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Category:REPORTABLE OCCURRENCE REPORT (SEE ALSO AO LER)
MONTHYEARML20148S3141997-06-30030 June 1997 Ro:On 970422,Oconee Unit 2 Was Shut Down Due to Leak in Rcs. Leak Was Caused by Crack in Pipe to safe-end Weld Connection at RCS Nozzle for HPI Sys A1 Injection Line.Unit 1 Was Shut Down to Inspect Hpis Injection Lines & Implement Ldst Mods ML20117A5981992-11-23023 November 1992 Special Rept:On 921119,ability of Control Battery Racks to Withstand Seismic Event Could Not Be Confirmed & Batteries Declared Inoperable.Batteries Expected to Be Restored in TS Required Time ML20236T0791987-11-25025 November 1987 Advises LER 269/87-09,re Degradation of More than One Functional Unit of Emergency Power Switching Logic for Units 2 & 3,in Preparation & Will Be Submitted by 871215. Incident Originally Discussed in Special Rept ML20210J6671987-02-0303 February 1987 Special Rept:On 861113-14,1206 & 23,spurious Fire Alarms Annunciated in Control Room.On 870118,unit Shut Down Due to Problems W/Detectors.Cause Undetermined.Technicians Investigating Potential Problem W/Detectors ML20215N4011986-10-20020 October 1986 Special Rept:On 860808,during Shutdown for Maint,Found Unidentified Wires in Environmentally Qualified Limitorque motor-operated Valves.Caused by Mfg Deficiency.Wires Replaced ML20209C1871986-08-13013 August 1986 Special Rept:On 860707,fire Barrier Penetration Nonfunctional.Caused by Design Deficiency Due to Ineffective Communication Between Design Groups.Fire Watch Established. Notice Initiated Requiring Installation of Fire Wall ML20212D2221986-07-29029 July 1986 Special Rept:On 860606,determined That Inadequate Assurance Existed Re Use of Qualified Grease in All Limitorque Operators.Appropriate Programs Not Updated to Reflect Revs. Lubrication Records Reviewed ML20210N5641986-04-14014 April 1986 Special Rept:On 860206,fire Wall Determined to Be Degraded. Caused by Personnel Failure to Recognize That Removing Small Amount of Pyrocrete Would Degrade Fire Wall.Fire Wall Repaired & Declared Fully Functional.Part 21 Related ML20137D6481985-11-22022 November 1985 Ro:On 851119,Keowee Hydro Unit 2 Inoperable Beyond Oconee Tech Spec Limit Due to Burned Out Laminated Copper Connection Between Two Coils.Caused by Cracked Brazement. Connector & Field Coils Will Be Replaced ML20135D7781985-08-21021 August 1985 Ro:On 850722,CRD Dc Breaker CB-1 Failed Trip Time Requirement During Channel C Reactor Protective Sys on-line Test.Cause of Failure Could Not Be Determined.Failed CB-1 Breaker Placed in Tripped Position ML20129G0441985-05-24024 May 1985 Ro:On 850425,batch of Powdex Resin from Powdex Cells 1A & 1D Transferred to Chemical Treatment Pond 2 Instead of Powdex Backwash Tank.Caused by Misalignment of Valve CTP-7.Valve Correctly Positioned ML20108E5341985-02-14014 February 1985 Special Rept:On 850114,CRD Dc Breaker Failed Slow During Channel D Reactor Protective Sys on-line Test.Caused by Sticking Trip Latch Roller Bearings & Excessive Trip Latch Operating Torque.Breaker Front Frame Replaced ML20112D0771984-12-14014 December 1984 Special Rept:On 841109,many Fire Barriers Did Not Meet Surveillance Insp Acceptance Criteria & Declared Inoperable. Caused by Const/Installation Deficiency,Component Failure/ Malfunction & Some Unknown Causes.Firestops Repaired ML20099E0241984-10-24024 October 1984 Special Rept:On 840927,discovered That Contaminated Oil Shipped to Lee Steam Station for Disposal by Incineration. Caused by Misinterpretation of Regulations.Shipments of Contaminated Oil Halted ML20093F1911984-10-0808 October 1984 RO 269/83-16,revising 831107 Commitment Re Completion Date of 850101 to Relocate Hydrogen Purge Unit Connection Near Permanent Hookup Connections on Each Unit for Hydrogen Recombiner ML20093L5061984-10-0505 October 1984 Special Rept:On 840906,batch of Powdex Resin from Powder Cells 2D & 2E Transferred from Plant to Chemical Treatment Pond 1 Instead of to Powdex Backwash Tank.Caused by Misalignment of Valves of Chemical Treatment Ponds 5 & 6 ML20106B4791984-10-0303 October 1984 Special Rept:On 840928,power Circuit Breaker 22 Explosively Short Circuited,Causing Power Circuit Breaker 9 to Open, Isolating 230 Kv Overhead Line from Primary OL Power Source. Breaker Reclosed ML20096A1061984-08-22022 August 1984 Suppl to Rev 1 to RO-287/83-13:containment Isolation Valve 3CS-5 Declared Inoperable Due to Leakage Past Seat. Investigation Into Valve Failure Conducted & Diaphragm Replaced ML20094N8601984-07-27027 July 1984 RO 269/83-20 Re Trip Shaft & Bearing Assembly Portions of CRD Breaker Front Frame Assemblies.Nine of 17 GE Frames Defective.Util Awaiting Schedule for Delivery of New Frames ML20092A4291984-06-0606 June 1984 Special Rept:On 840419,during Fuel Reshuffling for Cycle 8, Fuel Assembly FA 0297 Became Stuck in Fuel Location E-10 During Insertion & Fuel Assembly FA 029Q Damaged.Caused by Inadequate Procedure Change ML20092A3841984-04-30030 April 1984 Updated RO-269/83-20 Submitted on 840111 Re Two CRD Breakers Experiencing Delay During Testing.Ge Will Ship CRD Breaker Front Frame Assemblies on 840514.Installation Will Be Complete on All Three Units by 840731 ML20084G4851984-04-18018 April 1984 Updated RO 269/83-17:seals at Conduit Connections Defective. Scotchcast 9 Epoxy Resin Will Be Utilized to Seal Conduit Connections,Dow Corning RTV 3145 Applied to Conduit Fittings & Conduit/Cable Seals Will Be Upgraded ML20082R7561983-12-0202 December 1983 Ro:On 831015-16,standby Bus 2 Deenergized to Verify Emergency Power Path & CT-3 Startup Transformer Locked Out. Caused by Failure of Two Insulators Causing Short to Ground. Info Supersedes 831101 Rept ML20082H5161983-11-21021 November 1983 Ro:Re Loss of Power on Both Standby Buses W/Both Units Out of Svc.Investigation Incomplete.Necessary Info Will Be Submitted by 831202 ML20082C6081983-11-14014 November 1983 Ro:On 831109,while Units Out of Svc for Planned Maint,Lee 6C Gas Turbine Tripped off-line,deenergizing Standby Buses & Placing Units in Degraded Mode Beyond Tech Spec Limit.Cause Undetermined.Next Rept by 831118 ML20078P9651983-11-0202 November 1983 Ro:On 831028,while Unit Out of Svc,Lee 6C Gas Turbine Tripped & Deenergized Both 4,160-volt Standby Buses.Cause Unknown.Lee 5C Turbine Placed on-line to Sys Grid. Investigation Continuing ML20081K0951983-11-0101 November 1983 Ro:On 831015-16,w/Unit 1 Out of Svc,Standby Bus 2 Deenergized to Allow Operability Verification of Underground Emergency Power Path in Accordance W/Tech Specs.On 831015, CT-3 Underwent Lockout.Caused by Bad Insulators ML20078P8841983-10-31031 October 1983 Ro:On 831026,w/unit Out of Svc for Maint,Lee Steam Station Gas Turbine Tripped,Deenergizing Both Standby Buses.Cause Not Determined.Redundant Buses Available ML20081B2521983-10-17017 October 1983 Ro:On 831012,standby Buses Deenergized to Allow for Operability Performance Testing of Standby Bus Breakers Per Tech Specs.Testing Caused Degraded Mode Beyond Tech Spec Limit ML20078H4121983-10-0404 October 1983 Ro:On 830929,while Energizing 4,160-volt Standby Buses,Lee 6C Gas Turbine Tripped off-line,deenergizing Both Standby Buses & Placing Two Operating Units in Degraded Mode.Cause Undetermined Since Unit Has No Event Recorder ML20080P3271983-09-27027 September 1983 Ro:On 830922,w/both Keowee Hydro Units Out of Svc for Planned Maint,Lee 6C Gas Turbine,Being Used to Energize Buses,Tripped Off Line.Both Standby Buses Deenergized & Units 1 & 3 Placed in Degraded Mode ML20080M0261983-09-16016 September 1983 Updated RO 287/83-07.Investigation Incomplete.Next Rept Expected by 831030 ML20080G2351983-09-0606 September 1983 RO 270/83-09:on 830802,hydraulic Snubber Noted Technically Inoperable for More than 72 H.Investigation Incomplete.Next Rept Will Be Submitted by 830912 ML20076C3291983-08-15015 August 1983 RO 287/83-07:followup to Rept Submitted on 830708. Investigation Incomplete.Supplemental Rept Expected by 830915 ML20072J2031983-06-24024 June 1983 Ro:On 830527,certain Containment Isolation Valves May Have Failed in non-ES Position Due to Loss of Dc Power. Investigation & Rept Will Be Completed & Reviewed by 830708 ML20073Q0121983-04-19019 April 1983 Corrected RO 269/83-07:on 830303,during Insp of Manual Containment Isolation Valves,Valve CF-19 Discovered Open. Caused by Personnel Error.Valve Closed.Core Flood Procedure & Reactor Bldg Manual Checklist Changed ML20069K4141983-04-15015 April 1983 Updated ROs 287/83-04,269/83-05 & 269/83-10:repts Being Reviewed & Will Be Submitted No Later than 830419 ML20072T7011983-03-30030 March 1983 RO-287/83-04 Will Not Be Submitted by 830331 as Planned.Rept Re Open Valve on Emergency Hatch Leak Rate Test Pressurization Line Incomplete.Rept to Be Submitted by 830414 ML20072T6971983-03-30030 March 1983 RO-269/83-10 Will Be Delayed Due to Continuing Investigation of Incident Re Partially Opened Interpersonnel Emergency Door Following Testing.Rept Should Be Submitted No Later than 830415 ML20073C4071983-03-25025 March 1983 Informs That RO-287/83-04 Not Reportable.Results of Seismic Analysis Indicate Letdown Line Was Seismically Operable W/Lead Blankets Attached.Pipe Stress,Support Restraint & Equipment Nozzle Loads within Allowable Limits ML20069E3741983-03-11011 March 1983 Ro:On 830225,reactor Protective Sys Pump Power Monitor Sys Failed to Meet Operability Requirements.Investigation Incomplete at Present Time.Rept Will Be Submitted by 830325 ML20070K5851982-12-23023 December 1982 Ro:On 821213,Region 2 Informed of Two Manual Containment Isolation Valves Discovered Open.Rept Providing Details Delayed Due to Investigation.Rept Will Be Completed & Submitted by 821231 ML20070K7311982-12-23023 December 1982 RO 287/82-14:primary to Secondary Leak Discovered in Steam Generator 3B.Rept Will Not Be Submitted Until 830107 Contrary to Previous Commitment ML20065L7761982-10-14014 October 1982 Ro:On 821014,Unit 2 Core Relief Valves Declared Inoperable Due to Analysis Prompted by B&W Safety Concern.Unit 3 Valves Were Offsite Undergoing Ring Adjustment.Immediate Shutdown of Unit 2 Commenced ML20063N2791982-09-0707 September 1982 Informs That RO-269/82-15 Re Electrically Inoperable Valve CCW-8 Will Be Submitted by 820921.Investigation Incomplete ML20063M0851982-09-0303 September 1982 Advises That RO-269/82-16 Re Separation of safety-related Cables Will Not Be Filed.Review & Evaluation Determined That Separation of Specified Cables Conforms to Established Criteria.No Further Action Required ML20063M1031982-09-0101 September 1982 Ro:On 820818,five Reactor Coolant Pump Closure Studs Determined to Be Degraded in Size Below Acceptable SAR limits.RO-287/82-09 Will Be Completed,Reviewed & Submitted by 820910 ML20062J1721982-08-0505 August 1982 RO 270/82-10:on 820722,util Informed NRC That Upper Surge Tank Indicator Read Below Tech Spec Min Required Water Level.Investigation & Preparation of Rept Incomplete.Final Review & Rept Expected by 820819 ML20071K3471982-07-20020 July 1982 RO 269/82-13:on 820706,emergency Feedwater Pump Declared Inoperable When Required Surveillance Testing Discovered Not Performed.Investigation & Rept Will Be Completed,Reviewed & Submitted by 820803 ML20058D8291982-07-16016 July 1982 RO 270/82-09:on 820616,valve 2FDW-316 Would Not Close Completely After Sampling & Affected Flow Path Declared Inoperable.Investigation & Rept Will Be Completed,Reviewed & Submitted on 820730 1997-06-30
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20206P1501999-01-0505 January 1999 LER 98-S03-00:on 981207,security Officer Discovered Uncontrolled Safeguards Info Drawing.Caused by Failure to Follow Established Procedures & Policies.Drawing Was Controlled by Site Security.With ML20216F9931998-12-31031 December 1998 Piedmont Municipal Power Agency 1998 Annual Rept ML20198E6381998-12-17017 December 1998 LER 98-S02-00:on 981130,security Access Was Revoked Due to Falsification of Criminal Record.Individual Was Escorted from Protected Area & Unescorted Access Was Restricted. with ML20153G4601998-09-30030 September 1998 USI A-46 Seismic Evaluation Rept, Vols 1-2 ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils ML15261A4681998-09-0404 September 1998 Safety Evaluation Supporting Amends 232,232 & 231 to Licenses DPR-38,DPR-47 & DPR-55,respectively ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML20247L9041997-12-31031 December 1997 1997 Annual Rept for Duke Energy Corporation & Saluda River Electric Cooperative,Inc,Financial Statements as of Dec 1997 & 1996 Together W/Auditors Rept ML20198J7651997-10-15015 October 1997 Safety Evaluation Accepting 10-yr Interval Insp Program Plan Alternatives for Listed Plants Units ML20148S3141997-06-30030 June 1997 Ro:On 970422,Oconee Unit 2 Was Shut Down Due to Leak in Rcs. Leak Was Caused by Crack in Pipe to safe-end Weld Connection at RCS Nozzle for HPI Sys A1 Injection Line.Unit 1 Was Shut Down to Inspect Hpis Injection Lines & Implement Ldst Mods ML20148H2501997-06-0505 June 1997 Safety Evaluation Accepting Proposed Restructuring of Util Through Acquisition Of,& Merger W/Panenergy Corp ML20210E3591997-03-27027 March 1997 Part 21 Rept Re Sorrento Electronics Inc Has Determined Operation & Maint Manual May Not Adequately Define Requirements for Performing Periodic Surveillance of SR Applications.Caused by Hardware Failures.Revised RM-23A ML20134N7121997-02-20020 February 1997 Safety Evaluation Accepting Relief Request 96-04 for Plant ML20138L2151997-01-31031 January 1997 Monthly Operating Repts for Jan 1997 for Oconee Nuclear Station,Units 1,2 & 3 ML20138L2281996-12-31031 December 1996 Revised Monthly Operating Repts for Dec 1996 for Oconee Nuclear Station,Units 1,2 & 3 ML20133C1231996-12-23023 December 1996 Informs Commission of Staff Review of Request for License Amends from DPC to Perform Emergency Power Engineered Safeguards Functional Test on Three Oconee Nuclear Units ML20115F2471996-07-0303 July 1996 Part 21 Rept Re Piping (Small Portion of Unmelted Matl Drawn Lengthwise Into Bar During Drawing Process) Defect That Existed in Bar as Received from Mill.Addl Insp Procedure for Raw Matl Instituted ML20107M8931995-10-31031 October 1995 Nonproprietary DPC Fuel Reconstitution Analysis Methodology ML17353A4341995-10-31031 October 1995 Rev 1 to BAW-2245, Initial Rt of Linde 80 Welds Based on Fracture Toughness in Transition Range. ML17264A1181995-07-31031 July 1995 Response to Part (1) of GL 92-01,Rev 1,Suppl 1. ML20086M0851995-06-29029 June 1995 DPC TR QA Program ML20077R3631994-12-31031 December 1994 Monthly Operating Repts for Dec 1994 for Bfnpp ML20236L5971994-12-29029 December 1994 SER in Response to 940314 TIA 94-012 Requesting NRR Staff to Determine Specific Mod to Keowee Emergency Power Supply Logic Must Be Reviewed by Staff Prior to Implementation of Mod ML20064L2001994-01-31031 January 1994 Final Rept EPRI TR-103591, Burnup Verification Measurements on Spent-Fuel Assemblies at Oconee Nuclear Station ML20062K7481993-12-0101 December 1993 ISI Rept for Unit 2 McGuire 1993 Refueling Outage 8 ML20056E5171993-08-31031 August 1993 Technical Review Rept, Tardy Licensee Actions ML20046C1291993-08-0202 August 1993 LER 93-007-00:on 930701,determined That Unit 1 Ssf Rc Makeup Sys Inoperable in Past Due to Design Deficiency.Operations Procedures Revised to Reflect Newly Calculated Operating Limits for Rc Makeup Pump,Rcps & RCS.W/930802 Ltr ML20056G0131993-07-27027 July 1993 Rev 0 to ISI Rept Unit 2 Oconee 1993 Refueling Outage 13 ML20044G5311993-05-26026 May 1993 Suppl to 921207 Part 21 Rept Re Declutch Sys Anomaly in Certain Types of Valve Actuators Supplied by Limitorque Corp.Limitorque Designed New Declutch Lever Which Will Be Available in First Quarter 1993 ML20126J5961992-12-31031 December 1992 Part 21 Rept Re Potential Loss of RHR Cooling During Nozzle Dam Removal.Nozzle Dams May Create Trapped Air Column Behind Cold Leg Nozzle Dam.Mod to Nozzle Dams Currently Underway. Ltrs to Affected Utils Encl ML20117A5981992-11-23023 November 1992 Special Rept:On 921119,ability of Control Battery Racks to Withstand Seismic Event Could Not Be Confirmed & Batteries Declared Inoperable.Batteries Expected to Be Restored in TS Required Time ML20097G0421992-05-31031 May 1992 Analysis of Capsule OCIII-D Duke Power Company Oconee Nuclear Station Unit-3 ML20077D0671991-11-15015 November 1991 Nonproprietary Version of Rev 0 to Boric Acid Corrosion of Oconee Unit 1 Upper Tubesheet ML20067A5241990-12-31031 December 1990 Final Submittal in Response to NRC Bulletin 88-011, 'Pressurizer Surge Line Thermal Stratification.' ML20042F3541990-04-30030 April 1990 Special Rept Re Failure to Prevent Performance Degradation of Reactor Bldg Cooling Units.Caused by Mgt Deficiency & Inadequate Program.Cooling Unit Declared Inoperable & Removed from Svc for Cleaning & Placed Back in Operation ML17348A1621990-03-27027 March 1990 Part 21 Rept Re Matls W/Programmatic Defects Supplied by Dubose Steel,Inc.Customers,Purchase Order,Items & Affected Heat Numbers Listed ML19332D5391989-10-31031 October 1989 Core Thermal-Hydraulic Methodology Using VIPRE-01. ML20042F2321989-08-31031 August 1989 Nonproprietary DCHF-1 Correlation for Predicting Critical Heat Flux in Mixing Vane Grid Fuel Assemblies. ML20205F3211988-10-10010 October 1988 Part 21 Rept Re Potential Deviation from Tech Spec Concerning Ry Indicators Due to Operating Temp Effect on Analog Meter Movement.Initially Reported on 881006.Customers Verbally Notified on 881006-07 ML20154K2091988-09-0909 September 1988 Rev 0 to Response to NRC Bulletin 88-005,Nonconforming Matls Supplied by Piping Supplies,Inc at Folsom,Nj & West Jersey Mfg Co.... Proprietary Procedure 1404.1, Leeb Hardness Testing (Equotip).... Encl.Procedure Withheld ML20245D9541988-09-0606 September 1988 Part 21 Rept Re Condition Involving Inconel 600 Matl Used to Fabricate Steam Generator Tube Plugs & Found to Possess Microstructure Susceptible to Stress Corrosion Cracking ML20245B6061988-08-31031 August 1988 Inadequate NPSH in HPSI Sys in Pwrs, Engineering Evaluation Rept ML20239A6991987-11-30030 November 1987 Addendum 1 to Rev 2 to Integrated Reactor Vessel Matl Surveillance Program (Addendum) ML20236T0791987-11-25025 November 1987 Advises LER 269/87-09,re Degradation of More than One Functional Unit of Emergency Power Switching Logic for Units 2 & 3,in Preparation & Will Be Submitted by 871215. Incident Originally Discussed in Special Rept ML20236Q9491987-10-31031 October 1987 Monthly Operating Repts for Oct 1987 ML20235W9611987-09-30030 September 1987 Monthly Operating Repts for Sept 1987 ML20234B1861987-08-31031 August 1987 Monthly Operating Repts for Aug 1987 ML20237K4761987-07-31031 July 1987 Monthly Operating Repts for Jul 1987 ML20236Y0221987-07-0808 July 1987 Safety Evaluation Clarifying Determination of Acceptability of Test Duration for Performance of Integrated Leak Rate Test at Plant ML20235S6311987-06-30030 June 1987 Monthly Operating Repts for June 1987 1999-01-05
[Table view] |
Text
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- 1) ;
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- 4 1 Duur POWER GOMPANY P.O. BOX 33189 CHARLOT12. N.C. 28242 HALB. TUCKER - a *1 TEMNM i wwme. =v , yJ (704) 373-4831 l , p p 3\
l October 20, 1986 l
Dr. J. Nelson Grace, Regional Administrator U. S. Nuclear Regulatory Commission Region II 101 Marietta Street, NW, Suite 2900 Atlanta, Georgia 30323
Subject:
Oconee Nuclear Station Docket Nos. 50-269, -270, -287
Dear Dr. Grace:
By letter dated August 12, 1986, Duke Power Company (Duke) committed to provide to the NRC a Special Report documenting the findings of an investigation into the possible existence of unidentified wiring in Environmentally Qualified Limitorque Valve Operators. Accordingly, please find attached a Special Report concetning this incident.
Very truly yours,
/JBLLMs
- Hal B. Tucker PFG/35/slb Attachment xc: Mrs. Helen Pastis Office of Nuclear Reactor Regulation U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Mr. J. C. Bryant NRC Resident Inapector Oconee Nuclear Station 8611050355 861020 PDR ADOCK 05000269 S PDR h '
o .
L Duke Power Company Oconee Nuclear Station Special Report Possible Existence Of Unidentifed Wires l Within Environmentally Qualified Limitorque Valve Operators 4 ABSTRACT 4
Based upon results from'an inspection at other Duke Power facilities (McGuire l Nuclear Station and Catawba Nuclear Station), Oconee Unit's 1 environmentally qualified Limitorque Motor Operated Valves were inspected on Augsut 8, 1986, while the unit was shutdown for maintenance. In this inspection,' unidentified; wires were
~
found in several of the valve. operators. Further inspection of Units' 2 and 3 valve operators' revealed the existence of unidentified wires in them as well. All three units have operated at 100% power while the unidentified wires were installed.
At the time of discovery, Unit I was shutdown for a Steam Generator tube leak repair. Units 2 and 3 were operating at 100% power.
The corrective action taken was to begin replacing all unidentified and questionable wires with Environmentally Qualified wire. A Justification for continued operation was submitted to the NRC by a Duke letter dated August 12, 1986.
The cause for this incident has been assessed to be a manufacturing deficiency.
1 The supplier of the valve' operators did not ensure that only environmentally
- qualified wiring was utilized during the manufacturing process. A contributing.
cause is an inadequate procedure used during a Modification to replace questionable wires on Limitorque Operators in containment.
There were eight different types of wire found on the Environmentally Qualified Limitorque Operators. Seven of the wires have been qualified under various test reports to perform as necessary in the Locations in which they were found. The e eighth wire, Hypalon, was evaluated to be acceptable for the application in which it was found to be in. Thus the health and safety of the public was not endangered by this incident.
RACKGROUND The initial requirements of the Equipment Qualification (EQ) program were provided in 1967 by 10 CFR 50 Appendix A. The requirements given in 10 CFR 50. Appendix A were " Structures, systems, and components important to safety shall be designed to accommodate the effects of and to be compatible with the environmental conditions-
, associated with normal operation, maintenance, testing, and postulated accidents, including loss-of-coolant accidents". In 1978 IE Circular 78-08 was issued to
. address concerns of potential deficiencies in EQ by various Licensees. On February 8, 1979, IE Circular 78-08 was upgraded to Bulletin 79-01 due to the apparent i widespread EQ deficiencies throughout the industry.
The EQ program that we comply with now stems from Bulletin 79-01. The requirements for Environmental Qualification of electrical equipment important to safety are now provided in 10 CFR 50.49.- The EQ program must include and be based on temperature, pressure, humidity, chemical effects, radiation, aging, and other effects.
I Limitorque valve motor operators utilize internal wiring to connect various limit l and torque switches to control valve operation. All components utilized within the L operator must be environmentally qualified when used in a 10 CFR 50.49 application, i -
1
-l
' ' Specici Rsport .i Page Two j f
DESCRIPTION OF OCCURRENCE In 1964-65 Limitorque began manufacturing valve operators for Oconee. Duke specified the-functional application for each valve and Limitorque installed jumpers to conform to these specifications. At this time'there were no specific guidelines for an Equipment Qualification (EQ) program. However, the vendor, Babcock and Wilcox (B&W) issued a report showing the required manufacturing specifications for electric motor operators.
Part of the response of Duke Power for Bulletin 79-01 was to replace equipment that-did not meet the requirements of the EQ program. .A Modification was initiated to replace questionable wires on the- in-containment valve motor operators and the Reactor Building cooling units.
The Limitorque Operators have _ jumpers that go between the limit switch ' compartment i
and the torque switch compartment. These jumpers are standard on all Limitorques.
i There are also jumpers between limit switches and jumpers between torque switches
< that are installed to conform to the required functional application. These
- jumpers are also installed by Limitorque.
l When the modification was completed on Unit 3, there was no requirement to change the jumpers between the limit and torque switches. This was.because Duke was pursuing qualification of these jumpers from Limitorque. Due to this fact the limit to torque switch jumpers were not replaced on Unit 3.
, On Units 1 and 2 there was a requirement to replace these jumpers. No documentation had been received from Limitorque, so Design-felt that it .was best to replace them. The modification was implemented only on valves in containment.~
On January 14, 1986, the NRC issued Information Notice 86-03 concerning Environmental Qualification deficiencies in Limitorque Operators which had been-
. discovered at Zion in late September 1985, and subsequently at Sequoyah. Design Engineering (DE) reviewed the Information Notice for applicability to Duke Power.
, Their main concerns were for McGuire and Catawba since a modification had been
! implemented at Oconee supposedly alleviating the possibility of any deficiencies.
Realizing potential applicability, Design Engineering requested Limitorque to
. provide the control wiring manufacturer and style for operators supplied to Duke to j
j ensure traceability as required by 10 CFR 50.49.
.Limitorque responded on May 16, 1986, to the request for operator information.
Their information indicated that during the early years of manufacture, the i specific type of wiring used was not retained in their records. However, company l policy was to use type TW or TEW PVC insulated sire (TW, TEW, and TFF are all types j of PVC insulated wire). The company later switched to Raychem Flantrol wiring. In
. 1978, the~ company again switched to Rockbestos SIS.
l
! Based on the Limitorque information, DE concluded that Limitorque Operators containing the PVC wire were used only outside of containment at all of the Duke nuclear units. DE evaluated the worst case outside containment harsh environment , ,
as either a pipe rupture temperature excursion to 260 degrees F or post-acc! dent recirculation radiation of 3.1E 6 Rads (Total-Integrated Dose). The PVC wire was I then evaluated by DE and determined to be qualified.for. use in the harsh ,
environment. This evaluation was concluded on July 25, 1986. At this time, DE was' satisfied that Limitorque Operators were environmentally qualified.
1 l
. l Spfciel Rep:rt ;
Page Three l l
On July 28, 1986, the NRC began an inspection of DE's environmental qualification data for Limitorque Operators. This inspection ended on July 31, 1986, and concluded that data was complete. The NRC then inspected several operators at McGuire Nuclear Station. During that inspection, unidentifiable wiring was found within a Limitorque Operator. Catawba was notified of this finding and began inspection of Limitorque Operators on August 5, 1986. Unidentifiable w1 ring was also found in the Catawba operators.
Oconee was notified of these findings and began inspection on August 8, 1986. The in-contninment valves on Unit 3 had unidentified wires between the limit switches and the torque switches. An unidentifiable small black wire was, also, found in several operators in containment on all three units. All environmentally qualified valves in and outside of containment were included in this inspection. All unidentifiable and type TW or TEW jumper wires are being replaced with qualified wire at the time of inspection.
CAUSE OF OCCURRENCE The cause for this incident is attributed to a manufacturing deficiency.
Limitorque Corporation did not ensure that only environmentally qualified components were supplied with the operators. The unidentifiable insulation was determined to be Hypalon from analysis by Duke Power and CHEM-BAC Laboratories, Inc.
A contributing cause to the incident is attributable to a procedure deficiency.
The implementation procedure for the modification said, " Inspect the limit switch hookup wire in each M.O.V. If the hookup wire is not from an XJ type of cable, replace it with conductors from a Duke Power cable mark number XJ type cable." The procedure should have given reference drawing numbers and a list of the specific
- jumpers to be replaced.
CORRECTIVE ACTIONS l
Following the inspection performed on Unit 1, a limited inspection was made on Units 2 and 3. Based on the results of all inspections and evaluations of unidentified wires, a "Just'Ification for Continued Operation " (JCO) .for Units 2 and 3 were developed. These JCO's were submitted to the NRC along with a brief-
! report regarding this particular situation by a letter dated August 12, 1986.
On August 16, 1986 Unit I was returned to service following its maintenance outage, I at which time all Environmentally Qualified Limitorque Operators had been inspected and all unidentified and questionable wires were replaced. For Unit 2, all environmentally qualified Limitorque Operators were inspected and all unidentified L and questionable wires were replaced prior to the restart of the unit following its l . shutdown for refueling. Unit 2 was shutdown for refueling on August 16, 1986 and l was returned to service on October 14, 1986. On October 2, 1986, Unit 3 was l shutdown for maintenance due to equipment problems which brought the unit to cold l shutdown ' conditions. As a result all Environmentally Qualified Limitorque Operators for Unit 3 were inspected and all unidentified and questionable wires were replaced during the shutdown. In addition to the above, all Environmentally Qualified Limitorque Operators in the warehouse will be inspected and all unidentified and questionable wires will be replaced. Further, while Units 2 and 3 were operating, operation procedures were revised to preclude any unwanted actuations of in-containment Environmentally Qualified Limitorque
SpCcici Rep rt Page Four Operators that had not been inspected and rewired. These revisions include positioning the valve in its Engineered Safeguards (ES) position and removing power to the valve operator, or de-energizing the valve operator within 30 minutes following a containment isolation event, a time frame well before any insolution would became ineffective.
ANALYSIS OF OCCURRENCE The environmental conditions within the reactor building after an accident are of such an extreme nature.that certain specifications for wiring in vrdve operators are required. The synergistic effects of high radiation and high temperature are considered to be the most detrimental.
There were eight different. types of wire found on the Environmentally Qualified Limitorque operators at Oconee. These types were:
- 1. ITI hook-up wire
- 2. Rockbestos Firewall SIS
- 3. - Houston Wire and Cable XLPE
- 4. Vulkene (XLPE)
- 5. Thick insulation field run cable
- 6. High temperature braided wire
- 7. PVC (TFF & TW)
- 8. Hypalon The first seven types of insulation have been qualified under various test reports to perform as necessary in the locations in which they were found.
The eighth type, Hypalon, has been aged to a 40 year qualified like at 150 degrees C (302 degrees F) with no significant change in electrical properties (Reference OkoniteReportyo. 110E). EPRI Report NP-2129 indicates a recommended service limit of 5 X 10 Rads. Hypalon is susceptible to synergistic effects of elevated temperatures and radiation. Based upon the Oconee postulated environment, it is a conservative evaluation that no radiation / temperature synergistic effects would occur to render this type insulation ineffective prior to 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> after a loys of coolant accident (LOCA),~ at which time the accumulated dose approaches 1 X 10 Rads. With the revision to the operator procedures to preclude unwanted.
actuations, the intended safety function of these valves (containment isolation) would not have been impaired. Therefore, the health and safety of the public were not endangered.
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