ML20215K257
| ML20215K257 | |
| Person / Time | |
|---|---|
| Site: | Browns Ferry |
| Issue date: | 06/15/1987 |
| From: | Zech G NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II), NRC OFFICE OF SPECIAL PROJECTS |
| To: | White S TENNESSEE VALLEY AUTHORITY |
| Shared Package | |
| ML20215K262 | List: |
| References | |
| RTR-NUREG-0737, RTR-NUREG-737, TASK-1.B.1.2, TASK-TM NUDOCS 8706250275 | |
| Download: ML20215K257 (3) | |
See also: IR 05000259/1987014
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JUN 10 W
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. Docket Nos. 50-259,z50-260, and 50-296
License: Nos. DPR-33, DPR-52, and DPR-68
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fTgnnessee Valley Authority
(ATTN: Mr. S. ' A. ' White
Manager,of Nuclear Power-
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6N 38A Lookout Place-
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1101 Market Street
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Chattanooga, TN 37402-2801
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Gentlemen:
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SUBJECT:
(NRC INSPECTION REPORT-NOS. 50-259/87-14, 50-260/87-14',
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AND 50-296/87-14)
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This refers toithe. Nuclear Regulatory Commission (NRC) inspection conducted by
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G. L. Paulk .on March 1
. April 30,1987. The inspection included 'a review of
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activities authorized for your Browns Ferry-facility. At the conclusion of.the
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inspection, .the findings were discussed. with . those members' of .your staff -
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identified'in-the enclosed inspection report.
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Areas examined during the inspection included operational safety, maintenance
obshnation,
surveillance
testing
cbservation,
reportable ' occurrences,
configuration management, Restart Review Board and the Independent Safety.
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Engineering Group '(ISEG) activity, welding modifications, the lay up program,
and low' pressure turbine disc cracking,
Within these : areas, the inspection consisted. of selective examinations of
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procedures and representative- records,
interviews with personnel,. and
observation of activities in progress.
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The inspection findings indicate certain activities appeared to violate NRC
requirements.
The violation involved an : inoperable Control Room Emergency
Ventilation'(CREV) System.
The violation, references to pertinent require-
ments, and elements to be included in your response are described in the
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enclosed Notice of Violation (NOV). For the first example of the enclosed NOV,
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please ' address your reasons and corrective actions regarding the timeliness
a'spect of identifying . the actual low flow condition on the B train CREV
system.
Your attention .is. called to paragraph 7, Surveillance Testing observation,
where the Browns Ferry (BFN) quality assurance staff recently performed a
technical review of the BFN Surveillance Instructions (SI). The intent was to
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.' review ten percent of the 430 sis but was temporarily halted after about five
percent because it was concluded that the existing technical adequacy review
program was inadequate. A condition adverse to quality report was written and
the SI program was halted.
More management involvement in the implementation
of this p_rogram will be required to assure satisfactory completion of the
. program.
8706250275 070615
ADOCK 05000259
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JUN 151987
Engineering Group (ISEG)' staffing level at BFN.
As described in the BFN
Nuclear Performance _. Plan,: Volume 3, dated August 28, _1986, ..the BFN ISEG would
consist of three full-time engineers onsite.
NUREG 0737, Item I.B.1.2 speci-
fies that the ISEG should be comprised of a minimum of five dedicated, full-
time engineers.
However, a number less than five may be acceptable, but must
be_ justified'on a case-by-case basis. Our concern.is that based on our current
knowledge _of :the qualifications you intend to use in filling. the BFN ISEG
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positions, the experience level 'does not appear to justify going to fewer
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than five members. Since the ISEG staffing issue was also. raised in our_ review
of the BFN' Nuclear Performance Plan, you should ensure that your revision to
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Volume 3' addresses this question.
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- In accordance with'. Section 2.790 of the NRC's " Rules of Practice," Part 2,
Title 10, Code of Federal Regulations, a copy of this letter and.its' enclosures
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will be placed in the NRC Public Document Room.
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The responses directed by this. letter and the_ enclosures are not subject to the
clearance procedures of.the Office of Management and Budget issued under the
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Paperwork Reduction Act of_1980, PL 96-511.
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-Should you have any questions concerning this letter, please contact us.
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Sincerely,
ORIGINAL SIGNED BY
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GARY G. ZECH
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Gary G. Zech, Assistant Director,
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Inspection Programs
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Division of TVA Projects
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Office of Special Projects.
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Enclosures:
1.
Notice'of Violation
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2.
NRC Inspection Report
cp w/encls:
(Af. P. Pomrehn, Site Director
Browns Ferry Nuclear Plant
(f. L. Gridley, Director
Nuclear Safety and. Licensing
d A. Kirkebo, Acting Director,
Nuclear Engineering
, M J. May, Site Licensing Manager
bec w/encis:
(See page 3)
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