ML20237G621

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Forwards Deficiency Repts Re Letdown HX Mfg by Reco Industries for Info.Util Identified by Reco as Receiving One or More HX Under Purchase Order 546-CA2-240541-BM
ML20237G621
Person / Time
Site: Wolf Creek Wolf Creek Nuclear Operating Corporation icon.png
Issue date: 08/12/1987
From: Oconnor P
Office of Nuclear Reactor Regulation
To: Withers B
WOLF CREEK NUCLEAR OPERATING CORP.
References
NUDOCS 8708240159
Download: ML20237G621 (2)


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August 12, 1987 N'

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Docket'No. 50-482 Mr. Bart D. Withers

-President and Chief Executive'0fficer Wolf Creek Nuclear Operating Corporation Post Office Box 411 Burlington, Kansas 66839

Dear Mr. Withers:

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SUBJECT:

LETDOWN HEAT EXCHANGERS MANUFACTURED BY RECO INDUSTRIES, INC.

The enclosed reports, related to deficiencies in heat exchangers manu-

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factured by RECO Industries, are provided for your information.

Wolf Creek has been identified by RECO as receiving one or more heat exchangers from REC 0 under Purchase Order No. 546-CA2-240541-BM.

Sincerely, IC 3 Paul W. O'Connor, Project Manager Project Directorate - IV Division of Reactor Projects - III, IV, V and Special Projects

Enclosure:

As stated cc w/ enclosure:

See next p ge DIS-UTION bcketFile NRC PDR Local PDR PD4 Reading F. Schroeder J. Calvo P. Noonan P. O'Connor OGC-Bethesda E. Jordan J. Partlow ACRS (10)

PD4 Plant File l

1 PD4/LA PD4/PM PD4/D[

PNoonh P0' Connor: sr JCalvo 8/(9/87 8/p/87 8/g /87 I

B70B240159 870812 PDR ADOCK 050004B2 p

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Mr. Bart D. Withers Wolf Creek Generating Station Wolf Creek Nuclear Operating Corporation Unit No. I cc:

Jay Silberg, Esq.

Mr. Gerald Allen Shaw, Pittman, Potts & Trowbridge Public Health Physicist 1800 M Street, NW Bureau of Air Quality & Radiation Washington, D.C.

20036 Control Division of Environment Chris R. Rogers, P.E.

Kansas Department of Health Manager, Electric Department and Environment Public Service Commission Forbes Field Building 321 P. O. Box 360 Topeka, Kansas 66620 Jefferson City, Missouri 65102 Mr. Gary Boyer, Plant Manager Regional Administrator, Region III Wolf Creek Nuclear Operating Corp.

U.S. Nuclear Regulatory Commission P. O. Box 411 799 Roosevelt Road Burlington, Kansas 66839 Glen Ellyn, Illinois 60137 Regional Administrator, Region IV Senior Resident Inspector / Wolf Creek U.S. Nuclear Regulatory Commission c/o U. S. Nuclear Regulatory Commission Office of Executive Director P. O. Box 311 for Operations Burlington, Kansas 66839 611 Ryan Plaza Drive, Suite 1000 Arlington, Texas 76011 Mr. Robert Elliot, Chief Engineer Utilities Division Mr. Otto Maynard, Manager Licensing Kansas Corporation Commission Wolf Creek Nuclear Operating Corp.

4th Floor - State Office Building P. O. Box 411 Topeka, Kansas 66612-1571 Burlington, Kansas 66839 Resident Inspector / Wolf Creek NPS c/o U.S. Nuclear Regulatory Commission P. O. Box 311 Burlington, Kansas 66839

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e EIVED HRC REC Q i 7'" dgdustries, Inc.

#p sphis ey4fut Bor 25189, Richmond pirg>6sa 7J260 ]

June 16,1987 Te es 827g g ge ecopy 804/6434561 United States Nuclear Regulatory Commission Region 5

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1450 Maria Lane - Suite 210 Walnut Creek, California 94596-5368 Attention:

Mr. D. F. Kirsch

Reference:

Palo Verde Nuclear Generating j

Station - Unit 3 Letdown Heat Exchanger - Cracked Reactor Coolant Inlet Nozzle j

RECO Mfg. Serial No. N-2376 Bechtel Deficiency Report i 86-29

Dear Mr. Kirsch:

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Upon receipt and review of Bechtel DER

o. 86-29, RECO initiated an investigation to a:complish the following:

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1 1.

Identify the total number of Letdown Heat Exchangers manufactured by RECO Industries. Inc., including the customer's name and the location to which they were shipped.

2.

Review final documentation packages to determine if there were any documented unusual circumstances which would contribute to such a failure.

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3.

Determine what Corrective Action, if any, would be necessary to prevent a future recurrence.

Summary:

1.

A total of fifteen (15) letdown Heat Exchangers were identified as being manufactured by. RECO Industries, Inc.

A list identifying the RECO Job Numbers, Customers, Customer's Purchase Order Numbers, and location shipped is enclosed as a part of thf s re-port.

2.

A review of the final documentation package for the reported items did not produce evidence of any unusual circumstances whict would have contributed to such a {ap*ure.

on A review of the docume ation packages for the other fourtoen (14) items revealed that ere were several instances of dented tubes and dented edge preps on nozzles, which indicated improp'tr hand-ling. All of these instances were handled and repaired ir accord-ance with the established Quality Assurance Procedures.

None of the reported instances was of a serious nature, whi:h would contribute to a failure of the type reported.

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Page 2 United States Nuclear Regulatory Commission i

June 16, 1987 3.

RECO should take appropriate corrective action measures for improvement of handling the equipment during fabrication.

This, however, is not appropriate at this time since RECO closed their nuclear fabrication facility in Richmond, VA at the end of 1986 and have turned in their ASME "N" Certificates.

While there is no evidence in our records, and subsequent inspection of the other two units at the Palo Verde plant, to indicate that the type of conditions reported on the Letdown Heat Exchanger at Palo Verde, i

Unit 3 exists on the other units manufactured by RECO, it is 'our recom-mendation that the utilities be notified and that they perform a visual examination of the inlet and outlet nozzles on these units during normal re-fueling operations.

If we can be of any further' assistance please do not hesitate to call.

Very truly yours, RECO INDUSTRIES, INC.

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j Ronald E. Brooks C6rporate QA Manager

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CC:

W. S. Point, Jr.

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i RECO LET-D0'a*N IIEAT EXCHANGER LIST JOB NO.

CUS1DMER IDCATION -

P. O. NO.

N-2387 Combustion Engineering Boston Edison Co.

9603488 Pilgram 2 Gen. Sta.

N-2381 Combustion Engineering TVA 96034S5 Yellow Creek-Unit 2 N-2380 Combustion Engineering Duke Power Co.

9602911 Project 81 Cherokee Unit 2 N-2376 Combustion Engineering Arizona Public Service 9773806 Palo Verde Gen. Sta.

Unit 3 N-2374 Combustion Engineering Duke Power Co 9602915 Project 81 Perkins Unit 2 N-2373 Combustion Engineering Arizona Public Service 9602914 Palo Verde Gen. Sta.

Unit 2 l

N-2372 Combustion Engineering Duke Power Co.

9602918 l

Project 81 l

Cherokee Unit 1 N-2371 Combustion Engineering WPPSS Unit 5 9602910 N-2370 Combustion Engineering Arizona Public Service 9602912 Palo Verde Gen. Sta.

1 Unit 1 I

N-2369 Combustion Engineering WPPSS Unit 3 9602909 N-2284.10 Westinghouse Wolf Creek Gen. Sta.

See Below Lebo, Iansas

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I N-2284.20 Westinghouse Westinghouse See Below I

4255) 4454 Genesee St.

Buffalo, N. Y.

N-2284.30 Westinghouse Callaway Gen. Sta.

See Below Portland, Mo.

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f JOB NO.

CUSTOMER LOCATION P. O. NO.

N-2284.40 Westinghouse Westinghouse See Below 4454 Genesee St..e j Buffalo, N. Y. 14225-

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N-2284.50 Westinghouse Callaway Gen. Sta.

See Below l

Portland, Mo.

P. O. N0 s N-2284.10 546-CAZ-240541-BM N-2284.20 546-CAZ-240542-BM N-2284.30 546-CAZ-240543-BM N-2284.40 546-CAZ-240544-BM N-2284.50 546-CAZ-240545-BM e

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February 27, 1987 023-02098-JCH/DR1, BEGIOlwle5 U.S. Nuclear Regulatory Commission Region V 1450 Maria 14ne - Suite 210 Valnut Creek, California 94596-5368 Attention:

Mr. D. F. Kirsch, Director Division of Reactor Safety and Projects Palo Verde Nuclear Generating Station (PVNCS)

Units 1, 2, 3 Docket Nos. 50/528, $29, 530

Subject:

Final Report - DER 86-29 A 50.55(e) Condition Relating to letdown Heat Exchanger Nozzle Crack File: 87-006-216

Reference:

(A) Telephone conversation between R. C. Sorenson and D. R.

Iarkin on November 14, 1986.

(Initial Notification - DER 86-29)

(B) ANPP-39248, dated December 5,1986. (Interim Report - DER

(,

86-29)

(C) ANPP-39651, dated January 9, 1987.

(Time Extension - DER j

86-29)

(D) ANPP-40101, dated February 12, 1987.

(Tice Extension - DER 86-29)

I

Dear Sir:

i The NRC was notified of a potentially reportable deficiency in Reference (A),

an interim report by Reference (B), and a time extension by Reference (C) and (D).

Attached, is our final written report of the Deficiency under the requirements of 10CFR 50.55(e) and 10CFR21.

Very truly yours,

' W J. C. Haynes Vice President Nuclear Prgduction I

i JCH/DRL:kp i

Attachments cc: See Page 2 pn! w75 p,p

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Final Report - DER 86-29 Mr. D. F. Kirsch

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Director Page Two February 27, 1987 023-02098-JCH/DRL H

cc:

J. M. Taylor Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D. C.

20555 A. C. Gehr (4141) l R. P. Zimmerman (6295)

Records Center Institute of Nuclear Power Operations 1100 circle 75 Parkway - Suite 1500 Atlanta, Georgia 30339 I

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FINAL REPORT - DER 86-29 DEFICIENCY EVALUATION 50.55(e) s ARIZONA NUCLEAR POWER PROJECT (ANPP)

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PVNGS UNITS 1, 2, 3 l

I. Description of Deficiency On October 27, 1986, during Hot Fenetional Testing (HFT) in Unit 3, water was discovered leaking from the reactor coolant inlet nozzle of the Letdown Heat Exchanger (tag no. 3M-CHN-E02) located in the Auxiliary Building. 2he nozzle (identified as Nozzle A on vendor print N001-7.03-28-7) had a 120* circumferential, through-wall crack that was detectable by visual and dye penetrant examination. The Letdown Heat Exchanger is manufactured by Richmond Engineering Company (RECO) and suppliet' by Combustion Engineering under the NSSS contract.

II. Evaluation 2his section of the report covers an evaluation of the physical evidence,

. probable cause.s, supportive analysis, and the root cause conclusion.

Also discussed are Units 1 and 2 operability, transportability, and safety assessment.

A. Evaluation of Physical Evidence

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Various physical inspections were performed af ter identification of the nozzle failure. The following summarizes the results of these inspections.

1.

Nozzle / Piping Configuration Nozzle A is a 2-1/2 inch diameter, Schedule 40, stainless steel (SA312-TP304) pipe stub, attached to the heat exchanger shell by a full penetration, double-ended bevel weld, which is reinforced with an external 1/2 inch fillet weld. (See Figure 1) 2his nozzle configuration conforms to ASME III, Class 2 Code requirements.

The 2 inch inlet piping connected to the nozzle rises vertically 3 feet 4 inches upstream of the nozzle, and then runs horizontally out of the heat exchanger room. The piping is supported on this horizontal run by a three-way restraint Ic:sted approximately 3

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feet from the riser.

2.

Visual Inspection of Damaged Nozzle A visual inspection performed by the an ANPP metallurgist of the cracked nozzle resulted in the following observations:

The failure occurred on the top side of the nozzle adjacent to the toe of the reinforcing weld. As indicated in Figure 1, the toe of the

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o weld adjacent to the failure had been ground back leaving a groove approximately 1/32 inch deep by 1/8 inch wide and 2 inches long where the failure occurred. In addition, the geometry of the weld

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did not provide a smooth transition between the vessel and nozzle. As discussed later, this geometry and groove resulted in a stress concentration which significantly contributed to the nozzle failure.

The failure consisted of a main through-vall circumferential crack approximately 3 inches long 'on the nozzle exterior, and two other disconnected cracks parallel to the first, which did not penetrate the nozzle wall. The main crack was not perpendicular to the nozzle surface, but sloped back under the fillet veld at a slight angle. The length of this crack on the nozzle interior was about 1 inch shorter than on the nozzle exterior. This indicates that the crack started on the outside at the toe of the reinforcing fillet veld (where the groove was located) and propagated through the nozzle base metal. The main crack appears to be made up of two smaller hairline cracks that grew together as they propagated. This is a typical configuration for a high cycle / low stress fatigue failure.

Inspection of the nozzle indicated no evidence of plastic deformation, nor was there any indication of movement and/or distortion of the inlet piping.

The Meta 11urgist's disposition of the failure mechanism was fatigue based on his visual examination.

3.

Pipe Strain

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Prior to repairing the nozzle, the inlet piping was cut loose from the nozzle and the free movement was measured as 1/8 inch,1/8 inch, and 1/4 inch in the horizontal, vertical, and axial directions, respectively. Since the piping could be moved easily

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by hand into alignment with the nozzle, cold pipe strain is not

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considered to be a cause of failure. Hot pipe strain due to thermal growth of the piping system at operating temperatures has been determined by analysia to be within Code allowables.

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Metallurgical Defects Removal of a sample of the fractured material for metallurgical examination prior to the initial repair work was attempted.

l However, due to the nozzle configuration and the unknown slope of

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the crack a sample could.not be obtained and still maintain the integrity of the nozzle for subsequent repair.

The repaired nozzle was metallurgically examined in situ by a metallurgist. A Texas Nuclear Alloy Analyzer was used to deter-mine the chemical makeup of the original weld metal (Nozzle A) not disturbed by the repair, Nozzle B (outlet nozzle), and the shell wall. Ibe analyses indicated that all of these materials conformed

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to specification requirements. A severn gauge was also used to determine the ferrite content of the Nozzle A weld material.

Readin6s of 7.5 to 10 percent were obtained, which indicate a

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ferrite content sufficient to suppress formation of microfissures in the weld metal.

5.

Vendor Fabrication and inspection Review of the vendor Code Data Package did not identify that -

Nozzle A had been repaired in the vendor's shop prior to shipment. The nozzle is certified as having met Code (ASME Section III, Class 2) requirements, including passing liquid penetrant-examination and hydrostatic testing in the vendor's

-shop.

In addition, the nozzle passed a system hydrostatic test in the field prior to flushing.

According to Article NC-4424 of the Code, grinding by the fabricator is permitted to obtain a weld surface sufficiently free of grooves, valleys, and abrupt ridges as long as the weld or base metal meets thickness requirements. All design thickness require-ments were met. In this case, however, grinding lef t grooves in a valley along with an abrupt ridge rather than smoothing out such undesirable features. 'It is concluded that vendor grinding produced the grooves since there was no record of field repairs.

6.. Damage During Shipment or Installation There were no marks on the heat exchanger to suggest that damage

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occured af ter manufacture, and there is no record of field repairs being performed prior to the failure.

Therefore, improper handling during shipment, installation, or start-up is not considered a cause of failure.

B. Evaluation of Probable Causes The potential failure mechanisms resulting in a crack of this type are tensile (ductile) overload, liquid metal embrittlement, stress corrosion cracking, weld metal microfissures, and fatigue. Each of these mechanisms were evaluated as summarized in the following sections.

1.

Tensile overload Tensile overload was determined not to be the cause for failure because there was no plastic deformation of the nozzle, nor were there signs of pipe support movement or distortion.

2.

Liquid Metal Embrittlement Cracks associated with liquid metal embrittlement occur at tempera-tures higher than the eutectic point of the metals involved. The crack pattern due to liquid metal embrittlement is craze type

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  • rather than showing well defined directionality as seen in the observed -

failure.

For a thin vall stainless steel pipe such as Nozzle A liquid metal embrittlement is possible only due to contamination during the welding process

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during fabrication and is usually found either by a surf ace examination with a liquid penetrant or during the hydrostatic test. Since the heat exchanger did not leak on hydrotesting and was free of linear dye penetrant indications (as determined by a review of the Code data package), liquid metal embrittlement' is not considered the cause of the failure.

3.

Stress Corrosion Cracking (SCC)

Two mechanisms of stress corrosion cracking were evaluated. These were 1) Intergranular Stress Corrosion Cracking (IGSCC) and,

2) Transgranular Stress corrosion Cracking (TCSCC).

The nozzle crack started in the heat affected zone (RAZ) of the veld at the bottom of the notch. However, the crack did not follow the HA2, but instead propagated through the unaf fected base metal. The KAZ is where the greatest degree of sensitization would occur, and an intergranular stress corrosion crack would classically be expected to propagate in the sensitized grain structure of the HA2.

Therefore IGSCC is not considered to be a possible failure mode.

To have TCSCC, a corrodent containing chlorides must be present typically at or above 140 degrees F (in the pH ranges around 7).

While the microstructure is always susceptible to SCC, these conditions would normally occur on the nozzle ID during hot start

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up.

The crack started on the CD of the nozzle which is a most I

unlikely place for TCSCC to initiate.

The ID of the nozzle would be the most likely place for the initiation of either IGSCC or TCSCC.

Thus it was concluded that SCC was not the cause of the failure.

4.

Microfissuring Full austenetic weld metal is subject to microfissuring. However, when there is at least three percent ferrite present in the weld metal (more than seven percent ferrite in the weld metal was actually present), the risk of cracking is minimized. Also, i

microfissuring is a phenomenon confined to the weld metal and I

therefore 'is not a cause for cracks occuring in the base metal.

Fatigue Based on the above, tensile overload, liquid metal embrittlement, stress corrosion cracking, and microfissuring were eliminated as causes of the failure. The physical appearance and location of the crack identifies fatigue as the mechanism of the nozzle failure. The cause of the fatigue failure is established in the following sections.

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4 C. Supporting Analysis In evaluating the possibility that random transients or unanticipated C

cyclical loads could have caused the nozzle to fail, several areas potentially affecting nozzle loads were identified and evaluated using static and dynamic analysis techniques in accordance with the methods and procedures of Section NB-3600 of the ASME Code. All potential load contributors, except for seismic loads, were considered in the evaluation of stresses.

The evaluation reconstructed the history of loads at the nozzle from the start of flushing operations up to its failure during HFT. The evaluation also considered hypothetical loads resulting from worst case misoperation of the letdown system control valves that would generate pressure transients and hydraulic loads.

The various factors that could contribute to nozzle overstressing were divided into two main categcries for evaluation; high cycle / low stress loads and, low cycle /high stress loads.

The high cycle / low stress loads result from flow induced vibration that could occur during flushing and system operation.

The design of the piping system was evaluated for natural frequency of vibration, vibration displacement, and the resulting forces and stresses. To assess the ability of high cycle fatigue as being the cause of the nozzle failure, a fracture mechanics evaluation was performed. The fracture mechanics evaluation establishes a threshold stress amplitude range that would result in propagating a crack and the number of I

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cycles required for the nozzle to fail. In order to determine if this failure mechanism was possible, expected stresses due to flow induced vibration were compared to the minimum required threshold value for crack propagation.

The low cycle /high riress loads result from operational thermal and hydraulic transierats in the letdown system. These transients were evaluated to establish stresses induced in the nozzle and the integrated effect on nozzle integrity. A cumulative usage factor (UF) evaluation was performed in accordance with the ASME Code Section NB-3600. To account for the groove at the toe of the weld, stress indices for socket weld joints were used in en ASME III Code Class 1 fatigue evaluation in accordance with Section NB-3683.2 (Note, the letdown heat exchanger is an ASME Code Class 2 vessel).

In summary, the following sections will show that the most probable sequence of events resulting in nozzle failure was high cycle / low stress fatigue crack propagation to or near through-wall during flushing.

This was followed by low cycle /high stress transient conditions occuring during hot functional testing.

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l Table 1 provides summary of the evaluation of transient and cyclical loads.

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1.

High Cycle / Low Stress Loads Flow induced vibration will be amplified by the natural frequencies of the piping system and can provide a high number of stress cycles in a short time period (hours or days rather than i

months or years). The stress amplitude necessary for fatigue crack initiation and propagation is dependent on the vibration amplitude and frequency. As noted in Section II.A.2 & 5, the weld geometry and presence of the groovc with grinding marks provided a site for stress concentration and crack initiation. Fracture mechanics data provides an estimate of the range of minimum stress amplitudes necessary for fatigue crack propagation.

1.1 Fracture Mechanics Evaluation The fracture mechanics analysis demonstrates that a crack initiating at a sharp grinding mark or scratch would propagate under the applied cyclic loads. This was determined-using the following equation:

6Kth = C (46th)(Fa (Ref. 1, 2, 3) where 4K h = threshold stress intensity factor range; ksi[lC5 t

C = shape factor 4(th = threshold stress range (=2 x threshold stress

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amplitude); ksi a = flaw depth; in Based on a simplified model approximating the groove and the flaw as a planer flaw perpendicular to the axis of the pipe, the minimum stress amplitude for fatigue crack propagation was determined to range from 7.0 to 3.5 ksi.

Due to the conservatism in this model as compared to the actual condition, it is concluded that the threshold stress is at the lower end of this range. This conclusion is supported by review from an independent consultant (Reference 4).

Vibration displacements of 0.48 mil at 3.5 inches from the toe of the fillet veld will provide 3.5 ksi stress at the top of the nozzle.

The rate of fatigue crack propagation was determined using the folicwing equation:

da/dN = C E S ( AX)D

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n__

4 s

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Where da/dN = rate of crack advaecenent; inch per cycle

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C = material constant = 1.59 x 10-9 (inch / cycle)/

(ksi(Tn)n n = material constant = 3.3 S = R ratio correction factor = (1.0 - 0.5R )-4 2

E = 1.0 for air R - stress ratio ( (i min /(max) = 0.6 for 4 K=5;

= 0.79 for o K-3.5 Substituting 4 K = 5 or 3.5 ksi gfin, da/dN = 0.7 or 0.4 x 10-6 inch / cycle The above calculation shows that even with stresses at the lower threshold stress amplitude (e.g. 3.5 Ksi), a crack will propagate to 0.4 inch depth in one tillion cycles.

Both of the above calculations represent a reasonable basis for quantitative fatigue failure analysis.

1.2 Flow-induced Vibration Sources Two flow conditions existed that could give the requisite number of cycles, that of the normal steady state flow vibration and the flow induced vibration during system flushing operations.

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1.2.1 Normal Steady State Flow Measurements were made during normal flow conditions during HFT ioetween 50 and 90 gpm) and the displace-ment was found to be 0.035 mil at 3.5 inches from the toe of the weld. A calculation was performed with results provided in Table 1.

Based on the fracture mechanics evaluation, normal steady state flow results in stress levels well below the crack propagation threshold that will not adversely affect the integrity of the heat exchanger nozzle.

1.2.2 Flushing Flow The Unit 3 flush of the letdown system piping occurred in January,1986, lasted approximately 44 hours5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> at an estimated flow rate of 200 spa based on pump characteristics and piping configurations. One of the applicable flush paths (per Flushing Procedure 91FL-3CH03) is shown on Figure 2.

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3.

l The theory of turbulent boundary layers suggest that the fluctuating energy in the turbulent layer varies

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as the square of the mean flow velocity (Reference 5).

It is reasonable to assume that the vibration of the pipe wall is proportional to the pressure fluctuations in the boundary layer. The piping vibration levels levels, measured at a distance of 3.5 inches from the toe of the weld for steady state flows of 50 gpm to 90 gpm were extrapolated to that for the estimated flushing flow rate of 200 gpm. At 200 gpm, the extrapolated range of vibration levels would be from 0.2 mil to 0.6 mil displacement. The lower threshold calculated for crack propagation is 0.48 mil displace-ment, which is well within the range of estimated flushing flow rate induced vibration displacements.

Increasing the flow rate to 200 gpm will result in a greater contribution from the higher frequency components, (Reference 8), which will further increase the piping response beyond the 0.2 mil to 0.6 mil displacement extrapolated above. Conservatively this was not considered.

If a conservative vibration range of 3 to 10 Hz is assumed, then 475,000 to 1.6 million cycles would result from the flushing operation. Therefore, there were a sufficient number of stress cycles (approximately 500,000 cycles for crack propagation of

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0.2 inch) to propagate the crack to or near through-wall.

In summary, it is concluded that estimated flow induced vibration during the flushing process, when combined with the existing nozzle groove and grind mark conditions, is reasonably projected to cause crack propagation to or near through-wall.

2.

Low Cycle /High Stress Loads Fluid temperature, pressure and flow rate data were recorded during hot functional testing in October 1986 just prior to the nozzle failure. Forcing functions due to various system transients were also determined. A fatigue evaluation of the combined effects was performed utilizing the criteria of ASME Section III Article NB-3600 as delineated below. It was concluded that the transiente experienced during Hot Functional Testing were not sufficient to. significantly contribute to a fatigue crack propagation of the nozzle, but may have been the mechanism during HPT to result in final breach of the pressure bundary.

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L1 Evaluation of HTT hermal Transients 2

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The HPT thermal and flow transient' data was reduced to histograms and used in Beebril coc/pdter program ME-643 to calculate the OT, dT,Jf and T ' terms (ue to the 1

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b thermal transients { rapid temperature changes). These terms were then used alorug with loads due to dead weight, pressure.

and thermal expansion in 3echtel computer program ME-913 to determine peak, thermal gradient and discontinuity stresses.

he program also determines the load set pairs and calculates corresponding usage f actor.

D e methodology utilizes the techniques of Article NB-3600. To account for the existing groove,, stress indices for girth fillet veld to socket veld fittings.were usumed per Table NB-3683.2-1. D e results of this evaluation'are shown in Table 1.

The temperature and flow transients that were recorded during HTT prior to the nozzle failure were compared to the transients given in the design specification and found to be less severe.

2.2 HTT Pressure Transients n e effects of pressure transients are discussed in the paragraphs below. De enveloping effect of these transients and the temperature transients evaluated above were analyzed and resulted in a total cumulative usage factor of less than 0.1.

This result is well below a usage factor of 1.0 allowed by the Code.

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2.2.1 Evaluation of Backpressure Control Valve Closure he peak dynamic loads on' letdown piping resulting from the transients reported during HTT were

alculated using the system response data to the transients. During cycling of the pressure valves PV-201P and PV201Q, thi letdown flow was completely interrupted when switching from one PV to the other due to a closed blockvalve upstream of the other PV.

Using the marinum letdown flow, letdown heat exchanger outlet pressure, and valve characteristic data, the transient loads' vere calculated for pipe segments between the letdown heat exchanger and the level control valve. D e loads are caused by the pressure wave propagating from the closed pressure valve toward the reactor coolant loop and are a function of the rate of change of pressure and veJocity'.

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The static forcing function from the abott' analysis was modeled into Bechtel computet program ME-101 to determine the loading at the letdown heat exchanger nozzle. Rese loads yere included in conjunction with thermal and pressure ' transients in the enveloping calculation discussed above.

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m 2.2.2 Evaluation of Valve Cycling In order to evaluate the forces generated near the

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inlet nozzle of the letdown heat exchanger du'e to the cycling of one of the level control valves, a computer model of the letdown piping from the RCS connection to the purification ion exchanger' unit was developed.

This model, run on Bechtel's inhouse computer Code NE 820, included the regenerative and letdown heat exchangers. The back pressure valve was modeled as a control valve which opened or closed attempting to maintain constant backpressure as its upstream pressure increased or decreased,'respectively. The level control valve was cycled from its initially throttled position to fully closed, then to fully open and then fully closed and so on.

The opening and closing times of the level control-valve were based on actual field test data and were 0.78 seconds and 1.84 seconds, respectively. The back pressure valve was opened / closed in 0.56 seconds.

Forcing functions were generated due to the level control valve cycling and the back pressure valve reacting to the pressure change.

The time history forcing function from the above analysis was compared with the loads of 2.2.1 and

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found to be enveloped.

2.3 Evaluatico of Nozzle post Repair Valve Cycling Vibration Data Following repair of the failed nozzle, displacement measurements were recorded by a transducer counted on the nozzle while the actdown and back pressure control valves were cycled. This was performed to determine the transient loading to the repaired nozzle. A calculation was per!N reed to determine the stress levels at the nozzle induced due to the measured displacements. The resulting cyclic stresses are significantly below that required for fatigue crack propagation. -

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2.4 Hypothesized Water Hammer Due to Level Control Valve Misoperation

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The worst case dynamic load hypothesized for the letdown piping system would be a water. hammer event as a result of valve misoperation. A hypothetical situation was postulated under which, as a consequence of misoperation of the level control and pressure control valves, a partial voiding of the system piping occurs.

Under this scenario, it was assumed that the level control vcives are closed while the pressure control valves are open.

This would result in the j

depressurization and flashing of the stagnant fluid downstream of the level control valves.

With the cooling water continuing to flow on the shell side of the heat exchanger, the steam will be condensed creating a void in the piping between the I

i level control valve and the beat exchanger. The opening of the level control valve at a later time will cause the void to be collapsed and cause water hammer loads in the piping. These water hammer loads were developed utilizing the configuration of the letdown system piping, valve characteristic data, and process conditions upstream and downstream of the system boundary. Based on these data steam / liquid impact velocities and corresponding water hammer loads on the piping are calculated.

C This condition could occur during manual shif ting of the letdown control valves. However, steps 17.4.6 and 17.4.7 of pVNGS operating procedure 410P-ICH01 require warmup of the line between the control valves and the letdown heat exchanger via the letdown control valve 4

bypass line (valve CENHV526). The procedures also require slow operating of the letdown control valve in order to reduce the potential for severe water hammer loading.

This allows the back pressure valve to 4

modulate smoothly.

I A calculation was performed using the postulated loads from the above evaluation. The resulting stress at the nozzle was conservatively calculated to be 22,000 psi. Utilizing the stress indices discussed in II.C.I.1 to account for the groove on the nozzle, this conservative loading by itself would require approximately 1500 occurrences to reach a usage factor of 1.0.

Using the stress indices for a tapered

. k-

.______-____-_A

u transition joint to approximate the ungrooved nozzle, the loading would require approximately 18,000 occurrences to reach a usage factor of 1.0.

Based on the number of cyles required, this hypothetical scenario is not considered to be a factor in the fatigue failure in the Unit 3 nozzle.

These results demonstrate that the transients experienced during HFT -

and those hypothesized were not sufficient to significantly contribute to a fatigue crack propagation of the nozzle. However, they may have been the mechanism during HFI to result in final breach of the -

pressure boundary.

l D. Root Cause 6

The root cause of the failure is high cycle / low stress fatigue based on physical evidence, test data, and analyses.

The conclusions reached are as follows:

1.

The primary root cause is believed to be the geonetry of the weld area including the presence of the circumferential groove with grinding marks into the base metal where the crack occurred.

2.

The origin and visual characteristics of the cracks are typical of high cycle fatigue failures in a ductile material such as stainless steel.

The nozzle was subjected to flushing performed in January,1986 at sufficient velocities during the 44 hour5.092593e-4 days <br />0.0122 hours <br />7.275132e-5 weeks <br />1.6742e-5 months <br /> flush

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period to result in a large nunber of low stress cycles at stress levels that have been projected to be of sufficient magnitudes to have reached the range for crack propagation. Four days af ter the y

start of hot functional testing in October 1986, the nozzle failure was observed.

This followed a series of transients during HTT which may have caused the final breach in the pressure 4

bounda ry.

Independent consultants (References 6 and 7) have confirmed the conclusions reached with regards to the potential flow induced stresses and susceptibility to failure.

3.

All mechanisms other than high cycle / low stress fatigue have been eliminated.

Fased on the visual evidence, analytical results, and the elimination of the other failure mechanisms, it is concluded that the nozzle veld condition in combination with the flow induced vibration during the flushing of this line condition is the most probable mechanism to result in a high cycle - low stress fatigue failure.

i L a o

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E. Units 1 and 2 Operation h e condition identified in Unit 3 was evaluated for applicability to

-h Units 1 and 2 with the following results:

i 1.

Visual examinations, for evidence of leakage, were performed on-both units letdown heat exchangers initially. This was done at the first opportunity f or each unit (i.e., unit shut down). The results confirmed no evidence of leakage.

2 Subsequently, NDE (liquid penetrant) inspections were performed on the inlet and outlet nozzles of the Unit 1 and 2 letdown heat exchangers. The inspection confirmed that no' fatigue cracks were present.

Unit 2's welds did not have grooves around the toe of the weld, however, the general profile of the weld did not provide a snooth transition from vessel to nozzle. The liquid penetrant exam did l

not reveal any indications.

Unit l's welds had similar. profiles as Unit 3 and had the same type groove around the toe of the weld. Liquid penetrant erans did reveal indications that were determined to be superficial.

As a prudent action, the Unit 1 and 2 letdown heat exchanger inlet and outlet nozzle welds have been reworked in the field to remove the grooves and improve the weld profile to eliminate any areas of stress concentration.

This provides futher assurance that these

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nozzles will be satisfactory for the intended service.

3.

Cyclic stresses during normal plant operation have been shown to be acceptacle by testing and/or analyses.

Based on the above, and on the FSAR/CESSAR ar,alysis and the safety assessment in Section II.G of the consequences of postulated breaks in the letdown lines outside containment, continued use of the letdown heat exchanger did not and does not pose a hazard to the safe operation of Units 1 and 2.

F. Transportability The letdown nozzle crack problem has been determined to be not transportable to other areas of Palo Verde due to the following reasons:

1.

The Unit 1 and 2 letdown heat exchangers inlet and outlet nozzles, which have similar veld configurations, experienced hydraulic and thermal transients, and was put through a similar flush operation, did not have any indications of any fatigue crack initiations after several thousand hours of operation. This would indicate that the Unit 3 nozzle fatigue failure wcs the result of a unique combination of physical and operational fattors limited to that nozzle.

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m___________

E.

2.

The letdown heat exchangers are the only equipment manufactured by RECO for Palo Verde. Since the root cause of the failure is believed to be unique to this nozzle veld geometry and

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workmanship, it is not expected that this condition ezists-in any other location at Palo Verde. To provide additional assurance of this, a review applicable to other vendor supplied components in safety related systems, will be conducted. See corrective action section.

3.

This-type nozzle configuration (i.e. small bore pipe stub-ins) is a standard practice allowed for by the ASME Code.

There have been no generic industry notifications that problems exist with these i

type nozzles.

4.

The Unit 3 flushing operations of the letdown system could not have damaged other piping system components.

The piping system between the flushing connection and the nozzle is relatively

]

flexible. The nozzle is the only point of rigid fixity where pipe loads are concentrated. In-line components, such as valves which I

are remote from the failure location are an integral part of the piping system and any pipe motion would easily be transmitted through them without resulting in any significant stress inducement.

C. Safety Assessment A break in the letdown system during normal operation would cause a release of primary coolant and represent a failure of an ASME Code

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component. This could adversely affect the safety of operations because it would disrupt the normal operation of the primary system, limit the continued operation of the plant, potentially expose offsite and onsite personnel to a radiation hazard, and could result in injury to plant personnel in the area.

Per PVNGS FSAR/CESSAR Section 15.6.2, a double-ended break of a letdown line outside containment "results in a two-hour thyroid inhalation dose which is a small fraction of 10CFR100 guidelines." An analysis was performed to evaluate smaller breaks than those analyzed in CESSAR Section 15.6.2.

The spectrum of breaks analyzed ranged from a single-ended break down to the largest break that would remain undetected by the Auxiliary Building Lower Level Ventilation Exhaust Monitor (RU-9). None of the breaks analyzed resulted in doses higher than the letdown line break previously analyzed in the CESSAR, and all of the letdown breaks analyzed resulted in doses which are small fractions of 10CFR100 guidelines.

III. Deportability Assessment Based upon the above, this condition is being reported under 10CFR Part 50.55(e) and 10CFR Part 21. All requirements for reporting under the regulations have been addressed except 21.21(b)(3) subpart (vi) with regard to the names and locations of other facilities...

e

__._____-___m__._._

e IV. Corrective Action The nozzle crack was initially weld repaired under NCR NA-1942 in order C

in support HFT. After HTT was completed, additional welding was performed to increase the size of the reinforcing weld from the original 1/2 inch size to 3/4 inch. The final weld provides four benefits:

1. The highest stress point is moved into a region further down the nozzle which was relatively unaffected by fatigue.
2. The fatigued area is now bridged with new weld material which j

compensates for any fatigue-induced weakness in the nozzle.

3. The additional reinforcing fillet annealed the nozzle base metal that was affected by fatigue.
4. The groove marks have been removed and there is now a smooth transi' tion between vessel and. nozzle.

These improvements, together with the absence of any significant source of fatigue in the operating system, provide assurance that the nozzle will be satisfactory for its intended service.

Units 1 and 2 letdown heat exchanger nozzles have been reworked as a prudent action. ASME Section XI Inservice Inspection requires the letdown heat exchanger to be leak-tested every 3-1/3 years and hydrotested every 10 years.

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Although we believe the root cause of this failure to be unique to the veld geometry, and 11 sited to the letdown heat exchanger, we are in the process of reviewing other vendor supplied components in safety related systems for similar parameters (i.e., nozzle design and weld configuration, etc.).

This review will be complete prior to July 1,1987.

A copy of this report is being sent to Combustion Engineering and RECO for their evaluation and action.

V. References 1.

R. A. Smith, " Fatigue Thresholds," Vol. 1, 1982, pp 33-44

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2.

L. P Pook, " Fatigue Crack Growth Data for Various Materials Deduced from Fatigue Lives of Precracked Plates," Stress Analysis and Growth of Cracks, ASTM STP $13, pp 106-124,1972 1

3.

Evaluation of the Flaws in Austenitic Steel Piping, Transactions of l

the ASME, Journal of Pressure vessel Technology, Vol. 108, August 1986, pp 352-366 4.

Dr. Hircea D. Ratiu, DENG. Impe11 Corporation Walnut Creek, California 5.

A. A. Townsend, "Ihe Structure of Turbulent Shear Flow," Cambridge University,1976, Second Edition 6.

Iarry E. McKnight, President, McKnight & Associates, Registered Professional Metallurgical Engineer, Brea, California 7.

Dr. Mircea D. Ratiu, Gordon Hau, Robert Emerson, Impe11 Corporation Review of Unit 3 Letdown Heat Exchanger Nozzle Crack February 19-20, 1987 8.

J. C. Wachez, C.L. Bates, " Techniques for Controlling Piping Vibration and Failures," ASME Publication 76-Pet-18

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