ML20246A878

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Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp 50-344/89-13
ML20246A878
Person / Time
Site: Trojan File:Portland General Electric icon.png
Issue date: 06/28/1989
From: Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To: Cockfield D
PORTLAND GENERAL ELECTRIC CO.
References
NUDOCS 8907070118
Download: ML20246A878 (1)


See also: IR 05000344/1989013

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JUN 2 8 -1989

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" Docket No. 50-344

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Portland. General Electric Company

121 S. W. Salmon Street

Portland, Oregon '97204

Attention:

Mr. David W. Cockfield

Vice President, Nuclear

Thank you for your letter dated June 23, 1989, in response to our Notice of

Violation and Inspection Report No. 50-344/89-13, dated May 24, 1989,

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informing us of the steps you have taken to correct the items which we orought

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to your attention.

Your corrective actions will be verified during a future

inspection.

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Your cooperation with us is appreciated.

Sincerely,

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M. Mend ca, Act ng Chief

Reactor Projects Branch

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State of Oregon

A. Johnson-

G. Cook

B. Faulkenberry

J. Martin

Resident Inspector

Project Inspector

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REGION V

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David W. Cockfield Vice President, Nuclear

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June 23, 1989

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Trojan Nuclear Plant

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Docket 50-344

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License NPF-1

U. S. Nuclear Regulatory Commission

Attn: Document Control Desk

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Washington DC 20555

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Dear Sir:

Reply to Notice of Violation

Your letter of May 24, 1989 transmitted a Notice of Violation based upon

Nuclear Regulatory Commission Inspection Report 50-344/89-13 Appendix A.

Our reply to the Notice of Violation is provided in Attachment 1 to this

letter.

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Sincerely,

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Regional Administrator, Region V

U.S. Nuclear Regulatory Commission

Mr. William T. Dixon

State of Oregon

Department of Energy

Mr. R. C. Barr

NRC Resident Inspector

Trojan Nuclear Plant

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121 S.W. Salmon Street, Portland, Oregon 97204,503'464-8897

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Trojan Nuclear Plant.

Document Control Desk

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Docket 50-344'

June 23, 1989

License NPF-1-

Attachment 1

Page 1 of 2

Response to Notice of Violation

Violation A

Title 10, Code of Federal Regulkcions, Part 50, Appendix B, Criterion KI,

" Test Control", states in part:

"A test program shall be established to

assure that all testing required to demonstrate that systems and components

'will perform satisfactorily in service is identified and performed in

accordance with written test procedures which incorporate the requirements

and acceptance limits contained in applicable design documents".

Contrary.to the above, Temporary Plant Test (TPT)-235, " Remote Shutdown

Station Input / Output Verification", dated April 25, 1988, did not contain

sufficient testing to verify the interlocks and permissives associated with

MO-8702, Residual Heat Removal System suction isolation valve, functioned as

designed subsequent to modification.

Specifically, TPT stated in part,

" verify circuits interrupted by the Remote Shutdown Station (RSS)

installation will perform their control, indication, permissive and/or

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protective functions af ter restoration". However, testing performed'on

May 22. 1988 did not verify the permissive and interlock features of MO-8702

and subsequently, on April 9, 1989, the permissive and interlock features of

MO-8702 were found to be inoperable.

This is a Severity Level IV violation (Supplement 1).

Response

Portland General Electric (PGE) acknowledges the violation.

1.

Reason for the violation.

The reason for the violation was personnel error in determining the

retest requirements for the Temporary Plant Test (TFT) associated with

the instrument loops for MO-8702.

During original construction a

polarity error in the cable plug to Modules PB-405A/B was corrected by

reversing the wiring at the module terminal strip instead of at the

module connector. When Request for Design Change (RDC)85-052 (Remote

Shutdown Station Installation) required the rewiring of the as-designed

module terminal strip, a reversal of the polarity at the input to the

module resulted. Post modification testing should have discovered this

polarity error but it did not.

It was assumed by the engineer preparing

the test that the bistable and controller functions for MO-8702 were not

affected by the rewiring modification to the new Remote Shutdown

Station.

This assumption resulted in the Hagan Rack control, interlock,

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alarm outputs, and some indications not being fully tested. The retest

requirements set forth in the TPT only verified the operability of the

indications on the control room Hasan Racks.

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Trojan Nuclear Plant-

Document Control Desk

Docket 50-344

June 23, 1989

License NPF-1

Attachment 1

Page 2 of 2

2.

Corrective steps that have been taken and the results achieved,

a.

The ability of MD-8702 to be opened and shut from the control room

was verified.

The valve was left in the normal locked-open position

to support Mode 5 (cold shutdown) operation. Additionally,

automatic isolation capability was confirmed for MD-8701, the valve

which prevides a redundant isolation function to MO-8702.

b.

The input module PB-405A/B, to MO-8702, has been rewired to correct

the original polarity error.

c.

Nuclear Plant Engineering (NPE) has reviewed all of the Hagan Rack

circuitry modified by the RDC 85-052 (Remote Shutdown System)

installation. The review determined that all instrument and control

loops affected by RDC 85-052 have been satisfactorily tested or

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otherwise verified to be operating correctly. Plant System

Engineering (PSE) has performed an independent review of the

conclusions reached by NPE and concurs with NPE's findings.

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d.

Plant System Engineering Procedure (PSEP) 20-7 has been revised to

require that the system engineer and design engineer concur with

post-design change test requirements and results. This practice has

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been adopted for all design changes completed during the

1989 Refueling Outage.

e.

The Event Report (89-40) associated with the violation has been

reviewed and discussed at NPE/PSE Electrical Group meetings as a

lessons learned item.

Ensuring that adequate retest requirements

are specified for all components affected by an RDC was emphasized.

3.

Corrective steps that will be taken to avoid further violations.

a.

The Periodic Operating Test (POT-2-5-DB), which tests the interlocks

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for MD-8702, will be satisfactorily completed prior to entering

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Mode 4 (hot shutdown) following the current refueling and

maintenance outage.

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b.

The Quality Assurance Department will become more involved in

post-installation testing. An audit of Plant Systems Engineerin6

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(PSE) in July 1989 will include a review of post-installation

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testing.

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4.

Date when full compliance will be achieved.

Pull compliance has been achieved.

BW/3232W

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