ML20246A986

From kanterella
Jump to navigation Jump to search
Notice of Violation from Insp on 890523-0707.Violations Noted:Licensee Corrective Actions in Response to Findings Identified in Insp Rept 88-22,Detail 10 Re Electrical Cable Inadequate
ML20246A986
Person / Time
Site: Beaver Valley
Issue date: 08/11/1989
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20246A969 List:
References
50-334-89-12, 50-412-89-13, NUDOCS 8908230208
Download: ML20246A986 (1)


Text

.

p ,

I l

APPENDIX A l NOTICE OF VIOLATION Duquesne Light Company Docket Nos. 50-334 and 50-412 Beaver Valley Power Station, Units 1 and 2 License Nos. DPR-66 and NPF-73 As a result of the inspection conducted on May 23 - July 7,1989, and in ac-cordance with the " General Statement of Policy and Procedure for NRC Enforce-ment Actions," 10 CFR Part 2, Appendix C, the following violations were iden-tified:

A. 10 CFR Part 50, Appendix B, Criterion XVI requires that measures shall be established to assure that for conditions adverse to quality, the cause of the condition is determined and corrective action is taken to preclude repetition.

Contrary to the above, the licensee's corrective actions in response to findings identified by NRC in Inspection Report 88-22, Detail 10, regard-ing inadequate separation of safety related electrical cable were not ade-quate. Several similar discrepancies were identified by NRC on July 7, 1989.

Adequate cable separation still does not exist in the Unit 1 Cable Mezzanine.

This is a Severity Level IV Violation (Supplement I).

B. Technical Specification 6.8 requires that written procedures be estab-lished, implemented and maintained covering activities listed in Appendix A of Regulatory Guide 1.33, Revision 2, February,1978.

Maintenance Surveillance Procedure 2MSP-26.01-1 2 MSS-P446 First Stage Pressure Protection Channel III Test,Section V, Initial Conditions, specifies that the above test should not be performed if the at power, low pressurizer pressure reactor trip is actuated.

Contrary to the above, on May 27, 1989, the licensee performed 2MSP-26.01-I with the at power low pressurizer pressure reactor trip actuated. This resulted in a reactor trip.

This is a Severity Level IV Violation (Supplement I).

Pursuant to the provisions of 10 CFR 2.201, Duquesne Light Company is hereby required to submit to this office within thirty days of the date of the letter which transmitted this Notice, a written statement or explanation in reply, including: (1) the corrective steps which have been taken and the results achieved; (2) steps which will be taken to avoid further violations; and (3) the date when full compliance will be achieved. where good cause is shown, consideration will be given to extending this response time.

8005230208 890811 PDR ADOCK 05000354 g PDC