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Category:SAFETY EVALUATION REPORT--LICENSING & RELATED ISSUES
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & ML20217N3711999-10-13013 October 1999 Safety Evaluation Supporting Amends 111,111,104 & 104 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety ML20212A8261999-09-0808 September 1999 Safety Evaluation Supporting Amends 103 & 103 to Licenses NPF-72 & NPF-77,respectively ML20211A8131999-08-10010 August 1999 Safety Evaluation Supporting Amends 110 & 110 to Licenses NPF-37 & NPF-66,respectively ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station ML20206G6031999-05-0303 May 1999 Safety Evaluation Supporting Amends 108,108,101 & 101 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20206B5531999-04-23023 April 1999 Safety Evaluation Supporting Amends 107,107,100 & 100 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20205D6641999-03-26026 March 1999 Safety Evaluation Supporting Amends 99 & 99 to Licenses NPF-72 & NPF-77,respectively ML20205B5091999-03-26026 March 1999 SER Accepting Relief Requests 12R-24,Rev 0 & 12R-34,Rev 0, Related to Second 10-year Interval Inservice Insp for Byron Station,Units 1 & 2 ML20205C5101999-03-21021 March 1999 Revised Safety Evaluation Supporting Improved TS Amends Issued by NRC on 981222 to FOLs NPF-37,NPF-66,NPF-72 & NPF-77.Revised Pages Include Editorial Corrections ML20204G3831999-03-19019 March 1999 Safety Evaluation Accepting Second 10-yr Interval ISI Request for Relief 12R-11 ML20155B6711998-10-26026 October 1998 Safety Evaluation Accepting Requests for Relief Associated with Second 10-yr Interval ISI Program Plan ML20154N1641998-10-15015 October 1998 Safety Evaluation Supporting Amends 105,105,97 & 97 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20154F5071998-10-0606 October 1998 Safety Evaluation Supporting Amends 104,104,96 & 96 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20154D4401998-10-0202 October 1998 Safety Evaluation Authorizing Second 10-yr Interval ISI Program Request for Relief 12R-30 for Plant,Units 1 & 2 ML20238F3281998-08-31031 August 1998 SER Approving Second 10-year Interval Inservice Insp Program Request for Relief 12R-14 for Braidwood Station,Units 1 & 2 ML20238F6551998-08-28028 August 1998 SE Authorizing Licensee Request for Relief NR-20,Rev 1 & NR-25,Rev 0 Re Relief from Examination Requirement of Applicable ASME BPV Code,Section XI for First ISI Interval Exams ML20237D4531998-08-18018 August 1998 Safety Evaluation Supporting Amends 94 & 94 to Licenses NPF-72 & NPF-77,respectively ML20248E0361998-05-26026 May 1998 Safety Evaluation Supporting Amends 103,103,93 & 93 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20216C1341998-05-0808 May 1998 Safety Evaluation Supporting Amends 102 & 102 to Licenses NPF-37 & NPF-66,respectively ML20217K6331998-04-20020 April 1998 Safety Evaluation Accepting Methodology & Criteria Used in Generating Flaw Evaluation Charts for RPV of Braidwood IAW Section XI of ASME Code ML20217K7171998-04-20020 April 1998 Safety Evaluation Accepting Requests for Relief NR-22,NR-23 & NR-24 for First 10-yr Insp Interval ML20216F4921998-03-11011 March 1998 Correction to Safety Evaluation Re Revised SG Tube Rapture Analysis ML20212H1851998-03-0606 March 1998 SE Approving Temporary Use of Current Procedure for Containment Repair & Replacement Activities Instead of Requirements in Amended 10CFR50.55a Rule ML20197B7531998-03-0404 March 1998 SER Accepting License Request for Relief from Immediate Implementation of Amended Requirements of 10CFR50.55a for Plant,Units 1 & 2 ML20203A2821998-02-0303 February 1998 Safety Evaluation Supporting Amends 101,101,92 & 92 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20199G2591998-01-28028 January 1998 Safety Evaluation Rept Accepting Revised SG Tube Rupture Analysis ML20199J0371998-01-23023 January 1998 Safety Evaluation Supporting Amends 98,98,89 & 89 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20199F3751998-01-22022 January 1998 Safety Evaluation Supporting Amends 97,97,88 & 88 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20199H0031998-01-21021 January 1998 SER Accepting Pressure Temp Limits Rept & Methodology for Relocation of Reactor Coolant Sys pressure-temp Limit Curves & Low Temp Overpressure Protection Sys Limits for Byron Station,Units 1 & 2 & Braidwood Station,Units 1 & 2 ML20199C1401998-01-16016 January 1998 SER Accepting Request to Integrate Reactor Vessel Weld Metal Surveillance Program for Byron,Units 1 & 2 & Braidwood,Units 1 & 2 Per 10CFR50 ML20199A7011998-01-16016 January 1998 SER Approving Exemption from Requirements of 10CFR50.60 for Byron Station,Units 1 & 2 & Braidwood Station,Units 1 & 2 ML20199C1721998-01-15015 January 1998 Safety Evaluation Supporting Amends 96,96,87 & 87 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20199C1231998-01-13013 January 1998 Safety Evaluation Granting Second 10-yr Inservice Insp Program Plan Relief Request ML20197G0041997-12-11011 December 1997 Safety Evaluation Accepting First 10-yr Interval Insp Program Plan,Rev 4 & Associated Requests for Relief for Plant ML20203D4081997-12-0404 December 1997 Safety Evaluation Supporting Amends 94,94,86 & 86 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20198H3211997-12-0303 December 1997 Safety Evaluation Re Licensee Submittal of IPE for Plant, Units 1 & 2,in Response to GL 88-02, IPE for Severe Accident Vulnerabilities ML20202E5781997-11-25025 November 1997 Safety Evaluation Supporting Amends 93 & 93 to Licenses NPF-37 & NPF-66,respectively ML20198R3061997-10-27027 October 1997 Staff Evaluation Rept Concluding That Licensee IPE Complete Wrt Info Requested by GL 88-20 & Process Meets Intent of Subj GL ML20211L2151997-10-0303 October 1997 Safety Evaluation Supporting Licensee Relief Request,Per 10CFR50.55a(a)(3)(i) ML20217C1681997-09-22022 September 1997 Safety Evaluation Accepting Request for Relief from ASME Code,Section Iii,Div 2 for Repair of Damaged Concrete Reinforcement Steel NUREG-1335, Staff Evaluation Rept Concluding That Licensee IPE Complete Wrt Info Requested by GL 88-20 & Associated Guidance, NUREG-13351997-08-28028 August 1997 Staff Evaluation Rept Concluding That Licensee IPE Complete Wrt Info Requested by GL 88-20 & Associated Guidance, NUREG-1335 ML20210K7091997-08-13013 August 1997 Safety Evaluation Supporting Amends 91 & 84 to Licenses NPF-66 & NPF-77,respectively ML20210K4151997-08-13013 August 1997 Safety Evaluation Supporting Amends 92,92,85 & 85 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20141L9321997-05-29029 May 1997 Safety Evaluation Accepting Use of ASME Boiler & Pressure Vessel Code,Section Ix,Code Cases 2142-1 & 2143-1 for Reactor Coolant Sys for Plants ML20141K3181997-05-23023 May 1997 Safety Evaluation Supporting Amend 83 to License NPF-72 ML20141B5551997-05-13013 May 1997 SE Accepting First 10-yr Interval Inservice Insp Program Plan Request for Relief NR-29 for Braidwood Station,Units 1 & 2 1999-09-08
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217G9961999-10-14014 October 1999 SER Accepting First 10-year Interval Inservice Insp Requests for Relief for Plant,Units 1 & ML20217N3711999-10-13013 October 1999 Safety Evaluation Supporting Amends 111,111,104 & 104 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20217H5221999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Byron Station, Units 1 & 2.With BW990066, Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Braidwood Station, Units 1 & 2.With ML20217P6351999-09-29029 September 1999 Non-proprietary Rev 6 to HI-982083, Licensing Rept for Spent Fuel Rack Installation at Byron & Braidwood Nuclear Stations ML20217A1691999-09-22022 September 1999 Part 21 Rept Re Engine Sys,Inc Controllers,Manufactured Between Dec 1997 & May 1999,that May Have Questionable Soldering Workmanship.Caused by Inadequate Personnel Training.Sent Rept to All Nuclear Customers ML20212A7441999-09-10010 September 1999 Safety Evaluation Concluding That Alternatives Contained in Relief Request 12R-07 Provide Acceptable Level of Quality & Safety ML20212A8261999-09-0808 September 1999 Safety Evaluation Supporting Amends 103 & 103 to Licenses NPF-72 & NPF-77,respectively BW990056, Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Braidwood Station, Units 1 & 2.With ML20212B9261999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Byron Station,Units 1 & 2.With 05000454/LER-1998-005, :on 980307,reactor Manually Tripped.Caused by Indeterminate Rod Sequencing Problem.Halted Rod Insertion & Exercised Bank Overlap Thumbwheel Switch to Clean Contacts. with1999-08-20020 August 1999
- on 980307,reactor Manually Tripped.Caused by Indeterminate Rod Sequencing Problem.Halted Rod Insertion & Exercised Bank Overlap Thumbwheel Switch to Clean Contacts. with
ML20210R6421999-08-13013 August 1999 ISI Outage Rept for A2R07 ML20211A8131999-08-10010 August 1999 Safety Evaluation Supporting Amends 110 & 110 to Licenses NPF-37 & NPF-66,respectively ML20210U8111999-08-0404 August 1999 SER Granting Licensee Relief Requests VR-1,VR-3 & Portion of VR-2 Pursuant to 10CFR50.55a(a)(3)(ii).Relief Request VR-4 Does Not Require Explicit NRC Approval Because Relief Applies to Valves Not Required by 10CFR50.55a BW990048, Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With1999-07-31031 July 1999 Monthly Operating Repts for Jul 1999 for Braidwood Station, Units 1 & 2.With ML20210R3431999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Byron Station, Units 1 & 2.With ML20210K9861999-07-30030 July 1999 Safety Evaluation Accepting Licensee 60-day Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs ML20210E2251999-07-21021 July 1999 B1R09 ISI Summary Rept Spring 1999 Outage, 980309-990424 M990002, Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function1999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function ML20216D3841999-07-12012 July 1999 Revised NFM9900022, Braidwood Unit 2 Cycle 8 COLR in ITS Format & W(Z) Function ML20209G1751999-07-0808 July 1999 SG Eddy Current Insp Rept,Cycle 9 Refueling Outage (B1R09) ML20207H8071999-06-30030 June 1999 Rev 0 to WCAP-15178, Byron Unit 2 Heatup & Cooldowm Limit Curves for Normal Operations ML20207H7941999-06-30030 June 1999 Rev 0 to WCAP-15180, Commonwealth Edison Co Byron,Unit 2 Surveillance Program Credibility Evaluation ML20209H3711999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Byron Station, Units 1 & 2.With ML20207H7851999-06-30030 June 1999 Rev 0 to WCAP-15183, Commonwealth Edison Co Byron,Unit 1 Surveillance Program Credibility Evaluation ML20207H7771999-06-30030 June 1999 Rev 0 to WCAP-15177, Evaluation of Pressurized Thermal Shock for Byron,Unit 2 BW990038, Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Braidwood Station, Units 1 & 2.With ML20207H7621999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) ML20207H7561999-06-28028 June 1999 Pressure Temp Limits Rept (Ptlr) 05000456/LER-1998-004-02, :on 980903,MSSVs Were Tested in Excess of Required Setpoint.Caused by Suspected Metallic Bonding. Evaluated Disc Removed from One of Valves & Reviewed Historical Data to Assess Cause of Test Failures1999-06-16016 June 1999
- on 980903,MSSVs Were Tested in Excess of Required Setpoint.Caused by Suspected Metallic Bonding. Evaluated Disc Removed from One of Valves & Reviewed Historical Data to Assess Cause of Test Failures
05000456/LER-1999-001-06, :on 990516,both Trains of LPSI Were Declared Inoperable.Caused by Leakage of SI Accumulator Water.Design Changes Were Implemented to Install Local High Point Vents in Common Portion of Rh Sys Piping to 1B & 1C RCS1999-06-15015 June 1999
- on 990516,both Trains of LPSI Were Declared Inoperable.Caused by Leakage of SI Accumulator Water.Design Changes Were Implemented to Install Local High Point Vents in Common Portion of Rh Sys Piping to 1B & 1C RCS
05000457/LER-1999-003-03, :on 990519,spurious Spiking of Indication on Intermediate Range Neutron Flux Channel N36 Resulted in Unit 2 Reactor Trip.Cause Unknown.Personnel Stabilized Reactor in Shutdown Condition Using Appropriate Emergency Procedures1999-06-15015 June 1999
- on 990519,spurious Spiking of Indication on Intermediate Range Neutron Flux Channel N36 Resulted in Unit 2 Reactor Trip.Cause Unknown.Personnel Stabilized Reactor in Shutdown Condition Using Appropriate Emergency Procedures
05000454/LER-1999-003-02, :on 990513,automatic Reactor Occurred Due to Human Error During Surveillance Procedure.Appropriate Mgt Action Taken with Instrument Maint Involved & Sp Bsir 3.1.6-200 Revised.With1999-06-11011 June 1999
- on 990513,automatic Reactor Occurred Due to Human Error During Surveillance Procedure.Appropriate Mgt Action Taken with Instrument Maint Involved & Sp Bsir 3.1.6-200 Revised.With
05000454/LER-1999-002-03, :on 990509,missed TS Surveillance Was Noted. Caused by Error in Design Package.Changed Monthly Surveillance Procedure for Containment Isolation Valves1999-06-0808 June 1999
- on 990509,missed TS Surveillance Was Noted. Caused by Error in Design Package.Changed Monthly Surveillance Procedure for Containment Isolation Valves
ML20209H7481999-05-31031 May 1999 Revised Monthly Operating Repts for May 1999 for Braidwood Station,Units 1 & 2 BW990029, Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Braidwood Stations, Units 1 & 2.With ML20195J8001999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Byron Station,Units 1 & 2.With ML20207B6481999-05-25025 May 1999 SER Accepting Revised SGTR Analysis for Byron & Braidwood Stations.Revised Analysis Was Submitted to Support SG Replacement at Unit 1 of Each Station 05000454/LER-1999-001-05, :on 990422,depressing Both Feedwater Isolation Reset Pushbuttons Leads to LCO 3.0.3 Entry.Caused by Implementation Error in Procedure Review for Conversion to Its.Review of Procedures Will Be Conducted1999-05-21021 May 1999
- on 990422,depressing Both Feedwater Isolation Reset Pushbuttons Leads to LCO 3.0.3 Entry.Caused by Implementation Error in Procedure Review for Conversion to Its.Review of Procedures Will Be Conducted
05000457/LER-1999-002-02, :on 990424,ESFA Was Noted.Caused by High Water Level in 2C Sg.Sg Blowdown Sys Was Placed in Operation & SG Water Level Was Returned to Normal Operating Range1999-05-21021 May 1999
- on 990424,ESFA Was Noted.Caused by High Water Level in 2C Sg.Sg Blowdown Sys Was Placed in Operation & SG Water Level Was Returned to Normal Operating Range
ML20195B2591999-05-19019 May 1999 Rev 66a to CE-1-A,consisting of Proposed Changes to QAP for Dnps,Qcs,Znps,Lcs,Byron & Braidwood Stations 05000457/LER-1999-001-03, :on 990414,reactor Tripped Due to Main Generator & Turbine Trip.Caused by Spurious Generator Stator Ground relay,GIX-104 Relay,Actuation.Voltage Regulator Parts Replacement Program Was Developed.With1999-05-14014 May 1999
- on 990414,reactor Tripped Due to Main Generator & Turbine Trip.Caused by Spurious Generator Stator Ground relay,GIX-104 Relay,Actuation.Voltage Regulator Parts Replacement Program Was Developed.With
ML20206G6031999-05-0303 May 1999 Safety Evaluation Supporting Amends 108,108,101 & 101 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20206R6991999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Byron Station Units 1 & 2.With BW990021, Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With1999-04-30030 April 1999 Monthly Operating Repts for Apr 1999 for Braidwood Station, Units 1 & 2.With M980023, Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A)1999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20195C7961999-04-28028 April 1999 Rev 2 to NFM9800233, Byron Station Unit 2 COLR for Cycle 8A (BY2C8A) ML20206B5531999-04-23023 April 1999 Safety Evaluation Supporting Amends 107,107,100 & 100 to Licenses NPF-37,NPF-66,NPF-72 & NPF-77,respectively ML20205P7001999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Byron Station,Units 1 & 2.With ML20205N9241999-03-31031 March 1999 Analysis of Capsule X from CE Byron Unit 2 Rv Radiation Surveillance Program 1999-09-08
[Table view] |
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i SAFETY EVALUATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION SUPPORTING AMENDMENT NO. 28 TO FACILITY OPERATING LICENSES NOS. NPF-37 AND NPF-66 i
BYRON STATION, UNITS 1 AND 2 1
_ DOCKET NOS. 50-454 AND 50-455 AND SUPPORTING AMENDMENT NO. 17 TO FACILITY OPERATING LICENSES NOS. NPF-72 AND NPF-77 BRAIDWOOD STATION, UNITS 1 AND,2 i
DOCKET NOS. 50-456 AND 50-457.
i
1.0 INTRODUCTION
1 On July 8,1983, the' Nuclear Regulatory Commission (NRC) issued Generic Letter 83-28 which described actions to be taken by licensees to resolve concerns raised by the Salem ATWS events.
Item 4.3 of this letter requested licensees and applicants to modify the reactor trip system on Westinghouse and Babcock &
Wilcox PWRs to automatically actuate the shunt trip attachment of the reactor j
trip breakers.
Based on their review of the proposed Westinghouse design for i
automatically uctuating the shunt trip device, the staff concluded that revisions to the plant technical specifications were needed to provide for surveillance testing of the shunt and undervoltage trip devices during power operation. On May 23, 1985, the staff issued Generic Letter 85-09 to all i
Westinghouse PWR licensees which clarifico the original requireiaent for testing the trip devices by requiring that the shunt ano undervoltage trip devices be tested independently during power operation.
In aodition, i
independent testing of the control' room manual trip switch and wiring to both trip devices and testing of the reactor trip bypass breakers were required.
These changes are considered necessary by the staff to ensure reliable operation of the reactor trip breakers.
l 2.0 EVALUATION l
By letter dated December Edison Company (the licensee 23,)1987, supplemented April 3, 1989, Commonwealth submitted proposed revisions to the Byron /Braidwood i
Technical Specifications based upon the NRC staff evaluation of the Westinghouse shunt trip attachment design and the requirements of Generic Letter 85-09.
In response to the hRC requirements, the following Technical Specification revisions j
were proposed.
j 8906010131 890522 I PDR ADOCK 05000454; P
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-__--__ - -_ - - -- - _ O
e f. s 1.
Functional Unit 22 is being added to Technical Specification Table 2.2-1.
This change is being made to be consistent with Technical Specification Tables 3.3-1 and 4.4-1, which also reference the Reactor Trip Bypass Breakers.
2.
Action 9 is being deleted from, and Action 12 is being added to, Functional Unit 20 on Technical Specification Table 3.3-1.
Action 12 is broken down into two independent requirements. Action 12-a invokes the actions stated in Action 14 of Generic Letter 85-09. This action permits continued operation for up to 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> when one of the Reactor Trip Breaker diverse trip features is found to be inoperable. After this 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> period elapses, Action Statement 12-b must be entered. Action Statement 12-b was previously Action 9.
The words " Channel" have been replaced with " Reactor Trip Breaker" for clarity. This Action will require the unit to be placed in Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> for any failure not addressed by Action 12-a.
3.
Functional Unit 22 is being added to Technical Specification Table 3.3-1.
The addition of Functional Unit 22 is necessary to provide both a condition of applicability and action statement for the Reactor Trip Bypass Breakers. The condition of applicability was chosen to be whenever the Reactor Trip Bypass Breaker is racked in and closed for the purpose of bypassing a Reactor Trip Breaker with the Unit in Modes 1 or 2, or in Modes, 3, 4, or 5 with the Control Rods capable of withdrawal.
With a Recctor Trip Bypass Breaker inoperable, Action 13 requires the breaker to be returned to an operable status prior to using the breaker for the purpose of bypassing a Reactor Trip Breaker. The first portion of this Action Statement is stated this way due to the normal mode of discovering an inoperable breaker through the Manual Shunt Trip test, required prior to breaker use in the proposed Note 16 to Technical Specification Table 4.3-1.
If the Bypass Breaker becomes inoperable after being racked in and closed for the purpose of bypassing a Reactor Trip Breaker, then the second portion of Action 13 will require the Unit to be placed in Hot Standby in 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, then the breaker must be restored to operable status within the next 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />, or the breaker must be opened in the next hour. These actions are based on the present Action Statement 9 and 10 for the Reactor Trip Breakers. The testing i
clause associated with Action 9 was removed from Action 9, due to it not being applicable in this configuration.
4.
Note 14 to Technical Specification Table 4.3-1 for Braidwood Station only is being deleted. This was a one time only change that has expired.
j 5.
Note 14 is being added to the Trip Actuating Device Operational Test for Functional Unit 1 on Technical Specification Table 4.3-1.
Note 14 requires that the appropriate signals reach the undervoltage and shunt trip relays for both the Reactor Trip and Bypass Breakers from the Manual Trip Switches. This note also provides an implementation time frame for this surveillance requirement. The implementation time frame chosen was due to this surveillance requiring the Unit to be in a shutdown condition to perform. The proposed change reflects the intent of Note 11 of Generic Letter 85-09.
i
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6.
Note 11 on the Trip Actuating Device Operational test for Functional Unit 20 on Technical Specification Table 4.3.1.is being revised. The s
requirements of Note 7 are being incorporated into Note 11 for clarity,
~
and Note 7 has been deleted from Functional Unit 20. Note 11 has been-revised to. combine the need to independently verify the operability of both the undervoltage trip and the shunt trip attachment. A requirement to test these functions following maintenance or adjustment has also been incorporated into Note 11.
7.
Functional Unit'22 is being added to Technical Specification Table 4.3-1.
Included with this function unit are Notes 15 and 16 which require manual Shunt Trip testing prior to the Reactor Trip Bypass Breaker being racked in and closed for the purpose of bypassing a' Reactor Trip Breaker.
The monthly frequency designation associated with Note 15 is being deleted.
The requirement to Shunt Trip test the Reactor Trip Bypass Breakers prior to use is-controlled through Note 15 which references bypassing a Reactor.
Trip Breaker.. Bypassing a Reactor Trip Breaker is required monthly in functional Unit 20 and therefore the Reactor Trip Bypass Breaker will be tested monthly.
Including the monthly frequency designation in Functional Unit 22 would be redundant and possibly lead to confusion.
Note 16 requires the Reactor Trip Bypass Breaker to be trip tested from an automatic undervoltage signal once per 18 months. The Surveillance Requirement poses a high potential to cause a unit trip if performed with the unit on line. Due to this potential for a unit trip, this r
surveillance is being viewed as a shutdown item. Therefore, Note 16 also contains an implementation time frame.
On the basis of its review of the above items, the staff concludes that the licensee has provided an acceptable response to these items as addressed in the NRC guidance requiring independent testing of the undervoltage and shunt trip attachments during power operation and independent testing of the control room manual switch contacts during each refueling outage. Therefore, the staff finds that these changes are consistent with the recommendations in Generic Letter 85-09 and are acceptable.
3.0 ENVIRONMENTAL CONSIDERATION
The amendment involves change in the installation or use of a facility component located within the restricted area as defined in 10 CFR Part 20.
The staff has determined that the amendment involves no significant increase in the amounts, and no significant change in the types, of any effluents that may be released offsite, and that there is no significant increase in individual or cumulative occupational radiation exposures. The Commission has previously issued a proposed finding that the amendment involves no significant hazards consideration and there has been no public comment on such finding. Accordingly, the amendment meets the eligibility criteria for categorical exclusion set forth in 10 CFR Section 51.22(c)(9). Pursuant to 10CFR51.22(b),noenvironmentalimpactstatementorenvironmentalassessment need be prepared in connection with the issuance of the amenoment.
a t' :p 4.0., CONCLUSION On the basis of the considerations discussed above, the NRC staff concludes that (1) there is reasonable assurance that the health and safety of'the public will not be endangered by operation in the proposed manner, (2) such
- activities will be conducted in compliance with the Commission's regulations,.
and (3) the issuance of.these amendments will not be inimical to the common defense and security or to the health and safety of the public.
Principal Contributors: Don Lasher and Leonard N. 01shan Dated:
May 22, 1989 t'
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