ML20234D181

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Forwards Insp Rept 50-245/87-09 on 870420-24.Deficiencies Noted from List Discussed in Encl Potential Enforcement Findings
ML20234D181
Person / Time
Site: Millstone Dominion icon.png
Issue date: 07/01/1987
From: Crutchfield D
Office of Nuclear Reactor Regulation
To: Mroczka E
NORTHEAST NUCLEAR ENERGY CO.
Shared Package
ML20234D185 List:
References
NUDOCS 8707070127
Download: ML20234D181 (7)


See also: IR 05000245/1987009

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UNITED STATES

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NUCLEAR REGULATORY COMMISSION

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WASHINGTON, D. C. 20555

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July 1, 1987

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Docket No. 50-245

Northeast Nuclear Energy Company

ATTN: Mr. Edward J. Mroczka

Senior Vice President - Nuclear

Engineering and Operations

Post Office Box 270

Hartford, Connecticut 06141-0270

Gentlemen:

SUBJECT:

INSPECTION NO. 50-245/87-09 (04/20/87 - 04/24/87)

This refers to the inspection performed by Messrs. E. T. Baker and P. J. Prescott

of the Nuclear Regulatory Comission (NRC) Vendor Inspection Branch on April 20-24,

1987, at Millstone Unit 1 of activities authorized by NRC License No. DPR-21.

Our findings were discussed with Mr. J. Stetz and others of your staff at the

conclusion of the inspection.

The purpose of this inspection was to review the check valve testing programs

at Millstone Unit 1.

Particular attention was directed to the ability of the

testing to establish disk and seat integrity, location of check valves in

relation to turbulence generators, maintenance and failure history, and the

licensee's response to the Institute of Nuclear Power Operations' (INP0's)

SignificantOperatingEventReport(SOER)86-3concerninginspectionand

testing of check valves.

The findings of this inspection were that (1) you did not report the failure

te pass a leak tightness test of 8 of 12 check valves in the nitrogen supply

system to the automatic depressurization system valves; (2) you failed to take

corrective action to eliminate the recurrence of rust particles, which caused

the 8 check valves mentioned in (1) above to leak again; and (3) you failed to

ensure the adequacy of one test procedure, which was written to test four

low-pressure coolant injection (LPCI) pump discharge check valves, but actually

resulted in only two of the valves being tested for isolation function.

Additionally, the procedure for testing shutdown cooling pump discharge check

valves was r M sed to shift the inspection of the isolation function to the

pump testing procer ure. Although the valve inspection was deleted from the valve

test procedures it was not added to the pump test procedure. These deficiencies

have been cla!- fied as Potential Enforcement Findings 50-245/87-09-01,

50-245/87-09-02,ind 50-245/87-09-06,

8707070127 870701

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ADOCK 05000245

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Northeast Nuclear Energy Company

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July 1, 1987

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Discussio'hs concernirig the. response to the SOER did not elicit any indications

of significant changes to the current testing and inspection programs.

It-

appeared that correceive, as opposed to preventive, maintenance was being

performed for the chec'; valves examined.

The potential enforcemd t findings are being referred to the NRC Region

office

for review and appropriate action. .Should you have any questions on this matter,

we would be pleased to discuss them with you.

Sincerely,

D nn b

rute kield, Dir

tor

Division of Reactor Proje s - III, IV, V

and Special Projects

Office of Nuclear Reactor Regulation

Enclosures:

1.

Potential Enforcement Findings

50-245/87-09-01,50-245/87-09-02,

50-245/87-09-06

2.

Inspection Report No. 50-245/87-09

cc w/ enclosure:

See next page

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Northeast Nuclear Energy Company

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July 1, 1987

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cc w/ enclosures:

Gerald Garfield, Esquire

Mr. Richard M. Kacich, Manager

Day, Berry & Howard

Generation Facilities Licensing

Counselors at Law

Northeast Utilities Service Company

City. Place

Post Office Box 270

!

Hartford, Connecticut 06102-3499

Hartford, Connecticut 06141-0270

Wayne D. Romberg

Vice President, Nuclear Operations

)

Northeast Utilities Service Company

Post Office Box 270

Hartford, Connecticut 06141-0270

Bradford S. Chase, Under Secretary

Energy Division

)

i

Office of Policy and Management

80 Washington Street

Hartford, Connecticut 06160

Regional Administrator, Region I

U.S. Nuclear Regulatory Commission

631 Park Avenue

King of Prussia, Pennsylvania 19406

Mr. J. Stetz, Plant Superintendent

Millstone Unit 1

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Northeast Nuclear Energy Company

P. O. Box 128

Waterford, Connecticut 06385

Resident inspector

c/o U.S. Nuclear Regulatory Commission

Millstone Nuclear Power Station

P. O. Box 811

Niantic, Connecticut C6357

First Selectman of the Town

of Waterford

Hall of Records

200 Boston Post Road

Waterford, Connecticut 06385

Kevin McCarthy, Director

Radiation Control Unit

Department of Environmental Protection

State Office Building

Hartford, Connecticut 06106

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POTENTIAL ENFORCEMENT FINDINGS

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Northeast' Nuclear Energy Company

Docket No. 50-245

Millstone Nuclear Power Station Unit 1

License No. DPR-21

As a result of the NRC inspection conducted at Millstone Unit 1 on April 20-24,

1987, and in accordance with the " General Statement of Policy and Procedures

for NRC Enforcement Actions," Title 10 of the Code of Federal Regulations

Part 2 (10 CFR 2), Appendix C (1986), the following potential enforcement

findings were identified:

A.

Potential Enforcement Finding 50-245/S7-09-01

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10 CFR 50.72 (b)(2)(1) requires that the NRC be notified within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

of any event, found while the reaccor is shut down, that, had it been

found while the reactor was in operatw n, would have resulted in the

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nuclear power plant's principal safety barriers being seriously degraded

or being.in an unanalyzed condition that significantly compromises plant

safety.

10 CFR 50.72 (b)(2)(iii) requires a similar notification, any

condition that alone could have prevented the fulfillment of the safety

function of systems that are needed to safely shut down the reactor or

to mitigate the consequences of an accident.

Contrary to the above, the licensee failed to notify the NRC that 8 of 12

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check valves in the nitrogen supply system to the automatic depressurization

system (ADS) valves failed to pass the required leak test r.onducted on

November 2,1985.

The licensee also stated that a licensee event report

(LER) had not been submitted.

B.

Potential Enforcement Finding 50-245/87-09-02

10 CFR 50, Appendix B, Criterion XVI, " Corrective Action," requires that

in the case of significant conditions adverse to quality, measures shall

be established to ensure the cause of the condition is determined and

corrected to preclude recurrence.

Contrary to the above, although the licensee determined that the check

valves in the ADS failed the leak test on November 2, 1985 (see PEF

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67-09-01) because of rust particles on the seat of the valves, the licensee

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did not take any action to prevent recurrence of the problem. The licensee

knew that the ring header, which supplies nitrogen to the accumulators,

has extensive internal surface corrosion.

C.

Potential Enforcement Finding 50-245/87-09-06

10 CFR 50, Appendix B, Criterion VI, " Document Control," in part requires

that procedures, including changes, be reviewed for adequacy.

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Contrary to the above:

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1.

Station Procedure SP622.7 was written to test the opening and closing

of all four low-pressure coolant injection (LPCI) pump discharge

\\ check valves. However, the test resulted in only two of the valves

being verified as closed because of the sequence of running the

pumps and the inspection / testing criteria for verifying valve

closure.

2.

Station Procedure SP623.20 was revised September 10, 1986, deleting

testing of the shutdown cooling pump discharge check valves. The

valve testing was supposed to be transferred to Surveillance Procedure

1060-38 which covered testing the pumps. However, a review of that

procedure revealed that the valve testing was not adced to Surveillance

Procedure 1060-38 after it was deleted from SP623.20.

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