unit to perform its design function during a seismic event. Identified U2 control rods associated with HCU accumulators that had riser brackets installed incorrectly were declared inoperable. This condition has been corrected since initial identification, restoring all control rods to operable status. Reference IR 2407342. This notification is made pursuant to 10CFR 50.72(b)(3)(v) regarding the reportability of multiple failures that could have prevented fulfillment of a safety function. The NRC Resident Inspector will be notified.

  • * * RETRACTION FROM MATT SEELEY TO HOWIE CROUCH AT 1144 EST ON 12/22/14 * * *

The purpose of this notification is to retract the ENS notification made on November 6, 2014 (ENS 50597). An Engineering Evaluation has determined that the function of the affected U2 CRD HCU Accumulators was not affected as discussed in Chapters 6 and 15 of the Updated Final Safety Analysis Report. Therefore, the threshold for reporting the issue as an event or condition that could have prevented the fulfillment of a safety function was not met (NUREG 1022, Revision 3, Event Report Guidelines Section 3.2.7). The NRC Resident Inspector has been notified. Notified R3DO (Dickson).

ENS 4972715 January 2014 13:23:00Drywell Radiation Monitor Inoperable

At 0723 (CST) hours on January 15, 2014, the 2A Drywell Radiation Monitor was declared inoperable after exhibiting erratic performance. This monitor provides the input into one division of the primary containment isolation logic for a Group II isolation. As a result, the channel was placed in a tripped condition in accordance with Technical Specification 3.3.6.1, Condition B. Given both divisions are required to complete the Group II isolation logic, this condition is reportable in accordance with 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function. The 2A Drywell Radiation Monitor has been repaired and restored to an operable condition. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JAMES BURKE TO JOHN SHOEMAKER AT 1447 EST ON 2/7/14 * * *

The purpose of this notification is to retract the ENS notification made on January 15, 2014 (ENS 49727). Upon further investigation it was verified that the Drywell Radiation Monitors do not mitigate the consequences of an accident as discussed in Chapters 6 and 15 of the Updated Final Safety Analysis Report and the Technical Specifications Bases for 3.3.6.1. Therefore, the threshold for reporting the issue as an event or condition that could have prevented the fulfillment of a safety function was not met (NUREG 1022 Revision 3 - Event Report Guidelines Section 3.2.7). The NRC Resident Inspector has been notified. Notified the R3DO (Orlikowski).

ENS 494074 October 2013 01:45:00Unit 2 High Pressure Coolant Injection (Hpci) Inoperable Due to Drain Line Leak

On October 3, 2013, at 2045 (CDT) hours, a defect (pinhole through-wall leak) was identified on the drain line for the LS 2-2365, HPCI TURBINE INLET DRAIN POT LEVEL SWITCH. The defect was identified during investigation of leakage near LS 2-2365. The LS 2-2365, HPCI TURBINE INLET DRAIN POT LEVEL SWITCH, is provided to detect a failure of the HPCI steam trap during standby line-up. The location of the defect, is in Class 2 Safety related piping. HPCI is a single train safety system and this notification is being made in accordance with 10CFR50.72(b)(3)(v)(D). The instrument isolations for LS 2-2365 have been close and the leak has been isolated. There is no increase to plant risk and RCIC (Reactor Core Isolation Cooling) is available. The licensee will inform the NRC Resident Inspector.

  • * * RETRACTION ON 11/7/13 AT 1412 EST FROM JEFFERY JACOBSON TO DONG PARK * * *

The purpose of this notification is to retract the ENS report made on October 4, 2013, at 0212 EDT (ENS Report # 49407). Upon further investigation the pinhole through-wall leak discovered in the Unit 2 HPCI room was in a weld at a 'Tee' downstream of the Unit 2 HPCI turbine inlet drain pot level switch (LS 2-2365) on drain line 2-2386B-1-B. The defect was characterized as a 1/16-inch rounded hole due to gas porosity (with no evidence of cracking). A subsequent evaluation performed by Quad Cities Station considering the defect size, location, and characterization confirmed the Unit 2 High Pressure Coolant Injection (HPCI) system would have performed its safety function when required. Based on this subsequent evaluation, ENS Report # 49407 is being retracted. Note: On October 3, 2013, at 1155 CDT the Unit 2 HPCI drain line leak was isolated and HPCI was declared operable. The licensee has notified the NRC Resident Inspector. Notified R3DO (Lipa).

Through-Wall Leak
ENS 4891611 April 2013 18:00:00Degraded Electrical Connections

On April 11, 2013, at 1300 hours, during the performance of On-Line Automatic Depressurization System (ADS) Blowdown Logic Testing, two poor wiring connections were identified (the electrical leads were not properly compressed at their termination point). The electrical leads are associated with the B and C ADS valves. Quad Cities has five ADS valves which can be used to depressurize the Reactor Pressure Vessel under accident conditions. While the solenoids of these valves were actuated successfully during the recent Unit 1 refueling outage (which ended on April 8, 2013), the less than optimum configuration could have prevented the valves from actuating under design basis conditions. The degraded wiring for both valves was restored at 1741 hours (CDT). Given the potential impact on the ADS depressurization function, this event is reportable under 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 6/3/13 AT 1138 EDT FROM FRED SWIHART TO DONG PARK * * *

The purpose of this notification is to retract the ENS Report made on April 11, 2013, at 2110 EDT (ENS Report # 48916). Further evaluation performed by Quad Cities Station confirms the Unit 1, 3B and 3C Automatic Depressurization System (ADS) valves would have performed their safety functions when required. Based on this subsequent evaluation, ENS Report # 48916 is being retracted. Note: On April 11, 2013, at 1741 CDT the degraded wiring for the Unit 1, 3B and 3C ADS valves was repaired and both valves were returned to operable status. The licensee notified the NRC Resident Inspector. Notified R3DO (Orth).

ENS 4810815 July 2012 15:30:00Unit 1 High Pressure Coolant Injection (Hpci) Inoperable Due to Valve Leak

On July 15, 2012, at 1030 hours, a defect (pinhole through-wall leak) was identified on the 1-2301-29 valve (HPCI Steam Line to Main Condenser Isolation Valve). The defect was identified during a routine system walkdown. The 1-2301-29 valve (1" valve downstream of the HPCI drain pot) is normally open during HPCI standby operation and closes upon system initiation. Due to the location of the defect, the 1-2301-29 valve would not have completely isolated the steam line as designed. As a result, HPCI was declared inoperable. Given that HPCI is a single train system, this notification is being made in accordance with 10CFR50.72(b)(3)(v)(D). HPCI will remain inoperable until system repairs are complete. The NRC Resident Inspector has been informed.

  • * * RETRACTION AT 1216 EDT ON 8/17/2012 FROM DALE STEEL TO MARK ABRAMOVITZ * * *

The purpose of this notification is to retract the ENS Report made on July 15, 2012, at 1030 hours (ENS Report # 48108). Further evaluation performed by Quad Cities Station confirms the Unit 1 HPCI system would have performed its safety function. Based on this subsequent evaluation, ENS Report # 48108 is being retracted. Note: On July 21, the 1-2301-29 valve (HPCI Steam Line to Main Condenser Isolation Valve) was successfully repaired and HPCI was returned to Operable status. The licensee notified the NRC Resident Inspector. Notified the R3DO (Giessner).

Through-Wall Leak
ENS 4317720 February 2007 23:20:00Hpci Declared Inoperable Due to an Apparent Equipment Malfunction

On February 20, 2007 at 1720 hours, the High Pressure Coolant Injection (HPCI) system was declared inoperable. During a system walkdown the HPCI Motor Speed Changer (MSC) was discovered energized. The MSC controls HPCI turbine speed during system startup and shutdown, and should not have been energized at the time of the walkdown. Additional troubleshooting determined the MSC was not functioning properly, rendering the HPCI system inoperable. This event is being reported as a condition that could have prevented fulfillment of a safety function in accordance with 10CFR50.72(b)(3)(v)(D) because the HPCI system is a single train system and the loss of HPCI could impact the plant's ability to mitigate the consequences of an accident. In accordance with Technical Specification Action 3.5.1.F, the Reactor Core Isolation Cooling (RCIC) system was confirmed operable. Further troubleshooting and engineering evaluations are continuing. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION AT 1146 ON 3/5/2007 FROM ERIK MARKS TO MARK ABRAMOVITZ * * *

The purpose of this report is to retract the ENS report made on February 20, 2007 at 1720 hours (ENS #43177) under 10CFR50.72(b)(3)(v)(D), a condition that could have prevented fulfillment of a safety function. The initial report was made when the Unit 2 High Pressure Coolant Injection (HPCI) system was declared inoperable following a system walkdown that discovered the HPCI Motor Speed Changer (MSC) was energized. The MSC controls HPCI turbine speed during system initiation, and should not have been energized at the time of the walkdown since the system was not in operation. During troubleshooting the MSC responded slower than expected. Due to this unexpected behavior, it was not certain if HPCI could have met its design basis requirements. However, a subsequent engineering evaluation has determined that at the time of discovery, the HPCI system injection time would have been sufficient to meet its safety function. Repairs to HPCI were completed and the system was declared operable on February 22, 2007 at 0036 hours. The licensee notified the NRC Resident Inspector. Notified the R3DO (Orth).

Time of Discovery
ENS 4312426 January 2007 15:15:00Control Room Emergency Ventilation Air Conditioning (Crev Ac) System Declared Inoperable

On January 26, 2007 at 0915 hours, the Control Room Emergency Ventilation Air Conditioning (CREV AC) system was declared inoperable due to not meeting the surveillance acceptance criteria for the refrigeration condensing unit (RCU) during QCOS 5750-11 (Control Room Emergency Ventilation System Test - performed every 2 years). As result Technical Specification 3.7.5 Condition "A" was entered (30 day Limiting Condition of Operation). The CREV AC system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the CREV system is a single train system, and loss of the CREV AC could impact the plant's ability to mitigate the consequences of an accident. At this time, additional analysis is underway to determine the impact of the failure to meet the acceptance criteria on the CREV AC safety function. The NRC Resident Inspector was notified of this event by the licensee.

  • * * RETRACTION 01/28/07 AT 1651 EST FROM C. KRONICH TO MACKINNON * * *

Further evaluation performed by Quad Cities Station confirms the CREV AC system would have performed its safety function. A revised surveillance (QCOS 5750-11, Control Room Emergency Ventilation System Test) was re-performed successfully, and the CREV AC system was declared operable on January 28, 2007 at 0911 hours. Based on the subsequent evaluation and surveillance testing, ENS report # 43124 is being retracted. R3DO (Dave Passehl) notified. The NRC Resident Inspector was notified of this retraction by the licensee.

ENS 4180127 June 2005 16:50:00Minimum Switchyard Voltage Requirements Not Met

At 1150 on June 27, 2005 Quad Cities Station was notified that the calculated post-LOCA switchyard voltage is below the minimum acceptable value required to ensure offsite power will remain available following a design basis accident. The appropriate Technical Specification Actions have been taken for both Units. The ability of the Emergency Diesel Generators to fulfill their design function is not affected by this condition. This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. Actual Switchyard voltage at the time of this notification is 356 Kv. The required minimum post-accident switchyard voltage for current conditions is 352.9 Kv for Unit-1 and 351 Kv for Unit-2, while the projected post-accident voltage which prompted this notification is 349.8 Kv. At 1320 hrs on June 27, the projected post-accident voltage was 351.3kV. This prediction satisfies the minimum Unit 2 voltage requirement, but is still below the minimum voltage for Unit 1. This notification is similar to the condition reported on April 29, 2005 (EN #41652) and June 11, 2005 (EN #41766). The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM J. COX TO W. GOTT 1906 ET 08/09/05 * * *

The purpose of this report is to retract ENS report #41652 (April 29, 2005), ENS report 41766 (June 11, 2005), and ENS report #41801 (June 27, 2005). The reports were made following notification that the switchyard predicted voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for the units, and an ENS notification was made for a condition that could have prevented the fulfillment of a safety function. Each Quad Cities unit has two sources of off-site power. For a specific unit, one source is from the switchyard through the unit's Reserve Auxiliary Transformer (RAT) and the second source is from the switchyard through the opposite unit's RAT. Following further analysis of the loading on the RATs during an accident, it was determined that only one source of offsite power to each unit should have been considered inoperable. The analysis determined that because the RAT for the non-accident unit (i.e., the offsite source supplied through the opposite unit) would be carrying a much smaller load, it would not be subject to a degraded voltage condition and resultant isolation from the grid. Therefore, an accident on one unit would not affect the operability of the source of offsite power supplied through the opposite unit's RAT. As a result, only the source of offsite power supplied through the unit's RAT was inoperable. With one source of offsite power available at all times, there was no condition present that could have prevented fulfillment of a safety function, and therefore, these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (R. Lanksbury)

ENS 4176611 June 2005 18:10:00Minimum Switchyard Voltage Requirements Not Met

At 1310 on June 11, 2005 Quad Cities Station was notified that the calculated post-LOCA switchyard voltage is below the minimum acceptable value required to ensure offsite power will remain available following a design basis accident. The appropriate Technical Specification Actions have been taken for both Units. The ability of the Emergency Diesel Generators to fulfill their design function is not affected by this condition. This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. Actual Switchyard voltage at the time of this notification is 356 Kv. The required minimum post-accident switchyard voltage for current conditions is 352.9 Kv for U-1 and 351 Kv for U-2, while the projected post-accident voltage which prompted this notification is 347.4 Kv. This notification is similar to the condition reported on March 24, 2005 (EN #41524), April 4, 2005 (EN #41562) and April 11, 2005 (EN #41587). Both Units entered T.S. 3.8.1 which requires verification of EDG operability (completed) and continued monitoring of line voltages with restoration of at least one offsite-line to the required minimum within 24-hours. The licensee informed the NRC Resident Inspector.

  • * * UPDATE 1610 EDT ON 6/11/05 FROM RON RUSTICK TO S. SANDIN * * *

At 1505 CDT both Units exited T.S. 3.8.1 when projected post-accident line voltage reached 353.8 kV. Notified R3DO (Lara).

  • * * RETRACTION FROM J. COX TO W. GOTT 1906 ET 08/09/05 * * *

The purpose of this report is to retract ENS report #41652 (April 29, 2005), ENS report 41766 (June 11, 2005), and ENS report #41801 (June 27, 2005). The reports were made following notification that the switchyard predicted voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for the units, and an ENS notification was made for a condition that could have prevented the fulfillment of a safety function. Each Quad Cities unit has two sources of off-site power. For a specific unit, one source is from the switchyard through the unit's Reserve Auxiliary Transformer (RAT) and the second source is from the switchyard through the opposite unit's RAT. Following further analysis of the loading on the RATs during an accident, it was determined that only one source of offsite power to each unit should have been considered inoperable. The analysis determined that because the RAT for the non-accident unit (i.e., the offsite source supplied through the opposite unit) would be carrying a much smaller load, it would not be subject to a degraded voltage condition and resultant isolation from the grid. Therefore, an accident on one unit would not affect the operability of the source of offsite power supplied through the opposite unit's RAT. As a result, only the source of offsite power supplied through the unit's RAT was inoperable. With one source of offsite power available at all times, there was no condition present that could have prevented fulfillment of a safety function, and therefore, these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (R. Lanksbury)

ENS 4165229 April 2005 12:32:00Minimum Switchyard Voltage Requirements Not Met

At 0732 (CDT) on April 29, 2005 Quad Cities Station was notified that the calculated post-LOCA switchyard voltage was below the minimum acceptable value required to ensure offsite power would remain available following a design basis accident. As a result, both offsite power sources were declared inoperable and the appropriate Technical Specification Actions were taken for both Units. The ability of the Emergency Diesel Generators to fulfill their design function was not affected by this condition. This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. The condition was exited at 0836 (CDT) on April 29, 2005. The required minimum post-accident switchyard voltage is 352.9 KV (Unit 1) and 351.0 KV (Unit 2) while the projected post accident voltage, which prompted this notification, was 347.9 KV. During this timeframe, actual switchyard voltage was approximately 358 KV. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM J. COX TO W. GOTT 1906 ET 08/09/05 * * *

The purpose of this report is to retract ENS report #41652 (April 29, 2005), ENS report 41766 (June 11, 2005), and ENS report #41801 (June 27, 2005). The reports were made following notification that the switchyard predicted voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for the units, and an ENS notification was made for a condition that could have prevented the fulfillment of a safety function. Each Quad Cities unit has two sources of off-site power. For a specific unit, one source is from the switchyard through the unit's Reserve Auxiliary Transformer (RAT) and the second source is from the switchyard through the opposite unit's RAT. Following further analysis of the loading on the RATs during an accident, it was determined that only one source of offsite power to each unit should have been considered inoperable. The analysis determined that because the RAT for the non-accident unit (i.e., the offsite source supplied through the opposite unit) would be carrying a much smaller load, it would not be subject to a degraded voltage condition and resultant isolation from the grid. Therefore, an accident on one unit would not affect the operability of the source of offsite power supplied through the opposite unit's RAT. As a result, only the source of offsite power supplied through the unit's RAT was inoperable. With one source of offsite power available at all times, there was no condition present that could have prevented fulfillment of a safety function, and therefore, these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (R. Lanksbury)

ENS 4158711 April 2005 18:40:00Minimum Switchyard Voltage Requirements Not Met

At 1240 on April 11, 2005 Quad Cities Station was notified calculated post-LOCA switchyard voltage is below the minimum acceptable value required to ensure offsite power will remain available following a design basis accident. The appropriate Technical Specification Actions have been taken for both Units. The ability of the Emergency Diesel Generators to fulfill their design function is not affected by this condition. This event is being reported in accordance with 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. Actual Switchyard voltage at the time of this notification is 361 Kv. The required minimum post-accident switchyard voltage is 348.4 Kv, while the projected post-accident voltage which prompted this notification is 346.3 Kv. This notification is similar to the condition reported on March 24, 2005 (EN #41524) and April 4, 2005 (EN #41562). The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM C. STEFFES TO M. RIPLEY 1556 EDT 04/13/05 * * *

The purpose of this report is to retract the following ENS reports: 1) ENS # 41524 on March 24, 2005; 2) ENS # 41562 on April 4, 2005; and 3) ENS # 41587 on April 11, 2005. These reports were made following notification to Quad Cities that the switchyard voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for both units, and an ENS notification was made for a condition that could have prevented fulfillment of a safety function. The events occurred when Unit 1 was in a refueling outage and Unit 2 was operating at 85% power. Subsequent Engineering analysis has determined that with a unit shutdown, and the large 4 Kv loads on that unit not running, the required minimum post-accident switchyard voltage is reduced to 339.3 kV (for the shutdown unit). Given the new minimum post-accident switchyard voltage, it was confirmed that there was a source of off-site power available to the Station. Specifically for all three events, the projected post-accident switchyard voltage (which ranged between 343 kV to 347.5 kV) was higher than the required minimum post-accident switchyard voltage (339.3 kV) for the shutdown unit. As a result, there was no condition present that could have prevented fulfillment of a safety function, and thus these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (J. Madera)

ENS 415624 April 2005 22:07:00Minimum Switchyard Voltage Requirements Not Met

The following information was obtained from the licensee via facsimile (licensee text in quotes): On April 4, 2005, at 1607 hours (CDT), Quad Cities was notified that the switchyard voltage was below that required to ensure that offsite power would remain available following a design basis accident. Both sources of off site power were declared inoperable. The appropriate Technical Specification required actions were taken for both units. The ability of the Emergency Diesel Generators to perform their design function is not affected by this condition. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. This notification report is similar to the condition reported on March 24, 2005 (reference EN#41524 for additional information). Technical Specification minimum switchyard voltage is 348.4 KV. Switchyard voltage at 1607 hrs. was approximately 343.7 KV. Switchyard voltage at the time of NRC notification was 358 KV which is above the Technical Specification minimum. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM C. STEFFES TO M. RIPLEY 1556 EDT 04/13/05 * * *

The purpose of this report is to retract the following ENS reports: 1) ENS # 41524 on March 24, 2005; 2) ENS # 41562 on April 4, 2005; and 3) ENS # 41587 on April 11, 2005. These reports were made following notification to Quad Cities that the switchyard voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for both units, and an ENS notification was made for a condition that could have prevented fulfillment of a safety function. The events occurred when Unit 1 was in a refueling outage and Unit 2 was operating at 85% power. Subsequent Engineering analysis has determined that with a unit shutdown, and the large 4 Kv loads on that unit not running, the required minimum post-accident switchyard voltage is reduced to 339.3 kV (for the shutdown unit). Given the new minimum post-accident switchyard voltage, it was confirmed that there was a source of off-site power available to the Station. Specifically for all three events, the projected post-accident switchyard voltage (which ranged between 343 kV to 347.5 kV) was higher than the required minimum post-accident switchyard voltage (339.3 kV) for the shutdown unit. As a result, there was no condition present that could have prevented fulfillment of a safety function, and thus these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (J. Madera)

ENS 4152424 March 2005 15:30:00Minimum Switchyard Voltage Requirements Not Met

The following information was obtained from the licensee via facsimile (licensee text in quotes): Minimum Switchyard Voltage Requirements Not Met On March 24, 2005, at 0930 hours, Quad Cities was notified that the switchyard voltage was below that required to ensure that offsite power would remain available following a design basis accident. Both sources of off-site power were declared inoperable. The appropriate Technical Specification required actions were taken for both units. The ability of the Emergency Diesel Generators to perform their design function is not affected by this condition. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function given the predicted post-LOCA switchyard voltage. A preliminary engineering assessment indicates that one source of offsite power was available. Additional confirmatory reviews are being performed to determine if the safety function was preserved. At this time, grid/switchyard voltage has been restored. Minimum switchyard voltage required is 348.4 KV. The analyzed minimum voltage which prompted notification to the NRC was 347.5 KV. Switchyard voltage at the time of this report was ~359 KV. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM C. STEFFES TO M. RIPLEY 1556 EDT 04/13/05 * * *

The purpose of this report is to retract the following ENS reports: 1) ENS # 41524 on March 24, 2005; 2) ENS # 41562 on April 4, 2005; and 3) ENS # 41587 on April 11, 2005. These reports were made following notification to Quad Cities that the switchyard voltage was below the required value necessary to ensure that offsite power would remain available following a design basis accident. For each event, both sources of offsite power were declared inoperable, the appropriate Technical Specification required actions were taken for both units, and an ENS notification was made for a condition that could have prevented fulfillment of a safety function. The events occurred when Unit 1 was in a refueling outage and Unit 2 was operating at 85% power. Subsequent Engineering analysis has determined that with a unit shutdown, and the large 4 Kv loads on that unit not running, the required minimum post-accident switchyard voltage is reduced to 339.3 kV (for the shutdown unit). Given the new minimum post-accident switchyard voltage, it was confirmed that there was a source of off-site power available to the Station. Specifically for all three events, the projected post-accident switchyard voltage (which ranged between 343 kV to 347.5 kV) was higher than the required minimum post-accident switchyard voltage (339.3 kV) for the shutdown unit. As a result, there was no condition present that could have prevented fulfillment of a safety function, and thus these events are not reportable. The licensee notified the NRC Resident Inspector. Notified R3 DO (J. Madera)

ENS 4113919 October 2004 23:30:00High Pressure Coolant Injection (Hpci) Inoperable Due to Controller Signal Converter Trouble.

On October 19, 2004 at approximately 1830 hours CDT, Unit One was performing QCOS 2300-05, Quarterly HPCI Pump Operability Test. This was being performed to prove operability following maintenance work on various valves and the turning motor gear unit. At this time when the HPCI turbine was rolled, the HPCI Signal Converter Trouble alarm was received. The HPCI Flow Controller demand controlled at approximately 7250 gpm instead of controlling at the desired 5600 gpm. HPCI was determined not to be operable and was shutdown per procedure. Due to the unexpected behavior of the HPCI Flow Controller, at this time it is not certain if the HPCI will meet its safety function. Therefore, we are reporting this event under 10 CFR 50.72 (b)(3)(v). Licensee entered Tech Spec 3.5.1.(f) 14 day Limiting Condition of Operation (LCO) for HPCI. Reactor Core Isolation Cooling (RICI) is operable. All other Emergency Core Cooling Systems (ECCS) and the Emergency Diesel Generators (EDG) are fully operable if needed. The NRC Resident Inspector was notified of this event by the licensee.

  • * * RETRACTION J. DAVIS TO W. GOTT AT 1819 ON 10/28/04 * * *

The purpose of this report is to retract the ENS report made on October 19, 2004 at 2237 CDT (ENS #41139). The initial report was made following HPCI operability testing in accordance with QCOS 2300-05, Quarterly HPCI Pump Operability Test. When the HPCI turbine was rolled, the HPCI Signal Converter Trouble alarm was received. The HPCI Flow Controller failed to control at the desired 5600 gpm (instead, the system ramped to 7250 gpm). Due to the unexpected behavior, it was not certain at the time if HPCI could have met its design basis requirements. However, a subsequent review of this event has determined that HPCI would have performed its safety function. The Signal Converter failed in a manner that prevented automatic flow control, but did not prevent HPCI from initiating and ramping to full flow (i.e., the turbine high speed stop). In this condition, HPCI would have met corresponding Technical Specifications and Accident Analysis requirements. The circuit board was replaced and the Signal Converter and flow controller feedback loop were re-calibrated. The Unit 1 HPCI turbine's automatic flow control was successfully tested on October 20, 2004. The Licensee notified the NRC Resident Inspector. Notified R3DO (R. Garner)