ML20244D897
| ML20244D897 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 04/13/1989 |
| From: | Ebneter S NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | Wilgus W FLORIDA POWER CORP. |
| Shared Package | |
| ML20244D899 | List: |
| References | |
| NUDOCS 8904240190 | |
| Download: ML20244D897 (2) | |
See also: IR 05000302/1989001
Text
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APR 131989
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Docket No. 50-302
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License No. DPR-72
F1orida Power. Corporation
Mr. W. S. Wilgus, Vice President,
Nuclear Operations
ATTN: Manager, Nuclear Operations Licensing
P. O. Box 219-NA-21
Crystal River, 'FL 32629
Gentlemen:
SUBJECT: NOTICE OF VIOLATION
(NRC INSPECTION REPORT NO. 50-302/89-01)
This refers to the Nuclear Regulatory Commission (NRC) inspection conducted by
.P. Holmes-Ray on January 1
27, 1989.
The inspection included a review of the
circumstances ' surrounding improperly sized ASCO solenoid valves installed in
the Instrument Air system.
The report documenting this inspection was sent to
you by letter dated February 17, 1989. As a result of this inspection, failures
to . comply = with NRC regulatory requirements were identified and NRC concerns
relative to the inspection findings were discussed in an Enforcement Conference
held on March 6,1989.
The violations -described in the enclosed Notice of Violation involved failure
to meet. the requirements of Technical Specification 3.6.3.1 and failure to
promptly idantify and correct conditions adverse to quality.
In accordance with the " General Statement of Policy and Procedure for NRC
Enforcement Actions," 10 CFR Part 2, Appendix C (1988) (Enforcement Policy),
the violations described in the enclosed Notice have been categorized as
Severity Level IV problems.
>
The violations described in the anclosed Notice involve your identification
of a discrepant condition and failure to take proper corrective action for
approximately 60 days.
At the Enforcement Conference, you attributed the root
cause to be inadequate training in that an engineering supervisor did not
recognize the safety significance of the discrepant condition.
These viola-
tions are further examples of programmatic problems in the Engineering / Technical
Support SALP functional area for which you recently received a Category III.
Your response to this Notice should address both the violations and the larger
programmatic problems.
You are required to respond to this letter and the enclosed Notice and should
-follow the instructions. specified therein when preparing your response.
In
your response, you should document the specific actions taken and any
additional actions you plan to prevent recurrence.
890424019o 3904 3 2
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APR 137ggg
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In accordance with Section 2.790 of the NRC's " Rules of Practice," Part 2,
Title 10, Code of Federal Regulations, a copy of this letter and its enclosure
will be placed in the NRC Public Document Room.
The responses directed by this letter and the enclosure are not subject to the
clearance procedures of the Office of Management and Budget as required by the
Paperwork Reduction Act of 1980, Pub. L. No.96-511.
Sincerely,
Original signed by
Stewart D. Ebneter
Regional Administrator
Enclosure:
cc w/ encl:
G. L. Boldt, Vice President,
Nuclear Production
A. H. Stephens, General Counsel
R. C. Widell, Director, Nuclear
Operations Site Support
P. F. McKee, Director, Nuclear
Plant Operations
State of Florida
J. Lieberman, OE
bcc w/ encl:
NRC Resident Inspector
Document Control Desk
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