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Category:Letter type:RA
MONTHYEARRA24-008, Post-Outage Inservice Inspection (ISI) Summary Report2024-06-20020 June 2024 Post-Outage Inservice Inspection (ISI) Summary Report RA24-023, Response to NRC LaSalle County Station, Units 1 and 2, Integrated Inspection Report 05000373/2024001 and 05000374/20240012024-06-12012 June 2024 Response to NRC LaSalle County Station, Units 1 and 2, Integrated Inspection Report 05000373/2024001 and 05000374/2024001 RA24-011, 2023 Annual Radiological Environmental Operating Report2024-05-0303 May 2024 2023 Annual Radiological Environmental Operating Report RA24-009, 2023 Annual Radioactive Effluent Release Report2024-04-26026 April 2024 2023 Annual Radioactive Effluent Release Report RA24-010, Annual Dose Report for 20232024-04-24024 April 2024 Annual Dose Report for 2023 RA24-006, Cycle 21 Core Operating Limits Reports2024-03-11011 March 2024 Cycle 21 Core Operating Limits Reports RA23-072, Regulatory Commitment Change Summary Report2023-12-15015 December 2023 Regulatory Commitment Change Summary Report RA23-057, Registration of Use of Cask to Store Spent Fuel2023-08-11011 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-055, Registration of Use of Cask to Store Spent Fuel2023-08-11011 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-052, Registration of Use of Cask to Store Spent Fuel2023-08-0404 August 2023 Registration of Use of Cask to Store Spent Fuel RA23-051, Registration of Use of Cask to Store Spent Fuel2023-07-21021 July 2023 Registration of Use of Cask to Store Spent Fuel RA23-048, Registration of Use of Cask to Store Spent Fuel2023-07-14014 July 2023 Registration of Use of Cask to Store Spent Fuel RA23-045, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2023-06-30030 June 2023 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation RA23-047, Registration of Use of Cask to Store Spent Fuel2023-06-30030 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-018, Post-Outage Inservice Inspection (ISI) Summary Report2023-06-27027 June 2023 Post-Outage Inservice Inspection (ISI) Summary Report RA23-046, Registration of Use of Cask to Store Spent Fuel2023-06-23023 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-042, Registration of Use of Cask to Store Spent Fuel2023-06-16016 June 2023 Registration of Use of Cask to Store Spent Fuel RA23-029, 2022 Annual Radiological Environmental Operating Report2023-05-12012 May 2023 2022 Annual Radiological Environmental Operating Report RA23-028, Submittal of 2022 Annual Radioactive Effluent Release Report2023-04-28028 April 2023 Submittal of 2022 Annual Radioactive Effluent Release Report RA23-027, Annual Dose Report for 20222023-04-21021 April 2023 Annual Dose Report for 2022 RA23-025, Post Accident Monitoring Report2023-04-0707 April 2023 Post Accident Monitoring Report RA23-013, Submittal of Triennial Chlorine Survey Report2023-03-30030 March 2023 Submittal of Triennial Chlorine Survey Report RA23-019, Cycle 20 Core Operating Limits Reports2023-03-21021 March 2023 Cycle 20 Core Operating Limits Reports RA22-066, 150 Day Submittal Cover Letter2022-12-0202 December 2022 150 Day Submittal Cover Letter RA22-060, Regulatory Commitment Change Summary Report2022-11-30030 November 2022 Regulatory Commitment Change Summary Report RA22-051, Submittal of the Snubber Program Plan for the Fourth 10-Year Interval2022-11-16016 November 2022 Submittal of the Snubber Program Plan for the Fourth 10-Year Interval RA22-041, Unit 2 Cycle 19 Core Operating Limits Report Revision2022-10-0505 October 2022 Unit 2 Cycle 19 Core Operating Limits Report Revision RA22-029, Cycle 20 Startup Test Report Summary2022-06-10010 June 2022 Cycle 20 Startup Test Report Summary RA22-021, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2022-06-0808 June 2022 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA22-020, Annual Radiological Environmental Operating Report2022-05-13013 May 2022 Annual Radiological Environmental Operating Report RA22-018, Annual Dose Report for 20212022-04-22022 April 2022 Annual Dose Report for 2021 RA22-010, Cycle 20 Core Operating Limits Reports2022-03-21021 March 2022 Cycle 20 Core Operating Limits Reports RA21-059, Regulatory Commitment Change Summary Report2021-11-30030 November 2021 Regulatory Commitment Change Summary Report RA21-050, Completion of License Renewal Activities Prior to Entering the Period of Extended Operation2021-11-0909 November 2021 Completion of License Renewal Activities Prior to Entering the Period of Extended Operation RA21-051, County Station Physical Security Plan (Revision 18)2021-09-29029 September 2021 County Station Physical Security Plan (Revision 18) RA21-052, Registration of Use of Cask Store Spent Fuel2021-09-17017 September 2021 Registration of Use of Cask Store Spent Fuel RA21-046, Registration of Use of Cask to Store Spent Fuel2021-08-0505 August 2021 Registration of Use of Cask to Store Spent Fuel RA21-043, Cycle 19 Startup Test Report Summary2021-07-15015 July 2021 Cycle 19 Startup Test Report Summary RA21-031, 2020 Annual Radiological Environmental Operating Report2021-05-13013 May 2021 2020 Annual Radiological Environmental Operating Report RA21-029, Unit 2 - 2020 Annual Radioactive Effluent Release Report2021-04-29029 April 2021 Unit 2 - 2020 Annual Radioactive Effluent Release Report RA21-026, Annual Dose Report for 20202021-04-22022 April 2021 Annual Dose Report for 2020 RA21-016, Netco Rack Insert 10-year Surveillance Report2021-04-15015 April 2021 Netco Rack Insert 10-year Surveillance Report RA21-017, Post-Outage 90-Day Inservice Inspection (ISI) Summary Report2021-04-0909 April 2021 Post-Outage 90-Day Inservice Inspection (ISI) Summary Report RA21-019, Unit 2 Cycle 19 Core Operating Limits Reports2021-04-0707 April 2021 Unit 2 Cycle 19 Core Operating Limits Reports RA20-058, Licensee Post Exam Submittal Letter2020-12-0202 December 2020 Licensee Post Exam Submittal Letter RA20-044, Unit 2 - Unit 1 Cycle 19 Core Operating Limits Report2020-09-10010 September 2020 Unit 2 - Unit 1 Cycle 19 Core Operating Limits Report RA20-026, 2019 Annual Radiological Environmental Operating Report2020-05-13013 May 2020 2019 Annual Radiological Environmental Operating Report RA20-023, Annual Dose Report for 20192020-04-28028 April 2020 Annual Dose Report for 2019 RA20-016, Corrected Drawing for One-Line Electrical Power Supply for Containment Vent System Final Integrated Plan2020-03-24024 March 2020 Corrected Drawing for One-Line Electrical Power Supply for Containment Vent System Final Integrated Plan RA20-015, Triennial Chlorine Survey Report2020-03-20020 March 2020 Triennial Chlorine Survey Report 2024-06-20
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Exelon Generation Company, LLC www.exeloncorp.com Nuclear LaSalle County Station 2601 North 21" Road Marseilles, IL 61341-9757 RA-08-030 April 29, 2008 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 LaSalle County Station Unit 2 Facility Operating License No. NPF-18 NRC Docket Nos. 50-374
Subject:
Technical Specifications Section 5.6.6, "Post Accident Monitoring Instrumentation Report" The purpose of this letter is to submit a Post Accident Monitoring Instrumentation Report as required by LaSalle County Station (LSCS) Technical Specifications (TS) Section 5.6.6, "Post Accident Monitoring (PAM) Instrumentation Report."
On March 16, 2008, during the performance of LOS-RP-Q3, "Main Steam Isolation Valve Scram Functional Test," on Unit 2, the closed indication for the 2B inboard Main Steam Isolation Valve (MSIV) (2B21 -F022B) did not illuminate as expected. The Reactor Protection System function worked as expected during the surveillance test.
This discrepancy of an inoperable indication channel for Function 6 in Table 3.3.3.1-1, "Penetration Flow Path PCIV Position," required entry into TS Section 3.3.3.1, "Post Accident Monitoring (PAM) Instrumentation," Condition A for one or more Functions with one required channel inoperable, with a Required Action to restore the channel to OPERABLE status within 30 days.
Restoration of the channel within the 30-day requirement was not feasible due to the significant power reduction and containment entry required to perform the necessary troubleshooting and repairs. If the Required Action and associated Completion Time of TS 3.3.3.1 Condition A cannot be met, Condition B must immediately entered with a Required Action to initiate action in accordance with Specification 5.6.6.
In accordance with TS Section 5.6.6, a report shall be submitted within 14 days outlining the preplanned alternate method of monitoring, the cause of the inoperability, and the plans and schedule for restoring the instrument channel to an operable status. The attached report contains the required information.
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Should you have any questions concerning this matter, please contact Mr. Terrence Simpkin at (815) 415-2800.
Respectfully, Danie .Eright6 Site Vice President LaSalle County Station Attachment cc: Regional Administrator - NRC Region III NRC Senior Resident Inspector - LaSalle County Station
Post Accident Monitoring (PAM) Instrumentation Report Inoperable Channel For Penetration Flow Path PCIV Position Preplanned Alternate Method of Monitoring An alternate method of monitoring the isolation function of the 2B inboard Main Steam Isolation Valve (MSIV) has been implemented. The alternate method is to verify that Process Computer point D449 indicates 'valve closed" for 2B21-F022B. Computer point D449 is fed from a different set of contacts on the same limit switch (Limit Switch 1) that is fully functional. These contacts operate at the same values (91% moving closed and 94% moving open) as the failed
'valve closed" indication.
The alternate method was verified to work properly during the March 16, 2008, occurrence.
Apparent Cause of the Inoperability The most likely cause is that the limit switch contacts have not made up for a closed indication.
The limit switch is located in the drywell, and there is no further troubleshooting that can be performed without a significant power reduction and a containment entry to confirm the origin of this indication discrepancy.
Plans and Schedule for Returninq Function to Operable Status LaSalle County Station (LSCS) is planning on restoring the 2B MSIV indication channel to an OPERABLE status during the next refueling outage on Unit 2 (L2R1 2), scheduled for March 2, 2009, or at the next Unit 2 forced outage that requires a drywell entry to return the Unit to service.