ML20249C801
ML20249C801 | |
Person / Time | |
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Site: | Salem |
Issue date: | 12/02/1976 |
From: | Dreher F, Roy G, Thompson D NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
To: | |
References | |
PNO-76-204, NUDOCS 9807010215 | |
Download: ML20249C801 (2) | |
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Category:PRELIMINARY NOTIFICATION OF EVENT OR OCCURRENCE (PNO
MONTHYEARPNO-I-99-043, on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power1999-09-16016 September 1999
[Table view]PNO-I-99-043:on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power PNO-I-98-057, on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal1998-12-0101 December 1998 PNO-I-98-057:on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal PNO-I-93-068, on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R)1993-12-0707 December 1993 PNO-I-93-068:on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R) PNO-I-93-062, on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan1993-11-12012 November 1993 PNO-I-93-062:on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan PNO-I-93-060, on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified1993-11-0303 November 1993 PNO-I-93-060:on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified PNO-I-93-032, on 930627, Licensee Resolved Latest Issue Re Card Failures in Rod Control Power Cabinet.Licensee Completed Root Cause Evaluation & Briefed AIT on Site.Press Release Planned within 2 Wks1993-06-28028 June 1993 PNO-I-93-032:on 930627, Licensee Resolved Latest Issue Re Card Failures in Rod Control Power Cabinet.Licensee Completed Root Cause Evaluation & Briefed AIT on Site.Press Release Planned within 2 Wks PNO-I-93-030, during Startup of Plant from Recent Refueling Outage Multiple Failures Experienced in Sys. Augmented Insp Team Dispatched to Investigate Failures.Team Expects to Complete Work in 1 Wk1993-06-0707 June 1993 PNO-I-93-030:during Startup of Plant from Recent Refueling Outage Multiple Failures Experienced in Sys. Augmented Insp Team Dispatched to Investigate Failures.Team Expects to Complete Work in 1 Wk PNO-I-92-075, upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes1992-12-15015 December 1992 PNO-I-92-075:upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes PNO-I-90-056, on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed1990-07-23023 July 1990 PNO-I-90-056:on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed PNO-I-90-043, on 900523,supervisor W/No Operations Responsibilities Failed Random Alcohol Test W/Presence of Alcohol Above Program Limits (.04).Site Access Suspended & Individual Entered Licensee Rehabilitation Program1990-05-25025 May 1990 PNO-I-90-043:on 900523,supervisor W/No Operations Responsibilities Failed Random Alcohol Test W/Presence of Alcohol Above Program Limits (.04).Site Access Suspended & Individual Entered Licensee Rehabilitation Program PNO-I-88-020, on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom1988-02-16016 February 1988 PNO-I-88-020:on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom ML20217F8541987-10-27027 October 1987 PNS-I-87-017:on 871026,fireman Received Call of Bomb Threat at Plant.Search of Facility Proved Negative PNO-I-87-099, on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway1987-10-26026 October 1987 PNO-I-87-099:on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway PNO-I-87-075A, on 870812,visual Insp Identified No Significant Corrosion of Reactor Vessel Studs After Finding Leak on 870807.Further Insp of Degraded Vessel Components Will Be Formalized After Cleaning Affected Areas1987-08-13013 August 1987 PNO-I-87-075A:on 870812,visual Insp Identified No Significant Corrosion of Reactor Vessel Studs After Finding Leak on 870807.Further Insp of Degraded Vessel Components Will Be Formalized After Cleaning Affected Areas PNO-I-87-060, on 870703,unit Removed from Svc to Make Repairs to Low Pressure Turbines 21 & 22.Unit Being Maintained in Hot Shutdown.Licensee Expects to Complete Turbine Gasket Repairs within 14 Days1987-07-0606 July 1987 PNO-I-87-060:on 870703,unit Removed from Svc to Make Repairs to Low Pressure Turbines 21 & 22.Unit Being Maintained in Hot Shutdown.Licensee Expects to Complete Turbine Gasket Repairs within 14 Days PNO-I-87-059, on 870626,operators Received High Vibration Alarm on Bearing 6 of Low Pressure Turbine 22.Bearing Vibration Increased & High Pitched Noise Discovered.Licensee Elected to Remove Unit from Svc1987-06-26026 June 1987 PNO-I-87-059:on 870626,operators Received High Vibration Alarm on Bearing 6 of Low Pressure Turbine 22.Bearing Vibration Increased & High Pitched Noise Discovered.Licensee Elected to Remove Unit from Svc PNO-I-87-038, on 870429,licensee Learned That Control Room Operator Tested Positive for Use of Controlled Substance. Employee Will Be Terminated.Individual Acceptance Into Rehabilitation Program Under Consideration1987-04-29029 April 1987 PNO-I-87-038:on 870429,licensee Learned That Control Room Operator Tested Positive for Use of Controlled Substance. Employee Will Be Terminated.Individual Acceptance Into Rehabilitation Program Under Consideration PNO-I-86-075, on 860916,operators Removed Unit 1 from Svc to Repair Steam Leak on High Pressure Turbine Steam Return Line.Leak Caused by Steam Erosion on Section of 20-inch Pipe.Affected Section of Pipe Replaced1986-09-18018 September 1986 PNO-I-86-075:on 860916,operators Removed Unit 1 from Svc to Repair Steam Leak on High Pressure Turbine Steam Return Line.Leak Caused by Steam Erosion on Section of 20-inch Pipe.Affected Section of Pipe Replaced PNO-I-86-073, on 860911,Unit 2 Tripped from 75% Power.Caused by Loss of Reactor Coolant Pumps 22 & 23 Due to Deenergization of Two Nonvital Buses.Unit Entered Cold Shutdown on 860913.Repair Completion Expected by 8609201986-09-15015 September 1986 PNO-I-86-073:on 860911,Unit 2 Tripped from 75% Power.Caused by Loss of Reactor Coolant Pumps 22 & 23 Due to Deenergization of Two Nonvital Buses.Unit Entered Cold Shutdown on 860913.Repair Completion Expected by 860920 PNO-I-86-066, on 860826,turbine Trip/Reactor Trip & Safety Injection Occurred During Troubleshooting on Steam Generator Level Indicator 22.Natural Circulation Established & Third Vital Bus & Nonvital Loads Reenergized1986-08-26026 August 1986 PNO-I-86-066:on 860826,turbine Trip/Reactor Trip & Safety Injection Occurred During Troubleshooting on Steam Generator Level Indicator 22.Natural Circulation Established & Third Vital Bus & Nonvital Loads Reenergized PNO-I-86-061, on 860806,equipment Qualification Discrepancy Identified W/Field Wiring within Limitorque Valve Operators in Containments.Both Units Shut Down to Replace Questionable Wires W/Qualified Wires1986-08-0707 August 1986 PNO-I-86-061:on 860806,equipment Qualification Discrepancy Identified W/Field Wiring within Limitorque Valve Operators in Containments.Both Units Shut Down to Replace Questionable Wires W/Qualified Wires PNO-I-86-054, on 860721,licensee Initiated Normal Shutdown from 100% Power to Inspect & Correct Main Generator Hydrogen Leak Into Stator Cooling Water Sys.Completion of Insp & Repairs Expected in Approx 7 Days1986-07-21021 July 1986 PNO-I-86-054:on 860721,licensee Initiated Normal Shutdown from 100% Power to Inspect & Correct Main Generator Hydrogen Leak Into Stator Cooling Water Sys.Completion of Insp & Repairs Expected in Approx 7 Days PNO-I-85-075, on 851006,plant Tripped.Caused by Condensation in Condenser Vacuum Sensing Line Reaching Sensor Causing Turbine Trip W/Automatic Reactor Trip.Plant in Cold Shutdown for Maint & Mod to Condenser1985-10-0707 October 1985 PNO-I-85-075:on 851006,plant Tripped.Caused by Condensation in Condenser Vacuum Sensing Line Reaching Sensor Causing Turbine Trip W/Automatic Reactor Trip.Plant in Cold Shutdown for Maint & Mod to Condenser PNO-I-85-071A, on 850927,Hurricane Gloria Located at Northampton,Ma Moving in Northeasterly Direction.Status Downgrade to Tropical Storm Expected Early Evening on 850927.Salem Unit 1 & Millstone Complex Suffered Damage1985-09-27027 September 1985 PNO-I-85-071A:on 850927,Hurricane Gloria Located at Northampton,Ma Moving in Northeasterly Direction.Status Downgrade to Tropical Storm Expected Early Evening on 850927.Salem Unit 1 & Millstone Complex Suffered Damage PNO-I-85-044, on 850628,RCS Water Inventory Balance Indicated Unidentified Leak Rate Increased from 0.72 Gpm (Tech Spec Limit Is 1.0 Gpm) on 850627 & Steam Observed Leaking from Inlet Flange of Pressurizer Relief Valve PR-41985-06-28028 June 1985 PNO-I-85-044:on 850628,RCS Water Inventory Balance Indicated Unidentified Leak Rate Increased from 0.72 Gpm (Tech Spec Limit Is 1.0 Gpm) on 850627 & Steam Observed Leaking from Inlet Flange of Pressurizer Relief Valve PR-4 PNO-IV-84-007A, on 840529,health Physicist Responded to Accident Site Located About 30 Miles East of Rock Springs,Wy on Interstate Highway 80.Shipping Containers Were Found to Be Intact W/No Detectable Leakage1984-05-31031 May 1984 PNO-IV-84-007A:on 840529,health Physicist Responded to Accident Site Located About 30 Miles East of Rock Springs,Wy on Interstate Highway 80.Shipping Containers Were Found to Be Intact W/No Detectable Leakage PNO-I-83-052, on 830520,plant Went Critical for First Time Since 830225.Reactor Startup & Required Reactor Trip Breaker Testing Completed within 24 H.Power Ascension to 100% Expected Over Next Several Days1983-05-23023 May 1983 PNO-I-83-052:on 830520,plant Went Critical for First Time Since 830225.Reactor Startup & Required Reactor Trip Breaker Testing Completed within 24 H.Power Ascension to 100% Expected Over Next Several Days PNO-I-83-049, all Licensee Commitments Required for Restart Completed.Actions to Assess & Mitigate Svc Water Biofouling in Support of Plant Heatup Anticipated to Occur on 830518 Completed1983-05-17017 May 1983 PNO-I-83-049:all Licensee Commitments Required for Restart Completed.Actions to Assess & Mitigate Svc Water Biofouling in Support of Plant Heatup Anticipated to Occur on 830518 Completed PNO-I-83-050, on 830513,100 Gallons of Contaminated Water Discharged from Auxiliary Bldg Sump Onto Ground Between Auxiliary & Fuel Handling Bldgs.Cause Under Investigation.No Offsite Release Occurred.Contaminated Soil Removed1983-05-13013 May 1983 PNO-I-83-050:on 830513,100 Gallons of Contaminated Water Discharged from Auxiliary Bldg Sump Onto Ground Between Auxiliary & Fuel Handling Bldgs.Cause Under Investigation.No Offsite Release Occurred.Contaminated Soil Removed ML20198B3651982-10-21021 October 1982 PNS-I-82-013:on 821020,employee at Plant Site Attempted Suicide at His Home Using Own .38 Caliber Handgun.Suicide Attempt Left Employee in Critical Condition as Result of Gunshot Wound to Head ML20028F9531982-08-17017 August 1982 PNS-I-82-010:on 820816,manual Isolation Stop Valve to Air Start Motors for 2C Diesel Generator Found in Shut Position. Possibly Caused by Deliberate Tampering.Operability Checks of All Rotating ECCS Equipment Conducted ML20028F9561982-08-16016 August 1982 PNS-I-82-009:on 820809,miscellaneous Ac 115-volt Distribution Panel 12 Lost Power Supply (Station Essential Controls Inverter 12) Due to Tripped Position of Inverter Breaker.Probably Caused by Sabotage.Surveillances Initiated PNO-I-81-106, on 810922,unit Taken off-line for Estimated 10-day Outage to Open,Inspect & Repair Steam Generator 21 & Resolve High Carryover Problems Found During Startup Testing1981-09-22022 September 1981 PNO-I-81-106:on 810922,unit Taken off-line for Estimated 10-day Outage to Open,Inspect & Repair Steam Generator 21 & Resolve High Carryover Problems Found During Startup Testing ML20216J7751978-10-23023 October 1978 PNO-78-180:on 781021,during Plant Startup,Shaft Seal on Number 13 RCP Failed.No Radioactivity Released in Environ. Exam & Repairs of RCP Seal in-progress.Plant Will Remain Shut Down for Estimated 3-5 Days ML20216J8701978-08-0303 August 1978 PNO-78-139:on 780802,while Operating Unit 1 Waste Evaporator & Discharging Evaporator Bottoms to Evaporator Bottoms Storage Tank,Leak Occurred in Connecting,Schedule 10,SS Piping ML20249A7361978-04-13013 April 1978 PNS-78-017:on 780413,member of Security Organization Received Telephone Call from an Unidentified Person Stating That Bomb Is in Const Site.Const Areas Were Evacuated & Searched.State of Nj & FBI Informed ML20248L0611978-04-13013 April 1978 PNO-78-080:on 780413,during Conduct of Emergency Drill,Which Involved Simulated Explosion,Simulated Injury to Workers & Actual Transport of Workers to Hosp,News Media Incorrectly Assumed Actual Event Occurred ML20248L8581978-03-16016 March 1978 PNO-78-046:on 780316,Unit 1 Shutdown to Investigate Vibration in Main Turbine Generator.Shutdown Expected to Last Min of 3 to 4 Wks ML20249A0991978-01-26026 January 1978 PNO-78-015:on 780123,unit Tripped from 100% Power,Due to Control Problem in Electrohydraulic Sys.During Outage Unit Was Cooled Down to Repair Steam Leaks in Two Steam Generator Manway Covers.State of Nj Informed ML20249A0451978-01-12012 January 1978 PNO-78-005:on 780111,orderly Unit Shutdown Because of Debris Accumulation & Icing of Circulating Water Intake Screens. Screens cleaned,de-iced & Preparations Made for Startup.Leak in Bonnet Gasket.Unit Maintained in Cold Shutdown Condition ML20151X9721977-10-18018 October 1977 PNO-77-186:on 771018,welding Cables in Contact with Cable Tray Located in Auxiliary Building Shorted,Caught Fire & Caused Damage to Cable Tray.Fire Extinguished by Site Personnel.Press Release Not Planned ML20151Y1231977-10-11011 October 1977 PNO-77-179:on 771009,due to Erroneous Valve lineup,600 Gallons of Liquid Waste Dumped to Circulating Water Discharge Pipe Instead of Tank Truck.Unit in Outage & Circulating Water Sys Shut Down.New Jersey State Notified ML20126D1901977-08-12012 August 1977 PNO-77-143:Pacific Pump Co Supplied Facilities W/Production Lot of 40 Pumps Mfg Using Shafts Made of Inferior Matl. Cause Unstated.All Utils W/Pumps Were Notified.Nrc Headquarters Notified on 770812 ML20151X6551977-07-11011 July 1977 PNO-77-125:on 770708,plant Was Shutdown When Packing Leak Occurred on 2 Auxiliary Spray Valve Inside Containment. Leak Was Measured at 11 Gpm & 13,000 Gallons of Primary Coolant Was Released to Containment ML20151X5421977-06-27027 June 1977 PNO-77-115:flashover Occurred When Planned Generator Trip Test from 100% Power Was Initiated by Manually Opening Two Generator Output Breakers.Investigation of Breaker Malfunction Will Be Made.Occurrence Was Reported on 770626 ML20151U9571977-06-0606 June 1977 PNO-77-097:on 770604,reactor Tripped from 100% Power on Low Flow Due to Loss of Rcp.Unit Placed in Cold Shutdown Mode. No Personnel Overexposures or Releases to Environ Occurred ML20151U1281977-04-13013 April 1977 PNO-77-054:on 770412,following Startup RCP (One of Four) Tripped When Power Was Lost to 4160 V Bus.Reactor Was Operated W/Three RCPs for Thirty Minutes ML20249A8941977-04-0707 April 1977 PNS-77-016:on 770406,Woodstown-Salem,NJ Radio Station Wjic Received Telcon from Unidentified Male Caller,Who Advised That Plant Going to Blow Baby. Threat Reported to Police Dept Who Advised Licensee.Search Produced Negative Results ML20151U3931977-02-24024 February 1977 PNO-77-032:on 770224,minor Radioactive Spill Occurred,When Valve line-up Error in Unit 1 Waste Holdup Sys Resulted in Floor Drain Backup.Roving Watch Found Leak & Personnel Dispatched to Correct Valve Lineup ML20236L1471977-01-17017 January 1977 PNO-77-011:on 770115,high Pressure Hydraulic Line on Number 12 MSIV Failed While Reactor Was Critical in Mode 2.Oil from Failed Line Sprayed on Insulation & Small Fire Resulted. Similar Line on Number 11 MSIV Failed on 770116.No Damage 1999-09-16 Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS MONTHYEARPNO-I-99-043, on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power1999-09-16016 September 1999
[Table view]PNO-I-99-043:on 990916,Hurricane Floyd Was Approaching Ccnpp,Sgs,Hcgs & Ocnpp.Hurricane Was Centered at Latitude 36.0 North & Longitude 76.6 West & Moving north-northeast at Approx 25 Mph.Plants Remain at Power IR 05000272/19990011999-04-0101 April 1999 Insp Repts 50-272/99-01 & 50-311/99-01 on 990117-0307.No Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support PNO-I-98-057, on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal1998-12-0101 December 1998 PNO-I-98-057:on 981130,util Commenced Shutdown of Salem Unit 2 to Repair 21 RCP Seal.Resident Inspectors Observed Portions of Plant Shutdown & Plan to Observe Continuing Maint Activities on RCP Seal IR 05000272/19982021998-07-0909 July 1998 Partially Deleted Insp Repts 50-272/98-202,50-311/98-202 & 50-354/98-202 on 980420-23.No Violations Noted.Major Areas Inspected:Conduct of Security & Safeguards Activities ML20217N6221998-04-24024 April 1998 Notice of Violation from Investigation Conducted by Oi. Violation Noted:Safeguard Event Log,Required to Be Maintained by Licensee,Was Not Complete & Accurate in All Matl Aspects ML20217E7851997-07-25025 July 1997 Investigation Rept 1-96-024 on 970725.No Noncompliance Noted.Major Areas Investigated:Allegations Re Failure to Make 10CFR73.71 Notification by Station Security Dept ML20202D0971997-03-31031 March 1997 Investigation Rept 1-95-013 on 970331.No Noncompliance Noted.Major Areas Investigated:Allegation Re Pse&G Intentionally Operated Outside Design Basis & Failed to Make Timely Notification to Nrc,Per 10CFR50.72 ML20137B6021997-03-18018 March 1997 Notice of Violation Identified in Correspondence Between 961105 & 970212.Violations Noted:Conducted Requalification Program Such That Annual Operating Test Not Provided for Fourteen Plant Licensed Operators in CY96 IR 05000272/19970031997-02-0505 February 1997 Attachment to Insp Repts 50-272/97-03 & 50-311/97-03 ,consisting of 970205 Slide Presentation Inadvertently Omitted from Repts ML20134B6741997-01-27027 January 1997 Notice of Violation from Insp on 961110-1221.Violations Noted:Vital Area Access Control & Badge Sys Requirements of Util Security Plan Were Not Implemented for Listed Examples IR 05000354/19960101997-01-27027 January 1997 Insp Rept 50-354/96-10 on 961110-1221.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering,Plant Support & Security Program Plan ML20133A4341996-12-11011 December 1996 Notice of Violation from Investigation Repts 1-94-006R & 1-94-053 on 940218-960430 & 941121-960425.Violation Noted: Licensee Through Former Manager of Nsr,Discriminated in Nov 93 & May 94 Against Former Onsite Safety Review Engineer ML20133A4491996-12-11011 December 1996 Notice of Violation from Insp on 960815-0903.Violation Noted:On 960814,vital Area Access Not Physically Controlled in That Positive Access Control Over Photobadge Keycards Compromised,Creating Opportunity for Unauthorized Access IR 05000272/19960131996-12-0303 December 1996 Insp Repts 50-272/96-13 & 50-311/96-13 on 960812-0920. Violations Noted.Major Areas Inspected:Engineering Performance Issues That Require Resolution Prior to Plant Restart ML20138H3031996-02-29029 February 1996 Notice of Violation from Insp on 961005-1113.Violation Noted:Alert for Loss of Annunciator Event Was Not Promptly Declared as Required by Ecg, Introduction & References, Section ML20135B2681995-04-11011 April 1995 Notice of Violation from Investigation 1-93-021R.Violation Noted:C Vondra Deliberately Caused Pse&G to Violate 10CFR50.7 by Discriminating Against Two Employees for Engaging in Protected Activities IR 05000272/19940341994-12-23023 December 1994 Insp Repts 50-272/94-34,50-311/94-34 & 50-354/94-28 on 941212-15.No Violations Noted.Major Areas Inspected:Security Plan & Implementing Procedures,Previously Identified Item, fitness-for-duty & Contingency Plan Implementation ML20071G7921994-06-30030 June 1994 Notice of Violation from Insp on 940613-17.Violation Noted: on 940616,SFM Failed to Search Vehicle Properly Until Questioning by NRC Prompted Supervisory Direction to Correct Search Deficiency IR 05000272/19940161994-06-30030 June 1994 Insp Repts 50-272/94-16,50-311/94-16 & 50-354/94-16 on 940613-17.Violations Noted.Major Areas Inspected:Protected Physical Barriers,Detection & Assessment Aids,Protected & Vital Area Access Control of Personnel,Packages & Vehicles ML20135A9461994-03-0909 March 1994 Notice of Violation & Proposed Imposition of Civil Penalty in Amount of $50,000.Noncompliance Noted:On 931012,maint on Breaker for electro-hydraulic Pump Was Conducted W/O Supervisor Ensuring Equipment Was Tagged & Safe to Work on PNO-I-93-068, on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R)1993-12-0707 December 1993 PNO-I-93-068:on 931203,ALCO Emergency Diesel Generator Cylinder Cracking Discovered.Health Physics Technician Noticed Coolant Leaking from Number 3 Cylinder Sleeve on Right Bank of Cylinders (3R) PNO-I-93-062, on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan1993-11-12012 November 1993 PNO-I-93-062:on 931112,informed That Current 30-day Contract Extension W/United Govt Security Officers of America Will Expire on 931115.Licensee Indicated That They Have Adequate Personnel Trained & Available to Satisfy Security Plan PNO-I-93-060, on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified1993-11-0303 November 1993 PNO-I-93-060:on 931102,fire Reported in 230 Volt Lighting Transformer in Turbine Bldg.Caused by Loose Electrical Connection.State of Nj Has Been Notified ML20058P9361993-10-15015 October 1993 Notice of Violation from Insp on 920614-0725.Violation Noted:Licensee Determined Several Instances in Which Personnel Assigned to Fire Watch Patrols Failed to Perform or Complete Function as Required by TS & Falsified Records IR 05000272/19910991993-07-29029 July 1993 Initial Draft SALP Repts 50-272/91-99,50-311/91-99 & 50-354/91-99 for 911229-930619 IR 05000272/19930181993-06-30030 June 1993 Physical Security Program Insp Repts 50-272/93-18, 50-311/93-18 & 50-354/93-17 on 930607-11.No Safety Concerns or Violations Noted.Major Areas Inspected:Security Program Plans & Protected & Vital Area Physical Barriers PNO-I-93-032, on 930627, Licensee Resolved Latest Issue Re Card Failures in Rod Control Power Cabinet.Licensee Completed Root Cause Evaluation & Briefed AIT on Site.Press Release Planned within 2 Wks1993-06-28028 June 1993 PNO-I-93-032:on 930627, Licensee Resolved Latest Issue Re Card Failures in Rod Control Power Cabinet.Licensee Completed Root Cause Evaluation & Briefed AIT on Site.Press Release Planned within 2 Wks PNO-I-93-030, during Startup of Plant from Recent Refueling Outage Multiple Failures Experienced in Sys. Augmented Insp Team Dispatched to Investigate Failures.Team Expects to Complete Work in 1 Wk1993-06-0707 June 1993 PNO-I-93-030:during Startup of Plant from Recent Refueling Outage Multiple Failures Experienced in Sys. Augmented Insp Team Dispatched to Investigate Failures.Team Expects to Complete Work in 1 Wk IR 05000272/19930021993-03-25025 March 1993 Insp Repts 50-272/93-02,50-311/93-02 & 50-354/93-02 on Stated Date.No Violations Noted.Major Areas Inspected: Operations,Radiological Controls,Maint & Surveillance Testing,Emergency Preparedness & Security IR 05000272/19920211993-01-27027 January 1993 Exam Repts 50-272/92-21OL & 50-311/92-21OL on 921214-17.Exam Results:All Six SRO Candidates Passed All Portions of Exam & Issued Licenses PNO-I-92-075, upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes1992-12-15015 December 1992 PNO-I-92-075:upon Investigation of Alarm Printed Out on Auxiliary Typewriter on 921213,operators Determined That Cpu for Overhead Annunciator (Oha) Had Failed to Perform, Resulting in Loss of Oha Sys for 1 H & 41 Minutes ML20086H3621991-11-26026 November 1991 Physical Security Insp Repts 50-272/91-29,50-311/91-29 & 50-354/91-22 on 911104-08.No Violations Noted.Major Areas Inspected:Previously Identified Items,Followup Actions in Response to 910410-14 Regulatory Review & Security Programs IR 05000272/19910101991-04-26026 April 1991 Partially Withheld Insp Repts 50-272/91-10,50-311/91-10 & 50-354/91-07 on 910401-05.No Violations Noted.Major Areas Inspected:Mgt Support,Security Programs Plans & Audits & Protected Area Access Control of Personnel IR 05000272/19900231990-11-0707 November 1990 Insp Repts 50-272/90-23,50-311/90-23 & 50-354/90-19 on 900925-28.No Violations Noted.Major Areas Inspected:Licensee Action on Previously Identified Items PNO-I-90-056, on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed1990-07-23023 July 1990 PNO-I-90-056:on 900722,potential Design Deficiency in Main Steam Isolation Sys Noted.Units Shut Down Until Final Analysis & Appropriate Corrective Actions Completed PNO-I-90-043, on 900523,supervisor W/No Operations Responsibilities Failed Random Alcohol Test W/Presence of Alcohol Above Program Limits (.04).Site Access Suspended & Individual Entered Licensee Rehabilitation Program1990-05-25025 May 1990 PNO-I-90-043:on 900523,supervisor W/No Operations Responsibilities Failed Random Alcohol Test W/Presence of Alcohol Above Program Limits (.04).Site Access Suspended & Individual Entered Licensee Rehabilitation Program IR 05000272/19900061990-03-15015 March 1990 Insp Repts 50-272/90-06,50-311/90-06 & 50-354/90-04 on 900226-0302.No Violations Noted.Major Areas Inspected: Radiological Environ Monitoring & Meteorological Monitoring Programs,Including Mgt Controls for Programs ML20246C4001989-08-15015 August 1989 Partially Deleted Insp Repts 50-272/89-19,50-311/89-17 & 50-354/89-15 on 890710-14 (Ref 10CFR73.21).Major Areas Inspected:Followup on Actions Taken in Response to Regulatory Effectiveness Review on 890410-14 ML20247B6651989-05-0909 May 1989 Mgt Meeting Rept on 890307 & 0413.Major Areas Discussed: Status of Plant,Training & Safety Programs & Self Assessment Programs IR 05000311/19870291988-03-23023 March 1988 Enforcement Conference Rept 50-311/87-29 on 880212. Violations Noted.Major Areas Discussed:Insp Rept 50-311/87-29 Re Safe Shutdown in Event of Fire IR 05000272/19880061988-03-18018 March 1988 Partially Withheld Physical Security Insp Repts 50-272/88-06,50-311/88-06 & 50-354/88-04 on 880201-05 (Ref 10CFR73.21).No Violations Noted.Major Areas Inspected: Procedures,Security Organization & Mgt Effectiveness IR 05000354/19860991988-03-0404 March 1988 SALP Rept 50-354/86-99 on 861201-880115 PNO-I-88-020, on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom1988-02-16016 February 1988 PNO-I-88-020:on 880216,CA Mcneill Named Executive Director - Nuclear W/Responsibility of Directing Nuclear Operations, Including Nuclear Dept Reorganization & Restart Efforts of Peach Bottom IR 05000272/19860991988-02-0505 February 1988 SALP Repts 50-272/86-99 & 50-311/86-99 for Oct 1986 - Dec 1987 IR 05000254/19870251987-11-23023 November 1987 Insp Repts 50-254/87-25 & 50-265/87-25 on 870922-1105. Violations Noted.Major Areas Inspected:Licensee Implementation of Generic Ltr 85-06 Re ATWS Mitigation Sys (25020) & Onsite Followup Events IR 05000272/19870261987-11-0909 November 1987 Exam Repts 50-272/87-26OL & 50-311/87-26OL on 870915-17.Exam Results:All Four Senior Reactor Operator Candidates Passed Written & Operating Exams ML20217F8541987-10-27027 October 1987 PNS-I-87-017:on 871026,fireman Received Call of Bomb Threat at Plant.Search of Facility Proved Negative PNO-I-87-099, on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway1987-10-26026 October 1987 PNO-I-87-099:on 871023,licensee Notified Region I of Addl Uncertainties in Onsite Electrical Distribution Sys Design W/Potential for Breaker Coordination Problems.Unit Shutdown Commenced on 871023.Analysis Underway IR 05000272/19870271987-10-20020 October 1987 Insp Rept 50-272/87-27 on 870921-25.No Violations Noted. Major Areas inspected:post-mod Test Program for Forthcoming Refueling Outage,Including Engineering Change (1EC) Packages,Mod Test Procedures & Test Specs IR 05000272/19870211987-08-17017 August 1987 Requalification Evaluation Repts 50-272/87-21OL & 50-311/87-26OL on 870615-19.Exam Results:Two Senior Reactor Operators & Three Reactor Operators Passed All Portions of Exam.Program Found Unsatisfactory,Per NUREG-1021 1999-09-16 |
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PRELIMINARY NOTIFICATION December 2, 1976 PRELIMINARY NOTIFICATION OF EVENT OR UNUSUAL OCCURRENCE--PNO-76-204 This preliminary notification constitutes EARLY notice of an event of POSSIBLE safety or public interest significance. The information presented is as initially received without verification or evaluation and is basically all that is known by IE staff on this date.
Facility:
Salem Unit No. 1 (DN 50-272)
Subject:
INADVERTENT SAFETY INJECTIONS Three inadvertent safety injections (sis) occurred at 10:39 p.m., 11:01 p.m.,
November 30 and 2:39 a.m., December 1, 1976. The reactor was in Mode 3 (hot shutdown) during each occurrence.
Initial criticality has not yet been achieved.
The first two sis were initiated by low Reactor Coolant System (RCS) average temperature (Tav) in conjunction with a spurious high steam flow signal in steam line 14. During these sis the following occurred:
1.
SI flow lasted for 3 minutes (First SI) and 2 minutes (Second SI).
2.
The reactor trip breakers did not open and the "B" SI Train valves did not actuate in either SI.
The third SI was initiated by low steam pressure in steam line 14 compared to the other lines. There was no SI flow because the boron injection tank valves were closed to' adjust boron concentrations due to the first two sis. Reactor trip breskers and valves in both SI trains operated properly.
The licensee's preliminary evaluations indicate the following:
1.
The reactor trip breakers and "B" SI train did not respond in the first two sis, probably because the duration of the actuation signal.gf was not sufficient to drop the bistables.
~d d 2.
The steer. safety valve in steam line 14 relieved below its setpoint due to an improper setting.
A Region I inspector is on site reviewing the occurrences.
CONTINUE s
I 9007010215 761202 PDR I&E I
PNO-76-204 PDR i
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Pcge 2 December 2, 1976 Continued PNO-76-204 Media interest is expected because of close attention given to occurrences at Salem. The State of New Jersey has been informed. A press release is not planned.
NRC, Region I, (Philadelphia) received notification of this occurrence by telephone from the inspector onsite at 11:15 a.m., December 1, 1976. The information is current as of 3:00 p.m., December 1, 1976.
Contact:
FADreher, IE x27261 GWRoy, IE x27261 DThompson, IE x27541 Distribution:
Chairman Rowden Commissioner Mason S. J. Chilk, SECY Commissioner Gilinsky C. C. Kammerer, CA G. F. Murphy, JCAE Commissioner Kennedy L. V. Gossick, EDO K. R. Chapman, NMSS R. G. Ryan, OSP S. H. Hanauer, EDO E. Volgenau, OIE J. A. Harris, PA B. C. Rusche, NRR H. K. Shapar, ELD T. J. McTiernan, OIA Transmitted: PBldg
- H St
- HNBB Luge PRELIMINARY NOTIFICATION
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