05000328/LER-2021-002, Turbine Trio Function Inoperable Due to Slow to Close Turbine Throttle Valve
| ML22006A232 | |
| Person / Time | |
|---|---|
| Site: | Sequoyah (DPR-079) |
| Issue date: | 01/06/2022 |
| From: | Marshall T Tennessee Valley Authority |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| LER 2021-002-00 | |
| Download: ML22006A232 (7) | |
| Event date: | |
|---|---|
| Report date: | |
| Reporting criterion: | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
| 3282021002R00 - NRC Website | |
text
l\\14 TENNESSEE VALLEY AUTHORITY Sequoyah Nuclear Plant, Post Office Box 2000, Soddy Daisy, Tennessee 37384 January 06, 2022 ATTN : Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Sequoyah Nuclear Plant, Unit 2 Renewed Facility Operating License No. DPR-79 NRC Docket No. 50-328 10 CFR 50.73
Subject:
Licensee Event Report 50-328/2021-002-00, Turbine Trip Function Inoperable Due to Slow to Close Turbine Throttle Valve The enclosed licensee event report provides details concerning a slow to close turbine throttle valve that impacted the turbine trip function's response time to trip. This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B), as any operation or condition which was prohibited by the plant's Technical Specifications and in accordance with 10 CFR 50. 73(a)(2)(v), as an event or condition that could have prevented the fulfillment of a safety function of structures or systems that are needed to: (D) mitigate the consequences of an accident.
There are no regulatory commitments contained in this letter. Should you have any questions concerning this submittal, please contact Mr. Jeffrey Sowa, Site Licensing Manager, at (423) 843-8129.
Respectfu I ly, Digitally signed by Marshall, Marshall, Thomas B. Thomas B.
Date: 2022.01.06 10:32:39 -05'00' Thomas Marshall Site Vice President Sequoyah Nuclear Plant Enclosure: Licensee Event Report 50-328/2021-002-00 cc:
NRC Regional Administrator-Region II NRC Senior Resident Inspector-Sequoyah Nuclear Plant
Abstract
On October 28, 2021, Main Steam Throttle Valve 1 (TV-1 ), associated with the high-pressure turbine and turbine trip function, was replaced during the Unit 2 refueling outage. On November 5, Surveillance Requirement 3.3.2.9 was successfully completed for the Turbine Trip function. On November 8, at 2115 eastern standard time (EST),
during turbine overspeed trip testing, it was identified that TV-1 took longer than expected to close on the overspeed trip signal. In response, station personnel developed a support/refute matrix that included validating installation of an orifice block vice a flushing block in TV-1. This led to the discovery that TV-1 was installed with the incorrect block. The flushing block was replaced with the correct orifice block. On November 9, at 0700, SR 3.3.2.9 was successfully completed restoring the valve to operable status.
The cause of the event was the failure to follow procedural requirements regarding a quality critical maintenance (QCM) step. The maintenance procedure addressing quality critical maintenance requires that supervision/oversight must be present in the field during the execution of steps requiring additional oversight.
Contrary to this requirement, The TVA QCM signee performed the step in an independent verification role vice providing oversight and witnessing the installation of the correct orifice plate. Corrective actions included providing a briefing for Outage Services personnel regarding oversight responsibilities associated with QCM steps and revising the vendor's procedure "Critical Step" with photos and guidance to visually confirm and photograph blocks when installing.
I.
Plant Operating Conditions Before the Event
At the time of the event, Sequoyah Nuclear Plant (SON) Unit 2 was in Mode 1 at approximately 15 percent rated thermal power.
- 11.
Description of Event
A.
Event Summary
On October 28, 2021, Main Steam [EIIS: SB] Throttle Valve-1 (TV-1) [EIIS: SCV], associated with the high-pressure turbine [EIIS: TRB] and turbine trip [EIIS: JJ] function, was replaced during the Unit 2 refueling outage. On November 5, Surveillance Requirement 3.3.2.9 (Verify ESFAS [Engineered Safety Feature Actuation System] RESPONSE TIMES are within limit) was successfully completed for the Turbine Trip function.
On November 8, at 2115 eastern standard time (EST), during turbine overspeed trip testing, it was identified that TV-1 took longer than expected to close on the overspeed trip signal. During subsequent testing, TV-1 continued to close slower than expected. In response, station personnel developed a support/refute matrix that included validating installation of an orifice block vice a flushing block in TV-1. This led to the discovery that TV-1 was installed with the incorrect block.
The flushing block was replaced with the correct orifice block.
On November 9, at 0700, SR 3.3.2.9 was successfully completed restoring the valve to operable status. At 0745 a partial performance of turbine overspeed testing confirmed TV-1 was functioning as required.
During the Unit 2 refueling outage, TV-1 was one of several turbine control system valves replaced. Valves received from the vendor typically arrive with flushing blocks installed and are clearly labeled as such. Two of the replacement valves were received with labeled flushing blocks attached. TV-1 was received from the vendor without a labeled flushing block that appeared to be and was assumed to be the required orifice block for the valve. Total reliance was placed on the vendor method for labeling flushing blocks.
The delta in closing times between the November 5th ESFAS testing and the November 8th turbine overspeed testing is most probably the result of different system alignments during the tests. During the performance of ESFAS testing, the four main steam throttle valves are manipulated with the governor valves remaining closed and isolated from the Electrohydraulic Control (EHC) System. Whereas, during the performance of turbine overspeed trip testing, all the throttle valves and governor valves are manipulated. It is possible that additional flow in the EHC trip header, due to flow from the additional valves, could cause increased backpressure on the throttle drain to the trip header. With the flushing block installed on TV-1 rather than the required orifice, it is possible the backpressure on TV-1 could reduce the effectiveness of draining EH fluid to the trip header. This reduced flow would in turn slow the response of TV-1 to close. A condition report (CR) was initiated to evaluate if the system Page 2 of 6 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 (08-2020)
- 3. LER NUMBER YEAR SEQUENTIAL REV Sequoyah Nuclear Plant Unit 2 05000-328 NUMBER NO.
2021
- - 002
- - 00 alignment for surveillance testing and turbine overspeed testing should be similar.
A past operability evaluation (POE) determined TV-1 was inoperable from Mode 3 entry on November 5, 2021, at 0519 until November 9, 2021, at 0700, when turbine trip response time testing was completed with acceptance criteria met. Therefore, this event is reportable per 10 CFR 50. 73(a)(2)(i)(B) as any operation or condition which was prohibited by the plant's technical specifications. Additionally, the POE determined the turbine trip function requires four out of four throttle valves to close, and with TV-1 inoperable, the turbine trip function would not have been performed within the required 2.5 seconds (per the Final Safety Analysis Report (FSAR)). This constitutes an event or condition that could have prevented the fulfillment of a safety function necessary to mitigate the consequences of an accident, which is reportable under 10 CFR 50. 73(a)(2)(v)(D).
B.
Status of structures, components, or systems that were inoperable at the start of the event and contributed to the event:
No inoperable structures, components, or systems contributed to this event.
C.
Dates and approximate times of occurrences
Date/Time (EST)
Description
10/28/21 TV-1 installed during outage.
11/05/21, 0519 Unit 2 entered Mode 3 which required TV-1 to be operable; however, it was not.
1039 Turbine trip response time testing was completed with acceptance criteria met.
11/07/21, 0601 Unit 2 entered Mode 2 with TV-1 inoperable.
2253 Unit 2 entered Mode 1 with TV-1 inoperable.
11/08/21, 2115 CR 1734714 was initiated documenting the slow response of TV-1 observed during main turbine overspeed trip testing.
11/09/21, 0342 Mechanical Maintenance technicians found a flushing block installed in TV-1 and replaced it with the correct orifice block.
0700 Turbine trip response time testing was completed with acceptance criteria met.
0745 Main turbine overspeed trip testing was performed with acceptance criteria met. Page 3 of 6 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 (08-2020)
- 3. LER NUMBER YEAR Sequoyah Nuclear Plant Unit 2 05000-328 2021 D.
Manufacturer and model number of each component that failed during the event
There was no component that failed during the event.
E.
Other systems or secondary functions affected
There were no other systems or secondary functions affected by this event.
F.
Method of discovery of each component or system failure or procedural error
SEQUENTIAL NUMBER
- - 002 REV NO.
- - 00 Station personnel developed a support/refute matrix that included validating installation of the orifice block vice the flushing block in TV-1. This led to the discovery that TV-1 was installed with the incorrect block.
G.
Failure mode, mechanism, and effect of each failed component:
There was no component that failed during the event.
H.
Operator actions
Operators initiated CR 1734714 for TV-1 due to its slow closure time during main turbine overspeed trip testing.
I.
Automatically and manually initiated safety system responses
None.
111.
Cause of the Event
A.
Cause of each component or system failure or personnel error
The human performance factor related to this event was associated with supervision and oversight. The oversight requirement was to witness a step being performed vice verifying a step was performed.
B.
The cause of the event was the failure to follow procedural requirements regarding a quality critical maintenance (QCM) step. The maintenance procedure addressing quality critical maintenance requires that supervision/oversight must be present in the field during the execution of steps requiring additional oversight. Contrary to this requirement, The TVA QCM signee performed the step in an independent verification role vice providing oversight and witnessing the installation of the correct orifice plate.
The individual responsible for QCM oversight during the TV-1 valve replacement was a non-licensed, TVA employee in the Components Maintenance Optimization group. There were no schedule or situational pressures present. Page 4 of 6 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 (08-2020)
- 3. LER NUMBER Sequoyah Nuclear Plant Unit 2 05000-328 YEAR SEQUENTIAL NUMBER REV NO.
2021
- - 002
- - 00 IV.
Analysis of the Event
The primary functions of the Turbine Trip and Feedwater Isolation signals are to prevent damage to the turbine due to water in the steam lines, and to stop the excessive flow of feedwater into the steam generators (SGs). These Functions are necessary to mitigate the effects of a high-water level in the SGs, which could result in carryover of water into the steam lines and excessive cooldown of the primary system. Turbine Trip and Feedwater Isolation functions must be operable in Modes 1, 2, and 3 except when all main feedwater (MFW) isolation valves (MFIVs), MFW regulation valves (MFRVs), and associated MFRV bypass valves are closed or isolated by a closed manual valve when the MFW System is in operation and the turbine generator may be in operation.
Turbine Trip and Feedwater Isolation is also initiated by all Functions that initiate a Safety Injection (SI) signal.
Turbine trip is a required part of ESFAS as outlined in TS 3.3.2. The response time testing requirement for turbine trip is 2.5 seconds per the FSAR. TS 3.3.2 requires that the throttle valves close in 1.1 seconds (SR 3.3.2.9) so that, when combined with the other trip logic in a turbine trip signal, the overall response time testing requirement is met. The turbine trip function requires four-out-of-four throttle valves to close.
While the turbine was latched, the main turbine governor valves were available to remove steam flow from the main turbine. These valves function as a series valve to the throttle valves and receive the same trip signal that is supplied to the throttle valves. These valves are not response time tested, but at the time of this event, were all functioning correctly which includes tripping closed in a similar time to the throttle valve's design time. Additionally, there was no challenge with the Feedwater Isolation function or MSIVs. With the MSIVs available, the capability existed to mitigate a cooldown event by isolating all steam supplied from the reactor to the secondary plant.
V.
Assessment of Safety Consequences
There were no actual safety consequences because of this event. With TV-1 inoperable, there were additional methods to stop steam flow to the main turbine. One is by closure of the main turbine governor valves, and another, is closure of the MSIVs. In the event a turbine overspeed event occurred and turbine "missiles" released, the projected paths would not have been expected to damage the main control room or key safety related systems. A probabilistic risk assessment determined that increase to risk for Core Damage Frequency or Large Early Release Frequency is very small.
A.
Availability of systems or components that could have performed the same function as the components and systems that failed during the event:
With TV-1 inoperable, there were additional methods to stop steam flow to the main turbine, closure of the main turbine governor valves, and another, closure of the MS IVs. Page 5 of 6 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY 0MB: NO. 3150-0104 EXPIRES: 08/31/2023 (08-2020)
- 3. LER NUMBER YEAR Sequoyah Nuclear Plant Unit 2 05000-328 2021 SEQUENTIAL NUMBER
- - 002 B.
For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residual heat, control the release of radioactive material, or mitigate the consequences of an accident:
The event did not occur when the reactor was shut down.
C.
For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from discovery of the failure until the train was returned to service:
Operators documented the slow closure of TV-1 on November 8 at 2115. The valve was returned to operable status on November 9 at 0700. The elapsed time was 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> 45 minutes.
VI.
Corrective Actions
The event was entered into the Tennessee Valley Authority Corrective Action Program (CAP) under CRs 1734714 and 1734963.
A.
Immediate Corrective Actions
An extent of condition was performed for additional valves replaced during the Unit 2 refueling outage. Performed reaffirmation with personnel involved that QCM witness roles are for providing additional oversight of the performance of an evolution. It is not a concurrent or independent verification process.
B.
Corrective Actions to Prevent Recurrence or to reduce probability of similar events occurring in the future:
Corrective actions included providing a briefing for Outage Services personnel regarding oversight responsibilities associated with QCM steps and revising the vendor's procedure "Critical Step" with photos and guidance to visually confirm and photograph blocks when installing.
VII.
Previous Similar Events at the Same Site
There were no previous similar events at SQN occurring within the last three years.
VIII. Additional Information
There is no additional information.
IX.
Commitments
There are no commitments.
REV NO.
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