ML20235W815

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SALP Board Rept 50-395/87-23 for Jan 1986 - Jul 1987
ML20235W815
Person / Time
Site: Summer South Carolina Electric & Gas Company icon.png
Issue date: 10/09/1987
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML20235W807 List:
References
50-395-87-23, NUDOCS 8710190041
Download: ML20235W815 (33)


See also: IR 05000395/1987023

Text

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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101 MARIETTA STREET, N.W.

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ATLANTA, GEORGIA 30323

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ENCLOSURE

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SALP BOARD REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBER

50-395/87-23

SOUTH CAROLINA ELECTRIC AND GAS COMPANY

V. C. SUMMER

JANUARY 1, 1986 THROUGH JULY 31, 1987

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INTRODUCTION

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The Systematic. Assessment of. Licensee - Performance (SALP) program is an

integrated NRC staff effort to collect available observations and. data on

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a; periodic. basis and to evaluate licensee performance based upon this

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information.

SALP is supplemental to normal regulatory processes used to

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. ensure compliance with NRC rules -and regulations.: SALP is intended to be

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. sufficiently diagnostic to' provide a rational basis for allocati, J.NRC

resources and-to provide meaningful guidance to the licensee's management

to promote quality'and safety of plant construction and operation.

An NRC SALP. Board, composed of the of the staff members listed below, met'

on September 28,

1987, to review the collection of performance

observations and data- to assess the licensee performance in accordance

. with' the guidance . in' NRC Manual Chapter 0516, " Systematic Assessment

Performance."

.A summary of the guidance and' evaluation criteria is

provided II of this report.

This report is the SALP Board's assessment of the licensee's safety

performance at

V..C. Summer for the period January 1,

1986, through

July 31, 1987.

SALP Board'for Summer:

L.'A. Reyes, (Chairman) Director Division of Reactor Projects (DRP), RII

A. R. Herdt, Chief, Division of Reactor Safety (DRS), RII

J. P. Stehr, Director, Division of Radiation Safety and Safeguards (DRSS)

RII

E- G. Adensam, Director, Project Directorate II-1, NRR

.

J. B. Hopkins, Project Manager, NRR

D. M. Verre111, Chief, Reactor Projects Branch 1, DRP, RII

R

L. Prevatte, Senior Resident Inspector, Summer, DRP, RII

Attendees at SALP Meeting:

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K, D. Landis, Chief, Technical Support Staff (TSS), DRP, RII

H. C. Dance, Chief, Projects Section IB (PS1B), DRP, RII

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W. J. Tobin, Physical Security Section, DRSS, RII

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L. P. Modenos, Project Engineer, PS18, DRP, RII

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P. C. Hopkins, Resident Inspector, Summer, DRP, RII

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T. E. Conlon, Chief, Plant Systems Section, DRS, RII

R. W. Wright, Quality Assurance, DRS, RII

L. S. Mellen, Quality Assurance, DRS, RII

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C. M. Hosey, Chief, Facilities Radiation Protection Section, DRSS, RII

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J. B. Kahle, Chief,-Radiological Effluents and Chemistry Section, DRSS, RII

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D. M. Collins, Chief, Emergency Preparedness and Radiological Protection

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Branch, DRSS, RII

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R. A. Becker, Operations Engineer, NRR/PEB

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II.

CRITERIA

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Licensee performance is assessed in selected functional areas, depending

upon whether the facility has been in construction, preoperational, or

operating phase during the SALP review period.

Each functional area

normally represents areas which are significant to nuclear safety and'the

environment and which are normal programmatic areas.

Some functional

areas may not be assessed because of little or no licensee activities or.

lack of meaningful observations. .Special areas may be added to highlight

significant observations.

a

One.or more of the following evaluation criteria was used to assess each

functional area; however, the SALP Board is not limited to these criteria

and others may have been used where appropriate.

A.

Management involvement in assuring quality

B.

Approach to resolution of technical issues from a safety standpoint

C.

Responsiveness to NRC initiatives

D.

Enforcement history

E.

Reporting and analysis of reportable events (including responses to,

Analysis of, and corrective actions for)

F.

Staffing (including management)

G.

Training effectiveness and qualification effectiveness

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Based upon the SALP Board assessment, each functional area evaluated is

classified into one of three performance categories.

The definitions of

these performance categories are:

Category 1:

Reduced NRC attention may be appropriate.

Licensee

management attention and involvement are aggressive. and oriented

toward nuclear safety; licensee resources are ample and effectively

used so that a high level of performance with respect to operational

safety or construtt W is being achieved.

Category 2:

NRC attention should be maintained at normal level.

Licensee management attention and involvement are evident and are

concerned with nuclear safety; licensee resources are adequate and

are reasonably effective so that satisfactory performance with

respect to operational safety or construction is being achieved.

Category 3:

Both NRC and licensee attention should be increased.

Licensee management attention or involvement is acceptable and

considers nuclear safety, but weaknesses are evident; licensee

resources appear to be strained or not effectively used such that

minimally satisfactory performance with respect

to operational

safety or construction is being achieved.

The functional area being evaluated may have some attributes that would

place the evaluation in Category 1, and others that would place it in

either Category 2 or 3.

The final rating for each functional area is a

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composite of the attrib'utes tempered with,the-judgement of NRC management

as to theLsignificance of. individual items.

' The"SALP Board may also-include an appraisal 'of the performance trend. of a-

functional ' area.

This' performance trend. will' only be .used when both a

' definite trend of' performance within the' evaluation period'is discernible'

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- and- the Board believes that continuation of the trend may result in a

change of performance level. 'The trend,.if used, is defined as:

Improving:

Licensee performance was determined 'to be improving .near the

close of:the assessment period.

Declining: . Licensee performance was determined to be declining' near the~

close of.the assessment period.

III.' SUMMARY OF RESULTS

A-

Overall . Facility Evaluation

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The

licensee displayed an aggressive . attitude toward problem

identification arid solution.

The level

of

performance - was

satisfactory in all areas. Of the eleven program arens rated, six

were evaluated as Category. I and five as Category

2..

No Category 3

ratings : were assigned.

Problems in the Fire Protection and Plant

Operations areas,. identified in the ' previous SALP, received strict

management attention and oversight.

These' areas exhibited significant

improvement during'this evaluation period. A strength, also noted in=

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the previous SALP, was again identified in the areas-of Security and

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Safeguards,

Radiological

Controls and Maintenance.

Additional.

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-strengths were ' identified in the Surveillance,

Training and

Qualifications Effectiveness and Outages areas.

The licensee has

initiated a number of programs, - such as, ' scram ' reduction, personnel

error reduction, and system review that has helped focus attention on

proper operation and system identification.

B.

The performance categories for the current and previous SALP period

in each area are as follows:

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July 1, 1984-

Jan. 1, 1986-

Functional-Area

Dec. 31, 1985

July 31, 1987

Plant Operations

3

2

Radiological Control

1

1

Maintenance

1

1

Surveillance

2

1

Fire Protection

3

2

Emergency Preparedness

1

2

Security and Safeguards

1

1

Outages

2

1

Quality Programs and Administrative

2

2

Controls Affecting Quality

- Licensing Activities

2

2

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Training and Qualifications

2

1

Effectiveness

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IV.

PERFORMANCE ANALYSIS

A.

Plant Operations

1.

Analysis

During the assessment period, inspections were performed by the

resident and regional staffs.

Plant operations experienced two alignment problems associated

with the operation of swing pumps during the first few months of

the evaluation period.

As a result of these problems and

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weaknesses identified in the previous SALP, the licensee

initiated extensive changes to provide better control over plant

operations.

These changes included:

modifications to improve

plant system reliability in the condensate /feedwater system; an

employee awareness program;

root cause determination of

personnel errors; improvement in operator training; a team

building program; industrial safety awareness; a professional

awareness program; human performance error correction; increased

staffing and management presence to support operations during

plant startups. A management review board which consists of the

Vice President, Nuclear Operations; the Director, Nuclear Plant

Operation; the Director, Nuclear Services; the Director, Quality

Services; and the Plant Management Staff was initiated in 1986.

This group reviews all reactor trips and other plant significant

events to insure that the efforts and resources needed to insure

timely corrective action are available and actions are initiated

to preclude recurrence.

During the last twelve months of the SALP period, positive

results were achieved as a result of the above actions.

A

significant reduction in the number of overall violations (21

vs. 33 from last SALP period) and an improved operating

performance was achieved.

A comparison with the previous SALP

shows that reactor trips were reduced from 13 to 7 with only 2

trips in the last 12 months of the SALP period.

The forced

outage rate was reduced from 8.44 percent to 4.01 percent.

The

plant capacity factor was increased from 56.8 percent to 77.2

percent and the plant availability was increased from 63.4

percent to 80.5 percent.

V.C.

Summer achieved the second

highest capacity factor, 92.4 percent, and the highest plant

availability, 95.3 percent, for domestic Westinghouse Plants in

1986.

A shift engineer program to provide a degreed engineer on shift

was implemented in 1987.

The licensee also implemented a

college degree program in 1987. This program, conducted by the

University of Maryland, allows personnel in Operations and

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Nuclear Training areas to obtain a Bachelor of Science Degree in

Nuclear Science.

Several of the courses in this program are

being developed through funding provided by four utilities. The

above program should strengthen the onshift expertise and

improve plant safety.

South Carolina Electric and Gas Company initiated a program in

1986 to document and verify the detailed design basis for

selected plant systems, structures and components. This program

integrates

project

engineering

data,

historical

project

correspondence and engineering inputs to provide a detailed

description of the plant designs.

Three system reports have

been issued.

These documents provide a better technical

understanding of the present design and provide better data for

future design changes.

Seventeen systems, structures and

component designs are now under review with anticipated

completion dates of March 1988.

The Licensee also initiated a program in 1986 to perform safety

systems functional inspections. The inspection of the Emergency

Feedwater System has been completed.

The inspection of the

Emergency Power System is currently being conducted with an

anticipated completion date of December 1987.

Inspections are

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currently planned on ten other systems, at a rate of approxi-

mately two systems per year.

Deficiencies that have been

identified in the completed inspections are prioritized,

assigned required completion dates are tracked to completion.

Identified problems are also reviewed for generic application to

other systems. This program and the above detailed design basis

review have led to the identification and correction of safety

problems and increased licensee's k.nowlodge and understanding of

installed systems.

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The plant is clean and well maintained.

Plant and corporate

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management make frequent tours in the plant during normal work

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hours, back shif ts and weekends.

A control room enhancement

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program has provided an improved control room supervisors

console; upgraded equipment and habitability have provided an

atmosphere which promotes a more professional appearance and

attitude.

The operators are well trained, alert and responsive

to plant transients and events.

Control room demeanor has

improved since the previous assessment.

Four violations were identified. Violations (a) and (b), which

were associated with the alignment and operation of swing pumps,

led to the imposition of civil penalties. These items were the

result of the licensee's lack of documented design information

and knowledge of a complicated design.

The licensee's overall

corrective action on these two items was detailed and extensive

with positive results.

Violation (c) was the result of the

licensee transferring the engineered Safety Features Electrical

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busses from offsite power to the Emergency Diesel Generator

because of an imminent electrical storm. The licensee's action

reduced the independence between the onsite and offsite power

system, and reduced the availability of the preferred offsite

power source and with a potential to overload the ' diesel

generators under worst case accident conditions.

Violation (d)

was the result of a procedure not containing specific steps

required to start a service water booster pump if it should trip

on low suction pressure.

The violations are listed below,

a.

Severity Level III violation and a civil penalty for

failure to maintain two service water and two component

cooling water pumps operable.

(86-06)

b.

Severity Level III violation and a civil penalty for

failure to maintain the required charging / safety injection

pumps operable under certain design basis conditions.

(86-12)

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c.

Severity Level IV violation for failure to perform a 10 CFR 50.59 review prior to operating the Engineering Safety

Features electrical

busses on the Emergency Diesel

Generators.

(86-15)

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d.

Severity Level V violation for an inadequate operating

procedure for the service water booster pumps.

(87-14)

2.

Conclusions

Category:

2

3.

Board Recommendation

The board noted an improving trend towards the end of the SALP

period.

No change in NRC inspection activity is recommended.

B.

Radiological Controls

1.

Analysis

During the assessment period, inspections were performed by the

resident and regional staffs.

This included a confirmatory

measurements inspection using the Region Il mobile laboratory.

The licensee's health physics (HP) and radwaste processing

staffing levels compared favorably with other utilities having a

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facility of similar size. An adequate number of ANSI qualified

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licensee HP technicians were available to support routine

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operations.

During the 1987 refueling outage approximately 120

contract technicians were utilized to support the licensee's

staff.

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One- strength noted in-the health physics, radiological effluent

and environmental l surveillance program was the ' stability : of' the-

staff.

A low' turnover rate resulted in'an experienced group of

individuals: and provided the time ~ necessary to . implement an

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effective' and continuing training program for the technicians.

LThe licensee's radiation. work permit and respiratory protection

programs. are adequate . The licensee documented five skin' and

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ten clothing contaminations in 1986. .Through July 31-1987, the

licensee documented'74 cases"of skin contamination and 48 cases

of clothing contamination.

The 1987 increases..in skin / clothing

contaminations are 'related to the increased work activity during

the 1987 refueling and maintenance outage, the only major outage

.during the assessment period.

A Severity Level III violation was issued during the evaluation

period for a calculated overexposure to the hand of a worker.

The violation identified the failure to have a procedure for -

addressing the methodology for calculating the dose to the skin

from. highly radioactive particles.

The calculated overexposure

resulted from a high specific activity particle (hot particle)

on the skin of the hand which occurred while the individual was

working . in a clean area.

In the response to the Notice of

Violation,

the. licensee

requested

that

more

current

. international standards be used to calculate the dose to the

skin- for this ' exposure rather than the standards used as the

basis of 10 CFR 20. The methods proposed would result in a dose

significantly .less than the NRC quarterly limit.

On July 13,

1987, the NRC rejected the licensee's position and stated that

the Notice .of ' Violation was correct as written.

A second

request for reconsideration of- the Violation was received on-

August 7,

1987, and is being evaluated by the NRC.

The

violation represents an isolated occurrence in an usually strong

and aggressive radiation protection program maintained by the

licensee and did not indicate a significant program weakness.

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Management support and involvement in matters related to

radiation protection is evident.

During the evaluation period

licensee management authorized the purchase of whole body

friskers to improve the personnel monitoring program and

constructed a new building to house the dosimetry, whole body

counting, and respiratory fit testing activities.

Management

commitment to keeping radiation expcsure as low as reasonably

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achievable ( ALARA) is indicated by their involvement in the

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activities of the ALARA committee.

The licensee participated in the National Voluntary Laboratory

Accreditation Program (NVLAP) for personnel dosimetry and

received NVLAP accreditation for the program during the

evaluation period.

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The . licensee's; approach. to resolving health physics technical'

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overexposure event.

The' licensee ~ -routinely utilizes ccontract~

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issues'wasl excellent.as. evidenced by the dose evaluation forLthe-

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support toL supplement the. staff in:the various technical aspects-

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of the_ radiation protection program'.

The . licensee. exercised an ' aggressive contamination control

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program .with the decontamination crew reporting .to health

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- physics.

The contamination control program is .consideredJ the

- best in Region II. 'In 1986 the licensee reduced the total:

- contaminated area (excluding' the reactor building)' to 714 ft -

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(0.5%).. - The . total contaminated area increased to_5% just after

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the refueling outage and was back down to 1.8% or ,2,785 ft2 tv;

July 31, 1987. The licensee routinely' maintains less than 1% of

- the radiation control _ area (2000 square feet) as contaminated

during non-outage conditions.- The licensee's contro'1 of

contamination, useL of contamination containmentsand process

controls allowed personnel in . street clothes to enter the:

reactor. building (containment) during the refueling' outage.

During 1986,~the' license's cumulative exposure'was approximately

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23 person-rem ~ as- measured by' thermoluminescent dosimeter (TLD),

which was well below the 1986 national average of 397 person-rem

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per unit. This represents the lowest cumulative exposure for an.

' operating. light water reactor in the United States -in 1986.

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' Through July 31, 1987,. the cumulative exposure' as measured by-

TLD.was 558 person-rem. .The increase in dose from 1986.to 1987

is' explained by the fact that a major refueling and maintenance-

outage was conducted-in ,1987 while no significant outages' took

place in 1986. The majority of outage exposure resulted from

steam generator

activities.

Approximately- 300 person-rem

resulted from the peening, plugging, plug removal, eddy current

testing, and U-bend heat stress relief on the three generators.

The refueling outage in 1987 exceeded the outage exposure goal

of 485 person-rem by 62.7_ person-rem.

Participation in the NRC spiked sample analysis program showed

agreement with NRC results for all four nuclides. Confirmatory

measurements showed the ' licensee's measurement program to be

adequate with the exception of an incorrect volume being used to

determine radionuclides concentrations. This error, conservative

with respect to radiological safety,

resulted in a violation

but had no serious effect on the. program.

The licensee

responded quickly to this finding, initiating corrective action

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prior to completion of the inspection.

Both liquid and gaseous effluents were within limits for total

quantities of radioactive material released, with the gaseous

effluents being the lowest in the Region. Effluent releases for

the past three years are summarized in the Supporting Data and

Summaries,Section V. K.

1:e,see estimates of air dose and

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doses to the maximum exposed individuals were variable between

reporting periods, but were within the limits in the Technical

Specifications'.

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Significant progress has been made in developing the expertise

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and qualifications of the chemistry staff; however, the level of

staffing lacks depth.

Improvements were made during the

assessment period when the plant chemist returned to the

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chemistry staff from a special assignment.

The licensee was

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aggressive in the resolution of a problem related to oil

inleakage into the secondary coolant which required considerable

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chemistry staff manpower.

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In the areas of corrosion and water chemistry, the integrity of

the primary coolant pressure boundary had started to degrade

through primary-side stress induced cracking of steam generator

tubes.

The licensee's control of prima ry and secondary

chemistry was better than the criteria recommended by the Steam

Generator Owners Group.

The general corrosion (wastage) of

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carbon steel components has been maintained to a relatively

insignificant level as measured by the cleanliness of the

secondary water system.

A new computer system for chemistry

data has been installed, and a management system for trending

and statistical analysis has been implemented.

The licensee

iritisted prompt and adequate responses to the pipe thinning

issues described in IE Bulletin 87-01 and IE Notice 86-106 with

. Supplements.

During 1986, the licensee shipped a total of 3,966 ft3 of

radioactive waste with a total activity of 14.6 curies.

This

value is well below the 1986 national average of 7,448 f t3 per

reactor.

Through July 31, 1987, the licensee had shipped a

3 with a total activity of 488.4 curies. The

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total of 9,490 ft

total volume shipped as July 31, 1987, showed a significant

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increase (240%) in the volume of over the previous year. This

was due to the increased dry active waste generated in the 1987

refueling outage.

Radiological surveillance

and internal audits conducted by the

licensee were comprehensive and of sufficient depth to identify

problems and trends.

Five violations were identified.

a.

Severity Level III violation for extremity exposure in

excess of the limits of 20.101(a) for a one individual and

failure to have an adequate procedure to address skin dose

calculations due to high levels of skin contamination.

(86-22)

Note:

Licensee has partially denied tM s violation.

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b.

Severity Level

IV violation for failure to specify

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quantities :of carbon-14 and iodine-129 - on a shipment

manifest.

(86-04)

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c.

Severity Level IV violation for failure to adhere to -

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procedures

for

health

physics.

computer

software

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verification.

(86-04)

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d.

. Severity Level IV violation for failure to classify a

radioactive waste shipment properly.

(86-10)

e.

Severity Level: V violation for failure to verify the volume

of 'the geometries used to conduct surveys of gaseous

radioactive material releases to the environment.

(87-21)

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2.

Conclusion

Category:

1

3.

Board Recommendations

A reduced NRC inspection activity is recommended.

C.

Maintenance

1.

Analysis

During the assessment period, inspections were performed by the

resident and regional staffs.

The maintenance organization is adequately staffed and trained

to support the operation of the plant.

In 1986, a procedure

writer and a spare parts specialist were added to each

discipline and a maintenance engineer was assigned for heating,

ventilation

and

air conditioning.

Work activities are

controlled by well developed procedures and instructions.

The licensee continues to expand its use of the motor operated

valve analysis test system (MOVATS),

infrared analysis,

ferrographic oil analysis and vibration analysis to assist in

predictive maintenance.

Additional equipment has been obtained

for MOVATS and the data bank has been enlarged as additional

equipment is tested. The licensee has achieved success in their

use of INP0's Nuclear Plant Reliability Data System to predict

and identify failed parts.

The use of predictive maintenance

data to revise the schedule of preventative maintenance has led

to a reduction in equipment failures.

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A three year program to develop instrumentation and control (I &

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C) loop diagrams is approximately one-third complete.

An

in-depth NRC review of the inservice inspection and test program

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was conducted to insure that all required tests and inspections

are being performed.

The maintenance group has started a maintenance self-assessment

program review using INPO guidelines for the " Conduct of

Maintenance at Nuclear Power Stations".

This effort will take

several months to complete.

A new hot machine shop and calibration facility have been

constructed and placed in operation.

A metrology group was

formed to control all measuring and test equipment.

This group

consolidates under one supervisor and at one location those

functions which were previously performed in the I & C

electrical, mechanical and construction craf t area. All site

tools have been consolidated into one central tool issue room

for improved control and accountability.

A weakness in first line supervisory planning and direct

involvement in corrective maintenance was identified by licensee

,

management and other auditing groups. To correct this weakness,

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the licensee implemented formalized instruction to insure inore

direct involvement by supervisors in work planning, scheduling,

observation and review of werA activities.

A team building

program was implemented in 1986, to improve communication and

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supervisory insight 1.nto their responsibilities.

Specialized

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technical, supervisory and communications courses are being

develop and implemented to increase the skills and awareness of

first line supervisors.

Maintenance management has used quality assurance audits, QC

inspection reports, trend analysis reports and INP0 good

practices to monitor equipment performance and work practices.

The maintenance group interfaces well and is receptive to

constructive criticism from outside observers.

No violations were identified in this area.

2.

Conclusions

Category:

1

3.

Board Recommendation

A reduced NRC inspection activity is recommended.

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..D.

Surveillance

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During this assessment period, inspections 'were. performed by.

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.the resident ~ and regional staffs.

Areas inspected . included

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ins'ervice inspection, routine. surveillance testing, startup

testing following: re f uel i ng ~,

reactor physics' surveillance

testing,. ' integrated engineered safety. features' testing and 18

month and five year _ diesel.~ generator surveillance.

Staffing

and " training was: adequate and surveillance

were ' conducted

within the allotted time frame,

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The computerized Technical Specification Cross Reference system

has ~ been completed and is currently being validated.

This

system permits tracking .to insure technical

specification

compliance.

A. computerized Set Point Verification Data system

was purchased and was used to set the safety. . valve on the

pressurizer and steam generators during the last outage. This

system provides a printout of set point and the force used to

lift.the valves, Tests during the last outage demonstrated that-

the use of this system resulted in tests and data that. were

' repeatable and superior to previously used equipment.

,

A weakness in responsiveness to NRC. concerns was identified in .

,

the previous SALP. The licensee has' placed additional emph' sis

a

in this-area.

Managers are now assigned to each NRC item to

. provide single point accountability and insure that they are

-

addressed in a timely manner.

This increased sensitivity has

resulted in no identified NRC concern in this area.

The use of field standards for the majority of surveillance

tests has reduced the number of repetitive tests that must be

accomplished to achieve satisfactory results.

All changes to

surveillance tests are required to be routed through the

operations procedure writers group to insure correctness.

Errors noted in the review of surveillance tests'are now rcuted

back to the individual making the mistake for correction.

The Regulatory Support Group, which tracks all surveillance

tests, has been transferred from Regulatory Compliance to

Scheduling and Project Management.

This change places the

responsibility for scheduling and tracking completion of

surveillance tests under the same manager. Under this' single

manager, surveillance

are more easily incorporated into the

plant overall schedule.

This has additionally resulted in

improved coordination and a reduction in surveillance test

interface problems.

. !

,. . -

. - - _

_-

..

..

.

h

'

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p. ,

13

..The . licensee comple.ted L a review of the Inservice I'nspection

~

Program .to; insure Lthe- testing supported components required toi

.

achieve; plant cold shutdown. As a result of this review, .over

100-valves were added to this inspection program and additional

L

tests' are now required on some valves that were already in. the

'

!

program. A weakness associated with the training of operations

. personnel for-visual examination for' leakage was identified in

,

"

.the. previous. SALP.

The' responsibility for training and

<

qualification of ' operators for this ' function has been placed

m --

under the direction of Quality Control' Training. 'The. changes-

have led to a marked improvement in.this area.

On the advice- of a consultant, a- new thermal power program was

installed for -monitoring thermal power in August 1985.

The

program had errors in mathematics, statistics, engineering and

in the correlation between turbine pressure and thermal power.

In June 1986, in response to a report by another consultant and

errors identified by an ISEGl engineer, the program was changed

to an acceptable calculation based upon feedwater flow

measurement and enthalpy change. .Despite the difficulties the

thermal power did not exceed the technical specification' limit.

-The acceptance of the first change is indicative of a weakness

in the licensee' in utilizing consultants without critical

,

evaluation of their qualification and performance.

One violation was identified.

Severity Level V violation for failure to follow an

--

operating procedure and an indequate operating procedure.

(87-20)

2.

Conclusion

f

Category:

I

a

]

3.

Board Recommendation'

A reduced NRC inspection activity is recommended.

E.

Fire Protection

1.

Analysis

During this assessment period, inspections were conducted by the

,

regional- and resident inspection staffs of the licensee's

J

routine fire protection / prevention program and the corrective

actions associated with the outstanding issues from the June

,

1985. Appendix R inspection.

l

l

!

_

. . . _ . _ _ _

_._._._____.____________________J

_ _ -

_ _ - ._

__

_ - _ _ _

_

_

.

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14

n.

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.

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The licensee's

implementation

o f.

the fire: . prevention

.

b

administrative controls, general housekeeping'and.the control of

l

h

combustible and flammable materials in safety related areas of.

'

'

. the. plant were ' found to be satisf actory. -The fire . protection :

'"

,

J

l

exting'uishing, systems', fire detection . system . and fire barrier

assemblies - protecting systems requiredfor safe L shutdown. were

-found to be; functional.

.In. addition ~

the surveillance

,

inspection,' tests . and - maintenance' instructions for the' plant-

1

< fire protection systems' were found satisfactory cand met L the-

'd

criteria of the plant- technical. specifications.

The . licensee's ' fire. brigade organization,' staffing and training

were-evaluated. The: organization and staffing.of the ' brigade

'

+

meet'the~NRC guidelines and the plant'technica.1 specifications.

The. ' training . and drills for the- brigade were found to be

comprehensive with respect to assuring effective. and ' efficient

manual fire fighting operations.

The frequency, of brigade

<

training and drills met. or exceeded the NRC guidelines.

'

Overall,

the fire brigade training program is strictly

. implemented and well defined.

The. annual fire protection / prevention audit, the 24 month QA

fire protection program. audit performed by the licensee, and the

triennial ~ audit performed by an outside fire protection

organization were conducted within the specified frequency and

,

covered

all

of

the

essential

elements

of

the. fire

protection / prevention program.

The licensee had taken the

appropriate corrective actions on the discrepancies identified

by=these audits.

As ~

result of .' the issues stemming from the ' Appendix R

a

inspection conducted in' June 1985, and the licensee's' Appendix R

compliance re-evaluation, the ' licensee implemented a number of

plant modifications which resolved the separation concerns

associated with redundant hot standby' systems, the alternative

shutdown system concerns associated with inadequate remote

shutdown

stations,

and the associated circuit concerns

associated with fire. induced spurious signals.

All previous

identified discrepancy items have .been corrected during this

assessment period. The licensee's implementation of Appendix R

modifications was

timely and consistent with scheduled

commitments. In additior., the licensee's approach to resolving

. Appendix R technical issues was supported by intense management

involvement and control in assuring quality and indicated a

clear understanding of the technical issues by the licensee's

staff and a technically sound approach toward implementing

complex plant modifications.

_ _ _

_ - - _ _ _ _ - _ _ _ _ -

-_

.

.

-__

_.

--_

.

.

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Staffing for the routine : fire: protection ' program is~adequatecto

,

.

accomplish thel' goals of . the : position _within: normal work hours

'

with -only . occasional

overtime being:' expended. ..The; fire-

.,_

protection staff- positions, authorities and responsibilities' are

clearly defined; and personnel holding these' p'ositions.are wel1~

.

qualified lfo'r their. assigned duties.

'Three' violations were identified. Violation:(a) w'hich resulted.

'from the June 1985' Appendix' R Linspection: was Lissued in March 11,

1987; as'a Severity Level .III violation; this was discussed in

the ~1ast' SALP. Violations'(b) and'(c) were a result of failure

.to post' fire watches.

The violations are listed below.

a.

Severity : Level? III . violation- forf failure ~ to maintain one

train 1 of redundant systems - necessary. to maintain 'and

achieve hot standby conditions free from damage; and fire

barriers were. rendered' inoperable and action were not taken

i

to establish a' continuous or' hourly fire watch.

(85-26)

.b.

Severity Level IV violation involving failure to post fire

watch patrols while fire barriers were inoperable. '(86-06)-

c.

Severity Level IV violation involving failure to perform

,

Lhourly fire watch patrols.

(86-13)

2.

Conclusion.

Category:

2

..

3;

Board Recommendations

The board noted an improving trend. No change in NRC inspection

activity is recommended.

F.

Emergency Preparedness

1.

Analysis

During the assessment period, inspections were performed by

resident and regional staffs. There were two inspections of the

radiological emergency plan and procedures, and observation of

two annual radiological emergency preparedness exercises. Three

emergency plan revisions were reviewed.

!

The annual emergency preparedness exercises disclosed no adverse

findings regarding the licensee's emergency organization and

staffing.

An adequately staffed corporate emergency response

and planning organization routinely provided support to the

i

- -

- - - - _ _ _ _ _ _ _ _ _ - _ _ . _ _ _ _ _ _ _ _ _ _

._

_.

_

_ _ _ _ _ - _ _ _ _ _ _ _ _ _ _ _ -

b'

a.

6

E

16

.

plant.

Key positions in the corporate and plant emergency

response organizations were filled.

Corporate management was

directly involved . in the 1986 and 1987 annual emergency

preparedness exercises and followup critiques. .The licensee

continues to respond to. the NRC initiatives regarding emergency

c

preparedness issues promptly and effectively.

The essential elements of emergency response, demonstrated

during the . referenced exercises, were determined to be

acceptable.

Observation and critique of the annual emergency

preparedness exercises disclosed that the Emergency Preparedness

Plan. and procedures could be effectively implemented by the

licensee, although one violation, one weakness and several areas

for improvement were observed by the NRC. . These items were

formally documented, and the licensee committed to corrective

action consistent with regulatory requirements and guidance.

The principal items involved (1) a violation concerning an

inadequate procedure for notifying offsite authorities of an

emergency classification within 15 minutes (notification times

.

ranged from 15 minutes to 33 minutes during the course of the

l

exercise) and; (2) an exercise weakness for failure to include

offsite radiological emergency monitoring and surveillance

proceduns in field team kits, and identification of such

documents as " controlled procedures."

During the assessment period there was a violation for failure

to provide training to a key member of the Emergency

Organization regarding the " Fission Product Barrier Approach"

(FPBA) for Emergency Action Level (EAL) defining emergency

classifications.

This could lead to improper or delayed

classification of an emergency in an actual event. The. licensee

took prompt corrective action on this finding.

Inspections

disclosed that all other training of onsite and offsite

emergency organization personnel was consistent with the

requirements defined in the Emergency Plan and implementing

procedures.

The licensee, on December 10, 1985, changed the Emergency Plan

to implement a symptomatic EAL Matrix.

This matrix was

determined by the NRC as an unacceptable alternative to the

NUREG-0654, " Event-oriented Classification Scheme," in that it

appeared.to classify events as lower level emergencies than as

outlined in NUREG-0654 and because certain event based

classifications, such as loss of control of facilities to

intruders and station blackout, would be delayed.

After

correspondence and meetings with the NRC on the issues, the

licensee deleted proposed use of their form of FPBA and

reinstated the event oriented EALs consistent with NUREG-0654

guidance.

The other Emergency Plan revisions reviewed during

the subject assessment period were found to be consistent with

NRC guidance.

\\

_---_--______-_________O

'

.

.

17

S

Two violations were identified and as indicated above were not

indicative of a programmatic deficiency:

a.

Severity Level IV violation for an inadequate procedure

defining notification of offsite authorities of an

emergency.

(86-08)

b.

Severity Level V violation for failure to provide training

to a key member of the Emergency Organization regarding the

" Fission Product Barrier Approach" to event classification.

(86-05)

2.

Conclusion

Category:

2

3.

Board Recommendation

No change in NRC inspection activity is recommended.

G.

Security and Safeguards

1.

Analysis

During the evaluation period, inspections were performed by the

resident and regional staffs.

A Regulatory Effectiveness

Review (RER) was conducted in March 1986.

Security force staffing was adequate and consistent with that of

plants of similar size. The security staff had been trained to

perform required duties. The training program was extensive and

innovative with a well balanced mixture of hands-on and

classroom instruction which resulted in a highly capable and

motivated security force.

Observation of security force

activities during periods of inspection verified a quality

training program and a commitment to excellence by individual

members of the security force.

Site

management

exhibited

an

excellent

knowledge

and

understanding of security requirements and demonstrated support

of the security program.

l

The RER team visited the site and found no safeguards

I

vulnerabilities. Although not considered requirements, several

inadequacies and weaknesses were identified and received

immediate corrective action by the licensee.

The RER team

identified strengths in the Summer security program, in such

areas as barriers, maintenance program, training and tactical

deployment of the security force.

_ _ _ _

._

_ - _ _ - _ - _ - _ .

- _ - _ -

,

.(.

g.'*

-

.,

R

.

n.

,

18

i-

4 '

-

%

.

.The licensee recently - installed ai new' securityf computer to

enhanceithe: effectiveness of the security program. - Functional

operability:of the computer and associated systems .is pending

~

completion of testing and acceptance L of the? systems.

In

addition, .the construction of .a ' new access' control facility,

relocation of the affected protected. area fencing.: necessitated

by- the ,new access' control facility, installation.of: additional

closed circuit television (CCTV) cameras and an-- enhanced alarm

system is : indicative of an ongoing management commitment.. to. a

quality ' security program. The ; security equipment and facility

_

enhancements clearly add to the: effectiveness and operational-

capabilities of-the security organization.

l

One violation was identified.

The licensee had identified the

violation and provided prompt.and effective corrective action.

Severity Level IV violation for an unsecured vital area

-

floor grating. (87-12)

'2.

Conclusion

Category:

1

3

Bcard Recommendation

A reduced NRC inspection activity is recommended.

H.

Outages

1.

Analysis

During the . assessment period the unit underwent a 95 day.

refueling outage.

The resident inspectors observed refueling

operations.

Resident and regional based inspectors observed

outage activities.

j

I

The third refueling outage was completed on June 9, 1987. Major

"

activities accomplished during this outage included: refueling;

shot peening, stress relieving, tube plugging, tube removal and

eddy current testing of steam generator tubes; five year

overhaul on diesel generator B; overhaul of reactor coolant pump

A motor; seal replacement on reactor coolant pumps A and B;

reactor vessel inservice inspection; reactor baffle inspection

for jet impingement; inspection of the service water system for

microbiological induced corrosion and corbicula infestation;

inspection of feedwater piping as related to the Surry steam

,

line break and completion of design changes and modifications.

j

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.

19

!

The licensee's activities associated with the steam generator

-l

work appeared to be well planned and managed. , This work was

anticipated to be critical path and controlled other outage

-activities. Good communication, coupled with an excellent and

.

'

cooperative work relationship with the contractor, permitted

this work'to be-accomplished with minimal time on critical path

and little effect on other activities in the reactor building.

Taking 'into consideration the amount of work performed, the

number of concurrent activities being accomplished, and the fact

that some of the activities were a first for a " hot" plant, the

overall performance in this area was noteworthy.

Unanticipated problems such as relugging 1000 connections on the

Engineered Safety Features Load Sequencer, replacement of valve

internals on a RTD bypass manifold valve, rework of a ' reactor

coolant system leak on a reactor coolant pump and higher than

anticipated radiological conditions in the reactor building

extended the refueling outage by approximately 30 days.

Ninety-five design changes and modifications were completed

during the outage. These modifications consisted of 16 Appendix

R, 43 plant reliability, 28 TMI backfits for post accident

monitoring and control room human factors improvement, and eight

other miscellaneous items.

The maintenance group completed

the major portion of the work associated with Appendix R

modifications and feedwater piping inspections.

Maintenance

efforts in repairing the failed valve in the RTD bypass manifold

and the leak in a reactor coolant pump seal injection line were

examples of excellent work coordination and accomplishment under

difficult and demanding circumstances.

The licensee performed an inadequate design analysis and

modification that relocated the Service Water Pump air

temperature detectors near the pump room ceiling.

Correlation

testing was not done to ensure the ceiling air temperature

readings were representative of the air entering the pump motors

at floor level.

Subsequent temperature comparisons by the NRC

disclosed the ceiling detector readings were less (cooler) than

the actual air temperatures at pump level and the TS limit was

exceeded.

A new staff position of Associate Manager, Project Management

was added to the scheduling and project management area to

provide better scheduling and control of design changes and

modifications.

These changes have resulted in a definite

improvement in the number and timeliness of modification

,

completions.

A Modification and Contractor Services Group to

l

manage modification work and control contractor services was

j

established in 1987.

This group's handling of contractor

l

acquisition, training and day-to-day job management relieved

!

other site management of these functions and proved to be an

j

asset during the outage.

i

4

- - - - _ . _ _ - - . - - - _ - . . - _ _ _

_

.

__

. _ - -

- _ _ _

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___ - _ - _ - _

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" Integrated safeguards testing, . plant startup. and '. low L power

physics ' testing was closely monitored by the ' resident-inspectors

d

.and regional specialists. .Each activity appeared.'to be: well-

controlled'with adequate _ supervision and management oversight.

,

,

Inspectors reviewed the ISI/IST Program, procedures and records,

l

and ' observed inservice inspect' ion in progress.

Other ~ areas

l

examined by regional based inspectors included: .The licensee's

response'to license _ condition 2.C.'11. dealing with the volume of

material required to be examined - ultrasonically;. valve test

stroke' time -limits; . and steam generator' tube,

U-Bend,

stress-relief and tube-sheet-roll, transition-area, and ' shot

peening processing.

Acceptable evidence.of prior planning and-

control of. activities was noted.

Procedures and policies were

adhered to in the-ISI/IST area.

Training, qualification, and

certification of ISI/IST personnel continued to be good.

Licensee management involvement in the outage was evident by

-their daily presence in the . field observing critical work

activities and attendance at off hours outage staff meetings. A

critique. was conducted upon completion of outage.

All

identified deficiencies or needed improvements were documented

and given completion dates for corrective action.

,

Two violations were identified:

-a.

Severity level IV violation for failure of quality control

inspectors to adequately inspect and verify that steam

generator tubes were properly plugged in both' ends.

(87-11)

b.

Severity Level V violation for failure to perform an

adequate design analysis.

(87-20)

2.

Conclusion

Category:

1-

3.

Board Recommendation

A reduced NRC inspection activity is recommended.

I.

Quality Programs and Administrative Controls Affecting Quality

1.

Analysis

- During the assessment period inspections were performed by the

resident and regional inspection staffs.

I

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._

__

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21

-

L

For the purposes of.this assessment, this area is defined as the

'

~

l..

ability . of the licensee to . identify and correct their own

problems.

It. encompasses all plant activities, . all ' plant' .

. personnel, as well as .those -corporate functions and personnel'

.that provide services to' the plant. . The plant and corporate QA

staff have responsibility for verifyingLquality. The rating in .

,

!

this? area specifically denotes results for various: groups. in

achieving quality as .well 'as the QA . staff in . verifying that

quality.

The site engineering group appeared slightly understaffed t'o

fulfill the increased work' load as design work is shifting'from

,

'

. the design consultant to plant staff. . ~The most significant'

weakness in the program is the_ informality in the documentation

of design packages, particularly in the presentation of design

,

' input'. Another apparent discrepant area was - the inadequacy of

procedures and instructions to accomplish modification work and

inspections as illustrated by'.the electrical ' cable tray.

insulation citation.

The design group has improved the

performance of 10_CFR 50.59 evaluations, 10 CFR 21 evaluations

and Appendix R assessments.

Temporary modifications are

appropriately controlled by the same procedures used for

permanent modifications. Drawings are updated expeditiously

which minimizes the drawing change backlog.

.

'

QA does not orovide audit plans which has resulted in inadequate

prepratf oa and supporting documentation for some audits.

The

inadequate preparation has resulted in the failure to take

appropriate actions to prevent the reoccurrence of existing

problems. An example is the 1985 security audit (II-10-85-I)

and the 1985 security audit (II-14-86-I) which identified

repetitive problems relating to the control and distribution of

security procedures, however the 1987 audit did identify the

i

problem even though the problem continued to exist.

1

The ' review of the maintenance group activities indicated a

strong program which included mechanisms for the identification

and correction of problems in this area. Maintenance activities

appeared to receive adequate review to identify adverse trends.

The overall level of documentation in the maintenance area was

satisfactory.

QA's escalation of deficiencies is adequate. When issues are

escalated

there

is

evidence

of appropriate management

involvement.

The Quality Services area was reorganized in the January 1986

reorganization into three areas:

Quality Control, Quality

Assurance, and Materials and Procurement. These areas report to

the Director, Quality and Procurement Services.

- _ _ _ _ _ _ - - - _ _ - _ _ _ _ - _ _ _ _

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e

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22

In the Materials and Procurement area, the reorganization

1

resulted in improved efficiency by eliminating dual functions

I

previously performed in quality and procurement areas. Improved

)

'

communications and better management control led to a reduction

in the time required to obtain needed parts and resulted in a 75

1

percent reduction in the backlog of safety related parts on

order.

The Procurement Engineering Group is over 50 percent

complete on a four year program developing a comprehensive

" piece part" Q list of replacement parts for safety related

components.

The Quality Assurance area continues to perform the required

Type I and Type II surveillance and audits. They have followed

i

industry trends and are slanting these surveillance

toward

hardware and performance. They have initiated technical adequacy

,

audits in the areas of inservice inspection and design changes.

The reorganization. of Quality Services has led to a stronger

j

Quality Control Organization. Increased emphasis on working

i

conditions, training, morale, and professionalism has led to

l

improved and more professional inspections. A QC coordinator

'!

position has been established to address programs and training

]

needs. Improved supervision, management oversight and better

'

communications have resulted in a more professional organization

!

with improved creditability.

1

A review was performed on all sections of the SALP report in an

I

attempt to capture apparent strengths and weaknesses related to

management controls affecting quality.

1

a.

The following are some observed strengths in management

I

controls affecting quality:

1)

Plant supervision and management have assumed very

active rolls in ensuring that efforts and resources

needed to

insure timely corrective action are

available.

This is evident by the following:

a)

The licensee had the highest plant availability

for domestic Westinghouse plants;

b)

The management review board that was established

to review all reactor trips and other plant

significant events;

c)

Frequent management plant tours which encompass

all shifts;

d)

The initiation of a control room enhancement

program;

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_.

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'

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,

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e)

The high level of commitment in matters-relating

J

to radiation protection program resulting in what

is considered the best contamination control

'

program in the Region;

i

f)

Licensee initiated SSFI inspections;

g)

Continued responsiveness to NRC initiatives; and

h)

Outage

activities

were

well

coordinated,

communication between departments was good, and

the overall performance was good for a plant in a

third refueling outage.

(2) The Reactor Operator and Senior Reactor Operator

requalification

program

is

well

developed

and

administered.

(3) A program has been developed to document detailed

design basis for selected plant systems, structures,

and components.

This should result in a better

technical understanding of the present design and

provide for better future design change documentation.

b.

The following are some observed weaknesses in management

contro'is affecting quality:

(1) Manpower

levels

appear to be insufficient to

completely overview contractor activities and to react

to involved chemistry program needs.

(2) Corrective action is often not completely documented.

This

has

resulted in inadequate planning and

corrective action verification.

(3) Design inputs for design change packages are often not

formally identified, specifically approved, and do not

provide enough detail for a consistent basis for

design verification measures.

Three violations were identified:

1

a.

Severity Level IV violation for failure to provide design

input for modifications.

(87-20)

b.

Severity level V violation for failure to have adequate

procedures

when

installing

thermo-lag

fire

barrier

material.

(86-07)

1

I

i

_ _ _ - - _ -

- _ _ _ _ _

i

7" ..

.

24

l

c.

Severity Level V violation for inadequate review of

previous audit findings for adequacy of corrective action

,

implementation.

(87-20)

i

2.

Conclusion

Category:

2

1

3.

Board Recommendations

I

i

No change in NRC inspection activity is recommended.

J.

Licensing Activities

1.

Analysis

.

Management involvement has been constantly involved over the

assessment period.

Prior planning and involvement was evident

in both site and licensing activities during normal operation;

however, four needed license amendments were requested within

three months of the start of the last refueling outage. More

planning should be done in order to submit licensing actions

needed for an outage in a more timely manner. This would allow

.

for sufficient time for NRC to review involved submittals, like

the heat flux hot channel factor amendment request without

impacting startup from an outage.

Technical soundness and

,

quality was apparent in most submittals.

Examples of quality

!

submittal were the boron concentration and ESF response. This

level of quality should be maintained for future submittals.

The

licensee's determinations

regarding non significant/

significant hazards considerations have uniformly improved and

are generally of good quality.

The licensee has been very responsive to NRC initiatives. The

licensee provided a prompt and complete response to the NRC

request

for

information

regarding

documentation

of

implementation of approved regulatory as tracked by the Safety

Issues Management Systems.

In addition, the licensee was

extremely cooperative with the NRC control room habitability

survey.

The licensee's responsiveness to the staff's requests

for additional information have been prompt for plant specific

and most generic issues; however, a response on the generic

issue regarding relief and safety valves was not timely. The

licensee keeps the Project Manager informed on the status of

l

ongoing activities and has taken the initiative in discussions

,

L

and meetings.

l

The licensee continues to be informed of industry approaches

of plant safety issues and is aware of programs, problems

and resolution thereto, at other plants. This was accomplished

by participation in major industry advi so ry groups and,

__

- __

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_-

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.25

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particularly, by participation in owners . groups.

The;.. licensee

. joined EPRI .in July 1987. - This additional -membership . should

7

enhance 'their knowledge 'of - generic. iissues affecting ; the

electrical power industry.

y

The licensee is generally-timely in. reporting operational events

and Licensee Event Reports (LERs). An evaluation of-the content

and quality of a representative sample of LERs was performed.

~ The results 'of this evaluation indicate that, while' the' overall'

quality of the Summer LERs, for the three areas that. are

evaluated (i .e. , the : text, ' abstract,' and coded -fields), has

improved somewhat since the previous evaluation, the improvement

7

was less than expected.

For the current evaluation, Summer's

overall ' average. LER score i s .8.1, which' i s still. below the

current . industry average LER score (8.4)- [ scores are discussed.

in -NUREG-1022].

The quality 'of- seven , text discussions . remain

below' the industry average.

These are safety consequence,

identification of failed components, discussion of root cause,

corrective - actions, personnel error, operator. actions- that

affected the course of.-the event, and safety system responses.

It was noted however, that. starting in 1987 the LERs . were

written using an outline format (i.e., the last five Leks in the

sample).

The average score for these-'LERS may be indicative.of

,

an improvement beyond that shown for the' entire sample.

No-violations wcre. identified during this period

2.

Conclusion

Category:

2

3.

Board Recommendations

None

K.

Training and Qualifications Effectiveness

' 1.

Training Analysis

During the assessment period, inspections were performed.by the

resident and regional staffs.

Four of the five training

programs under Nuclear Operations Education and Training have

been accredited by the Institute of Nuclear Operations (INPO)

since 1984.

These are (1) Non-licensed Operators Training,

(2) Licensed

Operator

Training,

(3) Licensed

Operator

Requalification Training, and (4) Shift Technical Advisor.

The

fifth program, Nuclear Training-for Technical Staff and Managers

was initiated in late 1986, and was reviewed for INP0

accreditation in 1987.

1

l

- - _ _ _ _____ _

_

_ _ .

>

-- .

--

_ - _ - -

.

-

-

- _ _ _

__ -_-____ __

p e. , s

.

.

.

26

'

-

<

'

.

Four.of four Senior Reactor' Operators and eight of nine Reacto.r.

.

,

. 0perators ' passed the Nuclear Regulatory Commission's Licensing

examinations 'during this evaluation period. This high success

E

rate indicates the. licensed operator. training program is

!

effective.

m

"

The licensee. has a well Ldeveloped and administered Reactor

~

' Operator. 'and Senior ' Reactor Operator Requalification Program.

Feedback from students, supervisors and managers on' classroom-

presentations, . simulator ' activities and on-the-job training is

elicited ~and incorporated into the training program.

This

process also identifies training material deficiencies and

provides management with a stable assessment' of. student

participation as well as maintaining quality trained and updated

instructors in the training program.

There is a well defined, developed' and controlled tracking

system established which insures .that additions and ' changes- to

training . ' material- required - by

plant

changes

through-

modifications, technical specifications, licensee event reports,

INP0 significant operating event reports, industry events and-

Nuclear Regulatory Commission Notices are incorporated into.the

training and simulator programs.

,

The simulator. is routinely used to reproduce operational events,

evaluate . operator errors and- determine root causes and

corrective actions.

The training department reviews systems

procedures changes to identify areas of potential operator

errurs.

The Nuclear Technical Education and Training Programs for crafts

were revised to meet the INPD accreditation guidelines. Craft

training is performance based and there is a continuous ongoing

upgrade and development of training materials and lesson plans.

Instructors for craft training are certified.

The licensee

craft training, facilities and staff was evaluated by an INPO

accreditation team in March 1987. The licensee anticipates that

accreditation will be granted by the end of 1987-.

Maintenance has supported the implementation of INPO craft

training programs by providing assistance in developing training

manuals, lesson plans, other course materials and instructors.

A new classroom training facility has been constructed, and a

training laboratory for hands on training is being upgraded.

Management has strongly supported and provided the resources

necessary to implement these items.

No violations were identified in this area,

y,

_ __

_

_

_

1

A.

N

i

6D

-!

.4.-

7

1

J

.

27

q

2.

Conclusion

,

,

Ca.tegory:

1

j

3.

Board Recommendations

,

A reduced NRC inspection activity is recomm'nded.

e

i

-

V

SUPPORTING DATA AND SUMMARIES

j

A.

Licensee Activities

l

Significant achievements during 1986 iaeluded a piant availability of

I

95.3% and the cumulative radiation exposure of 23 person-rem.

Several self-initiated programs and reviews have. been initiated and

are on going as discussed in this report.

The third refueling was

-complete during a 95 day outage ending in June 1987.

Major

activities included shot peening and stress relieving of steam

generators, overhaul of diesel generator B, seal replacements of A

i

and B reactor coolant pumps, inarvice inspection, /eactor baffle

inspection for jet imp %giment, inspection of service water and

feedwater piping, ninety-five design changes and modifications and

numerous other repairs.

Problem identification, corrective and/or

.

improvement programs are identified in each of the functional areas.

These reflect upon a aggressive management and many pgrson years of

effort.

T

,

1

B.

Inspection Activities

The routine inspection program was performed during this period, with

special inspections conducted to augment the program as follows:

Control Room Habitability Survey, January 12-16, 1987.

-

Regulatory Effectiveness Review, March 3-7, 1986.

-

,

C.

Licensing pctivities

'

/

1.

NRR/ Licensing Meetings

Management site visit

02/05/86

Licensing status

03/21/86

Fire Protection

04/02/E6

l

Licensing status

05/08/86

Licensing status

06/12/86

F-S1 AR analysis

06/27/86

e

_ _ _ _ _

. _ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _ _ _

-.

>

. . . ..

.

28

-

lji

Licensing status

08/08/86

'3-Loop PWR topics .

10/16/86

Licensing status

01/27/87

Licensing status

03/05/87

Licensing status

03/26/87

,, ,

Management meeting

05/18/87

1

2.

NRR Site Visits

Licensing status meeting & plant tour

05/05/86

Badge training & Regulatory Effectiveness

03/5-7/86

Review

SPDS Audit

11/4-6/86

Badge Training & QA inspection exit

07/23-24/87

3.

Reliefs Granted

ASME Section XI Relief

06/03/87

4.

Licensee Amendments

19 issued (Amendments 49-67)

m

D.

Investigation Review

No major investigative activities occured during this time period.

['

E.

Escalated Enforcement Actions

1.

Civil Penalties

a.

Severity Level III problem with four violations and one

Severity Level IV violation on Component Cooling Water

trains inoperable - LCO. A $50,000 Civil Penalty (Issued:

April 15, 1986; 86E009).

b.

Severity Level III problem for misalignment of Charging

Pumps.

Two violations with a $50,000 Civil Penalty.

(Issued:

September 22, 1986; 86E033).

.

________m.

__ _

. .

-

-

-

._

-.

.

_

_

____ .

^

'

t

. j3 ,

>

,.;

-

.

F

29

c.

Severity: Level

III ' problem

for. fire

protection

requirements - Appendix R. LTwo violation with two examples,

each.

This matter was discussed in the ' previous SALP

report.

(Issued: March 11, 1987; 85E039).

l

.

2.

Actions without Civil Penalties-

<

Severity Level III problem with two violations, for. hand

-

overexposure.

The licensee is currently appealing this

y

matter.

(Issued:

March 10, 1987;'86E055)-,

3

Orders

Order imposing $50,000. Civil Penalty' was issued on September .19,.

1986 . for the Severity . Level III problem on the Component

,

Cooling Water trains inoperability. The Civil Penalty was paid

on October 17, 1986.-

F.

Enforcement Conferences Held During Appraisal Period

'1.

~ An ~ enforcement conference was. held in. the Region II office on

. February 28,-1986, to discuss the inoperability of Component

Cooling Water trains.

,

2.

An enforcement conference was held in the Region .II office on

July.3, 1986, to discuss the misalignment of the Charging-Pumps.

3.

An enforcement conference was held in the Region II office on

December 16, 1986, to discuss the' hand overexposure issue.

G.

Confirmation of Action Letters

None

H.

Licensee Event Report

During the evaluation period, 25 of 37 LERs submitted by the licensee

i

were' evaluated by the NRC staff to determine the event cause ' and

'

review the content. Summary of comments provided to the' licensee are

!

in the Licensing Activities section of this report. The distribution

!

of these events were as follows:

Cause

Number

Component Failure

5

-

Design

1

-

Construction, Fabrication,

or Installation

2

Personnel

- Operating Activity

6

i

..

-

_ _ . _

mm_

_.._._____________m_

_ . _

- - - -

'

j :o

,

'

p

'30

-

- Maintenance Activity

2

,

- Test / Calibration Activity

6

- Other

1

Out of Calibration

0

Other

2

>

Total

25

2.

10 CFR Part 21 Reports

-

Anchor Darling Check Valves, February 19, 1986, discussed

in LER 86-01

-

ESF Load Sequencer, June 5,1987, discussed in LER 87-10.

I.

Enforcement Activity

A summary of violations tabulated per SALP functional areas are

shown in the following table.

FUNCTIONAL

NUMBER OF DEVIATIO"S AND VIOLATIONS

AREA

IN EACH SEVERITY LEVEL

D

V

IV

III

II

I

Plant Operations-

1

1

2

Radiological Control

1

3

1

Maintenance

Surveillance

1

Fire Protection

2

1*

Emergency Preparedness

1

1

Security

1

Outages

1

1

Quality Programs and

2

1

Administrative Controls

Affecting Quality

!

Licensing Activities

Training and Qualifications

Effectiveness

Total

7

10

4*

u

previous SALP.

_

_ _ _ _ _ - _ _ _ _ _ _ _ _ - _ _ _ _

_

__ -

_-

- - - - - _ - _ -

I

p ,.

31-

.

.

}

'

l..

i

o

.

. .

. J .'

Reactor: Trips

.1.

February 2, 1986, reactor. power was 100% when_ power was removed

fromia condensate polisher control. panel;to support maintenance

activities. The-removal of power caused the condensate polisher

bypass valve deaerating tank 'to-

fail

closed. .i sol ati ng

.

4

condensate flow. The resulting low deaerating' tank water ~ level

'

' '

tripped- the feedwater pumps causing .a . turbine trip.

The-

electrical feeder . list did ' not identify the bypass valve as

receiving its control power from the panel.

2.

February 3,1986, the main turbine was =being rolled up to 1800;

. RPM at the fast startup rate. When turbine ' speed.. reached about

400 RPM, it . appears that the turbine control valves opened

'

rapidly causing a' sudden increase in speed,

The.. large. steam

'

demand caused a rapid decrease in main steamlinel pressure. The,

rate of decrease in.steamline pressure was sufficient.to' actuate

the steamline low pressure.bistables due to rate compensation

and cause a safety injection.

3.

April 2, .1986, while operating at 100% power, the loss 1 of

excitation of'. the- main. generator occurred when the exciter

brushes failed.

This

caused the generator and turbine to

,

trip.

4.

P,ay'31, 1986, reactor power was 100% and a surveillance test was

in progress. The bistables were tripped for one channel of the

,

power range nuclear instrumentation 'and a test signal was

j

inadvertently inserted in another channel.

The test signal

tripped the' .overtemperature delta-bistables and with the

bistables in the other instrument channel in the tripped-

condition, a 2 L out of 3 coincidence was met and tripped' the

reactor.

5.

June 26, 1986, reactor power was reduced to 90% in preparation

for the weekly turbine valve tests.

Before the testing was

begun, the feedwater isolation valve for Steam Generator'"A

failed closed causing a reactor trip.

Investigation revealed

that a solenoid valve had' an electrical connection which was

discolored and; appeared to have been contaminated with oil or

dirt.

Interruption of power to this solenoid failed the

feedwater isolation valve shut.

6.

July 27, 1986, reactor power was reduced to 90% for the monthly

test to the turbine control valves.

Three of the turbine

control valves were tested without incident. During the test of

the fourth control valve, the spurious operation of one of the

two pressure switches on the other control valves coincident

with the actual low EHC fluid pressure on the valve being tested

apparently indicated a turbine trip which caused a reactor trip.

- - _ _ _

._

.-

_ _ _ _ .

.c h ,

32

7.

June 16, 1987, reactor power 100% when Inverter 5904 failed,

deenergizing' protection Channel IV.

Power Range NI-44 failed

low, reducing programmed S/G 1evel to the no-load value.

Feedwater flow decreased responding to the new false low

programmed level.

The low-low S/G level trip setpoints which

are derived from the other three power range nuclear instruments

remained at full load values. Actual levels decreased below

the trip setpoints resulting in a low level trip.

.

K.

Effulent Summary for V. C. Summer Nuclear Station

TOTAL RELEASE IN CURIES

1984

1985

1986

. Gaseous Effluents

Fission and Activation Gases

1.64 E+1

1.41 E+2

1.39 E+1

(1,06E+4)

(9.37E+3)

(8.04E+3)

Iodine and Particulate

1.04 E-5

4.17 E-5

4.39 E-5

(9.56E-2)

(9.62E-2)

(4.60E-2)

Liquid Effluents

Fission and Activation Products 4.58

7.15 E-1

3.29 E-1

(3.27E+0)

(2.59E+0)

(2.11E+0)

i

Tritium

2.25 E+2

3.11 E+2

3.74 E+2

(7.23E+2)

(7.35E+2)

(7.42E+2)

Values in parentheses are Region II averages for PWRs.

Maximum Whole Body Dose Offsite in 1986:

4.55 E-2 mrem

,

I

l

l

l

- - _ _ _ - _ _ _ _ - _